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IDup Date Author Type Category Subject
  402   Sat Nov 21 13:58:30 2020 KojiElectronicsCharacterizationDark Current Measurement for InGaAs QPDs

Dark current measurement for InGaAs QPDs (OSI FCI-InGaAs-Q3000) has been done using Keithley 2450 and Frank's diode test kit. Frank's setup uses various custom instruments which are no longer exist, therefore the kit was used only for switching between the segments.

The diodes were serialized as 81, 82, 83, 84, continuing the numbering for the OMC QPDs. The numbers are engraved at the side and the back of the diode cans.

Overall, the QPDs nominally indicated the usual dark current level of <10nA.
SEG1 of #82 showed a lower voltage of reverse breakdown but this is not a critical level.
#83 showed variations between the segments compared to the uniform characteristics of #81 and #84.

Attachment 1: Q3000_dark_current.pdf
Q3000_dark_current.pdf
  403   Sun Nov 22 13:49:12 2020 KojiElectronicsCharacterizationImpedance Measurement for InGaAs QPDs

To know any anomaly to the junction capacitance of the QPD segments, the RF impedances were tested with a hand-made impedance measurement.
All segments look almost identical in terms of capacitance.

Measurement setup:
The impedance of a device can be measured, for example, from the complex reflection coefficient (S11). To measure the reflection, a bidirectional coupler was brought from the 40m. Attachments 1 and 2 shows the connection. The quantity A/R shows S11. The network analyzer can convert a raw transfer function to an impedance in Ohm.

Calibration and Measurement limit:
The network analyzer was calibrated with 1) a piece of wire to short the clips 2) 50ohm resistor 3) open clips. Then the setup was tested with these three conditions (again). Attachment 3 shows the result. Because of the impedance variation of the system (mainly from the Pomona clip, I guess), there looks the systematic measurement error of ~1pF or ~25nH. Above 100MHz, the effect of the stray impedance is large such that the measurement is not reliable.

The setup was tested with a 10pF ceramic capacitor and this indicated it is accurate at this level. The setup is sufficient for measuring the diode junction capacitance of 300~500pF.

Impedance of the QPD segments:

Then the impedances of the QPD segments were measured (Attachment 4). The segments showed the identical capacitance of 300~400pF level, except for the variation of the stray inductance at high freq, which we can ignore. Note that there is no bias voltage applied and the nominal capacitance in the datasheet is 225pF at 5V reverse bias. So I can conclude that the QPDs are quite nominal in terms of the junction capacitance.

(Ed: 11/23/2020 The RF components were returned to the 40m)

Attachment 1: impedance_measurement.pdf
impedance_measurement.pdf
Attachment 2: P_20201121_183830.jpg
P_20201121_183830.jpg
Attachment 3: impedance_test.pdf
impedance_test.pdf
Attachment 4: Q3000_impedance_test.pdf
Q3000_impedance_test.pdf
  404   Mon Nov 23 23:17:19 2020 KojiElectronicsCharacterizationThe dark noise of the Q3000 QPDs

The dark noise levels of the four Q3000 QPDs were measured with FEMTO DLPCA200 low noise transimpedance amp.

The measurement has been done in the audio frequency band. The amp gain was 10^7 V/A. The reverse bias was set to be 5V and the DC output of the amplifier was ~40mV which corresponds to the dark current of 4nA. It is consistent with the dark current measurement.

The measured floor level of the dark current was below the shot noise level for the DC current of 0.1mA (i.e. 6pA/rtHz).
No anomalous behavior was found with the QPDs.

Note that there is a difference in the level of the power line noise between the QPDs. The large part of the line noises was due to the noise coupling from a soldering iron right next to the measurement setup, although the switch of the iron was off. I've noticed this noise during the measurement sets for QPD #83. Then the iron was disconnected from the AC tap.
 

Attachment 1: Q3000_dark_noise_81.pdf
Q3000_dark_noise_81.pdf
Attachment 2: Q3000_dark_noise_82.pdf
Q3000_dark_noise_82.pdf
Attachment 3: Q3000_dark_noise_83.pdf
Q3000_dark_noise_83.pdf
Attachment 4: Q3000_dark_noise_84.pdf
Q3000_dark_noise_84.pdf
  405   Tue Nov 24 10:45:07 2020 gautamElectronicsCharacterizationThe dark noise of the Q3000 QPDs

I see that these measurements are done out to 100 kHz - I guess there is no reason to suspect anything at 55 MHz which is where this QPD will be reading out photocurrent given the low frequency behavior looks fine? The broad feature at ~80 kHz is the usual SR785 feature I guess, IIRC it's got to do with the display scanning rate.

Quote:

The measured floor level of the dark current was below the shot noise level for the DC current of 0.1mA (i.e. 6pA/rtHz).

  406   Tue Nov 24 12:27:18 2020 KojiElectronicsCharacterizationThe dark noise of the Q3000 QPDs

The amplifier BW was 400kHz at the gain of 1e7 V/A. And the max BW is 500kHz even at a lower gain. I have to setup something special to see the RF band dark noise.
With this situation, I stated "the RF dark noise should be characterized by the actual WFS head circuit." in the 40m ELOG.

  407   Fri Feb 5 07:40:37 2021 StephenSupplyGeneralOMC Unit 4 Build Machined Parts

OMC Unit 4 Build Machined Parts are currently located in Stephen's office. See image of large blue box from office, below.

Loaned item D1100855-V1-00-OMC08Q004 to Don Griffith for work in semi-clean HDS assy.

This includes mass mounting brackets, cable brackets, balance masses, etc. For full inventory, refer to ICS load Bake-9527 (mixed polymers) and Bake-9495 (mixed metals).

Inventory includes all items except cables. Plasma sprayed components with slight chipping were deemed acceptable for Unit 4 use. Cable components (including flex circuit) are ready to advance to fabrication, with a bit more planning and ID of appropriate wiring.

Attachment 1: IMG_8117.JPG
IMG_8117.JPG
  408   Thu May 20 17:03:50 2021 KojiGeneralGeneralSRS LCR meter SRS720 borrowed from Downs

Item loan: SRS LCR meter SRS720 borrowed from Downs. The unit is at the 40m right now for testing with an excelitas PD. Once it is done, the setup will be moved to the OMC lab for testing the high QE PDs

Attachment 1: P_20210520_154841.jpg
P_20210520_154841.jpg
  409   Sun May 30 15:17:16 2021 KojiGeneralGeneralDCPD AF capacitance measirement

Attachment 1: System diagram. The reverse bias voltage is controlled by DS335. This can produce a voltage offset up to 10V. A G=+2 opamp circuit was inserted so that a bias of up to +15V can be produced. The capacitances of the photodiodes were measured with SR720 LCR meter with a probe. DS335 and SR720 were controlled from PC/Mac via serial connections.

Attachment 2: Overview

Attachment 3: How was the probe attached to the photodiode under the test

Attachment 4: The bias circuitry and the power supply

Attachment 5: G=+2 amp

Attachment 1: PD_cap_meas.pdf
PD_cap_meas.pdf
Attachment 2: 20210529013015_IMG_0577.jpeg
20210529013015_IMG_0577.jpeg
Attachment 3: 20210529013114_IMG_0580_2.jpeg
20210529013114_IMG_0580_2.jpeg
Attachment 4: 20210529013200_IMG_0584.jpeg
20210529013200_IMG_0584.jpeg
Attachment 5: 20210529013229_IMG_0586.jpeg
20210529013229_IMG_0586.jpeg
  410   Sun May 30 15:32:56 2021 KojiGeneralGeneralDCPD AF capacitance measirement

Measurement result:

The capacitance at no bias was 460~500pF. This goes down to below 300pF at 1.0~1.5V reverse bias. At maximum +15V, the capacitance goes down to 200~220pF.

On this opportunity, the capacitances of a couple of Excelitas C30665 photodiodes were measured. In Attachment 2, the result was compared with one of the results from the high QE PDs. In general the capacitance of C30665 is lower than the one from the high QE PDs.

Attachment 1: highQEPD_capacitance.pdf
highQEPD_capacitance.pdf
Attachment 2: C30665_capacitance.pdf
C30665_capacitance.pdf
  411   Wed Jul 7 14:21:50 2021 StephenSupplyGeneralOMC Unit 4 Build Machined Parts

More explicit insights into the inventory for the Unit 4 build. Image of inventory included below.

Machined Parts:

Cable Components:

  • Hughes Circuits made us Kapton flex circuits. These have not been processed in any way.
  • Rich had supplied a spool of Gore 4-conductor in-vacuum wire (see below image). I returned the sppol for Rich but it is living in Downs and available for use.
  • PEEK cable ties were damaged during bake, and will be replaced by SYS inventory.

Retrofit/Repair Capabilities:

  • Aluminum reinforcement brackets D1600316
  • Glass reinforcement brackets (Edmund Optics 45-072 and 45-071)

ref: E1900034 and other associated documents.

Attachment 1: IMG_9238.JPG
IMG_9238.JPG
Attachment 2: IMG_9236.JPG
IMG_9236.JPG
  412   Thu Jun 23 21:03:33 2022 KojiFacilityGeneralMoving the small optical table to CAML (TCS Lab)

I've cleared the small optical table and wondered how to move it out of the room. Fortunately, the north side of the big table had wide enough clearance and let the 36" wide table go through. This was easy without moving other heavy stuff.

From here to the door, a bit of work is required. A possibility is to roll the laser blocking wall to the south side of the big table. This will require moving the shelving in the entrance area but it's not a lot of work compared to disassembling a part of the wall.

If this does not work somehow, we will consider removing the last panel of the wall and it will definitely allow the table to get out from the door.

Attachment 1: PXL_20220624_035628602.jpg
PXL_20220624_035628602.jpg
  413   Tue Jun 28 16:13:34 2022 KojiGeneralGeneralThe small optical table not small enough to get out

The table width was an inch too large compared to the door width. We need to tilt the table and it seemed too much for us. Let's ask the transportation for handling.

Photo courtesy by Juan

Attachment 1: IMG-5203.jpg
IMG-5203.jpg
  414   Fri Jul 15 22:14:14 2022 KojiGeneralGeneralOMC Lab recovery for the OMC #002 test

- The lab is chilly (18degC)

- Cleaned the lab and the optical table a bit so that the delicate work can be done. The diode test rig (borrowed from Downs - see OMC ELOG 408 and OMC ELOG 409) was removed from the table and brought to the office (to return on Monday)

- The rack electronics were energized.

- The OMC mirrors in use were returned to the cases and stored in the plastic box.

- The optical table was also cleaned. Removed the old Al foils. The table was wiped with IPA

- The OMC #4 was moved to the other part of the table, and then OMC #2 was placed in the nominal place (Attachment 1). Note that the "legs" were migrated from #4 to #2. There are three poles that defines the location of the OMC Transportation

- The lid was removed and the OMC was inspected (Attachment 2). Immediately found some more delamination of the epoxy beneath the cable bracket (Attachment 3). This needs to be taken care of before shipment.

- The cavity was already flashing as usual, and a bit of alignment made the TEM00 flashing.

- The locking was a little tricky because the LB unit seemed to have a gain-dependent offset. After some adjustment, robust locks were achieved. The cavity was then finely adjusted. Attachment 4 shows the CCD image of the reflection. The core of the spot is more or less axisymmetric as usual. There is also a large helo around the spot. I was not aware of this before. I may need to wipe some of the mirrors of the input path.

- As the satisfactory lock was achieved, I called a day by taking a picture of the table (Attachment 5).

Attachment 1: PXL_20220716_035922673.jpg
PXL_20220716_035922673.jpg
Attachment 2: PXL_20220716_025319391.MP.jpg
PXL_20220716_025319391.MP.jpg
Attachment 3: PXL_20220716_025334324.jpg
PXL_20220716_025334324.jpg
Attachment 4: PXL_20220716_035309066.jpg
PXL_20220716_035309066.jpg
Attachment 5: PXL_20220716_035411435.NIGHT.jpg
PXL_20220716_035411435.NIGHT.jpg
  415   Mon Jul 18 14:20:09 2022 KojiGeneralGeneralOMC #002 Plan Portal

== Initial Preparation ==

  • [Done] OMC #002 placement
  • [Done] OMC #002 locking
  • Details OMC ELOG 414

== Measurements ==

  • [Done] Transmission / Power budget before FirstContact OMC ELOG 416
  • [Done] Transmission / Power budget after FirstContact OMC ELOG 417
  • [Done] Backscatter measurement with a new deflection optics
    • [Done] Optics bonding done waiting for cure OMC ELOG 420 -> Returned the bond to Madeline OMC ELOG 424
    • [Done] Backscatter measurement
      • Measurement: 0.6 ppm OMC ELOG 422
      • (Transmission is 10~60mW. If the backscatter is the order of 1ppm or less, we expect the light level is ~10nW. Can we really detect it? How? ... OK... last time the measurement has been done with the stick PD type powermeter with baffles and the room light turned off (OMC ELOG 209). So it's not totally crazy.)
  • [Done] High QE PD preparation / install / QE check
    • [Done] High QE PD inventory check
      • A1-23    LLO OMC#001
      • A1-25    LLO OMC#001
      • B1-01    LHO OMC#003
      • B1-16    LHO OMC#003
      • B1-22    @CIT Cage B1 Cleaned/Installed
      • B1-23    @CIT Cage B2 Cleaned/Installed
      • C1-03    @CIT Cage B3 Cleaned
      • C1-05    Dead / CIT contamination test cav
      • C1-07    Dead / CIT contamination test cav
      • C1-08    @CIT Cage C2
      • C1-09    @CIT Cage C3
      • C1-10    @CIT Cage C4
      • C1-11    @CIT Cage D1
      • C1-12    @CIT Cage D2
      • C1-14    @CIT Cage D3
      • C1-15    Dead / CIT Cage D4
      • C1-17    LHO Spare
      • C1-21    LHO Spare
      • D1-08    not @CIT, maybe LLO Spare?
      • D1-10    not @CIT, maybe LLO Spare?
    • [Done] Install & QE check
  • [Done] Fiber input beam characterization OMC ELOG 421

== Repair / Preparation ==


== Shipping ==

  • [Done] Tools to ship to LLO OMC ELOG 448
    • CLASS B special tool kit (Allens / Pliers / Mighty-Mouse spanner / Spatula / etc)
    • FC kit
    • Electronic kit (PD connector / trans-impedance amp)
    • Spare High QE PDs
    • Power meters
    • Glass Beamdumps (for optical testing)
    • Cable bracket replacement kit (PEEK cable bracket / cable pegs / fastners / spare fasteners / kapton sheet / cable ties)
    • Emergency EP30-2 kit (excluding the bond)
       
  • [Done] OMC Pelican Filling (Stephen) / OMC Outerbox/insulation (Stephen/Downs) / OMC Shipment Aug 29, 2022 OMC ELOG 445

 

  416   Tue Jul 19 03:17:56 2022 KojiGeneralGeneralOMC #002 Power Budget before mirror cleaning

o Power Budget (2022/07/18)
NPRO ADJ -50 (min)
Fiber incident 62.8mW
Fiber output 45.1mW
Matching to the fiber 72%


DCPD T =  8.90  +/- 0.01  mW
REFPD  =  3.760  +/- 0.001 V

DCPD R =  8.82  +/- 0.01  V
REFPD  =  3.760 +/- 0.001 V

CM1    =  81.4  +/- 0.1   uW
REFPD  =  3.767 +/- 0.001 V

CM2    =  86.6  +/- 0.1   uW
REFPD  =  3.767 +/- 0.001 V

REFLPD
OFS    = -6.214 +/- 0.001 mV (beam blocked)
OFS_REF= +4.587mV

LOCKED =  57.5  +/- 0.5   mV
REFPD  =  3.970 +/- 0.003 V

UNLOCK =  2.816 +/- 0.003 V
REFPD  =  3.943 +/- 0.001 V

P_Inc  =  20.04 +/- 0.01  mW
REFPD  =  3.946 +/- 0.001 V
 


Analysis Result

- Cavity coupling 0.989 (1.1% junk&sidebands)

- Cavity R&T: R=756ppm, T=0.946
- OMC Throughput (Cavity T x First BS R): T=0.939
- Cavity loss per mirror 90 ppm / Round Trip Loss 432ppm

 

  417   Thu Jul 21 02:55:06 2022 KojiGeneralGeneralOMC #002 Power Budget after mirror cleaning

o Power Budget after FirstContact cleaning (2022/07/20)
NPRO ADJ -50 (min)
Fiber incident --.-mW
Fiber output --.-mW
Matching to the fiber ??%



DCPD T =  8.62  +/- 0.01  mW
REFPD  =  3.549  +/- 0.001 V

DCPD R =  9.46  +/- 0.01  V
REFPD  =  3.562 +/- 0.001 V

CM1    =  74.5  +/- 0.1   uW
REFPD  =  3.585 +/- 0.001 V

CM2    =  81.7  +/- 0.1   uW
REFPD  =  3.585 +/- 0.001 V

REFLPD
vOFS    = -6.197 +/- 0.001 mV (beam blocked)
vOFS_REF= +4.58mV

LOCKED =  47.6  +/- 0.2   mV
REFPD  =  3.596 +/- 0.003 V

UNLOCK =  2.700 +/- 0.003 V
REFPD  =  3.590 +/- 0.001 V

P_Inc  =  19.36 +/- 0.001  mW
REFPD  =  3.594 +/- 0.001 V


Analysis Result

- Cavity coupling 0.980 (2.0% junk&sidebands)

- Cavity R&T: R=229ppm, T=0.970 (previous T=0.946, 2.4% UP!)
- OMC Throughput (Cavity T x First BS R): T=0.963
- Cavity loss per mirror 42.8 ppm / Round Trip Loss 238ppm

  418   Thu Jul 21 13:21:27 2022 KojiGeneralConfigurationWindows laptop for WincamD Beam'R2 recovery

The Windows laptop for WincamD/Beam'R2 (DELL Vostro3300) was not functional.
- Windows 7 got stuck in the starting up process (Google "startup repair loop")
- The battery can't charge and the adapter connection is flaky

I decided to newly install Win10.
I made a new bootable Win10 DVD from the ISO downloaded from IMSS. The ISO file was converted to CDR using Disk Utility on Mac.
This deleted the past disk partitions. The installation process has no trouble and Win10 ran successfully. The machine is slow but still acceptable for our purpose.
Dataray Version 7.1H25Bk was downloaded from the vendor website https://dataray.com/blogs/software/downloads and installed successfully.
The devices ran as expected by connecting the heads and selecting the proper device in the software.

Then, the Win10 fell into "Hibernation Loop" and "Shutdown loop" (after disabling hibernation in the safe mode).
This is probably the combination of extremely slow windows update (feature update i.e. beta OS update) and the occasional shutdown due to the flakiness of the AC connection

Win10 was reinstalled and automatic Win update was disabled via windows policy manager or something like that. Still, it tries to download and update some of the updates (what's happening there!?


Here are my strong recommendations on how to use this laptop

  • Do not use any network connection. It will enable Windows Update kicks in and destroy the machine.
  • Use a USB stick for data transportation if necessary
  • The laptop should always be connected to the power supply at a stable location. (The adapter connection is flaky and the battery is dead)
  • Buy a replacement battery (maybe a 3rd-party cheap one
  • The Win10 DVD should always be inserted into the laptop's drive so that we can reinstall the windows anytime.
Attachment 1: IMG_1102.JPG
IMG_1102.JPG
  419   Thu Jul 21 14:35:35 2022 KojiGeneralGeneralBond reinforcement blocks for the invar brackets

Bond reinforcement blocks for the invar brackets:

  • Attachment 1: CLASS A glass prisms (the surplus of the 2016 repair)
  • Attachment 2: Dirty reiforcement bars made of Aluminum
  • There are also many dirty prisms in the kit obtained from Stephen
Attachment 1: IMG_1095.JPG
IMG_1095.JPG
Attachment 2: IMG_1091.JPG
IMG_1091.JPG
  420   Thu Jul 21 14:55:48 2022 KojiGeneralGeneralOptics bonding for the backscatter measurement

The backscatter beam is supposed to appear in the backpropagation path. The transmission of the OMC has a couple of optics, it's not easy to access that beam.
To try to deflect the beam either horizontally or vertically, small optical pieces were made. (Attachment)

These are the combination of the optics

- Thorlabs PF05-03 Fused Silica Mirror Blank (dia12.7mm x t 6.0mm) + Thorlabs 1/2"sq BB Dielectric Mirror BBSQ05-E03

- Thorlabs PF05-03 Fused Silica Mirror Blank (dia12.7mm x t 6.0mm) + Thorlabs ME05-G01 Protected Al Mirror (dia12.7mm x t 3.2mm) + Thorlabs MRA10-K13 Right-Angle Prism Nd:YAG 10mm

Torr seal was used as the bonding epoxy. It uses a 1:2 volume mixture (not easy because of the viscosity) and is relatively fast to cure (in a couple of hours).
The test piece showed some softness after 3~4 hours so I left the parts cured overnight at room temp (i.e. 18degC)

Attachment 1: IMG_1098.JPG
IMG_1098.JPG
  421   Thu Jul 21 17:47:00 2022 KojiGeneralGeneralThe profile of the beam incident on the fiber input coupler

The profile of the beam incident on the fiber input

The fiber input was deflected by a 45deg mirror. The beam profile was measured with WincamD. The beam was too strong (~60mW) even at the smallest pump power (ADJ -50) of the NPRO. So the two ND20 filters were added to the lens right before the 45 deg mirror and the camera.

The measured profile had some deviation from the nice TEM00 particularly around the waist. This could be a problem of the too small beam on the ND filter and the CCD.
This is not an issue as we just want to know the approximate shape of the beam.

For the fiber coupling, if we have the beam waist radius of ~200um it is sufficient for decent coupling.

Attachment 1: fiber_beam_profile.pdf
fiber_beam_profile.pdf
  422   Fri Jul 22 00:31:17 2022 KojiGeneralGeneralOMC #002 backscatter measurement

Measure the power ratio between the forward-propagating and reverse-propagating beams.

  1. Place a small deflecting mirror at the transmission.
  2. Place a flat mirror at the deflected transmission. When the alignment of this mirror is adjusted to retroreflect this beam, the DC of the cavity reflection PD increases, and also the CCD shows spurious fringes.
  3. This condition allows us to locate the power meter at the reverse-propagating spot of the transmission (Attachment 1)
  4. Place a black glass beam dump for the main (bright) transmission (Attachment 2)
  5. Now the power meter is receiving the counter-propagating beam. Turn off the room light and place an anodized Al baffle as shown in Attachment 2. Move the baffle to block only the counter-propagating. Move the baffle out. => Record the power meter reading with/without the baffle in the counter-propagating path. The difference is the power of the reverse-propagating beam.
  6. Now measure the power of the reflected main transmission. This tells us the power ratio between the foward- and back-propagating beams.
  7. Remove the small deflecting mirror and measure the power of the main transmission.
  8. Now the back-propagating power can be estimated from 6 and 7. The same amount is going back to the IFO path.
  9. The reflectivity can be calculated from the 7 and the transmission

- To increase the incident laser power, NPRO Current ADJ was set to be 0 (increased from -50)

- 1st:  Without the baffle 0.373 +/- 0.001 uW / With the baffle 0.318 +/- 0.001 uW
- 2nd: Without the baffle 0.370 +/- 0.001 uW / With the baffle 0.318 +/- 0.001 uW
- 3rd: Without the baffle 0.370 +/- 0.001 uW / With the baffle 0.317 +/- 0.001 uW

==> 53.3 +/- 0.6 nW

- The main transmission was 84.0mW
==> Backpropagation ratio was 0.634+/-0.007 ppm

- Direct measurement of the OMC was  after BS 96.6mW
==> Backpropagation power from the cavity: 61.3 +/- 0.7 nW

- Cavity transmission for the matched beam is Tcav RinputBS = 0.963
==> Incident resonant TEM00 power 100.3mW

- Reflection 61.3+/-0.7 nW x RinputBS = 60.8+/-0.7 nW
-> The effective reflectivity for the mode-matched resonant TEM00 beam incident on the OMC (1st steering mirror) is 0.606+/-0.007 ppm

Attachment 1: OMC_backscatter.pdf
OMC_backscatter.pdf OMC_backscatter.pdf
  423   Fri Jul 22 17:41:01 2022 KojiGeneralGeneralSRS LCR meter SRS720 returned to Downs

SRS LCR meter SRS720 was returned to Downs as before.

 

Attachment 1: PXL_20220723_002330805.jpg
PXL_20220723_002330805.jpg
  424   Fri Jul 22 17:47:38 2022 KojiGeneralGeneralC&B request for the reinforcement blocks

OMC Reinforcement blocks

1. P/N D1600316; Version v4; Type 01; Qty 30; Source Chemistry Machine Shop
2. P/N D1600316; Version v4; Type 02; Qty 15; Source Chemistry Machine Shop
3. P/N D1600316; Version v4; Type 01; Qty 40; Source Resource MFG PO S422806
4. P/N D1600316; Version v4; Type 02; Qty 40; Source Resource MFG PO S422806

Stephen asked Srinath for the ICS entry.
Stephen made the C&B request https://cleanandbake.ligo.caltech.edu/clean_and_bake/request/1708/

Madeline was asked to take care of the C&B.

Also, the Torr Seal box was returned to Madeline.

Attachment 1: PXL_20220722_222013127.jpg
PXL_20220722_222013127.jpg
  425   Mon Jul 25 18:25:04 2022 KojiGeneralGeneralA/C Filter was replaced
New filter PN
Grainger
TK70457312T Mini-Pleat Air Filter, Style - Air Filters Box, Performance Rating MERV 14, Nominal Filter Size 12x24x2
 
Previous filter PN
Global Industrial Equipment
Extended Surface Pleated Cartridge Filter Serva-Cell Mp4 Slmp295 12X24X2 Gl WBB431699
-> No longer available
  426   Tue Jul 26 00:01:59 2022 KojiGeneralGeneralOMC #002 delamination check 2

More epoxy delamination check:

DCPD R (Attachment 1): Found half delaminated

DCPD T (Attachment 2): Found half delaminated

QPD1/QPD2 (Attachment 3): Looks fine

------

In total we need to fix bonding of three invar bases (including the one for the cable bracket)

Attachment 1: IMG_1106.JPG
IMG_1106.JPG
Attachment 2: IMG_1107.JPG
IMG_1107.JPG
Attachment 3: IMG_1110.JPG
IMG_1110.JPG
  427   Tue Jul 26 00:12:58 2022 KojiGeneralGeneralHigh QE PD: QE measurements

- Installed the High QE PDs to OMC #002

  • B1-22@Cage B1 was installed to the transmission DCPD
  • B1-23@Cage B1 was installed to the reflection DCPD

Upon the installation, the legs of the PDs were cut by 3mm. Also, the tab of the PD could not be embedded in the DCPD housing. Therefore, the tabs were cut.

The alignment looked just fine. The weak reflections are directed to the black glass beam dumps.

- After the installation, the QEs were measured.

  • With Thorlabs S130C power meter, the QE was estimated to be ~95%. (Accuracy +/-7%)
  • With Thorlabs S401C power meter, the QE was estimated to be ~100%. (Accuracy +/-3%)

It is so confusing. So I decided to make the QE test setup.


Ophir RM9 with chopper (+/-5%): 8.97mW
Thorlabs S140C integrating sphere (+/-7%): 9.11mW
Thorlabs S130C PD power meter (+/-7%): 9.15mW
Thorlabs S401C thermal power meter (+/-3%): 8.90mW
So there looks ~3% discrepancy between S130C and S401C

Then tried to measure the QE of C1-03@Cage B3 with Ophir RM9
- Initial state: QE=0.95
- First FirstContact application: QE went up to 0.973
- Second FirstContact application: QE = 0.974, basically no change


To Do:
- Calibrate the trans-impedance amp with Keithley
- Apply FC to B1-22 and B1-23 to see if there is an improvement
- The power should be measured with S401C because the accuracy seems better (+/-3%).
- Take photos of the PD FC process

General To Do:

- Backscatter test 2nd trial

- Start applying the first contact to the optical surfaces
- Beam dump cleaning
- Apply FC cap to the PDs
- Delamination repair (light side)
- Delamination repair (dark side)
- Cable bracket replace (dark side)

 

Attachment 1: IMG_1118.JPG
IMG_1118.JPG
  428   Wed Jul 27 10:09:51 2022 KojiGeneralGeneral4+4 wire clamp in hand

Regarding: D1200971

- 4 CLASS A wire clamp obtained from the OMC spare
- 4 more DIRTY wire clamp obtained from WB experiments (they no longer use these)

Once the later ones are C&Bed, we have enough.

 

Attachment 1: PXL_20220727_072154009.jpg
PXL_20220727_072154009.jpg
  429   Wed Jul 27 10:34:09 2022 KojiGeneralGeneralHigh QE PD: QE measurements 2

- DLPCA-200 trans-impedance amplifier was calibrated.
  Keithley source meter 2450 was connected to the amp. Provide current and read the output voltage with the precision digital voltage meter (Agilent/Keysight).
  Gain: 999.7V/A@7mA, 999.6V/A@8mA

- From the power meter spec, Thorlabs S401C seemed the best (+/-3%). So the QEs of the 9 PDs were checked with this power meter again.

- All PDs exhibited the QE of 0.95~0.96. It's all relative as the power meter has a systematic error.
- Tried to clean B1-22 and B1-23 PDs. They didn't show significant improvement after the cleaning. To avoid the unnecessary risk of damaging the PDs, further cleaning was not performed. (Some photos were attached)

- What we can do is use this result as the relative measurements.
- For OMC#2, B1-22 is the DCPD(T) and B1-23 is the DCPD(R). C1-03 and C1-12 are the spares, according to this latest result.
- At LLO, we track down the source of the throughput reduction (-10%). The QEs of the PDs are going to be tested in the same setup at once to compare their PDs and our PDs.

PD Type SN Case DCV1 Pin [mW] dPin [mW] Power Meter DCV2 Avg(DCV) Std(DCV) DCVOFS (mV) Responsivity [A/W] dR QE dQE Date Note
IGHQEX3000 B1-22 B1 7.734 9.43 0.02 TL 401C 7.745 7.7395 0.006 -0.0260 0.821 0.002 0.957 0.002 July 26, 2022 clean1 / installed (T)
IGHQEX3000 B1-23 B2 7.679 9.26 0.02 TL 401C 7.709 7.6940 0.015 -0.0220 0.831 0.002 0.969 0.003 July 26, 2022 clean1 / installed (R)
IGHQEX3000 C1-03 B3 7.775 9.40 0.02 TL 401C 7.770 7.7725 0.003 -0.0450 0.827 0.002 0.964 0.002 July 26, 2022 clean3
                                 
IGHQEX3000 C1-08 C2 7.717 9.45 0.02 TL 401C 7.750 7.7335 0.017 -0.0430 0.819 0.002 0.954 0.003 July 26, 2022 initial
IGHQEX3000 C1-09 C3 7.737 9.50 0.05 TL 401C 7.776 7.7565 0.019 -0.0580 0.817 0.005 0.952 0.006 July 26, 2022 initial
IGHQEX3000 C1-10 C4 7.757 9.50 0.03 TL 401C 7.774 7.7655 0.009 -0.0650 0.818 0.003 0.953 0.003 July 26, 2022 initial
                                 
IGHQEX3000 C1-11 D1 7.826 9.66 0.01 TL 401C 7.828 7.8270 0.001 -0.0570 0.810 0.001 0.945 0.001 July 26, 2022 initial
IGHQEX3000 C1-12 D2 7.841 9.51 0.02 TL 401C 7.841 7.8410 0.000 -0.0410 0.825 0.002 0.961 0.002 July 26, 2022 initial
IGHQEX3000 C1-14 D3 7.769 9.55 0.01 TL 401C 7.789 7.7790 0.010 -0.0520 0.815 0.001 0.950 0.002 July 26, 2022 initial
Attachment 1: IMG_1119.JPG
IMG_1119.JPG
Attachment 2: IMG_1120.JPG
IMG_1120.JPG
  430   Wed Jul 27 10:34:30 2022 KojiGeneralGeneralOMC #002 Protective FirstContact Paint

The optical surfaces were coated with FirstContact to keep them clean / somewhat protected during the transportation.
The PD aperture was sealed with FirstContact "caps" (made by Kate in 2016?).

Attachment 1: IMG_1125.JPG
IMG_1125.JPG
  431   Wed Jul 27 23:52:18 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (1)

Parts check

- D1300052-V3 SN001 is going to be used (Attachment 1)

- This is the PEEK version of the cable bracket (Attachment 2). The side thread holes have no Helicoils inserted. This needs to be done!
 

Connector arrangement check / cable routing check

Attachment 3: Connector Arrangement from the Northside

Attachment 4: Connector Arrangement from the South side

Attachment 5: Cable routing (Northside down)

At this point, the delamination of the V shape beam dumps was visible. This is the subject of bonding reinforcement.

Attachment 1: IMG_1126.JPG
IMG_1126.JPG
Attachment 2: IMG_1135.JPG
IMG_1135.JPG
Attachment 3: IMG_1127.JPG
IMG_1127.JPG
Attachment 4: IMG_1129.JPG
IMG_1129.JPG
Attachment 5: IMG_1130.JPG
IMG_1130.JPG
  432   Thu Jul 28 00:28:15 2022 KojiGeneralGeneral OMC #002 Cable bracket replacement (2)

Connector unmounting

- (Attachment 1) The connector nut rings were removed using an angled needle nose plier. The connector shell has a tight dimension relative to the hole on the bracket. But of course, they could be extracted.

- The 4 screws mounting the bracket to the invar blocks were successfully removed. No extra damage to the bonding.

- (Attachment 2) The plan was to remove the cable pegs by unfastening the button head 1/4-20 screws from the bracket and then just replace the bracket with the new one. However, these screws were really tight. The two were successfully removed without cutting the PEEK cable ties. Two cable ties were necessary to be cut to detach the bracket+pegs from the fragile OMC. Then one screw was removed. However, the final one could not be unfastened. This is not a problem as we are not going to recycle the metal cable bracket... as long as we have spare parts for the new bracket.

- (Attachment 3) Right now, the new bracket is waiting for the helicoils to be inserted. So the OMC lid was closed with the cables piled up. Just be careful when the lid is open.

Attachment 1: IMG_1132.JPG
IMG_1132.JPG
Attachment 2: IMG_1133.JPG
IMG_1133.JPG
Attachment 3: IMG_1136.JPG
IMG_1136.JPG
  433   Thu Jul 28 00:46:47 2022 KojiGeneralGeneral Subject: OMC #002 Cable bracket replacement (3)

Checking the spare parts

- Conclusion for OMC#2: need PEEK cable ties
- for more OMCs: need more BHCS / PEEK cable ties / Helicoils

  • Helicoils: 1/4-20 0.375 helicoils / Qty 4 / Class A (Attachment 1)
    • looks like there are many more as the transport fixture bags (Attachment 2). Stephen noted that they are meant to be CLASS B
       
  • Cable pegs: D1300057 / Qty 24 + 3 recycled from OMC#2 / Class A (Attachment 3)
    • Requirement: 3+3+4 = 10 for the 4th OMC / 3x4 =12 for the cable bracket replacement -> we have enough
       
  • PEEK Cable Ties: Stephen reported they were deformed by baking heat... did not check how they are in the bags.
     
  • Button Head Cap Screws 1/4-20 length ? none found in the bags.
    • Qty 4 spare (forgot to take a picture) + 3 recycled. So we have sufficient for OMC#2
Attachment 1: IMG_1137.JPG
IMG_1137.JPG
Attachment 2: IMG_1148.JPG
IMG_1148.JPG
Attachment 3: IMG_1138.JPG
IMG_1138.JPG
  434   Wed Aug 10 18:42:27 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (4)

[Stephen Koji]

Now we got the C&Bed parts to continue to work on the cable bracket replacement.

1) Helicoil insertion

1/4-20 Helicoils were inserted into the 6 thread holes of D1300052. It went mostly okay. We witnessed that the Helicoil insertion tool delaminated the plating of the Helicoils upon insertion (Attachment 1). Stephen mentioned that this is not usual, but we didn't find anything further such as increased friction, more debris, etc. So we decided to go forward.

2) EP30-2 Kit

The EP30-2 kit was transferred from the 40m clean room to the OMC lab. The EP30-2 kit tracking was updated via C1900343

3) D1300052 reinstallation -> FAIL

Now resumed to the installation of D1300052 bracket. However, the hole size of the bracket is just a bit too small compared with the size of the mighty mouse connectors. It was already quite tight with the metal version. However, this PEEK version seems to have 0.1 mm further small diameter, and then the connectors do not penetrate the holes. The plan could be
1) Use a razor blade to shave the hole inner circle.
2) Use a cleaned drill bit to make the hole size 0.2mm bigger.

Attachment 1: PXL_20220809_235457354.jpg
PXL_20220809_235457354.jpg
Attachment 2: PXL_20220811_011910569.jpg
PXL_20220811_011910569.jpg
Attachment 3: PXL_20220811_013746139.jpg
PXL_20220811_013746139.jpg
  435   Thu Aug 11 15:24:57 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (5)

- The hole size extension is going forwared now.

- Madeline and Chub are cleaning (sonicating) a drill (29/64=0.4531")
- The parts in a bag were brought to the 40m C&B lab.

- The hole is going to be 11mil=0.28mm larger than the recommendation (0.442").
  It's not a D-hole. The connector has a rounded-rectangular flange that fits into the PEEK parts.
  So I don't think it's an issue.

- Chub has a proper spanner to fasten the nuts. We want to use it here and LLO.

 

  436   Mon Aug 15 21:31:56 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (6)

The cable bracket was successfully replaced.

  • Looking from the QPD side (North side in Attachment 1), the connectors for the DCPDs and PZT are sticking out, and the ones for QPDs are sticking to the other side. So only two rectangular holes (for QPDs) are facing north.
    • Top left is DCPDT
    • Top right is DCPDR
    • Bottom center is PZT
    • Bottom left is QPD (far/long)
    • Bottom right is QPD (near/short)
       
  • First, the cable pegs for the short sides are fastened with the original screws (Vented BHCS 1/4-20).
  • Then, the cables are started to be inserted from the bottom so that the nuts can be rotated with the spanner. The spanner helped a bit but the nut only has two positions to hook the spanner and the clearance is not sufficient to insert the spanner when one of the hook positions is facing the bottom. The enlarged hole (29/64") perfectly worked . The flange of the connector can be held with a rectangular hole, so a bit bigger hole than the connector size was not an issue. Finally, all the cables were attached to the bracket.
  • The bracket has not yet been fixed on the OMC breadboard yet. This was done with the four screws from the top. Along with the assembly document E1300201, the fastening torque was limited to 2 in-lb using a digital torque wrench.
  • Attachment 2 shows the view from the "North" side. Attachment 3 shows the view from the "South" side. The cables were not yet tied on the cable pegs on the long side of the bracket.
Attachment 1: IMG_1155.JPG
IMG_1155.JPG
Attachment 2: IMG_1149.JPG
IMG_1149.JPG
Attachment 3: IMG_1150.JPG
IMG_1150.JPG
  437   Mon Aug 15 22:06:18 2022 KojiGeneralGeneralOMC #002 new cable tie installed

[Stephen Koji]

New cable ties were installed on the cable pegs attached to the long sides of the cable bracket.

 

Attachment 1: IMG_1929.JPG
IMG_1929.JPG
Attachment 2: IMG_1930.JPG
IMG_1930.JPG
  438   Mon Aug 15 22:43:35 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (1)

[Stephen Koji]

Checked the delamination status:

  • The Invar bar on the cable bracket (DCPD side): Almost all delaminated (Attachment 1 left)
  • The invar bar on the cable bracket (QPD side): Rims still intact, center delaminated (Attachment 1 right)
  • The invar bar reinforced in 2016: One of the reinforcement bar half delaminated (Attachment 2)
Attachment 1: IMG_1926.JPG
IMG_1926.JPG
Attachment 2: PXL_20220816_011346581.jpg
PXL_20220816_011346581.jpg
  439   Mon Aug 15 22:49:03 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (2)

EP30-2 preparation

  • Two Al foil cups + A sheet of Al foil (for test cure)
  • Set a tube on the glue gun
  • Attach an applicator tube
  • Push a couple of times, and dispense the glue for a single stroke on a waste Al cup
  • Pour the 6g of glue to the other cup.
  • Add 0.3g of silica beads powder to the cup
  • Steer. Pick a few drops to the test cure Al foil
  • Bake the test piece for 15min in 200F (95degC) ==> Very good

#1 The Invar bar on the cable bracket (DCPD side)

Added short (frosted) Al bars (Attachment 1) to the short sides of the invar bar. (Attachments 2/3). Some glue was sucked into the delamination gap by capillary action (=good) (Attachment 4)

#2 The Invar bar on the cable bracket (QPD side)

Added short (frosted) Al bars to the short sides of the invar bar. (Attachments 3/5). Maybe some glue was sucked into the delamination gap??? Not so clear. (Attachment 4)

#3 The Invar bar reinforced in 2016

Added a short (frosted) Al bars to a short side of the invar bar (Attachment 6). On both sides of the 2016 reinforcement, rectangular prisms are added (Attachment 6)
Some capillary action is visible beneath the invar bar (Attachment 7)


Leave it as it is for a day

 

Attachment 1: PXL_20220816_011256007.jpg
PXL_20220816_011256007.jpg
Attachment 2: PXL_20220816_020441901.MP.jpg
PXL_20220816_020441901.MP.jpg
Attachment 3: PXL_20220816_022033189.jpg
PXL_20220816_022033189.jpg
Attachment 4: PXL_20220816_022234784.jpg
PXL_20220816_022234784.jpg
Attachment 5: PXL_20220816_020415355.jpg
PXL_20220816_020415355.jpg
Attachment 6: PXL_20220816_022108122.jpg
PXL_20220816_022108122.jpg
Attachment 7: PXL_20220816_022244417.jpg
PXL_20220816_022244417.jpg
  440   Wed Aug 24 02:51:23 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (3)

Inspection of the bonding on the suspension interface side. All look good.

Attachment 1: IMG_1156.JPG
IMG_1156.JPG
Attachment 2: IMG_1157.JPG
IMG_1157.JPG
Attachment 3: IMG_1158.JPG
IMG_1158.JPG
Attachment 4: IMG_1159.JPG
IMG_1159.JPG
Attachment 5: IMG_1160.JPG
IMG_1160.JPG
Attachment 6: IMG_1161.JPG
IMG_1161.JPG
Attachment 7: IMG_1162.JPG
IMG_1162.JPG
Attachment 8: IMG_1163.JPG
IMG_1163.JPG
  441   Wed Aug 24 02:53:46 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (1)

Inspection of the delaminations in the optics side

Attachment 1: IMG_1168.JPG
IMG_1168.JPG
Attachment 2: IMG_1169.JPG
IMG_1169.JPG
Attachment 3: IMG_1170.JPG
IMG_1170.JPG
Attachment 4: IMG_1171.JPG
IMG_1171.JPG
Attachment 5: IMG_1175.JPG
IMG_1175.JPG
  442   Wed Aug 24 02:57:43 2022 KojiGeneralGeneralEP30-2 bonding setup

EP30-2 bonding setup

Attachment 1: IMG_1178.JPG
IMG_1178.JPG
Attachment 2: IMG_1179.JPG
IMG_1179.JPG
Attachment 3: IMG_1180.JPG
IMG_1180.JPG
  443   Wed Aug 24 03:20:59 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (2)

Bonding

Attachment 1: IMG_1182.JPG
IMG_1182.JPG
Attachment 2: IMG_1183.JPG
IMG_1183.JPG
Attachment 3: IMG_1184.JPG
IMG_1184.JPG
Attachment 4: IMG_1185.JPG
IMG_1185.JPG
Attachment 5: IMG_1186.JPG
IMG_1186.JPG
Attachment 6: IMG_1187.JPG
IMG_1187.JPG
Attachment 7: IMG_1188.JPG
IMG_1188.JPG
Attachment 8: IMG_1189.JPG
IMG_1189.JPG
Attachment 9: IMG_1190.JPG
IMG_1190.JPG
Attachment 10: IMG_1191.JPG
IMG_1191.JPG
Attachment 11: IMG_1193.JPG
IMG_1193.JPG
  444   Wed Aug 24 03:26:43 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (3)

Inspection

 

Attachment 1: IMG_1199.JPG
IMG_1199.JPG
Attachment 2: IMG_1200.JPG
IMG_1200.JPG
Attachment 3: IMG_1201.JPG
IMG_1201.JPG
Attachment 4: IMG_1202.JPG
IMG_1202.JPG
Attachment 5: IMG_1203.JPG
IMG_1203.JPG
Attachment 6: IMG_1204.JPG
IMG_1204.JPG
Attachment 7: IMG_1205.JPG
IMG_1205.JPG
Attachment 8: IMG_1206.JPG
IMG_1206.JPG
  445   Wed Aug 24 11:29:47 2022 KojiGeneralGeneralOMC #002 ready for shipment

[Stephen Koji]

The OMC #002 is ready for shipment.

Attachment 1: Work done on Sept 19, 2022

Other attachments: Putting the OMC in the pelican case.

Attachment 1: IMG_1207.JPG
IMG_1207.JPG
Attachment 2: PXL_20220825_004259850.jpg
PXL_20220825_004259850.jpg
Attachment 3: PXL_20220825_004307204.jpg
PXL_20220825_004307204.jpg
Attachment 4: PXL_20220825_005423342.jpg
PXL_20220825_005423342.jpg
Attachment 5: PXL_20220825_005549985.jpg
PXL_20220825_005549985.jpg
  446   Thu Aug 25 14:22:08 2022 KojiGeneralGeneralLLO OMC #001 Ballast Mass investigation

Inspected the past LLO add-on mass configuration.

There are unknown masses at the DCPD side. It looks like a small SS mass with an estimated mass of 5g. But the DCC number is unknown.

We are going to add 10g on each corner as well as the damping aterial. We should be able to figure out the fastener / mass configuration.

Attachment 1: DSCN0917.JPG
DSCN0917.JPG
Attachment 2: DSCN0922.JPG
DSCN0922.JPG
Attachment 3: P6108705.JPG
P6108705.JPG
Attachment 4: P6108707.JPG
P6108707.JPG
Attachment 5: P6108706.JPG
P6108706.JPG
  447   Thu Aug 25 20:05:00 2022 KojiGeneralGeneralLLO OMC #001 Ballast Mass investigation

Here is the balance mass info for the LLO OMC#001 analyzed from the photographs

  • Added masses are: 50+10g, 50+20, 10+20+5, and 20+20+10 for the mass right above FM1/CM1/FM2 and CM2, respectively.
  • The length of the 1/4-20 screws seem L=3/4"~1"

If we attach the additional mass, longer 1/4-20 screws (1", 1" 1/8, 1" 1/4) are going to be used.

Attachment 1: balance_mass_config_LLO.pdf
balance_mass_config_LLO.pdf
  448   Fri Aug 26 22:29:02 2022 KojiGeneralGeneralTool Shipping Prep

Shipping preparation for the LLO trip

Started July 15, 2022 and finished Aug 30. So it took ~1.5 months (with a couple weeks of break)


Class B special tools

  • Screw Drivers 1
    • https://www.steritool.com/
    • https://www.steritool.com/precision-screwdrivers-mini.aspx
  • Screw Drivers 2
    • What I have seems S555Z-7
    • https://www.starrett.com/
    • https://www.starrett.com/dms/flipbooks/Cat-33/index.html?page=354
  • Allen Wrenches
    • Bondhus: These are not made of SS, but of so called protanium steel. I have a chrome finish one (BriteGuard) and K14 gold finish one (goldguard).
    • https://intl.bondhus.com/pages/goldguard-ball-end
    • https://intl.bondhus.com/pages/briteguard-ball-end
  • Scissors
    • VWR - Stainless Steel
    • Unknown PN /  probably this?
    • https://us.vwr.com/store/product/4527635/vwr-dissecting-scissors-sharp-blunt-tip
  • Forceps
    • VWR - Stainless Steel
    • https://us.vwr.com/store/product/4531765/vwr-hemostatic-forceps
  • Wire cutters
    • Looks like they are orthodontic wire cutters. One has the marking "Orthomechanic Stainless Steel" but the company does not sell cutters anymore. The other has a marking "333" but the company is unknown. Similar products can be found on Amazon
  • Long nose pliers - straight stainless steel
    • https://www.aventools.com/
    • https://www.aventools.com/long-nose-pliers-stainless-steel-6-2
  • Bent nose pliers - stainless steel
    • unknown 
  • Tweezers
    • Excelta 
    • The short one is 20A-S-SE. The longer one is 24-SA-PI, maybe?
    • https://www.excelta.com/
    • https://www.excelta.com/straight-laboratory-instruments-forceps
    • https://www.excelta.com/style-24-24-6-sa
  • Mighty-Mouse spanner
  • 2x driver bits for the digital torque wrench

First Contact Kit

  • FC bottole / PEEK mesh

Bonding kit (excl EP30-2 bond)

  • reinforcement bars (4 types)
  • bonding liner powder
  • tools: spatula / bond applying rod

Power meters (excl Power meter controller)

  • Thorlabs Thermal
  • Thorlabs Photodiode
  • Thorlabs Integrating Sphere

Electronics

  • preamp + power cable
  • PD testing kit (PD connector / DB9 break out / grabber-BNC)
  • Nitrile gloves

Cable bracket replacement kit

  • PEEK cable bracket (Helicoiled)
  • Cable pegs (x4 salvaged / spare)
  • fastners
  • kapton sheet
  • cable ties

Optics / Optomechanics

  • Optical fiber / spare fiber
  • OMC transport feet
  • OMC backscatter inspection prisms

Misc tools

  • digital torque wrench

=== Action done on Aug 30 ===

Fiber MM setup / Fiber coupler mount
Glass Beamdumps (for optical testing)
Flipper mirror
Thorlabs fiber coupler tool
General bent nose plier for fiber
Thorlabs collimator tiny allen
Spare High QE PDs

Spare OMC bags / Zip bags

Balance Mass 10g Qty 8 (Different Type D11*** 1.25" dia), 20g Qty 10 / Mass damper D1700301 -04 / Mass damper screws SHCS 1/4-20 x 1.25 Qty 25 / 1" screws and 1 1/8" screws

Shipping request: https://services1.ligo-la.caltech.edu/FRS/show_bug.cgi?id=25002


=== Low supply! ===

  • Masks
  • 7.0 gloves supply low
  • 7.5 glove completely gone
  • Wet vectra cloth
  • Dry vectra cloth
Attachment 1: PXL_20220831_025623318.jpg
PXL_20220831_025623318.jpg
Attachment 2: PXL_20220831_024518032.jpg
PXL_20220831_024518032.jpg
Attachment 3: PXL_20220831_030234581.jpg
PXL_20220831_030234581.jpg
  449   Tue Sep 20 08:54:33 2022 KojiGeneralGeneralPD cage arrangement

Upon the LLO work, the current PD arrangement in the cages are:
CAGE B
B1 OMC1 PDT (A1-23)
B2 OMC1 PDR (A1-25)
B3 original (C1-03)
B4 OMC2 PDT (B1-22)

CAGE C
C1 OMC2 PDR (B1-23)
C2 original (C1-08)
C3 original (C1-09)
C4 original (C1-10)

  450   Mon Sep 26 14:27:49 2022 KojiGeneralGeneralLLO OMC ICS work

OMC #001

OMC #002

  451   Mon Nov 7 21:16:16 2022 CamilleOpticsConfigurationSetting up the fiber couplers

[Camille, Koji]

Began setting up fiber assembly for OMC testing:
-Aligned fiber mount to maximize transmission through fiber
-Adjusted polarization at output of fiber to minimize s-polarized output.

Power measurements:
fiber input: 56.7 mW
fiber output:43.2 mW
s-polarized output: 700 uW

Attachment 1: PXL_20221108_003849213.jpg
PXL_20221108_003849213.jpg
Attachment 2: PXL_20221108_003909265.jpg
PXL_20221108_003909265.jpg
Attachment 3: PXL_20221108_003929309.jpg
PXL_20221108_003929309.jpg
ELOG V3.1.3-