40m QIL Cryo_Lab CTN SUS_Lab TCS_Lab OMC_Lab CRIME_Lab FEA ENG_Labs OptContFac Mariner WBEEShop
  40m Log, Page 278 of 335  Not logged in ELOG logo
ID Date Author Typeup Category Subject
  13223   Thu Aug 17 08:42:27 2017 SteveUpdatePSLPSL HEPA

The PSL HEPA was running noisy at 100V   The bearing is wearing out. I turned it down to 30V It is quiet there.

  13224   Thu Aug 17 10:41:58 2017 KiraUpdatePEMtemp sensor PCB

Got it to work. One of the connections was faulty. I decided to check the temperature measured against a thermometer. The sensor showed 26.1 C, but the thermometer showed 25.8 C after I let them both cool down after heating them up. The temperature of the thermometer was dropping at the time of measurement, but the temperature of the sensor was not. This is still a rough version of the final sensor, so I'm not sure what exactly causes this discrepancy.

Quote:

Tried taking the circuit from the breadboard to the PCB. I attached all the components to adapters that would allow them to be connected to the PCB. From the first picture, the first component is AD586, the second is AD590, and the third is LT1012, along with a resistor across it. I then soldered the connections between the components, as can be seen in the second picture. When I tested out this version of the circuit by hooking it up to the DC source, I got a reading of ~-15V. I will have to check all the connections to make sure there is contact where there should be one, and no contact where there shouldn't be. I had issues attaching the tiny AD590 and LT1012 to its adaptor, so the issue may lie there as well. I'll also check that each component is in working order as well.

Once I figure out where my error is, my plan is to build two more of these and place a metal object such that it contacts only the surface of the AD590s. This would allow me to compare the three values to the actual temperature of the metal, which would then tell me how accurate this setup is.

Note on the resistor: I measured all the resistors and chose three that had exactly 10.00k Ohm. The voltage detected is dependent on the resistor, so if we are to take three identical copies, I ensured that there would be no error due to the resistors being a little different.

 

  13225   Thu Aug 17 11:17:49 2017 gautamUpdateSUSMC1 <--> MC3 switched back

Seems like this modification didn't really work. There were several large MC1 glitches, and one of them misaligned MC1 so much that the IMC didn't relock for the last ~6 hours. I re-aligned MC1 manually, and now it is locked fine.

Quote:

Now that all the CDS overview lights are green, I decided to switch back the coil driver outputs to their original state so that the MC optics could be damped and the IMC relocked. I also restored the static PIT/YAW bias values to their original values.

MC1 has been quiet over the last couple of days, lets see how it behaves in the next few days. In all the glitches I have observed, if the IMC is locked and WFS loops are enabled, the loops are able to correct for the DC misalignment caused by the glitch. But the mcwfs off script is currently set up in such a way that the output history is cleared between IMC locks. I made two copies of the mcwfson/mcwfsoff scripts, called mcwfsunhold/mcwfshold respectively. They live in /opt/rtcds/caltech/c1/scripts/MC/WFS. I've also modified the autolocker script to call these modified scripts, such that when the IMC loses lock, the WFS servo outputs are held, while the input is turned off. The hope is that in this configuration, the autolocker can catch a lock even if there is a glitch on MC1.

I haven't tried locking the arms yet, but I think other IFO work discussed at the meeting (like arm loss estimation / cavity scans etc) can proceed.

 

 

  13226   Thu Aug 17 17:33:01 2017 gautamUpdateSUSMC1 <--> MC3 switched back

that's why the Autolocker clears the outputs; we don't want to be holding the offsets from the last ms of lock when it was all messed up; instead it would be best to have a slow (~mHz) relief script that takes the WFS controls and puts them onto the MC SUS sliders. This would then re-align the MC to the input beam rather than the input to the MC. Which is not the best idea.

Quote:

Seems like this modification didn't really work.

 

  13227   Thu Aug 17 22:54:49 2017 ericqUpdateComputersTrying to access JetStor RAID files

The JetStor RAID unit that we had been using for frame writing before the fb meltdown has some archived frames from DRFPMI locks that I want to get at. I spent some time today trying to mount it on optimus with no success crying

The unit was connected to fb via a SCSI cable to a SCSI-to-PCI card inside of fb. I moved the card to optimus, and attached the cable. However, no mountable device corresponding to the RAID seems to show up anywhere.

The RAID unit can tell that it's hooked up to a computer, because when optimus restarts, the RAID event log says "Host Channel 0 - SCSI Bus Reset."

The computer is able to get some sort of signals from the RAID unit, because when I change the SCSI ID, the syslog will say 'detected non-optimal RAID status'.

The PCI card is ID'd fine in lspci as "06:01.0 SCSI storage controller: LSI Logic / Symbios Logic 53c1030 PCI-X Fusion-MPT Dual Ultra320 SCSI (rev c1)"

'lsssci' does not list anything related to the unit

Using 'mpt-status -p', which is somehow associated with this kind of thing returns the disheartening output:

Checking for SCSI ID:0
Checking for SCSI ID:1
Checking for SCSI ID:2
Checking for SCSI ID:3
Checking for SCSI ID:4
Checking for SCSI ID:5
Checking for SCSI ID:6
Checking for SCSI ID:7
Checking for SCSI ID:8
Checking for SCSI ID:9
Checking for SCSI ID:10
Checking for SCSI ID:11
Checking for SCSI ID:12
Checking for SCSI ID:13
Checking for SCSI ID:14
Checking for SCSI ID:15
Nothing found, contact the author
 
I don't know what to try at this point.
  13228   Fri Aug 18 21:58:35 2017 gautamUpdateGeneralSUS model ASC input weirdness

I spent some time today trying to debug this issue.

Jamie and I had opened up the c1sus frontend to try and replace the RFM card before we realized that the problem was in the RCG code generator. During this process, we had disconnected all of the back-panel cabling to this machine (2 ethernet cables, dolphin cable, and RFM cables/fibers). I thought I may have accidentally returned the cables to the wrong positions - but all the status indicator lights indicate that everything is working as it should, and I also confirmed that the cabling is as it is in the pictures of the rack on the wiki page.

Looking at the SimuLink model diagram (see Attachment #1 for example), it looks like (at least some of) these channels are actually on the dolphin network, and not the RFM network (with which we were experiencing problems). This suggests that the problem is something deeper. Although I did see nans in some of the ETMX ASC channels as well, for which the channels are piped over the RFM network. Even more puzzling is that the ASC MEDM screen (Attachment #3) and the SimuLink diagram (Attachment #2) suggest that there is an output matrix in between the input signals and the output angular control signals to the suspensions. As Attachment #4 shows, the rows corresponding to ITMX PIT and YAW are zero (I confirmed using z read <matrixElement>). Attachment #3 shows that the output of all the servo banks except CARM_YAW is zero, but CARM_YAW has no matrix element going to the ITMs (also confirmed with z read <servoOutputChannel>). So 0 x 0 should be 0, but for some reason the model doesn't give this output?

GV Edit: As EricQ just pointed out to me, nan x 0 is still nan, which probably explains the whole issue. Poking a little further, it seems like this is an SDF issue - the SDF table isn't able to catch differences for this hold output channel.


As I was writing this elog, I noticed that, as mentioned above, the CARM_YAW output was "nan". When I restart the model (thankfully this didn't crash c1lsc!), it seems to default to this state. Opening up the filter module, I saw that the "hold output" was enabled.

Toggling that switch made the nans in all the SUS ASC channels disappear. Mysterious indecision.

All the points above stand - CARM_YAW output shouldn't have been going anywhere as per the output matrix, but it seems to have been responsible? Seems like a bug in any case if a model restarts with a field as "nan".

Anyways the problem seems to have been resolved so I'm going to try locking and dither aligning the arms now.

Rolf mentioned that a simple update could fix several of the CDS issues we are facing (e.g. inability to open up testpoints), but he didn't seem to have any insight into this particular issue. Jamie will try and recompile all the models and then we have to see if that fixes the remaining problems.

Quote:
 

I have to check where this signal is coming from, but for now I just turned the "ASC Input" switch off. More investigation to be done, but in the meantime, ASS dither alignment may not be possible.

After consulting with Jamie, I have just disabled all outputs to the suspensions other than local damping loop outputs. I need to figure out how to get this configuration into the safe.snap file such that until we are sure of what is going on, the models start up in this safer configuration.

 

  13229   Fri Aug 18 23:59:53 2017 gautamUpdateALSX Arm ALS lock

[ericq, gautam]

  • I was just getting the IFO aligned, and single arm lock going, when EricQ came in and asked if we could get some ALS data.
  • ALS beats seemed fine, in particular the X-Arm. The broad hump around ~70Hz that was present in my previous ALS update was nowhere to be seen - reasons unknown.
  • Copied over /opt/rtcds/caltech/c1/scripts/YARM/Lock_ALS_YARM.py to /opt/rtcds/caltech/c1/scripts/XARM/Lock_ALS_XARM.py. Could be useful when we want to do arm cavity scans.
  • Made appropriate changes to allow ALS locking of Xarm - the testpoint inaccessibility makes things a little annoying but for tonight we just used DQ channels in place (or slow channels when DQ chans were not available)
  • Calibration of X arm error signal seemed off - so we fixed it by driving a line in ETMX and matching up the peaks in the ALS error signal and POX11. We then updated the gain of the filter in the CINV filter bank accordingly.
  • Got some decent data - X arm stayed locked on ALS for >60mins, during which time the Y arm stayed locked on POY11, and the Y green also reained locked yes. There was no evidence of the X arm 00 mode randomly dropping out of lock tonight.
  • EQ will update with a sick comparison plot - today we looked at the ALS noise from the perspective of the Green Locking Izumi et. al. paper.
  • Y arm ALS noise didn't look so hot tonight - to be investigated...

Leaving LSC mode OFF for now while CDS is still under investigation


Not really related to this work: We saw that the safe.snap file for c1oaf seems to have gotten overwritten at some point. I restored the EPICS values from a known good time, and over-wrote the safe.snap file.

  13230   Sat Aug 19 01:35:08 2017 ericqUpdateALSX Arm ALS lock

My motivation tonight was to get an up-to-date spectrum of a calibrated measurement of the out-of-loop displacement of an arm locked on ALS (using the PDH signal as the out-of-loop sensor) to compare the performance of ALS control noise with the Izumi et al green locking paper. 

I was able to fish out the PSD from the paper from the 40m svn, but the comparison as plotted looks kind of fishy. I don't see why the noise from 10-60Hz should be so different/worse. We updated the POX counts to meters conversion by looking at the Hz-calibrated ALSX signal and a ~800Hz line injected on ETMX.

  13231   Mon Aug 21 09:08:54 2017 SteveUpdateSUStiny glitches

They are synchronised tiny glitches. They are not mechanical.
 

  13232   Mon Aug 21 13:07:08 2017 KiraUpdatePEMtemp sensor PCB

On Friday, I cleaned up the circuit so that there are only three connections needed (+15V, -15V, GND) and a BNC connector for reading the output. Today, I added in bypass capacitors. The small yellow ones are 0.1 microF ceramic, and the large ones are 100 microF electrolytic. They are used to stabilize the +15V and -15V inputs to the OP amp and minimize fluctuations, since it doesn't have a regulator for stability. I have also attached the circuit diagram for the OP amp only, where 1 are the electrolytic and 2 are the ceramic. The temperature is still about 2 degrees off, but if that difference is constant for all temperatures in our range we can just calibrate it later.

Here is a helpful link on bypass capacitors (thanks to Kevin for sending it to me).

As a note, the electrolytic capacitors do have a polarity, so it is important to place them correctly (the negative side is towards the lower voltage potential, and not always towards ground).

Quote:

Got it to work. One of the connections was faulty. I decided to check the temperature measured against a thermometer. The sensor showed 26.1 C, but the thermometer showed 25.8 C after I let them both cool down after heating them up. The temperature of the thermometer was dropping at the time of measurement, but the temperature of the sensor was not. This is still a rough version of the final sensor, so I'm not sure what exactly causes this discrepancy.

Quote:

Tried taking the circuit from the breadboard to the PCB. I attached all the components to adapters that would allow them to be connected to the PCB. From the first picture, the first component is AD586, the second is AD590, and the third is LT1012, along with a resistor across it. I then soldered the connections between the components, as can be seen in the second picture. When I tested out this version of the circuit by hooking it up to the DC source, I got a reading of ~-15V. I will have to check all the connections to make sure there is contact where there should be one, and no contact where there shouldn't be. I had issues attaching the tiny AD590 and LT1012 to its adaptor, so the issue may lie there as well. I'll also check that each component is in working order as well.

Once I figure out where my error is, my plan is to build two more of these and place a metal object such that it contacts only the surface of the AD590s. This would allow me to compare the three values to the actual temperature of the metal, which would then tell me how accurate this setup is.

Note on the resistor: I measured all the resistors and chose three that had exactly 10.00k Ohm. The voltage detected is dependent on the resistor, so if we are to take three identical copies, I ensured that there would be no error due to the resistors being a little different.

 

 

  13233   Mon Aug 21 14:53:32 2017 gautamUpdateVACRGA reset

[gautam, steve]

In the aftermath of the accidental vent, it looks like the RGA was shutdown.

We followed the instructions in this elog to restart the RGA.

Seems to be working now, Steve says we just need to wait for it to warm up before we can collect a reliable scan.

Quote:

We have good RGA scan now. There was no scan for 3 months.

 

  13234   Mon Aug 21 16:35:48 2017 gautamUpdateVACUPS checkup

[steve, gautam]

At Rolf/Rich Abbott's request, we performed a check of the UPS today.

Steve believed that the UPS was functioning as it should, and the recent accidental vent was because the UPS batteries were insufficiently charged when the test was performed. Today, we decided to try testing the UPS.

We first closed V1, VM1 and VA6 using the MEDM screen. We prepared to pull power on all these valves by loosening the power connections (but not detaching them). [During this process, I lost the screw holding the power cord fixed to the gate valve V1 - we are looking for a replacement right now but it seems to be an odd size. It is cable tied for now.]

The battery charge indicator LEDs on the UPS indicated that the batteries were fully charged.

Next, we hit the "Test" button on the UPS - it has to be held down for ~3 seconds for the test to be actually initiated, seems to be a safety feature of the UPS. Once the test is underway, the LED indicators on the UPS will indicate that the loading is on the UPS batteries. The test itself lasts for ~5seconds, after which the UPS automatically reverts to the nominal configuration of supplying power from the main line (no additional user input is required).

In this test, one of the five battery charge indicator LEDs went off (5 ON LEDs indicate full charge).

So on the basis of this test, it would seem that the UPS is functioning as expected. It remains to be investigated if the various hardware/software interlocks in place will initiate the right sequence of valve closures when required.


Quote:
 

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

 

  13237   Mon Aug 21 23:38:55 2017 gautamUpdateALSALS out-of-loop noise

I worked a little bit on the Y arm ALS today. 

  • Started by locking the Y arm to IR with POY, and then ran the dither alignment script to maximize Y arm transmission.
  • Green TRY DC monitor was around 0.16, whereas I have seen ~0.45 when we were doing DRFPMI locking.
  • So I went to the Y end table and tweaked the steering mirrors a little. I was able to get GTRY to ~0.42. I think this can be tweaked a little further but I decided to push on for tonight.
  • The beat amplitude on the network analyzer in the control room is comparable to the X arm beat now.
  • Adjusted the gain of the phase tracker servos, cleared phase history.
  • Looking at the ALS beat noise with the arms locked to IR and the slow ALS temperature control loops ON (see Attachment #1), the current measurements line up quite well with the reference traces.

I am now going to measure the OLTFs of both green PDH loops to check that the overall loop gain is okay, and also check the measurement against EricQ's LISO model of the (modified) AUX green PDH servos. Results to follow.


Some weeks ago, I had moved some of the Green steering optics on the PSL table around, in order to flip some mirror mounts and try and get angles of incidence closer to ~45deg on some of the steering mirrors. As a result of this work, I can see some light on the GTRY CCD when the X green shutter is open. It is unclear if there is also some scattered light on the RFPDs. I will post pictures + a more detailed investigation of the situation on the PSL table later, there are multiple stray green beams on the PSL table which should probably be dumped.


As I was writing this elog, I saw the X green lock drop abruptly. During this time, the X arm stayed locked to the IR, and the Y arm beat on the control room network analyzer did not jump (at least not by an amount visible to the eye). Toggling the X end shutter a few times, the green TEM00 lock was re-acquired, but the beatnote has moved on the control room analyzer by ~40MHz. On Friday evening however, the X green lock held for >1 hour. Need to keep an eye on this.

  13238   Tue Aug 22 02:19:11 2017 gautamUpdateALSALS OLTFs

Attachment #1 shows the results of my measurements tonight (SR785 data in Attachment #2). Both loops have a UGF of ~10kHz, with ~55 degrees of phase margin.

Excitation was injected via SR560 at the PDH error point, amplitude was 35mV. According to the LED indicators on these boxes, the low frequency boost stages were ON. Gain knob of the X end PDH box was at 6.5, that of the Y end PDH box was at 4.9. I need to check the schematics to interpret these numbers. GV Edit: According to this elog, these numbers mean that the overall gain of the X end PDH box is approx. 25dB, while that of the Y end PDH box is approx. 15dB. I believe the Y end Lightwave NPRO has an actuator discriminant ~5MHz/V, while the X end Innolight is more like 1MHz/V.

Not sure what to make of the X PDH loop measurement being so much noisier than the Y end, I need to think about this.

More detailed analysis to follow.

Quote:

 

I am now going to measure the OLTFs of both green PDH loops to check that the overall loop gain is okay, and also check the measurement against EricQ's LISO model of the (modified) AUX green PDH servos. Results to follow.

 

  13239   Tue Aug 22 15:17:19 2017 ericqUpdateComputersOld frames accessible again

It turns out the problem was just a bent pin on the SCSI cable, likely from having to stretch things a bit to reach optimus from the RAID unit.frown

I hooked it up to megatron, and it was automatically recognized and mounted. yes

I had to turn off the new FB machine and remove it from the rack to be able to access megatron though, since it was just sitting on top. FB needs a rail to sit on!

At a cursory glance, the filesystem appears intact. I have copied over the achived DRFPMI frame files to my user directory for now, and Gautam is going to look into getting those permanently stored on the LDAS copy of 40m frames, so that we can have some redundancy.

Also, during this time, one of the HDDs in the RAID unit failed its SMART tests, so the RAID unit wanted it replaced. There were some spare drives in a little box directly under the unit, so I've installed one and am currently incorporating it back into the RAID.

There are two more backup drives in the box. We're running a RAID 5 configuration, so we can only lose one drive at a time before data is lost.

  13240   Tue Aug 22 15:40:06 2017 gautamUpdateComputersOld frames accessible again

[jamie, gautam]

I had some trouble getting the daqd processes up and running again using Jamie's instructions.

With Jamie's help however, they are back up and running now. The problem was that the mx infrastructure didn't come back up on its own. So prior to running sudo systemctl restart daqd_*, Jamie ran sudo systemctl start mx. This seems to have done the trick.

c1iscey was still showing red fields on the CDS overview screen so Jamie did a soft reboot. The machine came back up cleanly, so I restarted all the models. But the indicator lights were still red. Apparently the mx processes weren't running on c1iscey. The way to fix this is to run sudo systemctl start mx_stream. Now everything is green.

Now we are going to work on trying the fix Rolf suggested on c1iscex.

Quote:

It turns out the problem was just a bent pin on the SCSI cable, likely from having to stretch things a bit to reach optimus from the RAID unit.frown

I hooked it up to megatron, and it was automatically recognized and mounted. yes

I had to turn off the new FB machine and remove it from the rack to be able to access megatron though, since it was just sitting on top. FB needs a rail to sit on!

At a cursory glance, the filesystem appears intact. I have copied over the achived DRFPMI frame files to my user directory for now, and Gautam is going to look into getting those permanently stored on the LDAS copy of 40m frames, so that we can have some redundancy.

Also, during this time, one of the HDDs in the RAID unit failed its SMART tests, so the RAID unit wanted it replaced. There were some spare drives in a little box directly under the unit, so I've installed one and am currently incorporating it back into the RAID.

There are two more backup drives in the box. We're running a RAID 5 configuration, so we can only lose one drive at a time before data is lost.

 

  13242   Tue Aug 22 17:11:15 2017 gautamUpdateComputersc1iscex model restarts

[jamie, gautam]

We tried to implement the fix that Rolf suggested in order to solve (perhaps among other things) the inability of some utilities like dataviewer to open testpoints. The problem isn't wholly solved yet - we can access actual testpoint data (not just zeros, as was the case) using DTT, and if DTT is used to open a testpoint first, then dataviewer, but DV itself can't seem to open testpoints.

Here is what was done (Jamie will correct me if I am mistaken).

  1. Jamie checked out branch 3.4 of the RCG from the SVN.
  2. Jamie recompiled all the models on c1iscex against this version of RCG.
  3. I shutdown ETMX watchdog, then ran rtcds stop all on c1iscex to stop all the models, and then restarted them using rtcds start <model> in the order c1x01, c1scx and c1asx. 
  4. Models came back up cleanly. I then restarted the daqd_dc process on FB1. At this point all indicators on the CDS overview screen were green.
  5. Tried getting testpoint data with DTT and DV for ETMX Oplev Pitch and Yaw IN1 testpoints. Conclusion as above.

So while we are in a better state now, the problem isn't fully solved. 

Comment: seems like there is an in-built timeout for testpoints opened with DTT - if the measurement is inactive for some time (unsure how much exactly but something like 5mins), the testpoint is automatically closed.

  13243   Tue Aug 22 18:36:46 2017 gautamUpdateComputersAll FE models compiled against RCG3.4

After getting the go ahead from Jamie, I recompiled all the FE models against the same version of RCG that we tested on the c1iscex models.

To do so:

  • I did rtcds make and rtcds install for all the models.
  • Then I ssh-ed into the FEs and did rtcds stop all, followed by rtcds start <model> in the order they are listed on the CDS overview MEDM screen (top to bottom).
  • During the compilation process (i.e. rtcds make), for some of the models, I got some compilation warnings. I believe these are related to models that have custom C code blocks in them. Jamie tells me that it is okay to ignore these warnings at that they will be fixed at some point.
  • c1lsc FE crashed when I ran rtcds stop all - had to go and do a manual reboot.
  • Doing so took down the models on c1sus and c1ioo that were running - but these FEs themselves did not have to be robooted.
  • Once c1lsc came back up, I restarted all the models on the vertex FEs. They all came back online fine.
  • Then I ssh-ed into FB1, and restarted the daqd processes - but c1lsc and c1ioo CDS indicators were still red.
  • Looks like the mx_stream processes weren't started automatically on these two machines. Reasons unknown. Earlier today, the same was observed for c1iscey.
  • I manually restarted the mx_stream processes, at which point all CDS indicator lights became green (see Attachment #1).

IFO alignment needs to be redone, but at least we now have a (admittedly rounabout way) of getting testpoints. Did a quick check for "nan-s" on the ASC screen, saw none. So I am re-enabling watchdogs for all optics.

GV 23 August 9am: Last night, I re-aligned the TMs for single arm locks. Before the model restarts, I had saved the good alignment on the EPICs sliders, but the gain of x3 on the coil driver filter banks have to be manually turned on at the moment (i.e. the safe.snap file has them off). ALS noise looked good for both arms, so just for fun, I tried transitioning control of both arms to ALS (in the CARM/DARM basis as we do when we lock DRFPMI, using the Transition_IR_ALS.py script), and was successful.

Quote:

[jamie, gautam]

We tried to implement the fix that Rolf suggested in order to solve (perhaps among other things) the inability of some utilities like dataviewer to open testpoints. The problem isn't wholly solved yet - we can access actual testpoint data (not just zeros, as was the case) using DTT, and if DTT is used to open a testpoint first, then dataviewer, but DV itself can't seem to open testpoints.

Here is what was done (Jamie will correct me if I am mistaken).

  1. Jamie checked out branch 3.4 of the RCG from the SVN.
  2. Jamie recompiled all the models on c1iscex against this version of RCG.
  3. I shutdown ETMX watchdog, then ran rtcds stop all on c1iscex to stop all the models, and then restarted them using rtcds start <model> in the order c1x01, c1scx and c1asx. 
  4. Models came back up cleanly. I then restarted the daqd_dc process on FB1. At this point all indicators on the CDS overview screen were green.
  5. Tried getting testpoint data with DTT and DV for ETMX Oplev Pitch and Yaw IN1 testpoints. Conclusion as above.

So while we are in a better state now, the problem isn't fully solved. 

Comment: seems like there is an in-built timeout for testpoints opened with DTT - if the measurement is inactive for some time (unsure how much exactly but something like 5mins), the testpoint is automatically closed.

 

  13244   Tue Aug 22 23:27:14 2017 ranaUpdateALSALS OLTFs

Didn't someone look at what the OLG req. should be for these servos at some point? I wonder if we can make a parallel digital path that we switch on after green lock. Then we could make this a simple 1/f box and just add in the digital path (take analog control signal into ADC, filter, and then sum into the control point further down the path to the laser) for the low frequency boost.

  13245   Wed Aug 23 10:11:46 2017 SteveUpdateVACvacuum valve specifications

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

  13246   Wed Aug 23 17:22:36 2017 gautamUpdateALSFiber ALS - reinstalled

I completed the revamp of the box, and re-installed the box on the PSL table today. I think it would be ideal to install this on one of the electronic racks, perhaps 1X2 would be best. We would have to re-route the fibers from the PSL table to 1X2, but I think they have sufficient length, and this way, the whole arrangement is much cleaner.

Did a quick check to make sure I could see beat notes for both arms. I will now attempt to measure the ALS noise with this revamped box, to see if the improved power supply and grounding arrangement, as well as fiber cleaning, has had any effect.

Photos + power budget + plan of action for using this box to characterize the green PDH locking to follow. 

For quick reference: here is the AM/PM measurement done when we re-installed the repaired Innolight NPRO on the new X endtable.

  13248   Thu Aug 24 00:39:47 2017 gautamUpdateLSCDRMI locking attempt

Since the single arm locking and dither alignment seemed to work alright after the CDS overhaul, I decided to try some recycling cavity locking tonight.

  • First, I locked single arms, ran dither alignment servos, and centered all test mass Oplevs. Note: the X arm dither alignment doesn't seem to work if we use the High-Gain Thorlabs PD as the Transmission PD. The BS loops just seem to pick up large offsets and the alignment actually degrades over a couple of minutes. This needs to be investigated.
  • Next, to get good PRM alignment, I manually moved the EPICS sliders till the REFL spot became roughly centered on the CCD screen.
  • Then I tried locking PRMI on carrier using the usual C1IFOConfigure script - the lock was caught within ~30 seconds.
  • The PRCL and MICH dither servo scripts also ran fine.
    • Centered PRM Oplev.
  • Next, I tried enabling the PRC angular feedforward.
    • OAF model does not automatically revert to its safe.snap configuration on model reboot, so I first manually did this such that the correct filter banks were enabled.
    • I was able to turn on the angular feedforward without disturbing the PRMI carrier lock. The angular motion of the POP spot on the CCD monitor was visibly reduced.
  • At this point I decided to try DRMI locking.
    • I centered the beam on the AS PDs with the simple Michelson.
    • Centered the beam on the REFL PDs with PRM aligned and PRC flashing through resonances.
    • Restored SRM alignment by eye with EPICS sliders.
    • Cavity alignment seemed alright - so I tried to lock DRMI with the old settings (i.e. from DRMI 1f locking a couple of months ago). But I had no success.
    • The behaviour of REFL55 (used for SRCL control) has changed dramatically - the analog whitening gain for this PD used to be +18dB, but at this setting, there are frequent ADC overflows. I had to reduce the whitening gain to +6dB to stop the ADC overflows. I also checked to make sure that the whitening setting was "manual" and not triggered.

Why should this have changed? I was just on the AS table and did re-center the beam onto the REFL 55 RFPD, but I had also done this in April/May when I was last doing DRMI locking. But I can't explain the apparent factor of ~4 increase in light level. I think I have some measurements of the light levels at various PDs from April 2017, I will see how the present levels line up.

Of course dataviever won't cooperate when I am trying to monitor testpoints.

I may be missing something obvious, but I am quitting for tonight, will look into this more tomorrow.


Unrelated to this work: looking at the GTRY spot on the CCD monitor, there seems to be some excess angular motion. Not sure where this is coming from. In the past, this sort of problem has been symptomatic of something going wonky with the Oplev loops. But I took loop measurements for ITMY and ETMY PIT and YAW, they look normal. I will investigate further when I am doing some more ALS work.

  13249   Thu Aug 24 17:36:11 2017 gautamUpdateCDSFSS Slow Python maintenance

A couple of weeks ago, I was trying to modernize the python version of the FSS Slow temperature control loops, when I accidentally ended up deleting it frown. There was no svn backup. So the old Perl PID script has been running for the last few days.

Today, I checked out the latest version that Andrew and co. have running in the PSL lab. I had to make some important modifications for the script to work for the 40m setup.

  1. The script is conveniently setup in a way that the channels it needs to read from / write to are read in from an .ini file. I renamed all the channels to match the appropriate 40m ones.
  2. We don't have a soft epics channel in which to define the setpoint for our PID servo (which is 0). Rather than poke around with slow machine EPICS records, I simply commented out this line in the script and included the hard-coded value of 0. When we modernize to the Acromag era, we can setup an EPICS channel + MEDM slider for the setpoint.
  3. The way the Perl script was setup, the error signal was pre-scaled by a factor of 0.01, supposedly to make the PID gains be of order 1. For consistency, I re-inserted this scaling, which awade and co. had removed.
  4. Modified the FSSslowPy.init file to call the script in accordance with the new syntax:
python FSSSlow.py -i FSSSlowPy.ini

Then I stopped the Perl process on megatron by running

sudo initctl stop FSSslow

and started the Python process by running

sudo initctl start FSSslowPy

I have now committed the files FSSSlow.py and FSSSlowPy.ini to the 40m svn.  Things seem to be stable for the last 20 mins or so, let's keep an eye on this though - although we had been running the Python PID loop for some months, this version is a slightly modified one. 

The initctl stuff still isn't very robust - I think both the Autolocker and the FSS slow servos have to be manually restarted if megatron is shutdown/restarted for whatever reason. It doesn't seem to be a problem with the initctl routine itself - looking at the logs, I can see that init is trying to start both processes, but is failing to do so each time. To be investigated. The wiki procedure to restart this process is up to date.

GV Edit 0000 25 Aug 2017: I had to add a line to the script that checks MC transmission before enabling the PID loop. Change has been committed to svn. Now, when the MC loses lock or if the PSL shutter is kept closed for an extended period of time, the temperature loop doesn't rail.

  13252   Fri Aug 25 01:20:52 2017 gautamUpdateLSCDRMI locking attempt

I tried some DRMI locking again tonight, but had no success. Here is the story.

  • I started out by going to the AS table and measuring the light level on the REFL55 photodiode (with PRM aligned and the PRC flashing, but LSC disabled).
    • The Ophir power meter reads 13mW
    • The DC output of the photodiode shows ~500mV on an oscilloscope.
    • Both of these numbers line up well with measurements I made in April/May.
  • Returned to the control room and aligned the IFO for DRMI locking - but LSC servos remained disabled.
    • At the nominal REFL55 whitening level of +18dB, the REFL 55 signals saturated the ADC (confirmed by looking at the traces on dataviewer).
    • But the signals still looked like PDH error signals.
    • Lowering the whitening gain to 6dB makes the PDH error signal horns peak around 20,000 counts.
    • Could this be indicative of problems with either the analog whitening gain switching or the LSC Demod Boards? To be investigated.
  • Tried enabling LSC servos with same settings with which I had success right up till a couple of months ago, but had no success.
    • If it is true that the REFL55 signal is getting amplified because of some gain stage not being switched correctly, I should still have been able to lock the SRC with a lowered loop gain - but even lowering the gain by a factor of 10 had no effect on the locking success rate.

Looks like I will have to embark on the REFL55 LSC electronics investigation. I was able to successfully lock the PRC on carrier and sideband, and the Michelson lock also seems to work fine, all of which seem to point to a hardware problem with the REFL55 signal chain.

I did a quick check by switching the output of the REFL55 demod board to the inputs normally used by AS55 signals on the whitening board. Setting the whitening gain to +18dB for these channels had the same effect - ADC overflow galore. So looks like the whitening board isn't to blame. I will have to check the demod board out.

 

  13253   Fri Aug 25 11:11:26 2017 gautamUpdateGeneralMC1 kicked again

Looks like MC1 got another big kick just under 4 hours ago. None of the other optics show any evidence of a glitch so it seems unlikely that this was some sort of global event. It's been well behaved for ~2weeks now. IMC was unlocked. I manually re-aligned MC1, at which point the autolocker was able to lock the IMC.

Looking at this plot, it seems that LR and UL coils seem to have the largest kicks. UR barely saw it. Not sure what (if anything) to make of this - apparently the optic moved by ~20urad with the UR magnet approximately the pivot.

  13254   Fri Aug 25 15:54:14 2017 gautamUpdateALSFiber ALS noise measurement

[Kira, gautam]

Attachment #1 - Photo of the revamped beat setup. The top panel has to be installed. New features include:

  • Regulated power supply via D1000217.
  • Single power switch for both PDs.
  • Power indicator LED.
  • Chassis ground isolated from all other electronic grounds. For this purpose, I installed all the elctronics on a metal plate which is only connected to the chassis via nylon screws. The TO220 package power regulator ICs have been mounted with the TO220 mounting kits that provide a thin piece of plastic that electrically insulates its ground from the chassis ground.
  • PD outputs routed through 20dB coupler on front panel for diagnostic purposes.
  • Fiber routing has been cleaned up a little. I installed a winding fixture I got from Johannes, but perhaps we can install another one of these on top of the existing one to neaten up the fiber layout further.
  • 90-10 light splitter (meant for diagnostic purposes) has been removed because of space constraints. 

Attachment #2 - Power budget inside the box. Some of these FC/APC connectors seem to not offer good coupling between the two fibers. Specifically, the one on the front panel meant to accept the PSL light input fiber seems particularly bad. Right now, the PSL light is entering the box through one of the front panel connectors marked "PSL + X out". I've also indicated the beat amplitude measured with an RF analyzer. Need to do the math now to confirm if these match the expected amplitudes based on the power levels measured.

Attachment #3 - We repeated the measurement detailed here. The X arm (locked to IR) was used for this test. The "X" delay line electronics were connected to the X green beat PD, while the "Y" delay line electronics were connected to the X IR beat PD. I divided the phase tracker Hz calibration factor by 2 to get IR Hz for the Y arm channels. IR beat was at ~38MHz, green beat was at ~76MHz. The broadband excess noise seen in the previous test is no longer present. Indeed, below ~20Hz, the IR beat seems less noisy. So seems like the cleaning / electronics revamp did some good. 

Further characterization needs to be done, but the results of this test are encouraging. If we are able to get this kind of out of loop ALS noise with the IR beat, perhaps we can avoid having to frequently fine-tune the green beat alignment on the PSL table. It would also be ideal to mount this whole 1U setup in an electronics rack instead of leaving it on the PSL table.

Quote:

Photos + power budget + plan of action for using this box to characterize the green PDH locking to follow. 

GV Edit: I've added better photos to the 40m Google Photos page. I've also started a wiki page for this box / the proposed IR ALS  system. For the moment, all that is there is the datasheet to the Fiber Couplers used, I will populate this more as I further characterize the setup.

  13255   Fri Aug 25 17:11:07 2017 ranaUpdateALSFiber ALS noise measurement

Is it better to mount the box in the PSL under the existing shelf, or in a nearby PSL rack?

Quote:

 

Further characterization needs to be done, but the results of this test are encouraging. If we are able to get this kind of out of loop ALS noise with the IR beat, perhaps we can avoid having to frequently fine-tune the green beat alignment on the PSL table. It would also be ideal to mount this whole 1U setup in an electronics rack instead of leaving it on the PSL table

 

  13257   Sun Aug 27 11:57:31 2017 ranaUpdateALSFiber ALS noise measurement

It seems like the main contribution to the RMS comes from the high frequency bump. When using the ALS loop to lock the arm to the beat, only the stuff below ~100 Hz will matter. Interesting to see what that noise budget will show. Perhaps the discrepancy between inloop and out of loop will go down.

  13260   Mon Aug 28 10:28:07 2017 SteveUpdateVACRGA scan 20 day after 17 Torr

The RGA was turned on 7 days ago.  It's 46 C now.   The X-arm room tem ~20 C

IFO pressure 6.5e-6 Torr at IT-Hornet gauge. Valve configuration vacuum normal.

  13261   Mon Aug 28 10:51:21 2017 steveUpdateSUSETMX damping recovered
  13262   Mon Aug 28 16:20:00 2017 gautamUpdateCDS40m files backup situation

This elog is meant to summarize the current backup situation of critical 40m files.

What are the critical filesystems? I've also indicated the size of these disks and the volume currently used, and the current backup situation. 

Name

Disk Usage

Description / remarks

Current backup status

FB1 root filesystem 1.7TB / 2TB
  • FB1 is the machine that hosts the diskless root for the front end machines
  • Additionally, it runs the daqd processes which write data from realtime models into frame files
Not backed up
/frames up to 24TB
  • This is where the frame files are written to 
  • Need to setup a wiper script that periodically clears older data so that the disk doesn't overflow.

Not backed up 

LDAS pulls files from nodus daily via rsync, so there's no cron job for us to manage. We just allow incoming rsync.

Shared user area 1.6TB / 2TB
  • /home/cds on chiara
  • This is exported over NFS to 40m workstations, FB1 etc.
  • Contains user directories, scripts, realtime models etc.

Local backup on /media/40mBackup on chiara via daily cronjob

Remote backup to ldas-cit.ligo.caltech.edu::40m/cvs via daily cronjob on nodus

Chiara root filesystem 11GB / 440GB
  • This is the root filesystem for chiara
  • Contains nameserver stuff for the martian network, responsible for rsyncing /home/cds
Not backed up
Megatron root filesystem 39GB / 130GB
  • Boot disk for megatron, which is our scripts machine
  • Runs MC autolocker, FSS loops etc.
  • Also is the nds server for facilitating data access from outside the martian network
Not backed up
Nodus root filesystem 77GB / 355GB
  • This is the boot disk for our gateway machine
  • Hosts Elog, svn, wikis
  • Supposed to be responsible for sending email alerts for NFS disk usage and vacuum system N2 pressure
Not backed up
JETSTOR RAID Array 12TB / 13TB
  • Old /frames
  • Archived frames from DRFPMI locks
  • Long term trends

Currently mounted on Megatron, not backed up.

Then there is Optimus, but I don't think there is anything critical on it. 

So, based on my understanding, we need to back up a whole bunch of stuff, particularly the boot disks and root filesystems for Chiara, Megatron and Nodus. We should also test that the backups we make are useful (i.e. we can recover current operating state in the event of a disk failure).

Please edit this elog if I have made a mistake. I also don't have any idea about whether there is any sort of backup for the slow computing system code.

  13263   Mon Aug 28 17:13:57 2017 ericqUpdateCDS40m files backup situation

In addition to bootable full disk backups, it would be wise to make sure the important service configuration files from each machine are version controlled in the 40m SVN. Things like apache files on nodus, martian hosts and DHCP files on chiara, nds2 configuration and init scripts on megatron, etc. This can make future OS/hardware upgrades easier too.

  13264   Mon Aug 28 23:22:56 2017 johannesUpdatePSLPSL table auxiliary NPRO

I moved the axuiliary NPRO to the PSL table today and started setting up the optics.

The Faraday Isolator was showing a pretty unclean mode at the output so I took the polarizers off to take a look through them, and found that the front polarizer is either out of place or damaged (there is a straight edge visible right in the middle of the aperture, but the way the polarizer is packaged prevents me from inspecting it closer). I proceeded without it but left space so an FI can be added in the future. The same goes for the broadband EOM.

There are two spare AOMs (ISOMET and Intraaction, both resonant at 40MHz) available before we have to resort to the one currently installed in the PSL.

I installed the Intraaction AOM first and looked at the switching speed of its first order diffracted beam using both its commercial driver and a combination of minicircuits components. Both show similar behavior. The fall time of the initial step is ~110ns in both cases, but it doesn't decay rapidly no light but a slower exponential. Need to check the 0 order beam and also the other AOM.

Intraaction Driver

   

Mini Circuits Drive

   

  13265   Tue Aug 29 01:52:22 2017 gautamUpdateSUSTest mass actuator calibration

[ericq, gautam]

Tonight, we decided to double-check the POX counts-to-meters conversion.

It is unclear when this was last done, and since I modified the coil driver electronics for the ITMs and BS recently, I figured it would be useful to get this calibration done. The primary motivation was to see if we could resolve the discrepancy between the current ALS noise (using POX as a sensor) compared to the Izumi et. al. plot.

Because we are planning to change the coil driver electronics further soon anyways, we decided to do the calibration at a single frequency for tonight. For future reference, the extension of this method to calibrate the actuator over a wider range of frequencies is here. The procedure followed, and the relevant numbers from tonight, are as follows.

Procedure:

  1. Set dark offsets on all DCPDs and LSC PDs.
  2. Look at the free swinging Michelson signal on ASDC.
    • For tonights test, ASDC was derived from the AS55 photodiode.
    • The AS110 photodiode actually has more light on it, but we think that the ADC that the DCPD board is interfaced to is running on 0-2V rather than 0-10V, as the signal seemed to saturate around 2000 counts. It is unclear whether the actual photodiode is saturating, to be investigated.
    • So we decided to use ASDC from AS55 photodiode with 15dB whitening gain.
    • There is also some issue with the whitening filter (not whitening gain) on ASDC - engaging the whitening shifts the DC offset. This has to be investigated while we get stuck into the LSC electronics.
  3. Look at the peak-to-peak swing of ASDC. Use algebraic expression for reflected power from Michelson interferometer to calibrate the ASDC slope at Michelson half-fringe. For the test tonight, ASDC_max = 1026 counts, ASDC_min = 2 counts.
  4. Lock the Michelson at half-fringe, with ASDC as the error signal.
    • Zero out the MICH elements in the RFPD input matrix.
    • Set the matrix element from ASDC to MICH in the DCPD LSC input matrix to 1.
    • The servo gain used was +0.005 on the MICH_A servo path.
    • A low-frequency boost was turned on.
  5. Use the sensing matrix infrastructure to drive a line in the optic of interest.
    • Tonight, we looked at ITMX and ITMY.
    • The line was driven at 311.1Hz, and the amplitude was 300 counts.
    • Download 60secs of ASDC data, demodulate at the driven frequency to find the peak height in counts, and using the slope of ASDC (in cts/m) at the Michelson half-fringe, calculate the actuator gain in m/cts.
    • ITMY: 2.55e-9 / f^2 m/count
    • ITMX: 2.65e-9 / f^2 m/count
    • These numbers kind of make sense - the previous numbers were ~5nm/f^2 /ct, but I removed an analog gain of x3 in this path. Presumably there has been some change in the N/A conversion factor - perhaps because of a change in the interaction between the optics' face magnets and the static magnetic field in the OSEMs?
  6. Lock the arms with POX/POY, and drive the newly calibrated ITMs.
    • So we know how many meters we are driving the ITMs by.
    • Looking at POX/POY, we can calibrate these into meters/count.
    • Both POX and POY were whitened.
    • POX whitening gain = +30dB, POY whitening gain = +18dB.
    • ITMX and ITMY were driven at 311.1Hz, with amplitude = 2counts.
    • Download 60 secs of data, demodulate at the drive frequency to find the peak height, and use the known ITM actuator gains to calibrate POX and POY.
    • POX: 7.34e-13 m / count (approx. 5 times less than the number in the Foton filter bank in the C1:CAL-CINV model).
    • POY: 1.325e-13 m / count
    • We did not optimize the demod phases for POX/POY tonight. 

Once these calibrations were updated, we decided to control the arms with ALS, and look at the POX spectrum. Y-arm ALS wasn't so stellar tonight, especially at low frequencies. I can see the GTRY spot moving on the CCD monitor, so something is wonky. To be investigated. But the X arm ALS noise looked pretty good.

Seems like updating the calibration did the job; see the attached comparison plot.

  13266   Tue Aug 29 02:08:39 2017 gautamUpdateALSFiber ALS noise measurement

I was having a chat with EricQ about this today, just noting some points from our discussion down here so that I remember to look into this tomorrow.

  • I believe that currently, the channels C1:ALS-BEATX_FINE_PHASE_OUT_HZ_DQ and the Y arm analog read out the frequency of the green beat, in Hz.
  • In the comparison I plotted, I WRONGLY divided the spectrum of the IR beat by 2, instead of multiplying in by 2, which is what should actually be done for an apples-to-apples comparison.
  • The deeper question is, what should this channel actually readout?
  • Looking at my codes from past arm scans etc, I see that I am dividing the downloaded data by 2 in order to convert the X-axis of these scans to "IR Hz". But this should really be all we care about.
  • So I think I will have to re-do the cts-to-Hz calibration in the ALS models. It should be possible to do ~10FSR scans with the IR beat, and then we can use the sideband resonances (presumably the sideband frequencies are known with better precision than the arm length, and hence the FSR) to calibrate the phase tracker.
  • I don't think this changes the fact that the Fiber ALS situation has been improved - but I will have to repeat the measurement to be sure. The improvement may not be as stellar as I tried to sell in my previous elog sad.

    Other thoughts: 

  • Can we make use of the Jetstor raid array for some kind of consolidated 40m CDS backup system? Once we've gotten everything of interest out of it...

  13267   Tue Aug 29 15:04:59 2017 gautamUpdateSUSETMY Oplev PIT loop gain changed

Last night, while we were working on the ALS, I noticed the GTRY spot moving around (in PITCH) on the CCD monitor in the control room at ~1-2Hz. The operating condition was that the arm was locked to the IR, and the PSL green shutter was closed, so that only the arm transmissions were visible on the CCD screens. There was no such noticable movement of the GTRX spot. When looking at the out-of-loop ALS nosie in this configuration (but now with the PSL green shutter open of course), the Y arm ALS noise at low frequencies was much worse than the X arm.

Today, I looked into this a little more. I first checked that the Y-endtable enclosure was closed off as usual (as I had done some tweaking to the green input pointing some days ago). There are various green ghost beams on the Y-endtable. When time permits, we should make an effort to cleanly dump these. But the enclosure was closed as usual.

Then I looked at the in-loop Oplev error signal spectra for the ITMY and ETMY Oplev loops. There was high coherence between ETMYP Oplev error signal and GTRY. So I took a loop transfer function measurement - the upper UGF was around 3.5Hz. I increased the loop gain such that the upper UGF was around 4.5Hz, with phase margin ~30degrees. Doing so visibly reduced the angular movement of the GTRY spot on the CCD. Attachment #1 shows the Oplev loop TF after the gain increase, while Attachment #2 compares the GTRX and GTRY spectra (DC value is approximately the same for both, around 0.4). GTRY still seems a bit noisier at low frequencies, but the out-of-loop ALS noise for the Y arm now lines up much more closely with its reference trace from a known good time. 

Quote:
 

Y-arm ALS wasn't so stellar tonight, especially at low frequencies. I can see the GTRY spot moving on the CCD monitor, so something is wonky. To be investigated.

 

  13268   Tue Aug 29 15:35:19 2017 SteveUpdateVACvacuum pump specifications & manuals

RP1 and RP3 roughing pump manual of Leybold D30A oily rotory pump

Fore pump of TP2 & TP3 Varian SH-100 Dry Scroll

TP2 and TP3 small turbo drag pump  Varian 969-9361 

TP2 and TP3 turbo controller Varian 969-9505

TP1 magnetically suspended turbo pump  Osaka TG390MCAB, sn360 and controller TC010M  and note : this  pump  running on 208VAC single phaseIt is not on the UPS !  

                                                             Osaka Maglev Manual        and Osaka Controller Communication Wiring                                                                                                                                

VC1 cryo pump CTI-Cryogenics Cryo Torr 8 sn 8g23925  SAFETY note: compressor single phase 208VAC and the head driver 3 phase 208VAC Compressor and driver have each separate power cord!

Installed at 40m wiki  also

Quote:

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

 

  13270   Tue Aug 29 20:04:09 2017 ranaUpdatePSLPSL table auxiliary NPRO

I don't understand why the 1st order diffracted beam doesn't go to zero when you shut off the drive. My guess is that the standing acoustic wave in the AO crystal needs some time to decay: f = 40 MHz, tau = 1 usec... Q ~ 100. Perhaps, the crystal is damped by the PZT and ther output impedance of the mini-circuits switch is different from the AO driver.

In any case, if you need a faster shut off, or want something that more cleanly goes to zero, there is a large (~1 cm) aperture Pockels cell that Frank Siefert was using for making pulses to damage photo diodes. There is a DEI Pulser unit near the entrance to the QIL in Bridge which can drive it.

  13271   Tue Aug 29 21:36:59 2017 johannesUpdatePSLPSL table auxiliary NPRO
Quote:

 there is a large (~1 cm) aperture Pockels cell that Frank Siefert was using for making pulses to damage photo diodes. There is a DEI Pulser unit near the entrance to the QIL in Bridge which can drive it.

I'll look for it tomorrow, but I haven't given up on the AOMs yet. I swapped in the ISOMET modulator today and saw the same behavior, both in 0th and 1st order. The fall time is pretty much identical. Gautam saw no such thing in the PSL AOM using the same photodetector.

1st order diffracted                                                          0th order

     

In the meantime I prepared the fiber mode-matching but realized in the process that I had mixed up some lenses. As a result the beam did not have a waist at the AOM location and thus didn't have the intended size, although I doubt that this would cause the slower decay. I'll fix it tomorrow, along with setting up the fiber injection, beat note with the PSL, and routing the fiber if possible.

  13273   Wed Aug 30 10:54:26 2017 gautamUpdateCDSslow machine bootfest

MC autolocker and FSS loops were stuck because c1psl was unresponsive. I rebooted it and did a burtrestore to enable PSL locking. Then the IMC locked fine.

c1susaux and c1iscaux were also unresponsive so I keyed those crates as well, after taking the usual steps to avoid ITMX getting stuck - but it still got stuck when the Sat. Box. connectors were reconnected after the reboot, so I had to shake it loose with bias slider jiggling. This is annoying and also not very robust. I am afraid we are going to knock the ITMX magnets off at some point. Is this problem indicative of the fact that the ITMX magnets were somehow glued on in a skewed way? Or can we make the situation better by just tweaking the OSEM-holding fixtures on the cage?

In any case, I've started listing stuff down here for things we may want to do when we vent next.

 

  13275   Wed Aug 30 15:00:06 2017 gautamUpdateGeneralEdgeswitch fiber swap

A couple of minutes ago, Larry W swapped the fibers to our 40m Edgeswitch (BROCADE FWS 648G) to a faster connection. This is the switch to which our gateway machine, NODUS, is connected. The actual swap itself happened at the core router in Bridge, and took only a few seconds. After the switch, I double checked that I was able to ssh into nodus from my laptop, and Larry informed me that everything is working as expected on his end.

Larry also tells us that the other edgeswitch at the 40m (Foundry Networks), to which most of our GC network machines are connected, is a 100MBPS switch, and so we should re-route the connections from this switch to the BROCADE switch at our convenience to take advantage of the faster connection.

  13276   Wed Aug 30 19:49:33 2017 gautamUpdateLSCREFL55 demod board debugging

Summary:

Today I tried debugging the mysterious increase in REFL55 signal levels in the DRMI configuration. I focused on the demod board, because last week, I had tried routing these signals through different channels on the whitening board, and saw the same effect. 

Based on my tests, everything on the Demod board seems to work as expected. I need to think more about what else could be happening here - specifically do a more direct test on the whitening board.

Details:

  • The demod board is a modified D990511 (marked up schematic + high-res photo to follow).
  • Initially, I tried probing the LO signal levels at various points with the board in the eurocrate itself, with the help of an extender card.
  • But this wasn't very convenient, so I pulled the board out to the office area for more testing.
  • The 55MHz LO signal going into the board is ~0dBm (measured with Agilent network analyzer)
  • I used the active probe to check the LO levels at various points along the signal chain, which mostly consists of attenuators, ERA-5SM amplifiers, and some splitters/phase rotators.
  • Everything seemed consistent with the expected levels based on "typical" numbers for gains and insertion losses cited in the datasheets for these devices.
  • I couldn't directly measure the level at the LO input to the mixer, but measuring the input to the ERA-5SM immediately before the mixer, barring problems with this amplifier, the LO input of the mixer is being driven at >17dBm which is what it wants.
  • Next, I decided to check the gain, gain imbalance and orthogonality of the demodulation.
  • For this purpose, I restored the board to the Eurocrate, reconnected the LO input to the board, and used a second Marconi at a slightly offset frequency to drive the PD input at ~0dBm.
  • Attachment #1 - The measured outputs look pretty balanced and orthogonal. The gain is consistent with an earlier measurement I made some months ago, when things were "normal". More bullets added after Rana's questions:
    • 300 MHz bandwidth oscilloscope used to acquire the data
    • I and Q outputs were from the daughter board
    • Data was acquired via ethernet data download utility
    • 20 MHz low-pass filter turned on on the Oscilloscope while downloading the data
Quote:

I did a quick check by switching the output of the REFL55 demod board to the inputs normally used by AS55 signals on the whitening board. Setting the whitening gain to +18dB for these channels had the same effect - ADC overflow galore. So looks like the whitening board isn't to blame. I will have to check the demod board out.

 


All connections have been restored untill further debugging later in the evening.

  13278   Thu Aug 31 00:19:35 2017 rana[^r]UpdatePSLIMC/FSS FAST gain

nominal changed from 22 to 23 dB to minimize PC drive RMS

previous loop gain measurement is sort of bogus (made on SR785); need some 4395 loop measurements and checking of crossover and error point spectrum

  13280   Thu Aug 31 00:52:52 2017 gautamUpdateLSCREFL55 whitening board debugging

[rana,gautam]

We did an ingenious checkup of the whitening board tonight.

  • The board is D990694
  • We made use of a tip-tilt DAC channel for this test (specifically TT1 UL, which is channel 1 on the AI board). We disconnected the cable going from the AI board to the TT coil driver board.
    • as opposed to using a function generator to drive the whitening filter, this approach allows us to not have to worry the changing offsets as we switch the whitening gain.
    • By using the CDS system to generate the signal and also demodulate it, we also don't have to worry about the drive and demod frequencies falling out of sync with each other.
  • The test was done by injecting a low frequency (75.13 Hz, amplitude=0.1) excitation to this DAC channel, and using the LSC sensing matrix infrastructure to demodulate REFL55 I and Q at this frequency. Demod phases in these servos were adjusted such that the Q phase demodulated signal was minimized.
  • An excitation was injected using awggui into TT1 UL exc channel.
  • We then stepped the whitening gains for REFL55_I and REFL55_Q in 3dB steps, waiting 5 seconds for each step. Syntax is z step -s 5 C1:LSC-REFL55_I_WhiteGain +1.0,15 C1:LSC-REFL55_Q_WhiteGain +1.0,15
  • Attachment #1 suggests that the whitening filter board is working as expected (each step is indeed 3dB and all steps are equal to the eye).
  • Data + script used to generate this plot is in Attachment #2.

I've restored all connections at that we messed with at the LSC rack to their original positions.

The TT alignment seems to be drifting around more than usual after we disconnected one of the channels - when I came in today afternoon, the spot on the AS camera had drifted by ~1 spot diameter so I had to manually re-align TT1. 

Quote:
 

Based on my tests, everything on the Demod board seems to work as expected. I need to think more about what else could be happening here - specifically do a more direct test on the whitening board.

  13281   Thu Aug 31 03:31:15 2017 gautamUpdateLSCDRMI re-locked!

After our Demod/Whitening electronics investigations suggested nothing obviously wrong, I decided to give DRMI locking another go tonight.

Surprisingly, there was no evidence of REFL55 behaving weirdly tonight, and I was able to easily lock the DRMI on 1f error signals using the recipe I've been using in the last few months.

Not sure what to make of all this frown.

I got in a ~15 minute lock, but I wasn't prepared to do any sort of characterization/ sensing / attempt to turn on coil-dewhitening, and I'm too tired to try again tonight. I was however able to whiten the error signals, as I have been able to do in the past. There is a ~45Hz bump in MICH that I haven't seen in the past.

I'll try and do some characterization tomorrow eve, but it's encouraging to at least get back to the pre-FB-failure state of locking.

  13282   Thu Aug 31 18:36:23 2017 gautamUpdateCDSrevisiting Acromag

Current status:

  • There is a single Acromag ADC unit installed in 1X4
  • It is presently hooked up to the PSL NPRO diagnostic connector channels
  • I had (re)-started the acquisiton of these channels on August 16 - but for reasons unknown, the tmux session that was supposed to be running the EPICS server on megatron seems to have died on August 22 (judging by the trend plot of these channels, see Attachment #1)
  • I had not set up an upstart job that restarts the server automatically in such an event. I manually restarted it for now, following the same procedure as linked in my previous elog.
  • While I was at it, I also took the opportunity to edit the Acromag channel names to something more appropriate - all channels previously prefixed with C1:ACRO- have now been prefixed with C1:PSL-

Plan of action:

  1. Hardware - we have, in the lab, in addition to the installed ADC unit
    • 3x 8 channel differential input ADC units
    • 2x 8 channel differential output DAC units
    • 1x 16 channel BIO unit
    • 2U chassis + connectors + breakout boards + other misc hardware that I think Johannes and Lydia procured with the original plan to replace the EX slow controls.
    • Some relevant elogs: Panel designs, breakout design, sketch for proposed layout, preliminary channel list.
      So on the hardware side, it would seem that we have everything we need to go ahead with replacing the EX slow controls with an Acromag system, although Johannes probably knows more about our state of readiness from a hardware PoV.
  2. Software
    • We probably want to get a dedicated machine that will handle the EPICS channel serving for the Acromag system
    • Have to figure out the networking arrangement for such a machine
    • Have to figure out how to set up the EPICS server protocol in such a way that if it drops for whatever reason, it is automatically restarted

 

  13283   Thu Aug 31 21:40:24 2017 gautamUpdateGeneralMC1 kicked again

There was a pretty large glitch in MC1 about an hour ago. The misalignment was so large that the autolocker wasn't able to lock the IMC. I manually re-aligned MC1 using the bias sliders, and now IMC locks fine. Attached is a 90 second plot of 2K data from the OSEMs showing the glitch. Judging from the wall StripTool, the IMC was well behaved for ~4 hours before this glitch - there is no evidence of any sort of misalignment building up, judging from the WFS control signals.

  13284   Fri Sep 1 08:25:08 2017 SteveUpdateSUSMC1 glitching

MC1, MC2 and MC3 damping turned off to see glitching action at 9:57am

Quote:

There was a pretty large glitch in MC1 about an hour ago. The misalignment was so large that the autolocker wasn't able to lock the IMC. I manually re-aligned MC1 using the bias sliders, and now IMC locks fine. Attached is a 90 second plot of 2K data from the OSEMs showing the glitch. Judging from the wall StripTool, the IMC was well behaved for ~4 hours before this glitch - there is no evidence of any sort of misalignment building up, judging from the WFS control signals.

 

  13285   Fri Sep 1 15:46:12 2017 KiraUpdatePEMtemp sensor update

I took off the AD590 and attached it to two long wires leading out from the board. This will allow us to attach the sensor to a metal block and not have to stick the whole board to it. I have also completed three identical copies of this and it's pretty much ready to be tested. According to Craig and Andrew's elog here, the sensor is very noisy and they added in a low pass filter to fix that, so that's something to consider for the final version of the circuit. I'll test what I have so far and see how that goes. We still need to figure out how to get readings from the sensors.

To attach the sensor to the metal block, I'll use some thermal paste and fasteners. I'll also put a thermometer on the block to record the actual temperature. I'll then wrap it in some insulation we have in the lab and have only some wires leading out of it to make measurements. I'll leave this setup overnight and record the outputs for about a full day. The fluctuations between the sensors will then indicate the noise of each individual sensor.

  13286   Fri Sep 1 16:27:39 2017 gautamUpdateSUSMC1 glitching

I re-enabled the MC SUS damping and IMC locking for some IFO work just now.

Quote:

MC1, MC2 and MC3 damping turned off to see glitching action at 9:57am

 

ELOG V3.1.3-