ID |
Date |
Author |
Type |
Category |
Subject |
11048
|
Wed Feb 18 19:06:40 2015 |
Koji | Update | LSC | ALS Fool impulse response |

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11041
|
Tue Feb 17 00:24:47 2015 |
rana, jenne | Update | LSC | ALS Fool filter updated for more cancellation |
Today we measured the TFs again and then updated the filter in the POY -> ALS FF path so as to get 10x better cancellation.

The cancellation went from ~10 dB to ~30 dB. This seems good enough. The new filter 'Comp1' is just constructed by eye. We then had to tune the filter module gain to a few %. Seems good enough for now, but we should really try to understand what it is and why it is the way that it is. In the above plot, the ORANGE trace is the old cancellation and the GREEN one is the new one. The filter TF is attached below - its not special, we made it by presing buttons in FOTON until the TF matched the measured TF of ALSY/LSC-MC_CTRL_FF_OUT.

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Attachment 1: ALSfoo_150216.png
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Attachment 2: 15.png
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11484
|
Thu Aug 6 11:45:01 2015 |
Jessica | Update | General | ALS Delay Line front panel testing |
Koji had suggested that I sync up the two function generators to ensure that they have the same base frequency and so that crosstalk will actually appear at the expected frequency. After syncing up the two function generators, I drove the following frequencies through each cable:
Conductive SMAs:
X: 29.537 MHz Y: 29.5372 MHz
Isolated SMAs:
X: 29.545 MHz Y: 29.5452 MHz
Each time, the difference between the frequencies was 200 Hz, so if there was crosstalk, a spike should appear in the PSDs at 200 Hz when frequencies are being driven through both cables simulataneously, but not when just one is on. We very clearly see a spike at 200 Hz in both the X arm and the Y arm with the conductive SMAs, indicating crosstalk. For the front panel with isolated SMAs, we see a spike at 200 Hz when both frequencies are on, but it is much less pronounced than with the conductive SMAs. It seems as though there will be crosstalk using either panel, just less with the isolated SMAs. |
Attachment 1: conductive_X.png
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Attachment 2: conductive_Y.png
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Attachment 3: isolated_X.png
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Attachment 4: isolated_Y.png
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11471
|
Thu Jul 30 18:58:36 2015 |
Jessica | Update | General | ALS Delay Line Box Front Panel Testing |
I tested both of the front panels (conductive and isolated SMAs) with the ALS Delay Line Box by driving extremely close frequencies through the cables. By doing this, we would expect that a spike would show up in the PSD if there was crosstalk between the cables.
In the plots below, for the conductive panel, the frequencies used were
X Arm: 22.329 MHz Y Arm: 22.3291 MHz
For the isolated panel, the frequencies were
X Arm: 22.294 MHz Y Arm: 22.2943 MHz
This gives a difference of 100 Hz for the conductive panel and 300 Hz for the isolated panel. Focusing on these areas of the PSD, it can be seen that in the Y Arm cable there is a very clear spike within 30 Hz of these differences when frequencies are being driven through both cables as opposed to the signal being in only the Y Arm. In the X Arms, the noise in general is higher when both cables are on, but there is no distinct spike at the expected frequencies. This indicates that some sort of crosstalk is probably happening due to the strong spikes in the Y Arm cables.
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Attachment 1: Xarm_diff.png
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Attachment 2: Yarm_diff.png
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Attachment 3: Xarm_isolated.png
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Attachment 4: Yarm_isolated.png
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11440
|
Thu Jul 23 20:54:42 2015 |
Jessica | Update | General | ALS Delay Line Box |
The front panels for the ALS delay line box came in last week. Some of the holes for the screws were slightly misaligned, so I filed those and everything is now put together. I just need to test both front panels to determine if the SMAs should be isolated or not.
Koji had also suggested making the holes in the front and back panel conical recesses so that flat head screws could be used and would counteract the anodization of the panel and avoid the SMAs being isolated. I think if we did that then conductivity would be ensured throughout the panel and also through the rest of the box. I also think one way we could test this before drilling conical recesses would be to test both front panels now, as one has isolated SMAs and one has conductive SMAs. If the anodization of the panel isolated the SMA regardless, we could potentially figure this out by testing both panels. But, would it also be that it is possible that the isolation of the SMA itself does not matter and so this test would tell us nothing? Is there a better way to test if the SMAs are being isolated or not? Or would this be more time consuming than just drilling conical recesses as a preventative measure? |
10396
|
Thu Aug 14 22:58:59 2014 |
rana, jenne | Summary | Green Locking | ALS DIFF tuning |
We've been having trouble tuning the ALS DIFF matrix. Trying to see if the MC2 EXC can be cancelled in ALS DARM by adjusting the relative gains in ALSX and ALSY Phase Tracker outputs.
There's a bunch of intermittent behavior. Between different ALS locks, we get more or less cancellation. We were checking this by driving MC2 at ~100-400 Hz and checking the ALS response (with the ALS loops closed). We noticed that the X and Y readbacks were different by ~5-10 degrees and that we could not cancel this MC2 signal in DARM by more than a factor of 4-5 or so. In the middle of this, we had one lock loss and it came back up with 100x cancellation?
Attached is a PDF showing a swept sine measurement of the ALSX, ALSY, and DARM signals. You can see that there is some phase shift between the two repsonses leading to imperfect cancellation. Any ideas? Whitening filters? HOM resonance? Alignment? |
Attachment 1: sweep.pdf
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17374
|
Fri Dec 30 11:38:45 2022 |
Paco | Summary | Calibration | ALS Calibration errors -- single arm actuation |
Here are my thoughts on calibration errors. This applies to the single arm actuation calibration, but may easily be extended to calibrate the DARM residual noise for example.
According to the math in this post, there are four parameters whose estimates build the total calibration uncertainty: arm length, wavelength, loop gain, and beatnote fluctuation. Below is a table for how each is measured, what the sources of statistical versus systematic error are, how large each relative contribution roughly is, and how we may improve on them.
|
Arm Length |
Wavelength |
ALS beat fluctuation |
AUX Loop gain |
Current Estimate |
FSR scan using ALS, reference to POX/POY (11 MHz) sideband. |
NPRO Specification |
DFD + Phase tracker |
Swept sine |
Statistical error |
Limited by scan range (e.g. DFD range) and resolution. |
No statistical error from specification |
Shot noise limited measurement ? |
Bendat Piersol Table 9.6 (depends on coherence) |
Systematic error |
Limited by freq reference offsets (Marconi), and residual POS-PIT coupling |
NPRO half tuning range |
Flicker noise (electronics, other) |
Swept sine bias and servo drift (thermal, flicker) |
Improvements |
More FSRs per scan at best possible resolution |
Iodine spectrsocopy |
Lower ALS residual frequency noise |
Higher AUX servo gain |
Arm length
Statistical
The arm length has been estimated before by locking the arm with the ALS beat, scanning the arm length and looking at the IR resonances. From the statistical uncertainty standpoint the limit seems to be number of measurable FSRs. Using these numbers, the statistical uncertainty comes to ~ 0.6%. Other attempts claim to have improved on this by almost an order of magnitude giving ~ 0.02%. Simply scanning over more FSRs should improve this as the usual square root number of measurements statistical error reduction.
Systematic
Systematic error comes from the frequency referenced on this measurement (the Marconi 11 MHz sideband oscillator), nonlinearities in the mostly linear scan (e.g. POS to PIT coupling). I think it's safe to neglect frequency offsets > 1 Hz because of the Rb clock reference and the Marconi's own calibration. I'm not sure about the POS to PIT coupling magnitude and whether F2A filters are helping here, but offset scan nonlinearities should distort the FSR nonuniformly and this error may have sneaked into the statistical estimate above. From the posts referenced above, the scan result seems extremely linear, but repeating the measurement and plotting the residuals may give an accurate estimate of the nonlinearity. I think either of the systematic errors discussed here should be below or around the ppm (0.0001%) level, but this should be confirmed.
Wavelength
Statistical
If we use the NPRO specification Mephisto's wavelength is 1064 nm and there is no statistical error.
If on the other hand we do iodine absorption spectroscopy, we may be able to see ~ 4 lines throughout the 30 GHz tuning range of the NPRO. Fun fact: 30 GHz correspond to 1 cm-1 (inverse centimeter). Assuming we can scan our laser with a 0.01 cm-1 resolution, it may be possible to estimate the absolute wavelength to 10 better than any line center. The ATLAS of iodine spectroscopy gives strong absorption lines around 532 nm to 0.001 cm-1, or 0.00001% accuracy. A simple Doppler broadened absorption should improve this further.
Systematic
If we use the NPRO specification the systematic error comes from the number of known significant figures ~ 0.047 %. A slightly better estimate comes from the Prometheus model with a frequency doubled output hitting near the P 83(33-0) line of iodine, at 18787.814 cm-1. This gives a nominal wavelength of 532.259 nm, or 1064.518 nm on the seed. Because the tuning range is 30 GHz, our systematic error may be +0.03 nm - 0.07 nm from 1064.52 nm. Taking the median of 0.05 nm, the relative systematic error from the Nd:YAG specification is 46.9 ppm = 0.0047%.
If on the other hand we do iodine spectroscopy, the systematic error will be dominated by the residual shifts on the iodine vapor, which are negligibly small compared to the Doppler broadened lines. They might add sub-ppm uncertainty to the absolute calibration.
Beat fluctuations
Statistical
The error in estimating beatnote fluctuations is statistically dominated if our beat detection is shot noise limited for example. Other stationary noises with power law spectra decaying faster than 1/f are subject to this effect. The allan deviation discriminates the timescales at which our measurement is dominated by statistical error. Currently our calibration lines have SNR of 10 to 100. Averaging seems to be limited to ~ 100 second timescales, so the statistical error on these measurements is ~ 0.1 to 1.0 %.
Systematic
As suggested in the above, the allan deviation discriminates the statistical dominated timescales for this measurement. There is a correspondence between noise spectra and allan deviation, so we should be able to point out what noises contribute to systematic drift in our ALS noise budget.
Loop gain
Statistical
Invoking Bendat and Piersol, Table 9.6 gives the statistical estimate of loop gain estimate with coherence gamma, and n_avg number of averages. Because of our resonant OL gain filters, assuming G ~ 100 there, and high coherence on the OLTF measurement so gamma ~ 0.9, with 12 averages we should get a relative loop gain error of 9.8%.
Systematic
Also from B&P, we should estimate how biased our TF is. This depends on delays, bandwidths, measurement device noises, etc. Furthermore, the analog electronics in the AUX servo should drift, but we neglect this contribution for now. A simple bias estimate (eq 9.75) tells us that the coherence is biased by the number of averages such that in our estimate above the unbiased coherence is roughly 0.897. This means our systematic contribution from TF bias is ~ 0.17 %.
We should remember that in the case of loop gain, the total error (systematic + statistical) gets an extra suppression factor of the order of the loop gain itself. Radhika's resonant digital gain filters should easily allocate 40 dB (or ~ 100) on every calibration line such that our total calibration error drops to the 0.1% level.
Conclusions
- The main calibration error (at the 1% level) seems to be from the ALS beat frequency. We can simply crank the SNR up, but we should work on the ALS relative stability. I think the low frequency end of the ALS residual frequency noise is currently limited by DFD... I wonder if we can improve on this by implementing a digital PLL (e.g. using a Moku)
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9872
|
Mon Apr 28 23:05:03 2014 |
Jenne | Update | LSC | ALS CARM and DARM settings |
[Jenne, Koji]
The IFO is being uncooperative tonight, and I have an early morning meeting, so I'm calling it a night.
Koji's filter module changes have been propagated from the Xarm to the Yarm, to CARM and to DARM. (Actually, Q overwrote the changes to Xarm on Sunday accidentally, so first he reverted those for us, and then we propagated the changes).
Today, with careful measuring, we find that for X and Y arms individually locked with the ALS, we want the gains to be +17 for the Yarm, and -17 for the Xarm (with the beatnote up-is-up convention). This puts the UGFs at 150 Hz.
We then switched over to CARM and DARM locking. We guessed that the gains should be a factor of 2 lower since we're pushing on both ETMs for DARM, and the MC2 actuator is roughly the same strength as the sum of the ETMs. In the end, after measuring the CARM and DARM loops, we find that the gains should be +7.5 for CARM, and +8.0 for DARM to set the UGFs at 150 Hz. The servo is a little bit delicate, so having too low of gain is not okay.
For some reason, we seem to be utilizing more actuator range with the new setup, so the limiters in the filter banks have been set to 11,000 (previously were 8,000), and the ALS watch script (ALSdown.py) threshold has been increased to 10,000 (previously 7,000).
When finding the IR resonances with the new scheme, we are having trouble holding lock throughout the scan. I have set the tramp for the coarse part of the scan to be 0.05 seconds (previously 0.01 seconds), which is an increase of a factor of 5 in the ramp time. This helps, but may still not be enough, since we don't always hold lock until both IR resonances are found.
Probably the most annoying thing from tonight is the fact that ETMY keeps drifting off, particularly in yaw, when locked. I don't have an explanation of why this is happening, but you can watch it happen sometimes, and the lock will be lost shortly thereafter. Definitely when we lose lock and the ETM gets kicked, it is far enough away in yaw alignment that I have to completely redo the Yarm alignment. This happens whether or not the ETMY oplevs are on.
To summarize, 3 scripts have been modified:
(1) ALSdown - threshold increased (Modification from last week - turns off the slow temp servos for the end lasers, clears histories)
(2) ALSfindIRresonance - increase ramp time
(3) Lock_ALS_CARMandDARM - final gain values set to 7.5 for CARM and 8 for DARM, no filters come on until gains all the way up, turns on new set of Koji filters. (Modification from last week - turns on the slow temperature servos for the end lasers) |
9702
|
Fri Mar 7 00:43:34 2014 |
manasa | Update | LSC | ALS C&D locked (on MC2 and ETMs) and IR resonance obtained |
[EricQ, Manasa]
ALS common locked by actuating on MC2 and ALS Differential locked by actuating on ETMX and ETMY (Stable lock acquired for over an hour). 
Common and Differential offsets were swept to obtain IR resonance in both the arms (arms stayed on resonance for over 15 minutes). 
Procedure:
1. Configured LSC settings to allow locking using ALS error signals.
2. Locked common and differential using ALS error signals
Aux matrix
ALSX ALSY
------------------------------
XARM 1 -1
YARM 1 1
-----------------------------
X arm servo settings:
FIlters: FM1, FM5, FM6, FM7, FM9
Gain = -8.0
Y arm servo settings:
Filters: FM1, FM5, FM6, FM7, FM9
Gain = +8.0
Out matrix
XARM YARM
------------------------
ETMX 1 0
ETMY 0 1
------------------------
3. Transitioned CARM control output to actuate on MC2 instead of ETMX
SUS-MC2_LSC servo gain = 1.0
The transition was done in very small steps : actuating on MC2 in -0.01 steps at the outmatrix upto -1.0 while reducing the ETMX actuation to 0 simultaneously.
DARM still stayed locked only with actuation on ETMY.
4. Transitioned DARM control to ETMX and ETMY.
Used ezcastep to step up DARM control (Y arm output) actuation on ETMX and step down the actuation on ETMY.
Final output matrix
Xarm Yarm
-----------------------
ETMX 0 -0.5
ETMY 0 0.5
MC2 -1.0 0
-----------------------
Noise plot in attachment.
5. Finding arm resonance
Used ezcastep to gradually build up offsets in CARM (LSC-XARM_OFS) to find IR resoance in one arm (Y arm).
Introducing a small (order of 0.5) DARM offset (LSC-YARM_OFS) shifted the Y arm off-resonance.
Used CARM offset to get back the Y arm to resonance.
Changing CARM and DARM offsets alternately while tracking the Y arm resonance got us to a point where we had both the arms resonating for IR.
6. At this point the MC decided to give up and we lost lock. 
Notes:
1. We found that the WFS2 YAW output filterbank had the output switched OFF (probably accidentally by one of us). This was reenabled. Please be careful while manually turning ON and OFF the MC WFS servos. |
Attachment 1: ALS_MC2CARM.pdf
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16333
|
Wed Sep 15 23:38:32 2021 |
Koji | Update | ALS | ALS ASX PZT HV was off -> restored |
It was known that the Y end ALS PZTs are not working. But Anchal reported in the meeting that the X end PZTs are not working too.
We went down to the X arm in the afternoon and checked the status. The HV (KEPCO) was off from the mechanical switch. I don't know this KEPCO has the function to shutdown the switch at the power glitch or not.
But anyway the power switch was engaged. We also saw a large amount of misalignment of the X end green. The alignment was manually adjusted. Anchal was able to reach ~0.4 Green TRX, but no more. He claimed that it was ~0.8.
We tried to tweak the SHG temp from 36.4. We found that the TRX had the (local) maximum of ~0.48 at 37.1 degC. This is the new setpoint right now. |
Attachment 1: P_20210915_151333.jpg
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9123
|
Wed Sep 11 23:34:37 2013 |
Masayuki | Summary | Green Locking | ALS locking in both arms |
[manasa, masayuki]
We locked the XARM and YARM with using ALS control loop and we succeeded to lock stably both arms. The performance of the ALS was tested with a measurement of the calibrated error signal. (attachment 1)
- red and blue : the in-loop noise of ALS of each arm.
- green and purple:Stability of the beat-note frequency with the MC and the arm freely running.
Discussion
In the high frequency region, YARM has larger noise than XARM, and these noises were not there in previous measurements by Koji and Manasa (elog8865). You can see that in both of in-loop noise and free running noise. These noises may be caused by the Green PDH servo or hte phase tracker servo or any other electrical staff. We will start noise budget of these servo.
At higher frequency than UGF of ASL control loop, the loop does not suppress the noises at all, but the inloop and free running noise are not equivalent. I have no idea about that so far.
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Attachment 1: noise.pdf
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9124
|
Wed Sep 11 23:43:10 2013 |
Koji | Summary | Green Locking | ALS locking in both arms |
What was the beat freq for each arm?
The HF noise level depends on the frequency of the beat note.
As the BBPD has the freq dependent noise level. (See this entry) |
9125
|
Thu Sep 12 00:07:26 2013 |
Masayuki | Summary | Green Locking | ALS locking in both arms |
Quote: |
What was the beat freq for each arm?
The HF noise level depends on the frequency of the beat note.
As the BBPD has the freq dependent noise level. (See this entry)
|
I'm not sure about the actual number of the beat frequency, but the beat frequency was almost same in both arms. And I took this measurement sometimes with slightly different beat frequency but the noise level didn't change so much. |
16614
|
Mon Jan 24 12:33:41 2022 |
rana | Configuration | Wiki | AIC Wiki: txz files allowed |
I updated the mime.local.conf file for the AIC Wiki so as to allow attachments with the .txz format. THis should be persistent over upgrades, since its a local file. |
14227
|
Wed Oct 3 18:15:34 2018 |
yuki | Configuration | ASC | AI board improvement |
[ Yuki, Gautam ]
I improved Anti-Imaging board (D000186-Rev.D), which will be put between DAC port and PZT driver board.
It had notches at f = 16.6 kHz and 32.7 kHz, you can see them in the plot attached. So I replaced some resistors as follows:
- R6 and R7 replaced with 511 ohm (1206 thin film resistor)
- R8 replaced with 255 ohm (1206 thin film resistor)
- R14 and R15 replaced with 549 ohm (1206 thin film resistor)
- R16 replaced with 274 ohm (1206 thin film resistor)
Then the notch moved to 65.9 kHz (> sampling frequency of DAC = 64 kHz, good!).
(The plot enlarged around the notch frequency and the plot of all channels will be posted later.)
All electronics and optics seem to be ready.
Reference, elog:40m/8857
Diagram, D000186-D.pdf |
Attachment 1: TF_AIboard.pdf
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14228
|
Thu Oct 4 00:44:50 2018 |
yuki | Configuration | ASC | AI board improvement |
[ Yuki, Gautam ]
I made a cable which connects DAC port (40 pins) and AI board (25 pins). I will check if it works.
Tomorrow I will change setup for improvement of AUX Y-end green locking. Any optics for IR will not be moved in my design, so this work doesn't affect Y-arm locking with main beam.
While doing this work, I will do:
- check if the cable works
- make another cable which connects AI board (10 pins) and PZT driver (10 pins).
- check if eurocate in Y-rack (IY4?) applies +/-5V, +/-15V and +/-24V. It will be done using an expansion card.
- improve alignment servo for X-end.
- setup alignment servo for Y-end.
- about optical loss measurement.
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7173
|
Tue Aug 14 11:33:14 2012 |
Jamie Alex Den | Update | CDS | AI and AA filters |
When signals are transmitted between the models running at different rates, no AI or AA filters are automatically applied. We need to fix our models.

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8857
|
Tue Jul 16 14:51:09 2013 |
gautam | Configuration | endtable upgrade | AI Board-D000186-Modified notches |
I tried shifting the notch frequencies on the D000186-revision D board given to me by Koji. The existing notches were at ~16 kHz and ~32 kHz. I shifted these to notches at ~64 kHz and ~128 kHz by effecting the following changes (see schematic for component numbering) on Channel 8 of the board-I decided to check things out on one channel before implementing changes en masse:
- R6 and R7 replaced with 511 ohm smts
- R8 replaced with 255 ohm smt
- R14 and R15 replaced with 549 ohm smts
- R16 replaced with 274 ohm smt
=> New notches should be at 66.3 kHz and 131.7 kHz.
I then measured the frequency response of the modified channel using the SR785, and compared it to the response I had measured before switching out the resistors. The SR785 only goes up to 102 kHz, so I cannot verify the 128 kHz notch at this point. The position of the 64 kHz notch looks alright though. I think I will go ahead and switch out the remaining resistors in the evening.
Note 1: These plots are just raw data from the SR785, I have not tried to do any sort of fitting to poles and zeros. I will do this at some point.
Note 2: All these smts were taken from Downs. Todd helped me locate the non-standard value resistors. I also got a plastic 25-pin D-sub backshells (the spares are in the rack), with which I have fashioned the required custom ribbon cables (40 pin IDC to 25 pin D-sub with twisted ribbon wire, and a short, 10pin IDC to 10pin IDC with straight ribbon wire).

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8875
|
Thu Jul 18 21:12:58 2013 |
gautam | Configuration | endtable upgrade | AI Board-D000186-All channels modified |
I carried some further modifications and tests to the AI Board. Details and observations here:
- I switched out the resistors for all the remaining 7 channels, using the same substitutions as detailed here.
- I then verified that the modified transfer function for all 8 channels using the SR785. I did not collect data for all the channels as netgpib was taking ages, but I did use the cursor on the screen to verify the position of the first notch at ~64 kHz. I noticed that all the channels did not have the lowest point of the notch at the same frequency. Rather, (at least on the screen), this varied between 63kHz and 67kHz. I would put this down to component tolerance. Assuming 5% tolerance shifts the theoretical notch frequency from 66268 Hz to 63112 Hz.
- After verifying the transfer functions, I went to 1Y4 and plugged the AI board into the eurocrate. I then connected the input of the AI board to the DAC output using my custom ribbon cable. Next, I used the excitation points set up earlier to send a 1 kHz, 32000 counts amplitude sine wave through the channels one at a time. I monitored the output using an oscilloscope and the LEMO monitor channels on the front panel of the board.
- I found that the single-ended output of the AI board swings between -10 V and 10 V (w.r.t ground, oscilloscope trace attached). This is good because this is the range of input voltage to the PZT driver boards required to realize the full actuation range of the PZTs.
- I also verified that the connections on the custom ribbon cable are correct (channel map was right) and that there were no accidental shorts (I checked other channels' output monitor while driving one channel).
I think the board is okay to be used now.

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16218
|
Tue Jun 22 11:56:16 2021 |
Anchal, Paco | Update | SUS | ADC/Slow channels issues |
We checked back in time to see how the BS and PRM OSEM slow channels are zero. It was clear that they became zero when we worked on this issue on June 17th, Thursday. So we simply went back and power cycled the c1susaux acromag chassis. After that, we had to log in to c1susaux computer and run
sudo /sbin/ifdown eth1
sudo /sbin/ifup eth1
This restarted the ethernet port acromag chassis is connected to. This solved this issue and we were able to see all the slow channels in BS and PRM.
But then, we noticed that the OPLEV of ITMX is unable to read the position of the beam on the QPD at all. No light was reaching the QPD. We went in, opened the ITMX table cover and confirmed that the return OPLEV beam is way off and is not even hitting one of the steering mirrors that brings it to the QPD. We switched off the OPLEV contribution to the damping.
We did burt restore to 16th June morning using
burtwb -f /opt/rtcds/caltech/c1/burt/autoburt/snapshots/2021/Jun/16/06:19/c1susaux.snap -l /tmp/controls_1210622_095432_0.write.log -o /tmp/controls_1210622_095432_0.nowrite.snap -v
This did not solve the issue.
Then we noticed that the OSEM signals from ITMX were saturated in opposite directions for Left and Right OSEMs. The Left OSEM fast channels are saturated to 1.918 um for UL and 1.399 um for LL, while both right OSEM channels are bottomed to 0 um. On the other hand, the acromag slow PD monitors are showing 0 on the right channels but 1097 cts on UL PDMon and 802 cts in LL PD Mon. We actually went in and checked the DC voltages from the PD input monitor LEMO ports on the ITMX dewhitening board D000210-A1 and measured non-zero voltages across all the channels. Following is a summary:
ITMX OSEM readouts
|
C1-SUS-ITMX_XXSEN_OUT
(Fast ADC Channels) (um) |
C1-SUS-ITMX_xxPDMon
(Slow Acromag Monitors) (cts) |
Multimeter measurements at input to Dewhitening Boards
(V) |
UL |
1.918 |
1097 |
0.901 |
LL |
1.399 |
802 |
0.998 |
UR |
0 |
0 |
0.856 |
LR |
0 |
0 |
0.792 |
SD |
0.035 |
20 |
0.883 |
We even took out the 4-pin LEMO outputs from the dewhitening boards that go to the anti-aliasing chassis and checked the voltages. They are same as the input voltages as expected. So the dewhitening board is doing its job fine and the OSEMs are doing their jobs fine.
It is weird that both the ADC and the acromags are reading these values wrong. We believe this is causing a big yaw offset in the ITMX control signal causing the ITMX to turn enough make OPLEV go out of range. We checked the CDS FE status (attachment 1). Other than c1rfm showing a yellow bar (bit 2 = GE FANUC RFM card 0) in RT Net Status, nothing else seems wrong in c1sus computer. c1sus FE model is running fine. c1x02 (the lower level model) does show a red bar in TIM which suggests some timing issue. This is present in c1x04 too.
Bottomline:
Currently, the ITMX coil outputs are disabled as we can't trust the OSEM channels. We're investigating more why any of this is happening. Any input is welcome.
|
Attachment 1: CDS_FE_Status.png
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16219
|
Tue Jun 22 16:52:28 2021 |
Paco | Update | SUS | ADC/Slow channels issues |
After sliding the alignment bias around and browsing through elog while searching for "stuck" we concluded the ITMX osems needed to be freed. To do this, the procedure is to slide the alignment bias back and forth ("shaking") and then as the OSEMs start to vary, enable the damping. We did just this, and then restored the alignment bias sliders slowly into their original positions. Attachment 1 shows the ITMX OSEM sensor input monitors throughout this procedure.
At the end, since MC has trouble catching lock after opening PSL shutter, I tried running burt restore the ioo to 2021/Jun/17/06:19/c1iooepics.snap but the problem persists |
Attachment 1: shake_and_damp.png
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13661
|
Wed Feb 28 19:13:25 2018 |
gautam | Update | ALS | ADC test for differential receiving in c1lsc |
[koji, gautam]
we did a bunch of tests to figure out the feasibility of the plan I outlined last night. Bottom line is: we appear to have a working 64 channel ADC (but with differential receiving that means 32 channels). But we need an aLIGO ADC adaptor card (I'm not sure of the DCC number but I think it is D0902006). See attached screenshot where we managed to add an ADC block to the IOP model on c1lsc, and it recognizes the additional ADC. The firmware on the (newly installed) working card is much newer than that on the existing card inside the expansion chassis (see Attachment #1).
Details:
- Watchdogged all optics because we expected messing around with c1lsc to take down all the vertex FEs. Actually, only c1sus was killed, c1ioo survived.
- Closed PSL shutter. Shut down c1lsc FE machine.
- Started out by checking the functionality of the two ADC cards I found.
- Turns out the one Jamie and I removed from c1ioo ~6months ago is indeed broken in some way, as we couldn't get it to work.
- Took us a while to figure out that we require the adaptor board and a working ADC card to get the realtime model to run properly. A useful document in understanding the IO expansion chassis is this one.
- Another subtlety is that the ADC card we installed today (photo in previous elog) is somewhat different from the ones installed in c1sus and c1lsc expansion chassis. But a similar one is installed at the Y-end at least. Point is, this ADC card seems to need an external power supply via a 4-pin Molex connector to work properly.
- We borrowed an adapter card from c1iscey expansion chassis (after first shutting down the machine).
- It seems like a RED GPIO0 LED on these ADC cards isn't indicative of a fault.
- Added an ADC part from CDS_PARTS library. Added an ADC selector bus and an "MADC" block that sets up the 64k testpoints as well as the EPICS readbacks.
- We were able to see sensible numbers (i.e. ~0 since there is no input to the ADC) on these readback channels.
- To restore everything, we first shutdown c1lsc, then restored the adaptor card back to c1iscey, and then rebooted c1iscey, c1lsc and c1sus. Recompiled c1x04 with the added ADC block removed as it would otherwise complain due to the absence of an adapter board.
- Did rtcds restart <model> on all machines to bring back all models that were killed. This went smoothly.
- IMC and Yarm locked smooth.
Note that we have left the working ADC card inside the c1lsc expansion chassis. Plan is to give Rolf the faulty ADC card and at the same time ask him for a working adapter board.
Unrelated to this work: we have also scavenged 4 pcs of v2 of the differential receiving AA board from WB EE shop, along with a 1U chassis for the same. These are under my desk at the 40m for the moment. We will need to re-stuff these with appropriate OpAmps (and also maybe change some Rs and Cs) to make this board the same as v6, which is the version currently in use. |
Attachment 1: c1lsc_ADCtest.png
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Thu Sep 6 14:21:26 2018 |
gautam | Update | CDS | ADC replacement in c1lsc expansion chassis |
Todd E. came by this morning and gave us (i) 1x new ADC card and (ii) 1x roll of 100m (2017 vintage) PCIe fiber. This afternoon, I replaced the old ADC card in the c1lsc expansion chassis, and have returned the old card to Todd. The PCIe fiber replacement is a more involved project (Steve is acquiring some protective tubing to route it from the FE in 1X6 to the expansion chassis in 1Y3), but hopefully the problem was the ADC card with red indicator light, and replacing it has solved the issue. CDS is back to what is now the nominal state (Attachment #1) and Yarm is locked for Jon to work on his IFOcoupling study. We will monitor the stability in the coming days.
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(i) to replace the old generation ADC card in the expansion chassis which has a red indicator light always on and (ii) to replace the PCIe fiber (2010 make) running from the c1lsc front-end machine in 1X6 to the expansion chassis in 1Y3, as the manufacturer has suggested that pre-2012 versions of the fiber are prone to failure. We will do these opportunistically and see if there is any improvement in the situation.
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Attachment 1: CDSoverview.png
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Fri Sep 7 12:35:14 2018 |
gautam | Update | CDS | ADC replacement in c1lsc expansion chassis |
Looks like the ADC was not to blame, same symptoms persist.
Quote: |
The PCIe fiber replacement is a more involved project (Steve is acquiring some protective tubing to route it from the FE in 1X6 to the expansion chassis in 1Y3), but hopefully the problem was the ADC card with red indicator light, and replacing it has solved the issue.
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Attachment 1: Screenshot_from_2018-09-07_12-34-52.png
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Mon Sep 10 12:44:48 2018 |
Jon | Update | CDS | ADC replacement in c1lsc expansion chassis |
Gautam and I restarted the models on c1lsc, c1ioo, and c1sus. The LSC system is functioning again. We found that only restarting c1lsc as Rolf had recommended did actually kill the models running on the other two machines. We simply reverted the rebootC1LSC.sh script to its previous form, since that does work. I'll keep using that as required until the ongoing investigations find the source of the problem.
Quote: |
Looks like the ADC was not to blame, same symptoms persist.
Quote: |
The PCIe fiber replacement is a more involved project (Steve is acquiring some protective tubing to route it from the FE in 1X6 to the expansion chassis in 1Y3), but hopefully the problem was the ADC card with red indicator light, and replacing it has solved the issue.
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Mon Aug 17 07:01:09 2009 |
Clara | Update | PEM | ADC noiseness |
I shorted the inputs on three channels and the outputs on three channels of the Guralp box, and I did similar things with the accelerometers. I was going to move the instruments themselves back, but I didn't have time, so they are still in the box in the corner. If the setup could stay as-is for at least a few hours, that would be awesome. |
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Wed Nov 8 16:39:24 2017 |
Kira | Update | PEM | ADC noise measurement |
Gautam and I measured the noise of the ADC for channels 17, 18, and 19. We plan to use those channels for measuring the noise of the temperature sensors, and we need to figure out whether or not we will need whitening and if so, how much. The figure below shows the actual measurements (red, green and blue lines), and a rough fit. I used Gautam's elog here and used the same function, (with units of nV/sqrt(Hz)) to fit our results. I used a = 1, b = 1e6, c = 2000. Since we are interested in measuring at lower frequencies, we must whiten the signal from the temperature sensors enough to have the ADC noise be negligible.
We want to be able to measure to accuracy at 1Hz, which translates to about current from the AD590 (because it gives ). Since we have a 10K resistor and V=IR, the voltage accuracy we want to measure will be . We would need whitening for lower frequencies to see such fluctuations.
To do the measurements, we put a BNC end cap on the channels we wanted to measure, then took measurements from 0-900Hz with a bandwidth of 0.001Hz. This setup is shown in the last two attachments. We used the ADC in 1X7. |
Attachment 1: ADC-fit.png
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Attachment 2: IMG_20171108_162532.jpg
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Attachment 3: IMG_20171108_162556.jpg
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Fri Mar 9 12:59:53 2018 |
Kira | Update | PEM | ADC noise measurement |
[Kira, Gautam]
I ceated a simple circuit that takes in 15V and outputs precisely 5V by using a 12V voltage regulator LM7812 and an AD586 that takes the output of the voltage regulator and outputs 5V (attachment 1). We plugged this into the slow channel and will leave it running for a few hours to see if we still have the fluctuations we observed earlier and also fit the noise curve. We'll also test the fast channel later as well. Attachment 2 shows the setup we have in the lab, with the red and white cable plugged into the +15V power supply and the red and black cable connected to the slow channel. |
Attachment 1: IMG_20180309_114345.jpg
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Attachment 2: IMG_20180309_125153.jpg
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Fri Jun 15 13:33:39 2012 |
yuta | Update | Green Locking | ADC noise contribution to ALS |
ADC noise is not a limiting noise source in a current ALS setup.
Below is the calibrated spectrum of C1:ALS-COARSE_I_ERR when
Y arm swinging with just damping (red; taken last night)
terminated before AA (green)
blocked PSL green beam (blue)
Blue and green curve tells us that noise from the beat PD to ADC is not contributing to the Y arm length sensing noise.
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Thu Apr 26 20:22:21 2018 |
Kevin | Update | PEM | ADC common mode rejection with new seismometer connections |
Yesterday I wired the outputs from the seismometers directly to the ADC input bypassing the old AA board circuit as is described in this elog. The old circuit converted the single-ended output from the seismometers to a differential signal. Today I looked at whether 60 Hz noise is worse going directly into the ADC due to the loss of the common mode rejection previously provided by the conversion to differential signals.
I split the output from the BS Z seismometer to the new board and to an SR785. On the SR785 I measured the difference between the inner and outer conductors of the seismometer output, i.e. A-B with A the center conductor and B the outer conductor, with grounded input. At the same time I took a DTT spectrum of C1:PEM-SEIS_BS_Z_IN1. Both spectra were taken with 1 Hz bandwidth and 25 averages. The setup is shown in attachment 1.
The spectra are shown in attachment 2. The DTT spectrum was converted from counts to volts by multiplying by 2 * 10 V/32768 cts where the extra factor of 2 is from converting from single-ended to differential input. If there was common 60 Hz noise that the ADC was picking up we would expect to see less noise at 60 Hz in the SR785 spectrum measured directly at the output from the seismometer since that was a differential measurement. Since both spectra have the same 60 Hz noise, this noise is differential. |
Attachment 1: setup.pdf
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Attachment 2: seismometerASD.pdf
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Wed May 16 21:02:22 2018 |
Kevin | Update | PEM | ADC common mode rejection with new seismometer connections |
As described in this elog, the ADC for the seismometers now has the signals wired directly to the ADC instead of going through an AA board or other circuit to remove any common mode noise. This elog describes one test of the common mode rejection of this setup. Guantanamo suggested comparing directly with a recent spectrum taken a few months before the new setup described in this elog.
Today I took a spectrum (attachment 1) of C1:PEM-MIC_2 (Ch17) and C1:PEM-MIC_3 (Ch18) with input to the ADC terminated with 50 Ohms. These are two of the channels plotted in the previous spectrum, though I don't know how that plot was normalized. It's clear that there are now strong 60 Hz harmonic peaks that were not there before, so this new setup does have worse common mode rejection. |
Attachment 1: ADC_noise.pdf
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Wed Nov 2 17:33:28 2011 |
Katrin | Update | Green Locking | ADC channels for slow control |
connector J9B of hardware ADC --> ch1 in software ADC --> GCY_ERR
connector J14 of hardware ADC --> ch11 in software ADC --> GCY_PZT
connector J15 of hardware ADC --> ch13 in software ADC --> GCY_REFL_DC
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Sun Aug 19 00:54:07 2012 |
Masha | Update | PEM | ADC channel switch, triangulation script |
Since the classification finally works (or seems to work..), I wrote triangulation scripts in Python which triangulate the signals, and a plotting script in Matlab which generates a heat map of seismic noise source locations. I switched the ADC Streckeisen and Trillium connections in order to better triangulate with the current channels, and will return them either tomorrow, or when I come back from Livingston so that we can have weekday data as well. |
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Thu Apr 8 20:58:17 2021 |
Koji | Update | CDS | ADC adapter boards assembly |
5x 16bit ADC adapter boards (D0902006) assembled. |
Attachment 1: P_20210408_205411_2_1.jpg
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Thu May 10 21:13:01 2012 |
Den | Update | Electronics | ADC 3 |
ADC 3 INPUT 4 (#3 in the c1pem model if you count from 0) is bad. It adds DC = ~1 V to the signal as well as noise. I plugged in GUR2 channels to STS1 channels (7-9). |
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Tue Oct 21 16:17:45 2008 |
Yoichi | Update | PSL | AD797 Oscillation in the FSS board |
I checked each op-amp's output in the FSS board to see if any indication of slew-rate saturation can be found.
PA85, which was the most suspicious one, actually has a very large slew rate limit (1000V/usec).
Its output swing was about 5V/usec. So PA85 was ok in terms of slew rate.
However, I found that an AD797 used at the first stage of the PC path was oscillating by itself, i.e. even without the loop closed.
The frequency was about 50MHz and the amplitude was large enough to reach the slew rate limit of this chip (the steepest slope was 30V/usec whereas the slew
rate limit of AD797 is 20V/usec).
I replaced it and another AD797 right after the oscillating one with AD829s. Just replacing the chips caused oscillation of AD829.
It was because there were no phase compensation capacitors connected to the pin 5 of AD829s.
Since the PCB was designed for AD797, there is no pattern for compensation caps. So I ended up putting Mica capacitors (47pF) across the pin 5 and the nearest ground point.
It worked and the oscillation stopped.
As I reported in an earlier elog, stopping the oscillation did not solve the problem of low FSS bandwidth. |
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Fri Apr 13 16:09:43 2012 |
Suresh | Update | Computer Scripts / Programs | ACAD 2002 installed on C21530 |
I have installed ACAD 2002 on one of the Windows machines in the Control Room. It is on the machine which has Solid Works (called C21530).
The installation files are in MyDocuments under Acad2002. This a shared LIGO license which Christian Cepada had with him.
I hope we will be able to open our optical layout diagrams with this and update them even though it is an old version.
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Fri Nov 7 08:08:00 2008 |
steve | Update | PEM | AC turned off in IFO room |
All tree AC units in IFO room 104 switched off at 7:45am
I'm looking for the periodic thump signal in the Vertex area
noted in entry 1113 of PEM-ACC_MC1 |
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Fri Feb 10 15:54:27 2012 |
steve | Update | PEM | AC turned back ON |
The air cond was off for 2 hrs. I just switched it back on at 15:51 |
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Wed Dec 19 11:53:23 2012 |
Steve | Update | VAC | AC removed |
Koji, Manasa, Jenne, Jamie, Bob and Steve
Access connector removed this morning and work has began in the IOO chamber. BE WARE OF ANTS !
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Attachment 1: workingatatm.png
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Mon Jul 29 16:04:40 2013 |
Steve | Update | VAC | AC removed |
Manasa, Eric, Evan, Koji and Steve,
Access connector removed in order to complete alignment. Light aluminum with acetate windows AC installed.
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Attachment 1: acout.png
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Attachment 2: AlAcACa.jpg
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Attachment 3: AlAcACb.jpg
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Mon Jul 29 16:15:13 2013 |
Koji | Update | VAC | AC removed |
Prior to the access connector removal, Manasa and I aligned the IFO mirrors.
The arms were locked and aligned by ASS. |
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Wed Mar 21 10:31:28 2012 |
steve | Update | SAFETY | AC power to ETMY turned off |
ETMY sus damping was disabled. Green locking laser and associated electronics turned off. Computers and power supplies turned off at rack 1Y4
The electricians picking up ac power from 1Y4 manual disconnect box and installing conduit line to ISCT-ETMY east end optical table.
There will be no more daisy chaining this way. |
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Wed Mar 21 11:32:47 2012 |
steve | Update | SAFETY | AC power to ETMX turned off |
Quote: |
ETMY sus damping was disabled. Green locking laser and associated electronics turned off. Computers and power supplies turned off at rack 1Y4
The electricians picking up ac power from 1Y4 manual disconnect box and installing conduit line to ISCT-ETMY east end optical table.
There will be no more daisy chaining this way.
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The power is back on at ETMY . c1iscey has not been restarted.
Now I'm turning ac power off at ETMX for the same job to be done. |
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Mon Jun 25 08:21:40 2012 |
steve | Update | General | AC power disturbance on Sat |
Quote: |
I was notified by CIT Utilities that there was a power surge or short power outage this after noon.
Lab conditions are normal: c1ioo is down. The south arm AC was off......I turned it back on.
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CALIFORNIA INSTITUTE OF TECHNOLOGY
FACILITIES MANAGEMENT
UTILITY & SERVICE INTERRUPTION
**PLEASE POST**
Building: CAMPUS
Date: Saturday, June 23, 2012
Time: 3:46 P.M.
Interruption: Electrical Power Disturbance
Contact: Tom Brennan, x-625-395-4984
*The City of Pasadena Water & Power Department had a 34,000-volt line event on Saturday June 23 at 3:46 p.m. This caused a city wide disturbance on the power grid. The Campus did not lose electrical power. However, the disturbance may have affected sensitive electronic equipment.
(If there is a problem with this Interruption, please notify the Service Center X-4717 or the above Contact as soon as possible.
If no response is received we will proceed with the interruption.)
Jerry Thompson,
Interim Director of Campus Operations & Maintenance
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Attachment 1: powerdisturbed.png
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Wed Mar 21 19:12:27 2012 |
steve | Update | Computers | AC power back on both ends |
Quote: |
Quote: |
ETMY sus damping was disabled. Green locking laser and associated electronics turned off. Computers and power supplies turned off at rack 1Y4
The electricians picking up ac power from 1Y4 manual disconnect box and installing conduit line to ISCT-ETMY east end optical table.
There will be no more daisy chaining this way.
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The power is back on at ETMY . c1iscey has not been restarted.
Now I'm turning ac power off at ETMX for the same job to be done.
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The power was turned back on at 4pm It took some time for Suresh to restart the computers. We have damping but things are not perfect yet. Auto BURTH did not work well. |
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Mon Apr 26 11:13:28 2010 |
steve | Omnistructure | PEM | AC on/off is working |
Quote: |
Koji and I wanted to turn off the IFO-room AC so the wind would not blow on MC1-3. We could not. The switches were probably bypassed when the power transformer was replaced at the last scheduled power outage.
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There is one three position manual/off/auto switch next to the filter for each unit at CES. They have to be in AUTO position when we want to turn AC on/off from the lab. |
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Fri Nov 7 10:52:57 2008 |
steve | Update | PEM | AC is back on |
The 20 minutes and 6 sec thumps are not related to the 40m ac units
This period is precisely right on so it is not likely mechanical as a source.
The time and frequency domain of this signal at attachment 2&3
First I had the chilling water cut off and later I turned off the fans
as 5 hrs temp plot shows |
Attachment 1: acf.jpg
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Attachment 2: acc_mc1.jpg
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Attachment 3: test.jpg
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Fri Nov 7 15:58:10 2008 |
rana | Update | PEM | AC is back on |
I'll bet Steve a dollar that it is mechanical. The attached PDF compares all of the accelerometers from right now.
You can see that the RMS in MC2 is way bigger than MC1.
In the second PDF file you can see the time series. I had to play around a lot with DTT to get it to work. The DTT/Foton
combo on Allegra is not stable, so make sure your work early and often.
In the plots shown, I am bandpassing the time series from 600-700 Hz. I found that doing so allowed the burp in MC1 to remain
large and reduce the extraneous fuzz in MC2. As you can see there is no such noise in MC2.
So its a noise around 600-700 Hz that comes on quickly and then shuts off after several seconds. Its also very periodic in that
it comes on around every 20 minutes. Steve also tells me (although he refuses to put in the elog) that it started up around
August 20th (?). I feel like someone in the 40m lab ought to be able to guess what this is at this point.
Please convince Steve to elog his findings about when the noise started.
If one goes out there and stands next to it when the trend predicts its happening it becomes clear what it is. |
Attachment 1: mc-acc.pdf
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Attachment 2: mc-acc-quad.pdf
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Wed Nov 23 14:47:14 2011 |
Jenne | Configuration | Environment | AC in the IFO room was off |
I turned it back on, maybe around 11am? Definitely a little while before the 12:30 meeting.
EDIT by KI:
Sorry, it's me. I was checking if AC was doing something bad on the ALS noise. |