ID |
Date |
Author |
Type |
Category |
Subject |
182
|
Thu Apr 17 21:39:25 2014 |
Koji | Optics | General | More alignment |
STORY:
- The cavity mirrors have scattering spots. The cavity alignment should have been scanned to find a cavity mode to have lowest loss possible.
BTW, We only have horizontal dof for the alignment scan.
- After some struggle nice cavity mode was found. The cavity transmission was 96% for the ideally matched TEM00 carrier.
- It turned out that this imposed too much beam shift in the input beam (~2mm).
- This big shift induces a lot of trouble for the peripheral optics (PDs, QPDs, sterring mirrors).
- What should we do???
Analysis:
- The beam needed to go up between CM1 and CM2 to have the right spots on them. ("UP" is the input side of the OMC).
- This imposed the beam between FM1 and FM2 moved up. In other word, for the given alignment of the FMs by the template,
We needed to hit the upper part of the FMs to have the spots on the CMs up.
Solution:
- The above argument suggets that the nominal beam will give us the right spots on the CMs if we rotate the FMs.
Of course this induces the spot move on the FMs. But this should not be the issue as the most of the loss seems to come from the CMs.
- How much misalignment show we give to the FMs? We want to shift the beam by 2mm on the CMs.
The length of the optical lever is ~0.25m. Therefore the mialignment angle should be
theta = 2e-3/2/0.25 = 4e-3 rad = 4mrad.
The template pad has ~20mm separation. The thickness of the shim should be 20mm*4mrad = 80um
- Our aluminum foil seems to have the thickness of 30-40um. We can't have this minimum thickness on the template pad as there is not enough compression pressure
=> Just use a single layer of Al piece to shim the FMs.
Attempt:
- The shims were inserted at the upper pads of the FMs.
- Aligned the input beam and the CMs so that the spots on the CMs are approximately recovered.
- Measure the cavity power budget
Pin: 34.7mW
Refl PD: offset = -7.5mV, unlock = 6.07V, inlock = 89.7mV
Ptrans = 32.5mW
Ptrans(CM2) = 0.181mW
Ptrans(CM2) = 0.184mW
Assume finesse of 400
==>
Pin: 34.7mW
Pjunk: 0.534mW
Pcoupled: 34.1mW
Mode matching: 98.5%
Cavity reflectivity in power: 0.00061
Cavity transmission in power: 0.951 (This is not a best number but acceptable.)
Loss per mirror: 75.4ppm
FM power refl/trans: 0.9923 / 7630ppm
CM1 power refl/trans: 0.999882 / 42.8ppm
CM2 power refl/trans: 0.999881 / 43.5ppm
Total roundtrip loss of the cavity (Loss + CM leakage): 388ppm
Result:
How much the input beam is away from the left wall of the OMC breadboard?
40.88mm from the template edge
8.36mm between the template edge and the bread board
=> 32.52mm
How much should this number be? 32.94mm from the solidworks model => With in 0.5mm! Nice!
Next:
- Just in case plce all of the optics and check if the beam is delivered within the alignment range of the optics
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187
|
Thu Jun 19 23:16:50 2014 |
Koji | Optics | General | All of the prisms have been glued |
- All of the PRISM mirrors have been glued
- 4 out of 5 beam dumps have been glued
TODO
EP30-2 gluing of the INVAR blocks for the PDs
PDs/QPDs need to be slightly lower -> order more shims
Remove the templates
Glue the last beam dump
Vibration test?
Bring the OMC to the bake lab
Vacuum baking
Bring it back to the OMC lab
Cabling / Wiring
Optical tests
Backscattering test
Packing / Shipping

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188
|
Fri Jun 20 18:59:12 2014 |
Koji | Optics | General | All of the invar blocks have been glued |
All of the INVAR blocks have been glued.
I found thinner shims in the stock.
On Monday, the template will be removed.
EP30-2 7g mixed with 0.35g of 75-90um sphere
TODO
EP30-2 gluing of the INVAR blocks for the PDs
PDs/QPDs need to be slightly lower -> order more shims
Remove the templates
Glue the last beam dump
Vibration test?
Bring the OMC to the bake lab
Vacuum baking
Bring it back to the OMC lab
Cabling / Wiring
Optical tests
Backscattering test
Packing / Shipping |
189
|
Mon Jun 23 21:54:16 2014 |
Koji | Optics | General | All of the gluing completed |
The bottom-side templates were removed.
The last beam dump was removed
TODO
ICS entry
Bring the OMC to the bake lab
Vacuum baking
Bring it back to the OMC lab
Cabling / Wiring
VIbratin test
Optical tests
Backscattering test
Packing / Shipping
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190
|
Tue Jun 24 18:43:15 2014 |
Koji | General | General | ICS entries for the OMC baking/assembly |
For baking:
- Assembly Name aLIGO Output Mode Cleaner
Assembly Number D1201439
- Part Name: Breadboard transport fixture
Part # / Drawing #: D1201515
TO BE ADDED TO THE ASSEMBLY after the bake: [DONE]
803-003-07M6-4PN-598A-0-Bulk-H42Q001
D1201274-V1-00-S009: OMC DCPD Housing (remove part)
D1201274-V1-00-S010: OMC DCPD Housing (remove part)
D1201275-V1-00-0006: OMC DCPD FACE PLATE (remove part)
D1201275-V1-00-0007: OMC DCPD FACE PLATE (remove part)
D1201280-V1-00-0006: OMC QPD HOUSING (remove part)
D1201280-V1-00-0007: OMC QPD HOUSING (remove part)
D1201281-V1-00-0006: OMC QPD FACE PLATE (remove part)
D1201281-V1-00-0007: OMC QPD FACE PLATE (remove part)
D1300052-V1-00-0003: aLIGO OMC BRACKET, CABLE CONNECTOR (remove part)
D1300057-v2-00-0021: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0022: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0023: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0024: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0025: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0026: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0027: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0028: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0029: aLIGO CABLE PEG (remove part)
D1300057-v2-00-0030: aLIGO CABLE PEG (remove part)
D1300060-V1-00-0005: aLIGO OMC BRACKET, MASS MOUNTING (remove part)
D1300060-V1-00-0006: aLIGO OMC BRACKET, MASS MOUNTING (remove part)
====================================
More entries to be added (Found in the LHO OMC entry) [DONE]
D1300371-V2-00-S1301806: ISC DCPD Cable for OMC-Breadboard Bracket to DCPD #1
D1300372-V2-00-S1301807: ISC DCPD Cable for OMC-Breadboard Bracket to DCPD #2
D1300373-V3-00-S1301810: ISC QPD Cable for OMC-Structure to Breadboard Bracket
D1300374-V2-00-S1301813: ISC QPD Cable for OMC-Breadboard Bracket to QPD #1 |
191
|
Fri Jun 27 12:29:50 2014 |
Koji | General | General | OMC baking |
The OMC went into the oven at around 2PM on Thursday. It will be baked at 80degC for 48 hours.
The RGA result will be obtained on Monday.
Link to the ICS entry

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192
|
Fri Jun 27 18:51:33 2014 |
Koji | General | General | Supply |
PTOUCH TAPE (12mm white) x 2
9V batteries |
193
|
Wed Jul 2 16:41:43 2014 |
Koji | General | General | OMC baking |
OMC is back from the oven today.
To Do:
Optical tests
- Cleaning
- Power Budget
- FSR measurement
- TMS measurement
- TMS measurement (with DC voltage on PZTs)
- PZT DC response
- PZT AC response
- QPD alignment
- DCPD alignment
- First Contact
Backscattering test
Cabling / Wiring
- Attaching cable/mass platforms
- PZT cabling
- DCPD cabling
- QPD cabling
Vibration test
Packing / Shipping |
194
|
Wed Jul 2 18:58:42 2014 |
Koji | General | General | Beam dump delamination |
While the OMC breadboard was being inspected, it was found that two out of five black-glass beam dumps showed sign of delamination.
(attached photos).
The base of the each beam dump is a fused silica disk (25mm dia.). The black glass pieces are bonded to the disk. The bond is EP30-2
epoxy without glass beads for bond lining. The disk is bonded on the fused silica bread board with Optocast UV low-viscous epoxy.
The delamination is about 70% of the bonded area. They don't seem to fall off immediately. But the glass pieces are not completely secure.
(i.e. finger touch can change the newton ring fringes) So there might be some risk of falling off during transportation.
The engineering team and I are exploring the way to secure them in-situ, including the method to apply UV epoxy with capillary action.
|
Attachment 1: beamdump_delamination.png
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|
195
|
Thu Jul 3 17:45:18 2014 |
Koji | General | General | Beam dump delamination |
Here is the resolution.
I'll apply fillets of EP30-2 along the edges of the black glass (See figure).
In order to allow the air escape from the gap, the inside of the V will not be painted.
In any case, I don't have a good access to the interior of the V.
Dennis assured that the outgassing level will be ok even if the EP30-2 is cured at the room temp if the mixture is good.
But just in case, we should run an RGA scan (after 50degC for 24hour vac bake).
I prefer to do this RGA scan right after all of the test and cabling and right before the shipment.
Dennis is checking if we can even waive the RGA scan owing to the small volume of the glue.

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196
|
Sun Jul 6 02:45:56 2014 |
Koji | Optics | General | FSR Measurement |
3rd OMC FSR / Finesse measurement
RF AM was injected by detuning a HWP. |
Attachment 1: finesse_measurements_log.pdf
|
|
200
|
Mon Jul 7 01:36:03 2014 |
Koji | General | General | To Do |
Optical tests
Cleaning
Power Budget
FSR measurement
TMS measurement
TMS measurement (with DC voltage on PZTs)
- PZT DC response
- PZT AC response
- QPD alignment
- DCPD alignment
Backscattering test
Cabling / Wiring
- Attaching cable/mass platforms
- PZT cabling
- DCPD cabling
- QPD cabling
Vibration test
Baking
First Contact
Packing / Shipping |
201
|
Tue Jul 8 04:08:06 2014 |
Koji | General | General | Expoxy reapplication for beam dumps |
Firstly, the excess epoxy was removed using a cleaned razor balde
Secondly, EP30-2 epoxy was applied at the exterior edges of the beam dump.
Interior of the V were glued at two points. This is to keep the gap away from being trapped
Here is the result of the gluing. Some epoxy was sucked into the gap by capillary action.
I believe, most of the rigidity is proivded by the bonds at the edges.
|
203
|
Thu Jul 10 01:39:38 2014 |
Koji | Electronics | General | PZT wire |
Rich came to the OMC lab. Pins for the mighty mouse connector were crimped on the 4 PZT wires.
We found the male 4pin mighty mouse connector in the C&B area.
The cable inventory was checked with ICS/DCC combo. It turned out that most of the on-board cables
are at LHO. We decided to send the OMC there and then the cables are installed at the site. |
Attachment 1: P7096669.JPG
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|
204
|
Thu Jul 10 08:34:57 2014 |
Koji | General | General | To Do |
Optical tests
Cleaning
Power Budget
FSR measurement
TMS measurement
TMS measurement (with DC voltage on PZTs)
PZT DC response
PZT AC response
QPD alignment
DCPD alignment
Backscattering test
Cabling / Wiring
Attaching cable/mass platforms
PZT cabling
- DCPD cabling (to be done at LHO)
- QPD cabling (to be done at LHO)
Vibration test
Baking
First Contact
Packing / Shipping |
212
|
Sun Jul 20 17:20:39 2014 |
Koji | General | General | The 3rd (LIO) OMC was shipped out to LHO |
The 3rd (LIO) OMC was shipped out to LHO on Friday (Jul 18) Morning.
At LHO
- All of the on-breadboard cables should be attached and tied down.
- Peel First Contact paint and pack the OMC for storage.
|
214
|
Thu Jul 31 15:07:53 2014 |
Koji | General | General | Item lending |
Tara: Laser Safety goggle -> Returned
Evan:
HP signal generator (990MHz) (prev. setting 32.7MHz / +3dBm)
Black glass beam dump
Dmass:
LB1005 Oct 24.
|
215
|
Mon Aug 4 18:59:50 2014 |
Koji | General | General | A memorandom |
On breadboarfd cabling for 3IFO OMC
D1300371 - S1301806
D1300372 - S1301808
D1300374 - S1301813
D1300375 - S1301815 |
216
|
Tue Aug 5 13:03:25 2014 |
Koji | General | General | Missing cable components |
DCPD Connector Face: Qty2 https://dcc.ligo.org/LIGO-D1201276
QPD Connector Face: Qty2 https://dcc.ligo.org/LIGO-D1201282
PD faster: 92210A07 Qty 4: MCMASTER #2-56 x .25 FHCS
Spare DCPD |
219
|
Sat Jan 17 11:40:04 2015 |
Koji | General | General | 3rd OMC completed |
Jan 15, 2015 3rd OMC completed
The face caps of the DCPD/QPD cables were installed (Helicoils inserted)
PD7&10 swapped with PD11(for DCPD T) and PD12(DCPD R).
Firct Contact coating removed
Note on the 3rd OMC
Before the 3rdOMC is actually used,
- First Contact should be applied again for preventing contamination during the installation
- DCPD glass windows should be removed |
220
|
Fri Jan 30 19:31:08 2015 |
Koji | General | General | Item lending |
Gabriele:
PZT HV Amp
Evan:
HP signal generator (990MHz) (prev. setting 32.7MHz / +3dBm)Returned March 23, 2016
Black glass beam dump
Dmass:
LB1005 Oct 24. This unit is permanently gone to Cryo lab. Acquired a new unit. Aug, 2016.
Quote: |
Tara: Laser Safety goggle -> Returned
Evan:
HP signal generator (990MHz) (prev. setting 32.7MHz / +3dBm)
Black glass beam dump
Dmass:
LB1005 Oct 24.
|
|
221
|
Tue Feb 3 18:23:49 2015 |
Koji | General | General | Item lending |
- The laser was removed and shipped to LHO today.
- UV illuminator / fused silica fiber light guide / UV power meter / UV face shield (Qty 2) will be shipped to MIT.
They are CIT properties except for the illuminator.
Quote: |
Gabriele:
PZT HV Amp
Evan:
HP signal generator (990MHz) (prev. setting 32.7MHz / +3dBm)
Black glass beam dump
Dmass:
LB1005 Oct 24.
Quote: |
Tara: Laser Safety goggle -> Returned
Evan:
HP signal generator (990MHz) (prev. setting 32.7MHz / +3dBm)
Black glass beam dump
Dmass:
LB1005 Oct 24.
|
|
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222
|
Wed Feb 4 20:07:24 2015 |
Koji | General | General | Item lending |
Shipment to MIT (L. Barsotti, J. Miller)
1. UV Illuminator (LESCO Super Spot MK III)
2. UV Power meter (American Ultraviolet AIB1001) Caltech property C30140
3. UV protection face shield (VWR UVC-803) Qty.2 Caltech property C30141/C30142
4. UV Fiber Optic Light Guide (American Ultraviolet OLB1081) C30143
All returned: Aug 30, 2016 |
Attachment 1: C30140_1.JPG
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Attachment 2: C30140_2.JPG
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Attachment 3: C30141.JPG
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Attachment 4: C30142.JPG
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Attachment 5: C30143.JPG
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223
|
Wed Feb 18 21:51:23 2015 |
Koji | General | General | Notes on OMC Transportation Fixtures & Pelican |
LLO has one empty OMC transportation fixture.
LHO has one empty OMC transportation fixture.
LHO has one OMC transportation fixture with 3IFO OMC in it.
LHO has the Pelican trunk for the OMC transportation. Last time it was in the lab next to the optics lab. |
226
|
Tue Jul 21 20:20:12 2015 |
Koji | General | General | Item lending |
Kate (ATF)
- 4ch color oscilloscope (Tektronix)
- Chopper controller
- Chopper with a rotating disk
|
235
|
Thu Aug 20 01:35:01 2015 |
Koji | Electronics | General | OMC DCPD in-vacuum electronics chain test |
We wanted to know the transimpedance of the OMC DCPD at high frequency (1M~10M).
For this purpose, the OMC DCPD chain was built at the 40m. The measurement setup is shown in Attachment 1.
- As the preamp box has the differential output (pin1 and pin6 of the last DB9), pomona clips were used to measure the transfer functions for the pos and neg outputs individually.
- In order to calibrate the measurements into transimpedances, New Focus 1611 is used. The output of this PD is AC coupled below 30kHz.
This cutoff was calibrated using another broadband PD (Thorlabs PDA255 ~50MHz).
Result: Attachment 2
- Up to 1MHz, the transimpedance matched well with the expected AF transfer function. At 1MHz the transimpedance is 400.
- Above 1MHz, sharp cut off at 3MHz was found. This is consistent with the openloop TF of LT1128.
|
Attachment 1: OMC_DCPD_Chain.pdf
|
|
Attachment 2: OMC_DCPD_Transimpedance.pdf
|
|
236
|
Wed Aug 26 11:31:33 2015 |
Koji | Electronics | General | OMC DCPD in-vacuum electronics chain test |
The noise levels of the output pins (pin1/pin6) are measured. Note that the measurement is done with SE. i.e. There was no common mode noise rejection. |
Attachment 1: OMC_DCPD_OutputNoise.pdf
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|
239
|
Sun Sep 6 16:50:51 2015 |
Koji | Electronics | General | Unit test of the EOM/AOM Driver S1500118 |
TEST Result: S1500118
Additional notes
- Checked the power supply. All voltages look quiet and stationary.
- Checked the internal RF cables too see if there is any missing shield soldering => Looked fine
- Noticed that the RFAM detector board has +/-21V for the +/-24V lines => It seems that this is nominal according to the schematic
- Noticed that the RFAM detector sensitivity were doubled fomr the other unit.
=> This is reated to the modification (E1500353) of "Controller Board D0900761-B Change 1" (doubling the monitor output gain)
- Noticed that the transfer function of the CTRL signal on the BNC and the DAQ output.
=> This is reated to the modification (E1500353) of "Servo Board D0900847-B Change 1" (servo transfer function chage)
=> The measured transfer function did not agree with the prediction from the circuit constants in this document
=> From the observation of the servo board it was found that R69 was not 200Ohm but 66.5 Ohm (See attachment 1).
This explained the measured transfer function. The actuator TF has: P 2.36, Z 120., K -1@DC (0.020@HF)
- Similarly, the TF between the CTRL port on the unit and the CTRL port on the test rig was also modified.
Noise level
Attachment 2
- The amplitude noise in dBc (SSB) was measured at the output of 27dBm. From the test sheet, the noise level with 13dBm output was also referred. From the coherence of the MON1 and MON2, the noise level was inferred. It suggests that the floor level is better than 180dBc/Hz. However, there is a 1/f like noise below 1k and is dominating the actual noise level of the RF output. Daniel suggested that we should check nonlinear downconversion from the high frequency noise due to the noise attenuator. This will be check with the coming units. |
Attachment 1: P9037810.JPG
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Attachment 2: RF_AM_spectra.pdf
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249
|
Tue Dec 29 12:15:46 2015 |
Koji | General | General | Glasgow polarizer passed to Kate |
The Glasgow polarizer was passed to Kate on Dec 17, 2015. |
262
|
Fri Jul 22 22:24:05 2016 |
Koji | General | General | HQEPD inventory |
As of Jul 22, 2016
As of Aug 11, 2016
As of Aug 16, 2016
A1-23 in Cage G https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-A1-23
-> Shipped to LLO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8181
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-1
= Replaced C30665 eLIGO PD (SN 01 in Cage G now) ICS: C30665GH-0-00-0001
-> Removed PD@LLO, Waiting for the shipment to CIT
A1-25 in Cage G https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-A1-25
-> Shipped to LLO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8181
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-1
= Replaced C30665 eLIGO PD (SN 02 in Cage G now) ICS: C30665GH-0-00-0002
-> Removed@LLO, Waiting for the shipment to CIT
B1-01 in Cage A https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-B1-01
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-3_2
= replaced C30665 eLIGO PD (SN 11 in Cage A now) ICS: C30665GH-0-00-0011
-> Removed PD@LHO
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8187
B1-16 in Cage A https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-B1-16
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-3_2
= replaced C30665 eLIGO PD (SN 12 in Cage A now) ICS: C30665GH-0-00-0012
-> Removed PD@LHO
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8187
C1-05 in Cage F https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-05
-> @CIT contamination test cavity
C1-07 in Cage F https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-07
-> @CIT contamination test cavity
C1-17 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-17
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Left @LHO as a spare
C1-21 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-21
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Left @LHO as a spare
D1-08 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-D1-08
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Moved to Cage A3
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8186
-> Arrived at CIT (Aug 16)
D1-10 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-D1-10
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Moved to Cage A4
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8186
-> Arrived at CIT (Aug 16) |
264
|
Mon Aug 15 10:09:10 2016 |
Koji | General | General | Prev H1 OMC shipped to CIT |
Previous H1 OMC shipped from LHO to CIT
https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8196 |
265
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Mon Aug 22 12:58:16 2016 |
Koji | General | General | UV bond samples -> Garilynn |
- FS base + Mounting Prism
- FS or SF2 1/2" piece + FS or SF2 1/2" piece
- FS? plate + FS or SF2 1/2" piece + FS or SF2 1/2" piece + FS? plate |
268
|
Fri Sep 9 14:34:31 2016 |
Koji | General | General | Item lending |
To 40m
First Contact Kit by Calum
Class A Kapton sheets
|
269
|
Fri Sep 9 19:43:32 2016 |
Koji | Optics | General | D1102211 OMC Diode Mount Glass Block went to Downs |
D1102211 OMC Diode Mount Glass Block (11pcs) have been given to Calum@Downs |
270
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Mon Nov 21 21:19:20 2016 |
Koji | Optics | General | LWE NPRO Laser / Input Optics / Fiber Coupling |
- About 1.5 month ago, an 700mW LWE NPRO has been brought to OMC Lab.
- The SOP can be found here.
- The base was made for the beam elevation of 3" height. Four 1" pedestals were attached to rise the beam elevation to 4".
- The output from the laser is ~740mW
- After the faraday and the BB EOM, the output is ~660mW
- After the usual struggle, the beam was coupled to the SM fiber. The output is 540mW. The coupling efficiency is >80%.
- Will proceed to the OMC cavity alignment. |
271
|
Wed Dec 7 19:18:10 2016 |
Koji | Optics | General | LWE NPRO Laser / Input Optics / Fiber Coupling |
FIber Input Mount 132deg
Fiber output mount 275deg
-> 525mW P: 517mW S: 8mW extinction ratio: 0.016 |
272
|
Wed Dec 7 21:18:35 2016 |
Koji | General | General | OMC placed on the table / the beam roughly aligned |
The OMC mode matching sled was fixed on the nominal part of the table. Then the OMC was located at the nominal position marked by three poles.
The input periscope was adjusted to have the input beam roughtly centered on the OMC QPDs. This made the beam from FM2 aligned to the missing CM1, and the beam just went through the hole of the mounting prism. Very promising!
I wanted to use the new (modified) mirror gluing fixture to hold a curved mirror on the mounting prism. It turned out that the fixture was neither cleaned nor assembled. I will ask Downs Team to help me to get the cleaned and assembled fixtures.
Meanwhile, I just reused the original gluing fixture upside down in order to proceed cavity alignment and locking. (Attachment 1)
In fact, once the mirror is placed on the mounting prism, the cavity started to flash without further alignment. I thank for the very precise (repeatable) alignment of the OMC optics and PD/QPDs.
The next steps are initial cavity locking, more alignment, and mode matching. |
Attachment 1: DSC_0082.jpg
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Attachment 2: DSC_0084.jpg
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Thu Dec 8 21:17:09 2016 |
Koji | General | General | OMC placed on the table / the beam roughly aligned |
The OMC cavity was locked. The alignment was precisely adjusted. The mode matching was optimized by the lens positions. The reflection during the lock is ~0.01 compared to the full reflection on non-resonance, meaning the mode matching is ~99%. The error signal was maximized (i.e. demod pahse was adjusted) by sweeping the modulation frequency. Note that the EOM is broad band. The modulation freq chosen today was 34.6MHz.
Some notes:
- The error signal has not been preamplified at all yet. Because of this, the reflection is very much sensitive to the input offset.
- The OMC needs wind shield to prevent from the noise caused by air turbulance.
- The laser PZT was actuated via the Thorlabs HV amp. Otherwise, the thermal path needs to be configured.
- One of the CCD monitor is dead. Needs more replacement.
- All the electronics should be moved to the rack. This required long BNC and SMA cables.
- The optical table needs cleaning. |
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Thu Jan 19 20:57:53 2017 |
Koji | Supply | General | Purchase |
Ordered:
Office Depot
v AA battery Qty. 24
v 9V battery Qty. 4
v Floor cable cover (6ft)
Thorlabs
v HV PZT Driver
v Lenses |
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Thu Feb 16 17:23:12 2017 |
Koji | Supply | General | Purchase |
- BNC Patch Panel
- 8x Amphenol Connex 112443 / Isolated BNC FEMALE TO FEMALE BULKHEAD ISOLATED ADAPTER - 50 ohm
- 4x Amphenol RF 31-4803-75 (75Ohm)
- 2x Handle HAMMOND 98H1240
- SMA Patch Panel
- 8x Isolated SMA-SMA adapter
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Fri Jun 23 01:58:11 2017 |
Koji | Optics | General | OMC #002 Repair - CM1 gluing |
[Alena, Koji]
Jun 21: Alena and Koji worked on gluing of the CM1 mirror on the OMC breadboard #002. This is an irregular procedure. Usually, the PZT mirror subassembly is prepared before the mounting prism is glued on the breadboard. In this occasion, however, a PZT and a mirror are bonded on an existing prism because only the damaged mirror and still functional PZT were debonded from the mouting prism.
For this purpose, the mirror and the PZT were fixed on the mounting prism with the modified fixture set (D1600338). The original PZT was reused, and the new mirror #8 was used. The alignment of the mirror was checked OK using the cavity beam before any glue was applied. The arrow of the CM mirror is facing up.
We mixed 8g EP30-2 (it was almost like 3~4 pushes) and 0.4g glass sphere bond lining. Along with EP30-2 procedure, the bond was mixed in an Al pot and tested with 200degF (~93degC) preheated the oven for 15min. The cured bond showed perfect dryness and crispness. The bond was painted on the PZT and the PZT was placed on the fixture. Then more bond was painted on the other side of the PZT. The mirror was placed in the fixture. The spring-loaded front plate was fixed, and the breadboard was left for a day. (Attachment 1~3)
Jun 22: The fixture was removed without causing any visible delamination or void. The attachment 4~6 show how wet the joint is (before baking). There were some excess of EP30-2, which bonded the fixture and the mounting prism as usual. The fixture was detached by prying the front piece against the rear piece with a thin allen key. Some of the excess bond on the mounting prism was removed by scratching.
The alignment of the cavity was checked with the cavity beam and it is still fine.
More photos can be found here: Link to Google Photos Album "OMC #002 Repair - CM1 gluing" |
Attachment 1: IMG_0857.JPG
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Attachment 2: IMG_0859.JPG
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Attachment 3: IMG_0860.JPG
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Attachment 4: IMG_0865.JPG
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Attachment 5: IMG_0868.JPG
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Attachment 6: IMG_0864.JPG
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Fri Jun 23 10:55:07 2017 |
Koji | Optics | General | Dust layer on black glass beam dumps? |
I wondered why the black glass beam dumps looked not as shiny as before. It was in fact a layer of dusts (or contaminants) accumulated on the surface.
The top part of the internal surface of the black glass was touched by a piece of lens tissue with IPA. The outer surface was already cleaned. IPA did not work well i.e. Required multiple times of wiping. I tried FirstContact on one of the outer surface and it efficiently worked. So I think the internal surfaces need to be cleaned with FC. |
Attachment 1: black_glass_dust.JPG
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Sat Jul 1 15:29:57 2017 |
Koji | Optics | General | Black glass cleaning / Final bonding for the emergency repair for OMC #002 |
[Alena, Koji]
Report of the work on June 30.
1. Cleaning of the black glass beam dumps
As reported in the previous entry, the beam dumps on the OMC breadboard exhibited accumulation of dusts or contaminants on the black glass surfaces. We worried about transfer of the dusts over a period or of the contaminant during baking. It was already known that the contaminants are persistent and not easy to remove only by drag wiping with IPA. So Alena brought a set fo tools to try. Here is the procedure described.
- Inventory (Attachment 1): A small glass beaker, TX715 Alpha® Sampling Swab, plastic brushes, syringes with pure IPA, inspection flash light, Vectra IPA soaked wipes
- Apply clean IPA on a brush. Some IPA should be removed by the IPA soaked wipe so as not to splash IPA everywhere. Rub a glass surface with the brush while the surface is inspected by the flash light. The strokes migrate the contaminants to the direction of wiping. So the brush should be moved outward. This does some cleaning, but it is not enough to remove smudges on the surface. Occasionally clean the brush with IPA poured in the small beaker.
- Apply clean IPA on a swab. Rub the surface with the swab outward. This removes most of the visible smudges.
We decided not to apply FirstContact on the beam dumps at this occasion. In any case, we need to apply FC on all the optical surfaces after the baking. We judged that the current cleanliness level of the beam dump does not affect the over all contamination of the OMC considering the FC application after the baking.
2. Gluing of the reinforcement Al bars on the delaminated Invar mounting brackets
One of the mounting bracket (=invar shim) on the top side (= suspension I/F side) showed the sign of delamination (Attachment 3). This invar is the one at the beam entrance side (Attachment 2).
EP30-2 was mixed as usual: 6g of EP30-2 was mixed with 0.3g glass sphere. The glue was tested with a cooking oven and the result was perfect. The glue was applied to two Al bars and the bars were attached on the long sides of the invar shim with the beveled corner down (to avoid stepping on the existing original epoxy) (Attachments 4, 5). The photo quality by my phone was not great. I will take better photos with a better camera next week.
Glue condition was checked on Monday Jul 3rd. It was all good. New photos were taken. OMC #002 Repair - Gluing of reinforcement AL bars |
Attachment 1: DSC_0347.jpg
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Attachment 2: DSC_0348.jpg
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Attachment 3: DSC_0350.jpg
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Attachment 4: DSC_0352.jpg
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Attachment 5: DSC_0354.jpg
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Sat Jul 1 21:33:18 2017 |
Koji | General | General | Some purchase notes |
- Forgot to close the cylinder valve...
v HEPA prefilter (20"x20"x1" MERV 7)
- Replace the filter for the air conditioning
v Texwipe TX715 SWAB http://www.texwipe.com/store/p-817-tx715.aspx
v Gloves ~3 bags
VWR GLOVE ACCTCH NR-LTX SZ7.0 PK25 79999-304 x3
VWR GLOVE ACCTCH NR-LTX SZ7.5 PK25 79999-306 x1
v Vectra IPA soaked cloths
v Sticky mats
- GLOVE ACCTCH NR-LTX SZ7 PK25 / 79999-304 / PK4
- GLOVE ACCTCH NR-LTX SZ7.5 PK25 / 79999-306 / PK1
- WIPER 100% IPA 23X23CM PK50. / TWTX8410 / PK2
- SWAB CLEANTIPS ALPHA PK100. / TW-TX715 / PK1
- MAT CLEAN ROOM 18X36IN BLUE / 89021-748 / CS1 (Qty4)
- FILTER PLET AIR MERV8 20X20X1 / 78002-422 / EA4 / Direct from Supplier
ORDERED AUG 9, 2017 |
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Wed Jul 5 16:59:44 2017 |
Koji | General | General | The OMC #002 was packed |
[Stephen Koji]
The OMC #002 was packed for the transportation to Downs.
===> And transported to Downs 227 on Jul 6th. |
Attachment 1: DSC_0360.JPG
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Fri Sep 8 15:14:05 2017 |
Koji | Facility | General | Preparation for the plumbing work |
[Steve, Aaron, Koji]
We've finished the preparation for the forthcoming plumbing work on (nominally) Sept 16th Saturday.
We've covered most of the west side of the OMC lab with plastic sheets and wraps.
Some tips:
- The plastic sheets Eric gave us were a bit too thin and pron to got torn. Thicker sheets are preferable.
- The blue tape that Eric gave us was very useful.
- The stretch wrap film, which I bought long time ago, was so useful. Office Depot "Office Depot(R) Brand Stretch Wrap Film, 20 x 1000 Roll, Clear" PN: 445013
- We also used patches of Kitchen Trash Bags to cover some small opening of the large sheets. Office Depot "Glad(R) Tall Kitchen Trash Bags, 13 Gallon, White, Box Of 28" PN 269268
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Attachment 1: DSC_0405.jpg
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Attachment 2: DSC_0406.jpg
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Attachment 3: DSC_0407.jpg
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Attachment 4: DSC_0408.jpg
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Attachment 5: DSC_0409.jpg
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Attachment 6: DSC_0410.jpg
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Attachment 7: DSC_0411.jpg
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Mon Nov 27 20:24:24 2017 |
Koji | General | General | A former LHO PD (Trans) removed from the OMC #002 for the shipment to Stockholm |
Attachment 1: The PD was removed from the transmission side of the OMC #002 (former LHO OMC - the one blasted by the optical pulse in Aug 2016).
It was confirmed that the PD has the scribing mark saying "A".
Attachment 2: This diode had no glass cap on it. The photodiode sensitive element is still intact. For ease of handling, it should be kept in a cage. There are four cages in the OMC lab, but they are ocuppied with the High QE PDs and others. So, the cage for this PD was offered by Rich from his office, meaning the cage was not clean.
Attachment 3: The sensor side is capped by a plate. This cap can be removed by unscrewing the two cap screws in the photo.
Attachment 4: The PD legs are shorted. (Just to match the style with the LLO one).
Attachment 5: Wrapped with AL foil and double bagged. (Repeat: It is not anything clean.)
Attachment 6: The bag was left on Rich's desk. |
Attachment 1: IMG_2826.JPG
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Attachment 2: IMG_2835.JPG
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Attachment 3: IMG_2833.JPG
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Attachment 4: IMG_2836.JPG
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Attachment 5: IMG_2837.JPG
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Attachment 6: DSC_0546.JPG
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Thu Nov 30 12:18:41 2017 |
Stephen | General | General | Preparation for Modal Testing on 4 December |
Norna Robertson, Stephen Appert || 29 Nov 2017, 2 pm to 4 pm || 227 Downs, CIT
We made some preparations for modal testing, but did not have enough time to make measurements. Below is an after-the-fact log, including some observations and photos of the current state of the OMC bench.
- Previous testing results at T1700471 (technical note in progress as of 30 Nov 2017).
- One goal of the next round: add damping material to equate with damping material of T1600494.
- Second goal of the next round: use a more localized sweep to better resolve the body mode around 1080 Hz -1100 Hz
- Transport Fixture was opened without issue, revealing the "Top" (suspending and cable routing) surface of the bench. Damping stacks were still in place from previous testing
- We removed the bolts from the damper stacks, but found that all masses with metal-viton interfaces had adhered to viton washers, causing the stacks to stick together.
- By using an allen key as a lever to wedge apart bottom mass and the bracket where they were joined by a viton washer, we separated the masses from the bracket.
- An allen key was used as a lever to push apart the two masses, which were also joined by a viton washer
- Once exposed, viton washers were pried from metal surfaces.
- After the damper stacks had been detached from the No viton washer appeared to leave any residue or particulate - the separated parts all appeared as clean as they had been at the onset.
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Sat May 5 22:51:04 2018 |
Koji | Optics | General | 3IFO EOM Optical test |
The 3IFO EOM test performed at the 40m. Result: 40m ELOG 13819 |
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Tue May 15 19:53:45 2018 |
Koji | Optics | General | EOM Q comparison |
Qs' were estimated with a lorentzian function (eye fit)
 = \frac{A/Q}{\sqrt{(1-(f/f_0)^2)^2+(f/f_0/Q)^2}})
Current LHO EOM (final version, modulation depth measurement 2018/4/5)
f0=9.1MHz, Q=18
f0=45.38MHz, Q=46
f0=118.05MHz, Q=30
Prev LHO EOM (RF transmission measurement 2018/4/13)
f0=9.14MHz, Q=53
f0=24.25MHz, Q=55
f0=45.565MHz, Q=62;
3IFO EOM (RF transmission measurement 2018/4/23)
f0=8.627MHz, Q=53
f0=24.075MHz, Q=60
f0=43.5MHz, Q=65 |