After checking the PMC servo card,
ramp signal goes to ext DC
HV in is applied properly,
HV out is fixed.
Now the PMC is scanning and working fine.
The alignment is done. Although optimization is still needed, I can work on the rest of the setup.
*note on PMC servo card
Ratio between Voltage input (Vin), V monitor (Vmon), and High Voltage output (HVout),
HVout = 24 Vin
Vmon = 1/50 HVout
Vmon = 24/50 Vin
see the attachment