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ID Date Author Type Categoryup Subject
  12337   Tue Jul 26 14:24:38 2016 KojiSummaryVACPurge compressed air system at LHO

I've visited the purge clean air system at LHO Yarm mid-station with John Worden.

The system is described C981637. There is a schematic in C981637-06-V (Vol.6).pdf although the schematic has some differences (or uncorrected mistakes).

This system is intended to provide positive pressure when a soft cover is attached to a chamber door. When the door is open, the purging does not help to keep the chamber clean because the flow is too slow. This protection has to be done with overhead HEPA filters (22x5000cfm). It may be possible that this purge air helps the tube not to allow dusts to come in. But before using this, the chambers and the tubes have to be cleaned, according to John.


- Here at the site, the purge air system is started up a day before the vent. This system is used for the vent air, the purge air, and turbo foreline filling.

- Air intake (attachment 1): At the site, the air is intaken from the VEA. We want to incorporate somewhat clean air instead of dirty, dusty, outside air.

- Initial filter (attachment 2): a high volume filter before the compressors.

- The compressors (attachment 3, 4) are 5x 6 horse power air compressor each goes up to 160 psi. They are turned on and off depending on the demand of the air. Which is turned on is revolved by the controller to equalize the compressor usage hours.

- The compressed air goes through the air cooler (heat exchanger) to remove the heat by the compressor work.

- This air goes through prefilters and accumulated in the air receiver (100psi) (attachment 5). This receiver tank has an automated vent valve for periodical water drainage at the bottom.

- The accumulated air is discharged to twin drier towers (attachment 6, blue). The tower is operated by the controller (attachment 7) alternately with a period of 4min (or 10min by setting). When one of the towers is working, a humid air comes from the bottom and the dry air is discharged from the top. A part of the dry air goes into the other tower from the top to the bottom and dries the tower. There is a vent at the bottom to discharge water periodically.

- The dried air goes through 4 types of filters. After the last filter, all of the plumbing should be made of stainless steel to keep cleanliness.

- The air goes to the pressure reducing regulator (attachment 8, gray). The final flow speed at the chamber side is 50cfm max, according to John.

- The lower pressure air goes through the final filter (attachment 8, blue). As the pressure is low, this filter is big in order to keep the volume of the air flow.

- The purge air is supplied to the chamber side with KF50 (attachment 9). There is a vent valve (attachment 10) for safety and also to run a dry air for at least a day before the use to clean up the supply line. The purge line is disconnected when no in use.

- The entire system (attachment 11) and size comparison (attachment 12).

 

Attachment 1: air_intake.jpg
air_intake.jpg
Attachment 2: initial_filter.jpg
initial_filter.jpg
Attachment 3: compressors1.jpg
compressors1.jpg
Attachment 4: compressors2.jpg
compressors2.jpg
Attachment 5: air_receiver_dryer.jpg
air_receiver_dryer.jpg
Attachment 6: drier.jpg
drier.jpg
Attachment 7: drier_controller2.jpg
drier_controller2.jpg
Attachment 8: pressure_regulator_and_last_filter.jpg
pressure_regulator_and_last_filter.jpg
Attachment 9: chamber_side_supply.jpg
chamber_side_supply.jpg
Attachment 10: vent_valve_for_line_cleaning.jpg
vent_valve_for_line_cleaning.jpg
Attachment 11: the_whole_system.jpg
the_whole_system.jpg
Attachment 12: size_comparison.jpg
size_comparison.jpg
  12338   Tue Jul 26 16:01:32 2016 SteveSummaryVACPurge compressed air system

Thanks for checking this out Koji

The builder in 1996 was Process System International, Inc ( Westborough, MA ) It does not exist any longer or I just could not find them. Flow diagramm at Atm1

Should I be keep looking for a company who could quote us for building a similar smaller unit with 10 - 15 cfm flowrate?

Note: my intension with the two mobile-overhead HEPA filter was the same as John Worden's " clean air overpressured tent " at chamber entrance.

Atm2, Our unit has 650 cfm, velocity 90 fpm at resistance 0.5"    It may be enough to give a little overpressure if we seal it well to the chamber

We use to use them to minimize dirt getting inside the chanbers.

Attachment 1: cleanAirSupl.pdf
cleanAirSupl.pdf
Attachment 2: mobileHEPA.jpg
mobileHEPA.jpg
  12339   Tue Jul 26 17:41:59 2016 KojiSummaryVACPurge compressed air system

We have no number for the CFM without calculation. We can't assume a random number like 10-15

  12483   Mon Sep 12 17:54:24 2016 SteveUpdateVACpumpdown 79

 We are pumping down. The annuloses are below 10 mTorr

The vacuum gauges are not communicating with the medm so there is no plot available.

The main volume pumping is stopped at P1 = 220 Torr  ( New SuperBee 174 Torr ) for overnight.

note: SuperBee was reading 791 Torr at atm and it was not set to 760 !

  12487   Tue Sep 13 16:16:28 2016 ChrisOmnistructureVACvacuum interlock bypassed

(Steve, Chris)

The pumpdown had stalled because of some ancient vacuum interlock code that prevented opening the valve V1 between the turbo pump and the main volume.

This interlock [0] compares the channels C1:Vac-P1_pressure and C1:Vac-PTP1_pressure, neither of which is functioning at the moment. The P1 channel apparently stopped reading sometime during the vent, and contained a value of ~700 torr, while the PTP1 channel contained 0. So the interlock code saw this huge apparent pressure difference and refused to move the valve.

To bypass this check, we used caput to enter a pressure of 0 for P1.

[0] /cvs/cds/caltech/state/from_luna/VacInterlock.st

  12488   Tue Sep 13 17:47:04 2016 SteveUpdateVACpumpdown 79 completed

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is off, not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

Quote:

(Steve, Chris)

The pumpdown had stalled because of some ancient vacuum interlock code that prevented opening the valve V1 between the turbo pump and the main volume.

This interlock [0] compares the channels C1:Vac-P1_pressure and C1:Vac-PTP1_pressure, neither of which is functioning at the moment. The P1 channel apparently stopped reading sometime during the vent, and contained a value of ~700 torr, while the PTP1 channel contained 0. So the interlock code saw this huge apparent pressure difference and refused to move the valve.

To bypass this check, we used caput to enter a pressure of 0 for P1.

[0] /cvs/cds/caltech/state/from_luna/VacInterlock.st

 

  12492   Wed Sep 14 09:44:09 2016 SteveUpdateVACpumpdown 79 completed

The pumpdown started at 9-12-2016

The IFO is at 5e-5 Torr vacuum normal after 73 day at atm.

ITMX needed to be freed and ETMY-UL is still misbehaving occasionally.

New pirani   and cold cathode gauges added at this vent. They were baked at 100 C for 6 hrs under vacuum.

Go to the Vac Rack to read IFO pressure from the gauge itself when Vac. Monitor is blank as it is now !

 

Quote:

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

 

 

Attachment 1: pd79.png
pd79.png
Attachment 2: pd79d2.jpg
pd79d2.jpg
Attachment 3: CCcg.jpg
CCcg.jpg
  12496   Thu Sep 15 10:36:32 2016 SteveUpdateVACpumpdown 79 day 3

IFO pressure 3.7e-5 Torr at new cold cathode InstruTech - Hornet

New items in vacuum:

1, ETMX sus tower with new baked sus wire, EP30-2 epoxied magnets, same at different locations also........ ..........  and 2 ruby wirestandoffs.

2, First Contact cleaned arm test masses only. This technic was a 1st time use in our vacuum system.

3, 50 mm ID green glass baffles at the ends

4, witness mirrors at ETMX and ITMY (old oplev mirrors) We observed a very dusty system: sides of optics, towers and tables were wiped. Hepa tents used at Y arm and BS

5, new pirani, cc gauge and 1.5" right angle valve

 

Quote:

The pumpdown started at 9-12-2016

The IFO is at 5e-5 Torr vacuum normal after 73 day at atm.

ITMX needed to be freed and ETMY-UL is still misbehaving occasionally.

New pirani   and cold cathode gauges added at this vent. They were baked at 100 C for 6 hrs under vacuum.

Go to the Vac Rack to read IFO pressure from the gauge itself when Vac. Monitor is blank as it is now !

 

Quote:

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

 

 

 

Attachment 1: vent78for73d.png
vent78for73d.png
  12525   Fri Sep 30 10:37:57 2016 SteveUpdateVACvacuum VME machines rebooted

[ Gautam and Steve ]

c1vac1 and c1vac2 were rebooted and the gauges are communicating now. V1, VA6, V5 and V4 were closed and disconnected to avoid unexpected valve switching. All went smoothly.

The new ITcc gauge is at 1e-5 Torr as CC1   This is the gauge that should be logged in slow channel.

TP2 fore line dry pump was replaced this morning after 382 day of operation.

TP3 dry pump is very noisy, but it's pressure still 47 mTorr

Quote:

[ericq, Gautam, Steve]

Following roughly the same procedure as ELOG 11354, c1vac1 and c1vac2 were rebooted. The symptoms were identical to the situation in that ELOG; c1vac1 could be pinged and telneted to, but c1vac2 was totally unresponsive. 

The only change in the linked procedure was that we did not shut down the maglev. Since I unwittingly had it running for days without V4 open while Steve was away, we now know that it can handle shorter periods of time than that...

Upon reboot, many channels were readable again, unfortunately the channels for TP2 and TP3 are still blank. We were able to return to "Vacuum normal state," but because of unknowned communication problems with VM1's interlock, we can't open VM1 for the RGA. Instead we opened VM2 to expose the RGA to the main IFO volumn, but this isn't part of the "Normal" state definite, so things currently read "Undefined state".

 

Attachment 1: rebooted.png
rebooted.png
  12530   Tue Oct 4 11:02:31 2016 SteveUpdateVACRGA is out of order

The last good rga scan at vent 78  day 38

Quote:

 

Quote:

RGA background scan

Quote:

Vacuum Status: Chamber Open

All chamber annuloses are vented.  Vac Monitor screen is not communicating with gauges. The valve position indicator are working.

RGA is pumped by Maglev through VM2

 

 

 

 

Attachment 1: lastBGscan.png
lastBGscan.png
  12537   Fri Oct 7 10:29:57 2016 SteveUpdateVACRGA removed

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

Attachment 1: RGAremoved.png
RGAremoved.png
  12556   Thu Oct 13 00:23:54 2016 ericqUpdateVACPre-vent prep

I have completed the following non-Steve portions of the pre-vent checklist [wiki-40m.ligo.caltech.edu]

  • Center all oplevs, transom QPDs (and IPPOS + IPANG if they are set up)
  • Align the arm cavities for IR and align the green lasers to the arms.
  • Update the SUS Driftmon values
  • Reconcile all SDF differences
  • Reduce input power to no more than 100mW (measured at the PSL shutter) by adjusting wave plate+PBS setup on the PSL table BEFORE the PMC. (Using the WP + PBS that already exist after the laser.)
  • Replace 10% BS before MC REFL PD with Y1 mirror and lock MC at low power.
  • Close shutter of PSL-IR and green shutters at the ends

All shutters are closed. Ready for Steve to check nuts and begin venting!

  12559   Thu Oct 13 16:48:34 2016 SteveUpdateVACvent 79 is completed

IFO is at atmosphere. The MC can be locked in air now.

The doors will be coming off tomorrow 8am sharp.

Do we want to install the ITM baffles?

What about the found OSEM filters?

 

Attachment 1: vent_79.png
vent_79.png
  12574   Thu Oct 20 09:17:08 2016 SteveUpdateVACPumpdown 80 has started

Pumping again after 7 days at atmosphere.

BS, ITMY and OMC chambers were open only.

Checked: jam nuts, viewport covers and beam shutters.

Oplev servo turned off and medm screens shots taken.

New item in vacuum:  green shade 14 glass beam block at IR-input [ from the PSL ] viewport to block green reflection-scatter.

Reminder: viewport is not AR coated for green!

 

 

 

Attachment 1: readyPd80.png
readyPd80.png
Attachment 2: beforePd80.png
beforePd80.png
Attachment 3: pd80at1h.png
pd80at1h.png
Attachment 4: 7d_atm.png
7d_atm.png
  12575   Thu Oct 20 15:59:52 2016 SteveUpdateVACPumpdown 80 has completed

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

Attachment 1: 7hPd80.png
7hPd80.png
Attachment 2: 8hPd80.png
8hPd80.png
Attachment 3: 9hPd80.png
9hPd80.png
  12577   Fri Oct 21 09:28:21 2016 SteveUpdateVACVac Normal reached

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

Attachment 1: VacNormal.png
VacNormal.png
  12589   Mon Oct 31 16:20:50 2016 SteveUpdateVACRGA is reinstalled

Quad rods and  ionizer kit: consisting of repeller cage, anode grid, focus plate and  filament were replaced....... under repair # RGA200/12 ECA 100416-12967

The electronic ECU is not connected. It is beeing pumped at IFO ITcc 9.7E-6 Torr vacNormal

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

  12633   Tue Nov 22 11:31:52 2016 SteveUpdateVACRGA is running again

The Rga was turned on yesterday.

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

Attachment 1: RGAisBack33d.png
RGAisBack33d.png
Attachment 2: pd80-560Hz-d33.png
pd80-560Hz-d33.png
Attachment 3: afterRepair1d.png
afterRepair1d.png
  12636   Wed Nov 23 11:32:13 2016 SteveUpdateVACTP3 drypump replaced again

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

  12642   Mon Nov 28 09:45:44 2016 SteveUpdateVACRGA scan at pumpdown day 40

The vacuum envelope ~1 C warmer today than 7 days ago. Bad peaks are coming down as normal.

 

Attachment 1: RGAscan_d40.png
RGAscan_d40.png
Attachment 2: d2_&_d7scan.png
d2_&_d7scan.png
Attachment 3: RGAd2.png
RGAd2.png
  12681   Thu Dec 22 09:37:20 2016 SteveUpdateVACRGA scan at day 63

Valve configuration: vacuum normal

RGA head temp: 43.5 C

Vac envelope temp: 23 C

 

Attachment 1: pd80-d63.png
pd80-d63.png
Attachment 2: pd80-580Hz-d63.png
pd80-580Hz-d63.png
  12698   Tue Jan 10 14:24:09 2017 SteveUpdateVACRGA scan at day 82

Valve configuration: vacuum normal

Vacuum envelope: 23C

Rga head: 44C

 

Attachment 1: pd80VNd82.png
pd80VNd82.png
  12774   Tue Jan 31 14:14:29 2017 ranaUpdateVACPressure watch script

I think this cron job is running on NODUS (our gateway) instead of our scripts machine:

*/1 * * * * /opt/rtcds/caltech/c1/scripts/Admin/n2Check.sh >> /opt/rtcds/caltech/c1/scripts/Admin/n2Check.log 2>&1

Quote:

Based on Jenne's chiara disk usage monitoring script, I made a script that checks the N2 pressure, which will send an email to myself, Jenne, Rana, Koji, and Steve, should the pressure fall below 60psi. I also updated the chiara disk checking script to work on the new Nodus setup. I tested the two, only emailing myself, and they appear to work as expected. 

The scripts are committed to the svn. Nodus' crontab now includes these two scripts, as well as the crontab backup script. (It occurs to me that the crontab backup script could be a little smarter, only backing it up if a change is made, but the archive is only a few MB, so it's probably not so important...)

moreover this script has a 90MB log file full of not finding its channel

I wish this script was in python instead of BASH and I wish it would run on megatron instead of nodus (why can't megatron send us email too?) and I wish that this log file would get wiped out once in awhile. Currently its been spitting out errors since at least a month ago:

Tue Jan 31 14:10:02 PST 2017 : N2 Pressure:

Channel connect timed out: 'C1:Vac-N2pres' not found.

(standard_in) 1: syntax error

  12853   Mon Feb 27 15:33:10 2017 SteveUpdateVACRGA scan at day 130

Valve configuration: vacuum normal

Vacuum envelope: 23.5 C

RGA head: 46.6 C

 

Attachment 1: rgascan@130d.png
rgascan@130d.png
  13047   Wed Jun 7 11:32:56 2017 SteveUpdateVACsmooth vac reboot

Gautam and Steve,

 

The medm monitor & vac control screens were totally blank since ~ May 24, 2017    Experienced vacuum knowledge is required for this job.

IDENTIFY valve configuration:

                        How to confirm valve configuration when all vac mons are blank?  Each valve has a manual-mechanical position indicator. Look at pressure readings and turbo pump controllers. VAC NORMAL configuration was confirmed based on these information.

Preparation: disconnect valves ( disconnect meaning: valve closes and stays paralized ) in this sequence VC2, VC1 power, VA6, V5, V4 & V1 power,      at ifo pressure 7.3E-6 Torr-it  ( it  = InstruTech cold cathode gauge )

                            This gauge is independent from all other rack  mounted   instrumentation and it is still not logged.

                            Switching to this valve configuration with disconnected valves will insure NOT  venting of the vacuum envelope by accidental glitching voltage drop or computer malfunction.

RESET  v1Vac1 .........in 2-3 minutes........ ( v1Vac1 - 2 )  the vac control screen started reading pressures & position

                    Connected cables to valves (meaning: valve will open if it was open before it was disconnected and it will be control able from computer ) in the following order: V4, V1 power, V5, VA6, VC2 & VC1 power,      at ifo 2E-5 Torr-it.....

                     ....vac configuration is reading VAC NORMAL,

                     ifo 7.4E-6 Torr-it

We have to hook up the it-cold cathode gauge to be monitored - logged !  this should be the substitute for the out of order CC1 pressure gauge.

Attachment 1: vac_reboot.png
vac_reboot.png
  13075   Tue Jun 20 16:28:23 2017 SteveUpdateVACRGA scan
Attachment 1: RGAscan243d.png
RGAscan243d.png
Attachment 2: RGAscan.png
RGAscan.png
  13132   Sun Jul 23 15:00:28 2017 JamieOmnistructureVACstrange sound around X arm vacuum pumps

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

  13134   Mon Jul 24 09:55:29 2017 SteveOmnistructureVACcontroller failer

Ifo pressure was 5.5 mTorr this Monday morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Maglev got warm ~38C but it was still rotating at 560 Hz normal with closed V1

Pressure plots are not available because of computer problems.

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

Attachment 1: TP2controllerFails.png
TP2controllerFails.png
  13142   Tue Jul 25 08:48:57 2017 SteveUpdateVACRGA scan at d278

The RGA did not shut down at the turbo pump controller failing.

Quote:

Ifo pressure was 5.5 mTorr this morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Magelv got warm ~38C but it was still rotating at 560 Hz normal with closed V1

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

 

Attachment 1: RGA278d.png
RGA278d.png
  13143   Tue Jul 25 14:04:06 2017 SteveUpdateVACturbo controller installed and we are running at vac normal

Gautam and Steve,

Spare Varian turbo-V 70 controller, Model 969-9505, sn 21612 was swapped in. It is running the turbo fine @ 50Krpm but it does not allow it's V4 valve to be opened............

It turns out that TP2 @ 75Krpm will allow V4 to open and close. This must be a software issue.

So Vacuum Normal is operational if TP2 is running 75,000 rpm

We want to run at 50,000 rpm on the long term.

Note: the RS232 Dsub connector on the back of this controller is mounted 180 degrees opposite than TP3  and old failed TP2 controller

 

PS: controller is shipping out for repair 7-28-2017

 

Attachment 1: TP2@75Krpm.png
TP2@75Krpm.png
  13171   Tue Aug 8 17:04:26 2017 SteveUpdateVACunintended pump down

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

Attachment 1: pumping_down.png
pumping_down.png
  13172   Tue Aug 8 17:44:11 2017 SteveUpdateVACunintended pump down

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

Attachment 1: stopped_pumping.png
stopped_pumping.png
  13175   Wed Aug 9 11:59:51 2017 SteveUpdateVACunintended pump down at vacuum normal

pd80b has reached Vac Normal. IFO pressure 0.5 mTorr

We need our vauum channels back in dataviewer.

Quote:

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

 

Attachment 1: pdc.png
pdc.png
Attachment 2: pd80b@vacnormal.png
pd80b@vacnormal.png
  13179   Wed Aug 9 16:34:46 2017 ranaUpdateVACVacuum Document recovered

Steve and I found the previous draft of the 40m Vacuum Document. Someone in 2015 had browsed into the Docs history and then saved the old 2013 version as the current one.

We restored the version from 2014 which has all of Steve's edits. I have put that version (which is now the working copy) into the DCC:  https://dcc.ligo.org/E1500239.

The latest version is in our Google Docs place as usual. Steve is going to have a draft ready for us to ready be Tuesday, so please take a look then and we can discuss what needs doing at next Wednesday's 40m meeting.

  13186   Thu Aug 10 15:45:34 2017 SteveUpdateVACaccidental vent to 17 Torr

Finally we got the cold cathode gauge working. IFO pressure 7e-6 Torr-it, vacuum normal valve configuration with all 4 ion pump gate valves closed at ~ 9e-6 Torr.  The cryo pump was also pumped yesterday to remove the accumulated outgassing build up.

The accidental vent was my mistake; made when I was replacing the battery pack of the UPS. The installed pack measured 51 V without any load. The "replace battery" warning light did not go out after the batteries were replaced. 

I then mistakenly and repeatedly pushed the "test" button to reset this, but I did not wait long enough for the batterries to get fully charged. The test put the full load on the new batteries and their charging condition got worse. I made the mistake when trying to put the load from the battery to online and pushed "O" so the power was cut and the computer rebooted to the all off condition. On top of this, I disconnected the wrong V1 cable to close V1.  As the computer rebooted it's interlock closed V1 at 17 Torr.

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

Attachment 1: Mag_UPS.jpg
Mag_UPS.jpg
Attachment 2: UPSbatteryPack.jpg
UPSbatteryPack.jpg
Attachment 3: closing_V1.jpg
closing_V1.jpg
  13233   Mon Aug 21 14:53:32 2017 gautamUpdateVACRGA reset

[gautam, steve]

In the aftermath of the accidental vent, it looks like the RGA was shutdown.

We followed the instructions in this elog to restart the RGA.

Seems to be working now, Steve says we just need to wait for it to warm up before we can collect a reliable scan.

Quote:

We have good RGA scan now. There was no scan for 3 months.

 

  13234   Mon Aug 21 16:35:48 2017 gautamUpdateVACUPS checkup

[steve, gautam]

At Rolf/Rich Abbott's request, we performed a check of the UPS today.

Steve believed that the UPS was functioning as it should, and the recent accidental vent was because the UPS batteries were insufficiently charged when the test was performed. Today, we decided to try testing the UPS.

We first closed V1, VM1 and VA6 using the MEDM screen. We prepared to pull power on all these valves by loosening the power connections (but not detaching them). [During this process, I lost the screw holding the power cord fixed to the gate valve V1 - we are looking for a replacement right now but it seems to be an odd size. It is cable tied for now.]

The battery charge indicator LEDs on the UPS indicated that the batteries were fully charged.

Next, we hit the "Test" button on the UPS - it has to be held down for ~3 seconds for the test to be actually initiated, seems to be a safety feature of the UPS. Once the test is underway, the LED indicators on the UPS will indicate that the loading is on the UPS batteries. The test itself lasts for ~5seconds, after which the UPS automatically reverts to the nominal configuration of supplying power from the main line (no additional user input is required).

In this test, one of the five battery charge indicator LEDs went off (5 ON LEDs indicate full charge).

So on the basis of this test, it would seem that the UPS is functioning as expected. It remains to be investigated if the various hardware/software interlocks in place will initiate the right sequence of valve closures when required.


Quote:
 

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

 

  13245   Wed Aug 23 10:11:46 2017 SteveUpdateVACvacuum valve specifications

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

  13260   Mon Aug 28 10:28:07 2017 SteveUpdateVACRGA scan 20 day after 17 Torr

The RGA was turned on 7 days ago.  It's 46 C now.   The X-arm room tem ~20 C

IFO pressure 6.5e-6 Torr at IT-Hornet gauge. Valve configuration vacuum normal.

Attachment 1: 20d_after_17_torr.png
20d_after_17_torr.png
  13268   Tue Aug 29 15:35:19 2017 SteveUpdateVACvacuum pump specifications & manuals

RP1 and RP3 roughing pump manual of Leybold D30A oily rotory pump

Fore pump of TP2 & TP3 Varian SH-100 Dry Scroll

TP2 and TP3 small turbo drag pump  Varian 969-9361 

TP2 and TP3 turbo controller Varian 969-9505

TP1 magnetically suspended turbo pump  Osaka TG390MCAB, sn360 and controller TC010M  and note : this  pump  running on 208VAC single phaseIt is not on the UPS !  

                                                             Osaka Maglev Manual        and Osaka Controller Communication Wiring                                                                                                                                

VC1 cryo pump CTI-Cryogenics Cryo Torr 8 sn 8g23925  SAFETY note: compressor single phase 208VAC and the head driver 3 phase 208VAC Compressor and driver have each separate power cord!

Installed at 40m wiki  also

Quote:

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

 

  13321   Tue Sep 19 11:05:26 2017 SteveUpdateVACRGA scan at day 334

 

 

Attachment 1: RGAscan334d.png
RGAscan334d.png
  13403   Fri Oct 27 10:14:11 2017 SteveUpdateVACRGA scan at day 372

Valve configuration: Vacuum normal

Note: Tp2 running at 75Krpm 0.25A 26C has a  load high pitch sound today. It's fore line pressure 78 mTorr. Room temp 20C

 

Attachment 1: RGA_scan_d372.png
RGA_scan_d372.png
  13407   Mon Oct 30 10:09:41 2017 SteveUpdateVACTP2 failed

 IFO pressure 1.2e-5 Torr at 9:30am

Quote:

Valve configuration: Vacuum normal

Note: Tp2 running at 75Krpm 0.25A 26C has a  load high pitch sound today. It's fore line pressure 78 mTorr. Room temp 20C

 

Atm. 1,  This was the vacuum condition  this morning.

               IFO P1  9.7 mTorr, V1 openV4 was in closed position , ~37 C warm Maglev at normal 560Hz rotation speed with foreline pressure 3.9 Torr because V4 closed 2 days ago when TP2 failed .....see Atm.3

               The error messege at TP2  controller was: fault overtemp.

I did the following to restored IFO pumping: stopped pumping of the annulose with TP3 and valves were configured so TP3 can be the forepump of the Maglev.

closed VM1 to protect the RGA,  close PSL shutter .....see Gautam  entry

aux fan on to cool down Maglev-TP1, room temp 20 C,

aux drypump turned on and opend to TP3 foreline to gain pumping speed,

closed PAN to isolate annulos pumping,

opened V7 to pump Maglev forline with TP3 running at 50Krpm, It took 10 minutes to reach P2  1mTorr from 3.9 Torr

aux drypump closed off at P2  1 mTorr, TP3 foreline pressure 362 mTorr.......see Atm.2

As we are running now:

IFO pressure 7e-6 Torr at Hornet cold cathode gauge at 15:50  We have no IFO CC1 logging now.  Annuloses are in 3-5 mTorr range are not pumped.

TP3 as foreline pump of TP1 at 50 Krpm, 0.24 A, 24 C, it's drypump forline pressure 324 mTorr

V4 valve cable is disconnected.

I need help with wiring up the logging of the Hornet cold cathode gauge.

 

 

 

Attachment 1: tp2failed.png
tp2failed.png
Attachment 2: ifo_1.0E-5_Torrit.png
ifo_1.0E-5_Torrit.png
Attachment 3: tp2failed2dago.png
tp2failed2dago.png
Attachment 4: 4days.png
4days.png
  13409   Mon Nov 6 09:09:43 2017 SteveUpdateVACsetting up new TP2 turbo

Our new Agilent Technology TwisTorr 84FS AG rack controller ( English Manual pages 195-297 )  RS232/485, product number X3508-64001, sn IT1737C383

This controller, turbo and it's drypump needs to be set up into our existing vacuum system. The intake valve of this turbo (V4) has to have a hardwired interlock that closes V4 when rotation speed is less than 20% of preset RPM speed.

The unit has an analoge 10Vdc output that is proportional to rotation speed. This can be used with a comperator to direct the interlock or there may be set software option in the controller to close the valve if the turbo slows down more than 20%

The last Upgrade of the 40m Vacuum System  1/2/2000 discribes our  vauum system  LIGO-T000054-00-R 

Here the LabView / Metrabus controls were replaced by VME processor and  an Epic interface

We do not have schematics of the hardware wiring.

We need help with this.

 

  13423   Fri Nov 10 08:52:21 2017 SteveUpdateVACTP3 drypump replaced

PSL shutter closed at 6e-6 Torr-it    

   The foreline pressure of the drypump is 850 mTorr at 8,446 hrs of seal life

V1 will be closed for ~20 minutes for drypump replacement..........

9:30am dry pump replaced, PSL shutter opened at 7.7E-6 Torr-it

  Valve configuration: vacuum normal as  TP3 is the forepump of the Maglev  & annuloses are not pumped.

Quote:

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

 

  13454   Sun Nov 26 19:38:40 2017 SteveUpdateVACTP3 drypump replaced again

The TP3 foreline pressure was 4.8 Torr, 50K rpm 0.54A and 31C........Maglev rotation normal 560 Hz.......    IFO pressure 7.2e- 6 Torrit was not effected

V1 closed ......replaced drypump.........V1 opened

IFO 6.9e-6 Torrit at 19:55, TP3fl 18 mT,  50Krpm 0.15A 24C

VM1 is still closed

 

Attachment 1: after_replacement.png
after_replacement.png
  13459   Thu Nov 30 10:38:39 2017 SteveUpdateVACannuloses are not pumped

Annuloses are not pumped for 30 days, since TP2 failed.  IFO pressure 7e-6 Torr it,  Rga 2.6e-6 Torr

Valve configuration: Vacuum Normal as TP3 is the forepump of Maglev, annuloses are not puped at 1.1 Torr

TP3 50K rpm,  0.15A  24C, foreline pressure 16.1 mTorr

 

Quote:

The TP3 foreline pressure was 4.8 Torr, 50K rpm 0.54A and 31C........Maglev rotation normal 560 Hz.......    IFO pressure 7.2e- 6 Torrit was not effected

V1 closed ......replaced drypump.........V1 opened

IFO 6.9e-6 Torrit at 19:55, TP3fl 18 mT,  50Krpm 0.15A 24C

VM1 is still closed

 

 

Attachment 1: AnnulosesNotPumped.png
AnnulosesNotPumped.png
  13495   Tue Jan 2 15:43:35 2018 SteveUpdateVACpumpdown after power outage

 

Quote:

There was a power outage.

The IFO pressure is 12.8 mTorr-it and it is not pumped. V1 is still closed. TP1 is not running. The Rga is not powered.

The PSL output shutter is still closed. 2W Innolight turned on and manual beam block placed in its beampath.

3 AC units turned on at room temp 84F

IFO pumped down from 44 mTorr to 9.6e-6 Torr with Maglev  backed with only TP3

Aux drypump  was helping our std drypump during this 1 hour period. TP3 reached 32 C and slowed down 47K rpm

The peak foreline pressure at P2  was ~3 Torr

Hornet cold cathode gauge setting:   research mode, air,

                                                            2830 HV  1e-4A  at 9.6e-6 Torr,

                                                         [  3110 HV  8e-5A at 7.4e-6 Torr one day later ]

Annuloses are at 2 Torr, not pumped

Valve configuration:  vacuum normal, RGA is still off

PSL shutter is opened automatically. Manual block removed.

End IR lasers and doublers are turned on.

 

NOTE: Maglev " rotation X " on vacuum medm screen is not working! " C1:Vac-TP1_rot " channel was removed.  Use " NORMAL X " for rotation monitoring.

*We removed this (i.e. rotation) field from the MEDM screen to avoid confusion.

Attachment 1: pumpdown_from_44_mTorr.png
pumpdown_from_44_mTorr.png
  13588   Tue Jan 30 10:22:20 2018 SteveUpdateVACRGA scan at day 175

pd80b rga scan at 175 day.  IFO pressure 7.3e-6 Torr-it

Condition: vacuum normal, annuloses not pumped. Rga turned on yesterday.

The rga was not on since last poweroutage Jan 2, 2018 It is warming up and outgassing Atm2

Attachment 1: RGApd80-b-468-175d.png
RGApd80-b-468-175d.png
Attachment 2: RgaOn20hrs.png
RgaOn20hrs.png
  13615   Wed Feb 7 15:50:42 2018 SteveUpdateVACIFO pressure monitoring

Hornet cold cathode gauge analoge output  [ DSub9 pin 3 and 7 ] are wired to go ETMX Acromag. It was reading 4.9V at 7.8e-6 Torr [ 3,110 V  8.35e-5A ] at the end of a 24ft BNC cable. Now it has to be hook up to an Acromag channel.

This will replace the not functioning C1: Vac-CC1_pressure

gautam: the motivation behind hooking this gauge up to our DAQ system is that non-vacuum-system-experts have a quick diagnostic to make sure everything is in order. This gauge is physically placed adjacent to V1, and so if something goes wrong with our vacuum pumps, we would see the effect here immediately. we did note that occassionally, the reading fluctuated by ~1V on the DMM used to check the voltage output at the end of the BNC cable, so we still need to run some long-term stability analysis once this channel is hooked up to the Acromag.  For future reference, in order to make this gauge work, we need to check that

  1. Error flag has been cleared.
  2. HV is ON (state has to be manually toggled).
Quote:

 

Quote:

There was a power outage.

The IFO pressure is 12.8 mTorr-it and it is not pumped. V1 is still closed. TP1 is not running. The Rga is not powered.

The PSL output shutter is still closed. 2W Innolight turned on and manual beam block placed in its beampath.

3 AC units turned on at room temp 84F

IFO pumped down from 44 mTorr to 9.6e-6 Torr with Maglev  backed with only TP3

Aux drypump  was helping our std drypump during this 1 hour period. TP3 reached 32 C and slowed down 47K rpm

The peak foreline pressure at P2  was ~3 Torr

Hornet cold cathode gauge setting:   research mode, air,

                                                            2830 HV  1e-4A  at 9.6e-6 Torr,

                                                         [  3110 HV  8e-5A at 7.4e-6 Torr one day later ]

Annuloses are at 2 Torr, not pumped

Valve configuration:  vacuum normal, RGA is still off

PSL shutter is opened automatically. Manual block removed.

End IR lasers and doublers are turned on.

 

NOTE: Maglev " rotation X " on vacuum medm screen is not working! " C1:Vac-TP1_rot " channel was removed.  Use " NORMAL X " for rotation monitoring.

*We removed this (i.e. rotation) field from the MEDM screen to avoid confusion.

 

Attachment 1: CC_analog.png
CC_analog.png
ELOG V3.1.3-