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ID Date Author Type Category Subject
  15871   Fri Mar 5 16:24:24 2021 gautamUpdateLSCREFL55 demod board re-installed in 1Y2

I don't have a good explanation why, but I too measured similar numbers to what Koji measured. The overall conversion gain for this board (including the +20dB gain from the daughter board) was measured to be ~5.3 V/V on the bench, and ~16000 cts/V in the CDS system (100Hz offset from the LO frequency). It would appear that the effective JMS-1-H conversion loss is <2dB. Seems fishy, but I can't find anything else obviously wrong with the circuit (e.g. a pre-amp for the RF signal that I missed, there is none).

I also attach the result of the measured noise at the outputs of the daughter board (i.e. what is digitized by the ADC), see Attachment #2. Apart from the usual forest of lines of unknown origin, there is still a significant excess above the voltage noise of the OP27, which is expected to be the dominant noise source in this configuration. Neverthelesss, considering that we have only 40dB of whitening gain, it is not expected that we see this noise directly in the digitized signal (above the ADC noise of ~1uV/rtHz). Note that the measured noise today, particularly for the Q channel,  is significantly lower than before the changes were made

  15870   Fri Mar 5 15:32:53 2021 KojiSummaryElectronicsA bunch of electronics received

The parts will be ordered by Koji The components for the additional BIO I/F have been ordered.

  15869   Fri Mar 5 15:31:23 2021 KojiUpdateLSCREFL55 demod board rework

Missed to note: The IF test was done at TP7 and TP6 using pomona clips i.e. brefore the preamp.

 

  15868   Fri Mar 5 15:03:28 2021 gautamSummaryElectronicsA bunch of electronics received

The PCBs for the D1002593 BIO I/F (5pcs ea of D1001050 and D1001266) were received (from JLCPCB) today. idk what the status of the parts (digikey?) is.

Quote:

Received additional front/rear panels. Updated the original entry and Wiki [Link]

  15867   Fri Mar 5 13:53:57 2021 gautamUpdateLSCREFL55 demod board rework

0 dBm ~ 0.63 Vpp. I guess there is ~4dB total loss (3dB from splitter and 1dB from total excess loss above theoretical from various components) between the SMA input and each RF input of the JMS-1-H mixer, which has an advertised conversion loss of ~6dB. So the RF input to each mixer, for 0dBm to the front panel SMA is ~-4dBm (=0.4 Vpp), and the I/F output is 0.34Vpp. So the conversion loss is only ~-1.5 dB? Seems really low? I assume the 0.34 Vpp is at the input to the preamp? If it's after the preamp, then the numbers still don't add up, because with the nominal 6dB conversion loss, the output. should be ~2Vpp? I will check it later.

Quote:

With LO3dBm. RF0dBm, and delta_f = 30Hz, the output Vpp of 340mV and the phase difference is 88.93deg. (Attachment 3/4, the traces were averaged)

  15866   Fri Mar 5 00:53:09 2021 KojiSummaryElectronicsA bunch of electronics received

Received additional front/rear panels. Updated the original entry and Wiki [Link]

 

  15865   Thu Mar 4 23:57:35 2021 KojiSummaryElectronicsInspection of the new custom dsub cables

I made the inspection of the new custom DSub cables (came from Texas).

The shelled version gives us some chance to inspect/modify the internal connections. (good)
The wires are well insulated. The conductors are wrapped with the foils and then everything is in the braid tube shield. The braid is soldered on one of the connectors. (Attachment  3/4 shows the soldering of the conductor by intentionally removing one of the insulations).

It wasn't clear that if the conductors are twisted or not (probably not).

  15864   Thu Mar 4 23:16:08 2021 KojiUpdateLSCREFL55 demod board rework

A new hybrid splitter (DQS-10-100) was installed. As the amplification of the final stage is sufficient for the input level of 3dBm, I have bypassed the input amplification (Attachment 1). One of the mixer was desoldered to check the power level. With a 1dB ATTN, the output of the last ERA-5 was +17.8dBm (Attachment 2). (The mixer was resoldered.)

With LO3dBm. RF0dBm, and delta_f = 30Hz, the output Vpp of 340mV and the phase difference is 88.93deg. (Attachment 3/4, the traces were averaged)

  15863   Thu Mar 4 15:48:26 2021 KojiSummaryPEMWatchdog tripped, Optics damped back

EQs seen on Summary pages
https://nodus.ligo.caltech.edu:30889/detcharsummary/day/20210304/pem/seismic_blrms/

  15862   Thu Mar 4 11:59:25 2021 Paco, AnchalSummaryLSCWatchdog tripped, Optics damped back

Gautam came in and noted that the optics damping watchdogs had been tripped by a >5 magnitude earthquake somewhere off the coast of Australia. So, under guided assistance, we manually damped the optics using following:

  • Using the scripts/SUS/reEnableWatchdogs.py script we re-enabled all the watchdogs.
  • Everything except SRM was restored to stable state.
  • Then we clicked on SRM in SUS-> Watchdogs, disabled the Oplevs, shutdown the watchdog.
  • We changed the threshold for watchdog temporarily to 1000 to allow damping.
  • We enabled all the coil outputs  manually. Then enabled watchdog by clicking on Normal.
  • Once the SRM was damped, we shutdown the watchdog, brought back the threshold to 215 and restarted it.

Gautum also noticed that MC autolocker got turned OFF by me (Anchal), we turned it back on and MC engaged the lock again. All good, no harm done.

  15861   Thu Mar 4 10:54:12 2021 Paco, AnchalSummaryLSCPOY11 measurement, tried to lock Green Yend laser

[Paco, Anchal]

- First ran burtgooey as last time.

- Installed pyepics on base environment of donatella

ASS XARM:
- Clicked on ON in the drop down of "! More Scripts" below "! Scripts XARM" in C1ASS.adl
- Clicked on "Freeze Outputs" in the same menu after some time.
- Noticed that the sensing and output matrix of ASS on XARM and YARM look very different. The reason probably is because the YARM outputs have 4 TT1/2 P/Y dof instead of BS P/Y on the XARM. What are these TT1/2?

(Probably, unrelated but MC Unlocked and kept on trying to lock for about 10 minutes attaining the lock eventually.)

Locking XARM:
- From scripts/XARM we ran lockXarm.py from outside any conda environment using python command.
- Weirdly, we see that YARM is locked??? But XARM is not. Maybe this script is old.
- C1:LSC-TRY-OUTPUT went to around 0.75 (units unknown) while C1:LSC-TRX-OUTPUT is fluctuating around 0 only.

POY11 Spectrum measurement when YARM is locked:
- Created our own template as we couldn't find an existing one in users/Templates.
- Template file and data in Attachment 2.
- It is interesting to see most of the noise is in I quadrature with most noise in 10 to 100 Hz.
- Given the ARM is supposed to be much calmer than MC, this noise should be mostly due to the mode cleaner noise.
- We are not sure what units C1:LSC-POY11_I_ERR_DQ have, so Y scale is shown with out units.


Trying to lock Green YEND laser to YARM:
- We opened the Green Y shutter.
- We ensured that when temperature slider og green Y is moved up, the beatnote goes up.
- ARM was POY locked from previous step.
- Ran script scripts/YARM/Lock_ALS_YARM.py from outside any conda environment using python command.
- This locked green laser but unlocked the YARM POY.

Things moving around:
- Last step must have made all the suspension controls unstable.
- We see PRM and SRM QPDs moving a lot.
- Then we did burt restore to /opt/rtcds/caltech/c1/burt/autoburt/today/08:19/*.snap to go back to the state before we started changing things today.

[Paco left for vaccine appointment]

- However the unstable state didn't change from restore. I see a lot of movement in ITMX/Y. PRM and BS also now. Movement in WFS1 and MC2T as well.
 - I closed PSL shutter as well to hopefully disengage any loops that are still running unstably.
 - But at this point, it seems that the optics are just oscillating and need time to come back to rest. Hopefully we din't cause too much harm today :(.
 


My guess on what happened:

  • Us using the Lock_ALS_YARM.py probably created an unstable configuration in LSC matrix and was the start of the issue.
  • On seeing PRM fluctuate so much, we thought we should just burst restore everything. But that was a hammer to the problem.
  • This hammer probably changed the suspension position values suddenly causing an impulse to all the optics. So everything started oscillating.
  • Now MC WFS is waiting for MC to lock before it stablizes the mode cleaner. But MC autolocker is unable to lock because the optics are oscillating. Chicken-egg issue.
  • I'm not aware of how manually one can restore the state now. My only known guess is that if we wait for few hours, everything should calm back enough that MC can be locked and WFS servo can be switched on.
  15860   Wed Mar 3 23:23:58 2021 gautamUpdateALSArm cavity scan

I see no evidence of anything radically different from my PSL table optical characterization in the IMC transmitted beam, see Attachment #1. The lines are just a quick indicator of what's what and no sophisticated peak fitting has been done yet (so the apparent offset between the transmission peaks and some of the vertical lines are just artefacts of my rough calibration I believe). The modulation depths recovered from this scan are in good agreement with what I report in the linked elog, ~0.19 for f1 and ~0.24 for f2. On the bright side, the ALS just worked and didn't require any electronics fudgery from me. So the mystery continues.

  15859   Wed Mar 3 22:13:05 2021 gautamUpdateLSCREFL55 demod board rework

After this work, I measured that the orthogonality was poor. I confirmed on the bench that the PQW-2-90 was busted, pin 2 (0 degree output) showed a sensible signal half of the input, but pin 6 had far too small an output and the phase difference was more like 45 degrees and not 90 degrees. I can't find any spares of this part in the lab - however, we do have the equivalent part used in the aLIGO demodulator. Koji has kindly agreed to do the replacement (it requires a bit of jumper wiring action because the pin mapping between the two parts isn't exactly identical - in fact, the circuit schematic uses a transformer to do the splitting, but at some unknown point in time, the change to the minicircuits part was made. Anyway, until this is restored, I defer the PRMI sideband locking.

Quote:

There were multiple problems with the REFL55 demod board. I fixed them and re-installed the board. The TFs and noise measured on the bench now look more like what is expected from a noise model. The noise in-situ also looked good. After this work, my settings for the PRMI sideband lock don't work anymore so I probably have to tweak things a bit, will look into it tomorrow.

  15857   Wed Mar 3 12:00:58 2021 Paco, AnchalHowToIMCMC_F ASD

[Paco, Anchal]

- Saved BURT backup in /users/anchal/BURTsnaps/
- Copied existing code for mode cleaner noise budget from /users/rana/mat/mc. Will work on this from home to convert it inot new pynb way.

Get baseline IMC measurements (passive):
- MC_F:
  - What is MC_F? Let's find out.
  - On MC_F Cal window titled 'C1IOO-MC_FREQ', we turned off ON/OFF and back on again.
  - Using diaggui, we measured ASD of MC_F channel in units of counts/rtHz.

[Rana, Paco]

- Using diaggui, measured ASD from a template (under /users/Templates) and overlay the 1/f noise of the NPRO (Attachment 1)

[Anchal, Paco]

- WFS Master
  - Went through the schematic and tried to understand what is happening.
  - Accidentally switched on MC WF relief (python 3). Bunch of things were displayed on a terminal for a while and then we Ctrl-C it.
  - The only thing we noticed that change is a slight increase in WFS1 Yaw, and a corresponding decrease in WFS1 Pitch, WFS2 Pitch, and WFS2 Yaw.
  - We need to find out what this script does.


Future work:

  • Create an automated script for taking MC_F_DQ spectrum and refer it against reference trace.
  • Use pynb to create a noise budget for mode cleaner.
  • Identify excess noise between 10-40 Hz.
  • Configure output matrix in WFS Master to reduce the noise. Automate this process as well.
  15856   Wed Mar 3 11:51:07 2021 YehonathanUpdateSUSOSEM testing for SOSs

I finished testing the OSEMs. I put all the OSEMs back in the box. The OSEMS were divided into several bags. I put the OSEM box next to the south flow bench on the floor.

I have uploaded the OSEM catalog to the wiki. I will upload the LED spot images later.

In summary:

Total 64 OSEMS, 31 long, 33 short.

Perfectly centered LED spots, ready for C&B OSEMS: 30, 12 long, 18 short.

Perfectly centered LED spots, need some work (missing pigtails, weird screws) OSEMS: 7, 5 long, 2 short.

Slightly off-centered (subjective) LED spots, ready for C&B OSEMS: 20, 7 long, 13 short.

Slightly off-centered (subjective) LED spots, need some work (missing pigtails, weird screws) OSEMS: 4 long

Defective OSEMS or LED spot way off-center: 3.

  15855   Tue Mar 2 19:52:46 2021 gautamUpdateLSCREFL55 demod board rework

There were multiple problems with the REFL55 demod board. I fixed them and re-installed the board. The TFs and noise measured on the bench now look more like what is expected from a noise model. The noise in-situ also looked good. After this work, my settings for the PRMI sideband lock don't work anymore so I probably have to tweak things a bit, will look into it tomorrow.

  15854   Tue Mar 2 13:39:31 2021 ranaUpdateLSCPRM violin filter excessive?

agreed, seems excessive. I always prefer bandstop over notch in case the eigenfrequency wanders, but the bandstop could be made to be just a few Hz wide.

 

  15853   Mon Mar 1 16:27:17 2021 gautamUpdateLSCPRM violin filter excessive?

The PRM violin filter seems very suboptimal - the gain peaking shows up in the MICH OLTF, presumably due to the MICH-->PRM LSC output matrix. I plot the one used for the BS in comparison in Attachment #1, seems much more reasonable. Why does the PRM need so many notches? Is this meant to cover some violin modes of PR2/PR3 as well? Do we really need that? Are the PR2/PR3 violin modes really so close in frequency to that for the 3" SOS? I suppose it could be since the suspension wire is thinner and the mass is lighter, and the two effects nearly cancel, but we don't actuate on PR2/PR3? According to the earlier elog in this thread, this particular filter wasn't deemed offensive and was left on.

Indeed, as shown in Attachment #2, I can realize a much healthier UGF for the MICH loop with just a single frequency notch (black reference trace) rather than using the existing "PRvio1,2" filter (FM2), (live red trace). The PR violins are eating so much phase at ~600 Hz.

Quote:

We turned off many excessive violin mode bandstop filters in the LSC.

  15852   Mon Mar 1 12:36:38 2021 gautamSummaryIMCgetting familiar with IMC controls

Pretty minor thing - but PMCT and PMCR were switched on Quad 2 for whatever reason. I switched them back because I prefer the way it was. I have saved snapshots of the preferred monitor config for locking but I guess I didn't freeze the arrangement of the individual quadrants within a quad. This would be more of a problem if the ITMs and ETMs are shuffled around or something like that.

Quote:
 

- Switched channels around on video controls; changed C1:VID-MON7 to 16, back to 30, then C1:VID-QUAD2_4 to 16, to 18, then 20, back to 16, to 14 (which identified as PMCT), to 1 (IMC). Anyways, looks like IMC is locked.

  15851   Mon Mar 1 11:40:15 2021 Anchal, PacoSummaryIMCgetting familiar with IMC controls

[Paco, Anchal]

tl;dr: Done no harm, no lasting change.

Learn burtgooey

- Use /cvs/cds/caltech/target/c1psl/autoBurt.req as input to test snapshot "/users/anchal/BURTsnaps/controls_1210301_101310_0.snap" on rossa after not succeeding in donatella

- Browse /opt/rtcds/caltech/c1/burt/autoburt/snapshots/TODAY just to know where the snapshots are living. Will store our morning work specific snapshots in local user directories (e.g. /users/anchal/BURTsnaps)

Identifying video monitors

- Switched channels around on video controls; changed C1:VID-MON7 to 16, back to 30, then C1:VID-QUAD2_4 to 16, to 18, then 20, back to 16, to 14 (which identified as PMCT), to 1 (IMC). Anyways, looks like IMC is locked.

[Yehonathan, Paco, Anchal]

Unlocking MC

- From IOO/LockMC, MC_Servo, FSS --> closed PSL shutter, reopen it and see the lock recovers almost instantly. Try MCRFL shutter, no effect. Toggled PSL shutter one more time, lock recovered.

- From IOO/LockMC, MC_Servo, toggle OPTION (after IP2A), lose and recover lock in similar fashion. MCRFL gets most of the light.

- Looked at IFO_OVERVIEW just to get familiar with the various signals.

 

  15850   Sun Feb 28 22:53:22 2021 gautamUpdateLSCmore PRMI checks here: what it is ain't exactly clear

I looked into this a bit more and crossed off some of the points Rana listed. In order to use REFL 55 as a sensor, I had to fix the frequent saturations seen in the MICH signals, at the nominal (flat) whitening gain of +18 dB. The light level on the REFL55 photodiode (13 mW), its transimpedance (400 ohm), and this +18dB (~ x8) gain, cannot explain signal saturation (0.7A/W * 400 V/A * 8 ~ 2.2kV/W, and the PRCL PDH fringe should be ~1 MW/m, so the PDH fringe across the 4nm linewidth of the PRC should only be a couple of volts). Could be some weird effect of the quad LT1125. Anyway, the fix that has worked in the past, and also this time, is detailed here. Note that the anomalously high noise of the REFL55_Q channel in particular remains a problem. After taking care of that, I did the following:

  1. PRMI (ETMs misaligned) locking with sidebands resonant in the PRC was restored - REFL55_I was used for PRCL sensing and REFL55_Q was used for MICH sensing. The locks are acquired nearly instantaneously if the alignment is good, and they are pretty robust, see Attachment #1 (the lock losses were IMC related and not really any PRC/MICH problem).
  2. Measured the loop OLTFs using the usual IN1/IN2 technique. The PRCL loop looks just fine, but the MICH loop UGF is very low apparently. I can't just raise the loop gain because of the feature at ~600 Hz. Not sure what the origin of this is, it isn't present in the analogous TF measurement when the PRMI is locked with carrier resonant (REFL11_I for PRCL sensing, AS55_Q for MICH sensing). I will post the loop breakdown later. 
  3. Re-confirmed that the MICH-->PRCL coupling couldn't be nulled completely in this config either.
    • The effect is a geometric one - then 1 unit change in MICH causes a 1/sqrt(2) change in PRCL. 
    • The actual matrix element that best nulls a MICH drive in the PRCL error point is -0.34 (this has not changed from the PRMI resonant on carrier locking). Why should it be that we can't null this element, if the mechanical transfer functions (see next point) are okay?
  4. Looked at the mechanical actuator TFs are again (since we forgot to save plots on Friday), by driving the BS and PRM with sine waves (311.1 Hz), one at a time, and looking at the response in REFL55_I and REFL55_Q. Some evidence of some funkiness here already. I can't find any configuration of digital demod phase that gives me a PRCL/MICH sensing ratio of ~100 in REFL55_I, and simultaneously, a MICH/PRCL sensing ratio of ~100 in REFL55_Q. The results are in Attachments #5
  5. Drove single frequency lines in MICH and PRCL at 311.1 and 313.35 Hz respectively, for 5 minutes, and made the radar plots in Attachments #2 and #3. Long story short - even in the "nominal" configuration where the sidebands are resonant in the PRC and the carrier is rejected, there is poor separation in sensing. 
    • Attachments #2 is with the digital REFL55 demod phase set to 35 degrees - I thought this gave the best PRCL sensing in REFL55_I (eyeballed it roughly by looking at ndscope free-swinging PDH fringes).
    • But the test detailed in bullet #4, and Attachments #2 itself, suggested that PRCL was actually being sensed almost entirely in the Q phase signal.
    • So I changed the digital demod phase to -30 degrees (did a more quantitative estimate with free-swinging PDH fringes on ndscope, horn-to-horn voltages etc).
    • The same procedure of sine-wave-driving now yields Attachments #3. Indeed, now PRCL is sensed almost perfectly in REFL55_I, but the MICH signal is also nearly in REFL55_I. How can the lock be so robust if this is really true? 
  6. Attachments #4 shows some relevant time domain signals in the PRMI lock with the sidebands resonant. 
    • REFL11_I hovers around 0 when REFL55_I is used to sense and lock PRCL - good. The m/ct calibration for REFL11_I and REFL55_I are different so this plot doesn't directly tell us how good the PRCL loop is based on the out-of-loop REFL11_I sensor.
    • ASDC is nearly 0, good.
    • POP22_I is ~200cts (and POP22_Q is nearly 0) - I didn't see any peak at the drive frequency when driving PRCL with a sine wave, so no linear coupling of PRCL to the f1 sideband buildup, which would suggest there is no PRCL offset.
    • Couldn't do the analogous test for AS110 as I removed that photodiode for the AS WFS - it is pretty simple to re-install it, but the ASDC level already doesn't suggest anything crazy here.

Rana also suggested checking if the digital demod phase that senses MICH in REFL55_Q changes from free-swinging Michelson (PRM misaligned), to PRMI aligned - we can quantify any macroscopic length mismatch in the PRC length using this measurement. I couldn't see any MICH signal in REFL55_Q with the PRM misaligned and the Michelson fringing. Could be that +18dB is insufficient whitening gain, but I ran out of time this afternoon, so I'll check later. But not sure if the double attenuation by the PRM makes this impossible.

  15849   Sun Feb 28 16:59:39 2021 rana, gautamUpdateLSCmore PRMI checks here: what it is ain't exactly clear

On Friday evening we checked out a few more things, somewhat overlapping with previous tests. All tests done with PRMI on carrier lock (REFL11_I -> PRC, AS55_Q-> MICH):

  • check that PRC drive appropriately minimizes in REFL55_Q. I:Q ratio is ~100:1; good enough.
  • put sine waves around 311 and 333 Hz into PRCL and MICH at the LSC output matrix using awggui and LSC osc. not able to adjust LSC/OSC output matrix to minimize the MICH drive in REFL_I.
  • measured the TF from BS & PRM LSC drive to the REFL55_I/Q outputs. very nearly the same audio frequency phase, so the problem is NOT in the electronics || mechanical transfer functions of the suspensions.

 

Further questions:

  1. is this something pathological in the PRMI carrier lock? we should check by locking on sidebands to REFL55 and REFL165 and repeat tests.
  2. Can it be a severe mode mismatch from IMC output to PRMI mode? the cavity should be stable with the flipped folding mirrors, but maybe something strange happening. How do we measure the mode-matching to the PRC quantitatively?
  3. huge RAM is ruled out by Gautam's test of looking at REFL demod signals: dark offset vs. offset with a single bounce off of PRM (with ITMs mis-aligned)
  4. if there is a large (optical) offset in the AS55_Q lock point, how big would it have to be to mess up the REFL phase so much?
  5. what is going on with the REFL55 whitening/AA electronics?

unrelated note: Donatella the Workstation was ~3 minutes ahead of the FE machines (you can look at the C0:TIM-PACIFIC_STRING on many of the MEDM screens for a rough simulacrum). When the workstation time is so far off, DTT doesn't work right (has errors like test timed out, or other blah blah). I installed NTP on donatella and started the service per SL7 rules. Since we want to migrate all the workstations to Debian (following the party line), lets not futz with this too much.


gautam, 1 Mar 1600: In case I'm being dumb, I attach the screen grab comparing dark offset to the single bounce off PRM, to estimate the RAM contribution. The other signals are there just to show that the ITMs are sufficiently misaligned. The PRCL PDH fringe is usually ~12000 cts in REFL11, ~5000cts in REFL55, and so the RAM offset is <0.1% of the horn-to-horn PDH fringe.

P.S. I know generally PNGs in the elog are frowned upon. But with so many points, the vector PDF export by NDS (i) is several megabytes in size and (ii) excruciatingly slow. I'm proposing a decimation filter for the export function of ndscope - but until then, I claim plotting with "rasterized=True" and saving to PDF and exporting to PNG are equivalent, since both yield a rasterized graphic.

  15848   Sat Feb 27 17:25:42 2021 gautamUpdateElectronicsProduction version of the HV coil driver tested with KEPCO HV supplies

I will try the test of switching out KEPCOs one at a time for the HP. Given that the passive RC filter doesn't filter out the excess, I am wondering if the KEPCO is somehow polluting the circuit ground? The measurement was made between the circuit side of R24 (see schematic) and a ground testpoint, so the passive R23/C15 pole should filter the noise above ~15 Hz.

Quote:

This is very disappointing. Even with KEPCO linear supply with the improved HV driver circuit, the noise level is significantly higher than the 20kOhm R thermal noise.

What is special with the HP supplies? Can you replace KEPCOs with the HP supply, one by one to specify which one is making the noise bad?

  15847   Fri Feb 26 20:20:43 2021 KojiUpdateElectronicsProduction version of the HV coil driver tested with KEPCO HV supplies

This is very disappointing. Even with KEPCO linear supply with the improved HV driver circuit, the noise level is significantly higher than the 20kOhm R thermal noise.

What is special with the HP supplies? Can you replace KEPCOs with the HP supply, one by one to specify which one is making the noise bad?

  15846   Fri Feb 26 16:31:02 2021 gautamUpdateElectronicsProduction version of the HV coil driver tested with KEPCO HV supplies

Koji asked me to test the production version of the coil driver with the KEPCO HV supplies. See Attachment #1 for the results. For comparison, I've added a single trace from the measurements made with the HP supplies. I continue to see excess noise with the KEPCO supplies. Note that in the production version of the board that was tested, there are a pair of 10uF bypass capacitors on the board for the HV supply lines. It is possible that one or both KEPCO supplies are damaged - one was from the ASY setup and one I found in the little rack next to 1X2. The test conditions were identical to that with the HP supplies (as best as I could make it so).

  15845   Thu Feb 25 20:37:49 2021 gautamUpdateGeneralSetting modulation frequency and checking IMC offset

The Marconi frequency was tuned by looking at 

  1. The ~3.68 MHz (= 3*f1 - fIMC) peak at the IMC servo error point, TP1A, and
  2. The ~25.8 MHz (= 5*f1 - fIMC) peak at the MC REFL PD monitor port. The IMC error point is not a good place to look for this signal because of the post-demodulation low pass filter (indeed, I didn't see any peak above the analyzer noise floor).

The nominal frequency was 11.066209 MHz, and I found that both peaks were simultaneously minimized by adjusting it to 11.066195 MHz, see Attachment #1. This corresponds to a length change of ~20 microns, which I think is totally reasonable. I guess the peaks can't be nulled completely because of imbalance in the positive and negative sidebands. 

Then, I checked for possible offsets at the IMC error point, by injecting a singal to the AO input of the IMC servo board (using the Siglent func gen), at ~300 Hz. I then looked at the peak height at the modulation frequency, and the second harmonic. The former should be minimized when the cavity is exactly on resonance, while the latter is proportional to the modulation depth at the audio frequency. I found that I had to tweak the MC offset voltage slider from the nominal value of 0V to 0.12 V to null the former peak, see Attachment #2. After accounting for the internal voltage division factor of 40, and using my calibration of the IMC error point as 13 kHz/V, this corresponds to a 40 Hz (~50 microns) offset from the true resonant point. Considering the cavity linewidth of ~4 kHz, I think this is a small detuning, and probably changes from lock to lock, or with time of day, temperature etc.

Conclusion: I think neither of these tests suggest that the IMC is to blame for the weirdness in the PRMI sensing, so the mystery continues.

  15844   Thu Feb 25 16:50:53 2021 gautamUpdateGeneralPRMI sensing matrix

After all the work at the LSC rack over the last couple of days, I re-locked the PRMI (ETMs misaligned), and measured the sensing matrix once again. The PRMI was locked using 1f error signals, with AS55_Q as the MICH sensor and REFL11_I as the PRCL sensor. As shown in Attachment #1, the situation has not changed, there is still no separation between the DoFs in the REFL signals. I will measure the MC lock point offset using the error point dither technique today to see if there is something there.

  15843   Thu Feb 25 14:30:05 2021 gautamUpdateCDSnew c1bhd setup - diskless boot

I've set up one 2U server unit received from KT in the control room area (the fans in it are pretty loud but other than that, no major issues with it being tested here). The IPMI interface is enabled and the machine is also hooked up to the martian network for diskless boot (usual login creds). I also installed a Dolphin interface card and the one-stop-systems host side card, and both seem to be recognized (the OSSI card has the "PWR" LED on, the Dolphin card shows up in the list of PCIe devices, but has no LEDs on at the moment). I actually can't find the OSSI card in the list of PCI devices, but maybe I'm not looking for the right device ID, or it needs the cable to be connected to the I/O chassis side to be recognized. Anyways, let the testing begin.

The machine previously christened c1bhd has been turned off and completely disconnected from the martian network (though I didn't bother removing it from the rack for now).

BTW - I think most of our 19" racks are deformed from years of loading - I spent 5 mins trying to install the rails (at 1Y1 and 1X7) to mount the supermicro on, and couldn't manage it. I could be missing some technique/trick, but i don't think so.

  15842   Wed Feb 24 22:13:47 2021 JonUpdateCDSPlanning document for front-end testing

I've started writing up a rough testing sequence for getting the three new front-ends operational (c1bhd, c1sus2, c1ioo). Since I anticipate this plan undergoing many updates, I've set it up as a Google doc which everyone can edit (log in with LIGO.ORG credentials).

Link to planning document

Please have a look and add any more tests, details, or concerns. I will continue adding to it as I read up on CDS documentation.

  15841   Wed Feb 24 12:29:18 2021 gautamUpdateGeneralInput pointing recovered

While working at the LSC rack, I lost the input pointing into the IFO (the TT wiring situation is apparently very fragile, and this observation supports the hypothesis that the drifting TTs are symptomatic of some electronics issue). After careful beam walking, it was recovered and the dither alignment system was used to maximize TRX/TRY once again. No lasting damage done. If I can figure out what the pin-mapping is for the TT coils in vacuum, I'm inclined to try installing the two HAM-A coil drivers to control the TTs. Does anyone know where I can find said pin-out? The wiki page links seem broken and there isn't a schematic available there...

Ok it should be possible to back it out from the BOSEM pin out, and the mapping of the in-vacuum quadrupus cable, though careful accounting of mirroring will have to be done... The HAM-A coil driver actually already has a 15 pin output like the iLIGO coil drivers that are currently in use, but the pin mapping is different so we can't just replace the unit. On the bright side, this will clear up 6U of rack space in 1Y2. In fact, we can also consider hooking up the shadow sensor part of the BOSEMs if we plan to install 2 HAM-A coil drivers + 1 Dual satellite amplifier combo (I'm not sure if this number of spares is available in what we ordered from Todd).

  15840   Wed Feb 24 12:11:08 2021 gautamUpdateGeneralDemod char part 3

I did the characterization discussed at the meeting today.

  1. RF signal at 100 Hz offset from the LO frequency was injected into the PD input on the demod boards.
  2. The digitized CDS channels were monitored. I chose to look at the C1:LSC-{PD}_I_OUT and C1:LSC-{PD}_Q_OUT channels. This undoes the effect of the analog whitening, but is before the digital phase rotation.
  3. Attachments #1 and Attachments #2 are for the case where the analog whitening is not engaged, white Attachments #3 and Attachments #4 are for when the whitening is engaged, and they look the same (as they should), which rules out any crazy mismatch between the analog filter and the digital dewhitening filter.
  4. I have absorbed the flat whitening gain applied to the various PDs in the cts/V calibration indicated on these plots. So the size of the ellipse is proportional to the conversion gain.

I think this test doesn't suggest anything funky in the analog demod/whitening/AA/digitization chain. We can repeat this process after the demod boards are repaired and use the angle of rotation of the ellipse to set the "D" parameter in the CDS phase rotator part, I didn't do it today.

  15839   Wed Feb 24 11:53:24 2021 gautamUpdateGeneralDemod char part 2

I measured the noise of the I/F outputs of all the LSC demodulators. I made the measurement in two conditions, one with the RF input to the demodulators terminated with 50 ohms to ground, and the other with the RFPD plugged in, but the PSL shutter closed (so the PD dark noise was the input to the demodulator). The LO input was driven at the nominal level for all measurements (2-3 dBm going in to the LO input, measured with the RF power meter, but I don't know what the level reaching the mixer is, because there is a complicated chain of ERA amplifiers and attenuators that determine what the level is). 

As in the previous elog, I have grouped the results into boards that do not (Attachment #1) and do (Attachment #2) have the low noise preamp installed. The top row is for the "Input terminated" measurements, while the bottom is with the RFPD plugged in, but dark. I think not a single board shows the "expected" noise performance for both I and Q channels. In the case where the preamp isn't installed and assuming the mixer is being driven with >17dBm LO, we expect the mixer to demodulate the Johnson noise of 50 ohms, which would be ~1nV/rtHz, and so with the SR785, we shouldn't measure anything in exceess of the instrument noise floor. With the low noise preamp installed, the expected output noise level is ~10nV/rtHz, which should just about be measurable (I didn't use any additional Low Noise front end preamp for these measurements). The AS55_I channel shows noise consistent with what was measured in 2017 after it was repaired, but the Q channel shows ~twice the noise. It seemed odd to me that the Q channels show consistently higher noise levels in general, but I confirmed that the SR785 channel 2 did not show elevated instrument noise at least when terminated with 50 ohms, so seems like a real thing.

While this is clearly not an ideal state of operation, I don't see how this can explain the odd PRMI sensing.

Quote:

For completeness, I will measure the input terminated I/F output noise levels later today. Note also that my characterization of the optical modulation profile did not reveal anything obviously wrong (to me at least). 

  15838   Wed Feb 24 10:23:03 2021 YehonathanUpdateSUSOSEM testing for SOSs

Continuing with the new rig, I measure the resistance of the cable leading to the coil to be 0.08+(0.52-0.08)+(0.48-0.08)=0.9ohm.

S/N

Coil Resistance

(ohm)

Coil Inductance

(mH)

PD Voltage

(V)

LED spot image

(Attachment #)

LED perfectly centered Ready for C&B and install Short/Long Notes
078 13.0 2.8 1.86 1 N Y L Reengraved
280 13.3 2.8 1.92 2

Y

Y L  
117 13.1 2.8 2.12 3 Y Y L Reengraved
140 inf       N N L  
146 12.8 2.8 1.83   Y Y L Reengraved
093 13.1 2.8 2.19   N Y L Reengraved
296 13.1 2.8 2.19   N Y L  
256 13.1 2.8 2.0   N Y L  
060 12.9 2.8 2.0   Y Y L Reengraved
098 13 2.8 1.95   N Y L Reengraved
269 13.2 2.8 1.92   Y Y L  
260 13.2 2.8 2.03   Y Y L  
243 13.1 2.8 1.94   N Y L  
080 12.9 2.8 2.38   Y Y L Reengraved
292 13.3 2.8 2.06   N Y L  
113 13 2.8 2.08   Y Y L Reengraved
251 13.1 2.8 2.04   Y Y L  
231 13.3 2.8 1.89   Y Y L filter not covering the entire PD area
230 13.3 2.8 1.92   Y Y L  
218 13.3 2.8 2.13   Y Y L  
091 13.2 2.8 1.98   Y N L No pigtail. Reengraved
118 13.3 2.8 2.15   Y N L No pigtail. Reengraved
302 13.2 2.8 2.06   Y Y L  
159 13 2.8 2.15   Y N S No pigtail. One cap screw too long. Reengraved.
016 13 2.8 2.54   Y N S No pigtail. Reengraved.
122

13.1

2.8 2.04   N N L No pigtail. Reengraved.
084 13 2.8 1.94   N N L No pigtail. Reengraved.
171 13.1 2.8 2.20   Y N L No pigtail. Reengraved.
052 12.9 2.8 1.75   Y Y S Reengraved.
106 13.1 2.8 1.62   Y Y S Reengraved.
096 13 2.8 2.05   Y Y S Reengraved. The OSEM fell on the floor. I rechecked it. Everything seems fine except the PD voltage has changed. It was previously 1.76
024 13 2.8 1.81   Y Y S Reengraved.
134 12.9 2.8 1.82   N Y S Reengraved.
081 12.9 2.7 1.85   Y Y S Reengraved.
076 12.9 2.8 1.91   N Y S Reengraved.
108 12.9 2.8 1.83   Y Y S Reengraved.
020 12.9 2.8 1.98   N Y S Reengraved.
031 12.9 2.8 1.74   Y Y S Reengraved.
133 13.1 2.8 1.65   Y Y S Reengraved.
007 13 2.8 1.74   Y Y S Reengraved.
088 12.8 2.8 1.77   N Y S Reengraved.
015 12.9 2.7 1.81   Y Y S  
115 13 2.8 1.89   Y Y S Reengraved.
009 12.9 2.8 1.78   Y Y S Reengraved.
099 13.1 2.8 2.00   Y Y S Reengraved.
103 12.9 2.8 1.82   N Y S Reengraved.
143 13.1 2.8 1.80   Y Y S Reengraved.
114 12.8 2.8 2.04   Y Y S  
155 13.1 2.8 1.90   N Y S Reengraved.
121 12.9 2.8 1.86   Y Y S Reengraved.
130 13 2.7 1.78   N Y S Reengraved.
022 13 2.8 1.92   N Y S Reengraved.
150 12.8 2.8 1.90   N Y S Reengraved.
144 12.7 2.7 1.86   N Y S  
040 12.9 2.8 1.70   N Y S Reengraved. way off-center
125 12.8 2.8 1.75   N Y S Reengraved.
097 12.9 2.8 1.81   N Y S Reengraved.
089 12.9 2.8 1.51   Y Y S Reengraved.
095 13 2.8 1.96   Y Y L Reengraved.
054 13.1 2.8 1.86   Y N L Have a long screw going through it. Reengraved.
127 13.1 2.9 1.82   N N L Have a long screw going through it. Reengraved.
135 12.7 2.8 1.75   N N L Have a long screw going through it. Reengraved.
046 13.1 2.8 2.08   Y N L Have a long screw going through it. Reengraved.
000 13.1 3.1 6.6 The LED light looks totally scattered. No clear spot N N S Made out of Teflon? Looks super old. Didn't engrave

Total: 63 OSEMS. Centered working OSEMS: 42. Will upload a more detailed summary to the wiki soon.

Note: The Olympus camera is eating the AA camera very quickly (need to replace every 1.5 days). I'm guessing this is because of the corrosion in the battery housing.

 

  15837   Wed Feb 24 10:09:16 2021 yehonathanUpdateSUSOSEM testing for SOSs

Yes, my phone camera mirrored the image. Sorry for the confusion.

I see you already uploaded the correct pin assignment.

Quote:

I can't obtain a consistent view between the existing drawings/photographs and your pin assignment. Please review the pin assignment again to check if yours is correct.

Looking from the back side and the wires are going down, the left bottom pin is "Coil Start" and the upper right adjacent pin is "Coil End". (See attachment)
So in your picture 1 should be the coil start and 4 should be the coil end, but they are not according to your table.

 

  15836   Tue Feb 23 23:12:37 2021 KojiSummarySUSSUS invacuum wiring

This is my current understanding of the in-vacuum wiring:
1. Facts

  • We have the in-air cable pinout. And Gautam recently made a prototype of D2100014 custom cable, and it worked as expected.
  • The vacuum feedthrough is a wall with the male pins on the both sides. This mirrors pinout.
  • On the in-vacuum cable stand (bracket), the cable has a female connector.

2. From the above facts, the in-vacuum cable is

  • DSUB25 female-female cable
  • There is no pinout mirroring

Accuglass has the DSUB25 F-F cable off-the-shelf. However, this cable mirrors the pinout (see the datasheet on the pdf in the following link)
https://www.accuglassproducts.com/connector-connector-extension-cable-25-way-female

3. The options are
- ask Accuglass to make a twisted version so that the pinout is not mirrored.

or
- combine Accuglass female-male cable (https://www.accuglassproducts.com/connector-connector-extension-cable-25-way-femalemale) and a gender changer (https://www.accuglassproducts.com/gender-adapter-25d)

4. The length will be routed from the feedthrough to the table via the stacks like a snake to be soft. So, it will require some extra length.

5. Also, the Accuglass cables don't have a flap and holes to fix the connector to a cable post (tower). If we use a conventional 40m-style DSUB25 post (D010194), it will be compatible with their cables. But this will not let us use a DSUB25 male connector to mate. In the future, the suspension will be upgraded and we will need an updated cable post that somehow holds the connectors without fastening the screws...

  15835   Tue Feb 23 20:55:19 2021 KojiUpdateSUSOSEM testing for SOSs

I can't obtain a consistent view between the existing drawings/photographs and your pin assignment. Please review the pin assignment again to check if yours is correct.

Looking from the back side and the wires are going down, the left bottom pin is "Coil Start" and the upper right adjacent pin is "Coil End". (See attachment)
So in your picture 1 should be the coil start and 4 should be the coil end, but they are not according to your table.

  15834   Tue Feb 23 00:10:05 2021 gautamUpdateGeneralDemod char part 1

I measured the conversion efficiencies for all the RFPD demod boards except the POP port ones. An RF source was used to drive the PD input on the demod board, one at a time, and the I/F outputs were monitored on a 300 MHz oscilloscope. The efficiency is measured as the percentage ratio V_IF / V_RF. 

I will upload the full report later, but basically, the numbers I measured today are within 10% of what I measured in 2017 when I previously did such a characterization. The orthogonality also seems fine. 

I believe I restored all the connections at 1Y2 correctly, and I can lock POX/POY and PRMI on 1f signals after my work. I will do the noise characterization tomorrow - but I think this test already rules out any funkiness with the demod setup (e.g. non orthogonality of the digitized "I" and "Q" signals). The whitening part of the analog chain remains untested.

Quote:

But I would still bet on demod chain funniness


Update 2/23 1215: I've broken up the results into the demod boards that do not (Attachment #1) and do (Attachment #2) have a D040179 preamp installed. Actually, the REFL11 AO path also has the preamp installed, but I forgot to capture the time domain data for those channels. The conversion efficiency inferred from the scope was ~5.23 V/V, which is in good agreement with what I measured a few years ago.

  • The scope traces were downloaded.
  • The resulting X/Y traces are fitted with ellipses to judge the gain imbalance and orthogonality.
  • The parameter phi is the rotation of the "bounding box" for the fitted ellipses - if the I and Q channels are exactly orthogonal, this should be either 0 or 90 degrees. There is significant deviation from these numbers for some of the demodulators, do we want to do something about this? Anyways, the REFL11 and AS55 boards, which are used for PRMI locking, report reasonable values. But REFL165 shows an ellipse with significant rotation. This is probably how the CDS phase rotator should be tuned, by fitting an ellipse to the digitized I/Q data and then making the bounding box rotation angle 0 by adjusting the "Measured Diff" parameter.
  • The gain imbalance seems okay across the board, better than 1dB.
  • The POX and POY traces are a bit weird, looks like there is some non-trivial amount of distortion from the expected pure sinusoid.
  • I measured the LO input levels going into each demod board - they all lie in the range 2-3dBm (measured with RF power meter), which is what is to be expected per the design doc. The exception the the 165 MHz LO line, which was 0.4 dBm. So this board probably needs some work. 
  • As I mentioned earlier, the conversion efficiencies are consistent with what I measured in 2017. I didn't break out the Eurocards using an extender and directly probe the LO levels at various points, but the fact that the conversion efficiencies have not degraded and the values are consistent with the insertion loss of various components in the chain make me believe the problem lies elsewhere. 

For completeness, I will measure the input terminated I/F output noise levels later today. Note also that my characterization of the optical modulation profile did not reveal anything obviously wrong (to me at least). 

  15833   Mon Feb 22 14:53:47 2021 gautamUpdateCDSdtt-ezca-tools installed on rossa

The defaults cds-crtools didn't come with some of the older ezcautils (like ezcaread, ezcawrite etc). This is now packaged for debian, so I installled them with sudo apt update && sudo apt install dtt-ezca-tools on rossa. Now, we don't have to needlessly substitute the commands in our old shell scripts with the more modern z read, z write etc.

I am wondering if there is a relative implicit minus sign between the z servo and ezcaservo commands...

  15832   Mon Feb 22 14:06:49 2021 YehonathanUpdateSUSOSEM testing for SOSs

Continuing with the OSEM testing. I measure the resistance of the wires from the RLC meter to the coil to be ~ 0.9ohm. I will subtract this number from the subsequent coil resistance measurements.

I took the old MC1 satellite box for powering the PD and LED in the OSEM assemblies. I connected an idc breakout board to J4 and powered the box with a DC supply according to the box's schematics.

After getting a bit confused about some voltage reading from one of the PD readouts Gautam came and basically redid the whole rig. Instead of using breakout boards, he powered the amplifier circuit directly from the DC supply. Then, to connect the OSEM pinboard directly to the J1 connector he made a DB25 ribbon cable where the two connectors are opposite to one another to mimic the situation with the vacuum feedthru. He also connected a DB25 to BNCs breakout cable, specific to the satellite box, to the J3 port to read the individual PDs through a BNC connector. We managed to confirm the normal operation of one OSEM (Normal PD voltage and LED light spot hitting the PD using a camera with no IR filter).

It was getting a bit late. Going to start checking the OSEMs tomorrow.

 

 

  15831   Sun Feb 21 20:51:21 2021 ranaUpdateGeneralHousekeeping + PRMI char

I'm curious to see if the demod phase for MICH in REFL & AS chamges between thi simple Mcihelson and PRMI. IF there's a change, it could point to a PRCL/f2 mismatch.

But I would still bet on demod chain funniness.

  15830   Sat Feb 20 16:46:17 2021 KojiSummaryElectronicsA bunch of electronics received

We received currently available sets. We are supposed to receive more coil drivers and sat amps, etc. But they are not ready yet.

 

  15829   Sat Feb 20 16:20:33 2021 gautamUpdateGeneralHousekeeping + PRMI char

In prep to try some of these debugging steps, I did the following.

  1. ndscope updated from 0.7.9 to 0.11.3 on rossa. I've been testing/assisting the development for a few months now and am happy with it, and like the new features (e.g. PDF export). v0.7.9 is still available on the system so we can revert whenever we want.
  2. Arms locked on POX/POY, dither aligned to maximize TRX/TRY, normalization reset.
  3. PRMI locked, dither aligned to maximize POPDC.
  4. All vertex oplevs re-centered on their QPDs.

While working, I noticed that the annoying tip-tilt drift seems to be worse than it has been in the last few months. The IPPOS QPD is a good diagnostic to monitor stability of TT1/TT2. While trying to trend the data, I noticed that from ~31 Jan (Saturday night/Sunday morning local time), the IP-POS QPD segment data streams seem "frozen", see Attachment #1. This definitely predates the CDS crash on Feb 2. I confirmed that the beam was in fact incident on the IPPOS QPD, and at 1Y2/1Y3 that I was getting voltages going into the c1iscaux Acromag crate. All manner of soft reboots (eth1 network interface, modbusIOC service) didn't fix the problem, so I power cycled the acromag interface crate. This did the trick. I will take this opportunity to raise again the issue that we do not have a useful, reliable diagnsotic for the state of our Acromag systems. The problem seems to not have been with all the ADC cards inside the crate, as other slow ADC channels were reporting sensible numbers.

Anyways, now that the QPD is working again, you can see the drift in Attachment #2. I ran the dither alignment ~4 hours ago, and in the intervening time, the spot, which was previously centered on the AS camera CRT display, has almost drifted completely off (my rough calibration is that the spot has moved 5mm on the AS CCD camera). I was thinking we could try installing the two HAM-A coil drivers to control the TTs, this would allow us to rule out flaky electronics as the culprit, but I realize some custom cabling would be required, so maybe not worth the effort. The phenomenology of the drift make me suspect the electronics - hard for me to imagine that a mechanical creep would stop creeping after 3-4 hours? How would we explain the start of such a mechanical drift? On the other hand, the fact that the drift is almost solely in pitch lends support to the cause being mechanical. This would really hamper the locking efforts, the drift is on short enough timescales that I'd need to repeatedly go back and run the dither alignment between lock attempts - not the end of the world but costs ~5mins per lock attempt.


On to the actual tests: before testing the hardware, I locked the PRMI (no ETMs). In this configuration, I'm surprised to see that there is nearly perfect coherence between the MICH and PRCL error signals between 100Hz-1kHz 🤔 . When the AS55 demodulated signals are whitened prior to digitization (and then de-whitened digitally), the coherence structure changes. The electronics noise (measured with the PSL shutter closed) itself is uncorrelated (as it should be), and below the level of the two aforementioned spectra, so it is some actual signal I'm measuring there with the PRMI locked, and the coherence is on the light fields on the photodiode. So it would seem that I am just injecting a ton of AS55 sensing noise into the PRCL loop via the MICH->PRM LSC output matrix element. Weird. The light level on the AS55 photodiode has increased by ~2x after the September 2020 vent when we removed all the unused output optics and copper OMC. Nevertheless, the level isn't anywhere close to being high enough to saturate the ADC (confirmed by time domain signals in ndscope).

To get some insight into whether the whole RF system is messed up, I first locked the arm cavities with POX and POY as the error signals. Attachment #3 shows the spectra and coherence betweeen these two DoFs (and the dark noise levels for comparison). This is the kind of coherence profile I would expect - at frequencies where the loop gain isn't so high as to squish the cavity length noise (relative to laser frequency fluctuations), the coherence is high. Below 10 Hz, the coherence is lower than between 10-100 Hz because the OLG is high, and presumably, we are close to the sensing noise level. And above ~100 Hz, POX and POY photodiodes aren't sensing any actual relative frequency fluctuations between the arm length and laser frequency, so it's all just electronics noise, which should be incoherent.

The analogous plot for the PRMI lock is shown in Attachment #4. I guess this is telling me that the MICH sensing noise is getting injected into the PRCL error point between 100Hz-1kHz, where the REFL11 photodiode (=PRCL sensor) isn't dark noise limited, and so there is high coherence? I tuned the MICH-->PRM LSC output matrix element to minimize the height of a single frequency line driving the BS+PRM combo at ~313Hz in the PRCL error point. 

All the spectra are in-loop, the loop gain has not been undone to refer this to free-running noise. The OLGs themselves looked fine to me from the usual DTT swept sine measurements, with ~100 Hz UGF.

  15828   Sat Feb 20 10:01:48 2021 gautamSummaryElectronicsA bunch of electronics received

Will we also be receiving the additional 34 Satellite Amplifier PCBs?

  15827   Fri Feb 19 18:22:42 2021 ranaUpdateLSCPRFPMI sensiing matrix woes

I would:

  1. look at the free swingin michelson. Should be able tu null that siggnal in all ports to define the Q phase.
  2. If things are weird, put an RF signal nto the demod board mhich is offset from the LO by ~100 Hz and verify the demod/whitening chain is kosher.
  3. Lock PRMI and drive lines > 200 Hz. If PRC/MICH are not orthogonal, then there may be a mis tuning of RF SB wavelength and cavity lengths.
  4. IF PRMI is sort of healthy, we could be having a weird SB resonance in the arms.
  15826   Fri Feb 19 16:55:26 2021 KojiUpdateSUSCoM Range on 3"->2" Adapter Ring for SOS

Jordan's screenshot actually shows that the vertical distance (Y) is 0.0000". We want to have the vertical distance of CoM from the wire clamping point to be 0.9mm in the nominal SOS design (this might need to be adjusted to have a similar pitch resonant freq for the different inertia of moment). Let's say it is ~mm ish.

The full range of the bottom dumbbell adjustment gives us the CoM adjustment range of +/-0.002” = +/-50um. This corresponds to an alignment range of +/-50mrad. And we want to set it within +/-500urad.
So we need to adjust the dumbbell position with the precision of 1/100 of the full range (precision of 0.5um).

The groove does not extend to the top of the clamp. The groove shallower than the wire diameter cause the hysteresis of the alignment. Also, the material of the pieces should be stainless steel. Al clamp is softer than the wire and will cause the groove to be dug on the material, causing increased bending friction and hysteresis again.

Saying, all of our suspended masses with Al stand-offs are suffering this issue to some extent. That was the reason to buy the ruby standoffs.

  15825   Fri Feb 19 16:14:16 2021 gautamUpdateSUSCoM Range on 3"->2" Adapter Ring for SOS

I briefly talked with Jordan about this. This suspension will have OSEMs right? With 400ohm series resistance for the coil drivers, we will have ~+/-20mrad actuation range. Of course we'd like to use as much of this for interferometry and not static pitch alignment correction (possibly even increase the series resistance to relax the dewhitening requirements). But what is the target adjustability range in mrad with the dumbell/screw config? My target in the linked elog is 500urad (not any systematic optimum, but will allow us to use most of the DAC range for interferometry). Are these numbers in inches commensurate with this 500urad?

On a related note - are there grooves for the wires to sit in on the side of the sleeve? We looked at the solidworks drawing, and noticed that the groove doesn't extend all the way to the top of the clamp. Also, the material of both the clamping piece and the piece onto which the wire is pressed onto is SS. Don't we want them to be Aluminium (or something softer than the wire) so that the wire makes a groove when the clamp is tightened?

Quote:

We want to move the CoM with the adjustment range so that the residual deviation is adjusted by the bottom dumbbell. 0.0003" is well within the range and good enough.

  15824   Fri Feb 19 16:06:01 2021 KojiUpdateSUSCoM Range on 3"->2" Adapter Ring for SOS

We want to move the CoM with the adjustment range so that the residual deviation is adjusted by the bottom dumbbell. 0.0003" is well within the range and good enough.

 

  15823   Fri Feb 19 15:17:51 2021 JordanUpdateSUSCoM Range on 3"->2" Adapter Ring for SOS

Adjusting the thickness of the cylindrical hole for the mirror on the 2" optic sleeve, from .6875" to .61" thick, moves the CoM to 0.0003" out of plane from the suspension wire. This is with the dumbell at its neutral point.

How close to zero do we need this to be? More fine tuning of that thickness can get it to zero, but this would require much tighter machining tolerance on that hole depth.

Moving the dumbell towards the back of the SOS assembly (noted as negative direction, with origin at the plane formed by the wires), moves the CoM to -0.002" from the plane.

Moving the dumbell towards the front of the SoS assmebly (positive direction wrt the plane formed by the suspension wire), moves the CoM to +0.0022" from the plane.

So the total adjustment range with the dumbell is -0.002"to 0.0022", with the plane formed by the wires as the origin.

See Attachments

  15822   Fri Feb 19 13:38:26 2021 gautamUpdateLSCPRFPMI

I forgot that I had already done some investigation into recovering the PRFPMI lock after my work on the RF source. I don't really have any ideas on how to explain (or more importantly, resolve) the poor seperation of MICH and PRCL sensed in our 3f (but also 1f) photodiodes, see full thread here. Anyone have any ideas? I don't think my analysis (=code) of the sensing matrix can be blamed - in DTT, just looking the spectra of the _ERR_DQ channels for the various photodiodes while a ssingle frequency line is driving the PRM/BS suspension, there is no digital demod phase that decouples the MICH/PRCL peak in any of the REFL port photodiode spectra.

  15821   Fri Feb 19 12:21:04 2021 YehonathanUpdateBHDSOS assembly

A summary of things that need to be fabricated/purchased/done:

Part What needs to be done How much more needed
SUSPENSION BLOCK Fabricate SS dowel pins for 1 suspension block. 2X(diameter 0.094"+-0.002, length 0.38"+-0.01)+2X(diameter 0.188"+-0.002, length 0.5"+-0.01)
WIRE CLAMP If using the opposite side is acceptable, we have enough.  
DUMBBELL STANDOFF Fabricate. Schematics. Need to check the size is compatible with the magnets we have. 40 + 10 for double stacking of side dumbbells. With the existing dumbbells, we'll have 18 spares.
SAFETY STOP, LONG Fabricate or buy. Schematics 4
OSEM assy Check if we have 35. Schematics  
SAFETY STOP, SMALL Fabricate or buy. Schematics 24
SAFETY STOP Fabricate or buy. Schematics 12
SS Spring Plunger Buy from McMaster. Find and check custom plungers around the X arm. 8
4-40 3/8" Ag SHCS Buy from uccomponents.com 30
4-40 1/2 Ag SHCS Buy from uccomponents.com 60
1/4-20 3/4 Ag SHCS Buy from uccomponents.com 150
1/4-20 5/4 Ag SHCS Buy from uccomponents.com 30
1/4 SS Lock Washer Buy from McMaster 30
1/4 SS Lock Wassher (Reduced OD) Buy from McMaster 30
Viton Tips Need to find stock Not sure. Existing eq stops have phosphor bronze springs. Should all of them be replaced with Viton?
Steel Music Wire There are 500ft of wire (enough for many SOSs) in a desiccator somewhere according to this elog  

 

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