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ID Date Author Type Category Subjectup
  16491   Mon Dec 6 18:23:04 2021 YehonathanUpdateBHDSOS assembly

I installed OSEMs on the LO1 SOS. To my surprise, the side magnet is not in the center of the side OSEM. It completely misses the LED as can be seen in the attachment.

Looking at the CAD model, it turns out the position of the OSEM on the left side plate is different from the position of the OSEM on the right side plate in the SOS tower.

We need to take the optic down, swap the right and left side blocks, and resuspend it.

There is not enough 🤦🏻‍♂️in the world

Attachment 1: signal-2021-12-06-165751_001.jpeg
signal-2021-12-06-165751_001.jpeg
  16497   Thu Dec 9 21:57:35 2021 YehonathanUpdateBHDSOS assembly

{Yehonathan, Tega}

We took the optic out of the SOS tower and removed the side blocks. We mounted new side blocks with wires already clamped in them in the reverse order.

The Adapter was placed back into the SOS and the wires were threaded through the wire clamp and suspended on the winches. The roll of the optic was balanced using a camera (attachment 1).

The pitch was balanced. this time I used 2 counterweights instead of 1 in order to not have to take so much of the weight out.

The mechanical resonances were measured by taking a 100 sec time series of QPD readout and doing PSD estimation (attachment 2). The mirror motion was damped as much as possible before taking the measurement.

3 peaks below 1.5Hz can be seen with frequencies of 755mHz (Yaw), 942mHz, 1040mHz (Pitch + Pos). The pitch/pos peaks are a bit close to each other, I bet if we go back to 1 counterweight the situation will be better.

While inserting the side OSEM I realized I didn't check the overall height of the adapter. The magnet was too high. I will fix it tomorrow and repeat the roll balancing.

 

Attachment 1: balancingsos2.png
balancingsos2.png
Attachment 2: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16505   Tue Dec 14 14:02:33 2021 YehonathanUpdateBHDSOS assembly

{Yehonathan, Paco}

I fixed the overall height of the adapter (attachment 1). I put an OSEM next to the side magnet. I positioned a camera in front of the SOS and connected it to my laptop for live streaming. I painted a line indicating the height of the OSEM plates and a line in between with the mean height. I discarded the wire clamp on the suspension block I released the wires from the winches and pulled on them until the magnet was roughly in the right position. I clamped the wires back on the winches and adjusted them until the magnet was on the middle line. I also verified that the roll of the adapter is aligned as before by making sure that the horizontal features on the adapter are parallel to the horizontal features on the SOS tower.

The wires were clamped to the suspension block using a new wire clamp.

I Found that locking the counterweight setscrew changes the alignment. Today we verified this effect. We released the setscrew and pre-compensated by adjusting the counterweight such that when the setscrew was locked the mirror was aligned.

We measured mechanical resonances (attachment 2). This time the yaw motion was very quiet so we got a smaller peak for the yaw. The peaks are the same as before. Y readout has peaks around the pitch and pos resonances that don't appear in the X readout. I'm not sure what they are. Maybe coming from the QPD electronics.

We locked the adapter using the EQ stops. We made sure the alignment stays close to ideal.

We installed OSEMs on the SOS. We chose suboptimal OSEMs because LO1 will only be used for steering. I made a spreadsheet copying the OSEM catalog into it. There we mark which OSEM goes where.

I cleaned the optic using the ion gun with a pressure of 30 PSI.

The next steps are:

1. Engrave the SOS tower.

2. Cut the wire at the winches and remove the winch adapter plate.

3. Wrap the SOS with foil.

4. Install the SOS in the vacuum chamber.

 

 

Attachment 1: magnetcentring.png
magnetcentring.png
Attachment 2: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16511   Wed Dec 15 22:09:53 2021 YehonathanUpdateBHDSOS assembly

{Paco, Yehonathan, Anchal}

I cut the wires from the winches and removed the winch adapter plate. I engrave  'LO1' on the SOS tower. Me and Paco wrapped the SOS with foil and transported it to Anchal who put it inside the ITMX chamber.

The transportation seems to be successful. Nothing broke. However, we found that even with the short side OSEM the LO1, as it is now, cannot sit in its designed position since ITMX's side OSEM stands in its way.

If there are magnets on both ITMX sides we can move its side OSEM to the other side. Another option is to resuspend LO1 with a side magnet on its left side.

 

  16518   Thu Dec 16 18:16:36 2021 YehonathanUpdateBHDSOS assembly

Today I glued magnets onto the new 3/4" mirror adapters. I also took the opportunity to make some more side magnets assemblies.

Yesterday I mounted PR3/SR2 3/4" thick mirror onto one of the new adapter. There seem to be no issues for now.

I started the process of suspending AS1 (E2000226-A). The Lambda Optic mirror with the closest specs has Rc = 2 m. I attached side blocks with clamped wires onto adapter number 7 - side block with a magnet on the right.

I then took one of the Lambda Optic mirrors and tried mounting it in the adapter. It was quite difficult to get it right. Unfortunately, I chipped the edge of the substrate (attachment 1) 🤦🏻‍♂️. I put the mirror back in the box and decided to use the spare mirror. I successfully mounted it into the adapter but when I put the clamping screws one of them fell on the mirror 🤦🏻‍♂️🤦🏻‍♂️. There is no visible damage though. I took some pictures (attachment 2-4).

I and Anchal then started suspending the mirror but then we found that one of the wires is dented in the middle 🤦🏻‍♂️🤦🏻‍♂️🤦🏻‍♂️. I'm burned out for today.

Late update: one nice thing that I found yesterday is that the glue is viscous enough to hold the dumbells without a metal sheet from above holding the magnets. This greatly simplifies the gluing process.

 

Attachment 1: chippedmirror.png
chippedmirror.png
Attachment 2: IMG_6311.JPG
IMG_6311.JPG
Attachment 3: IMG_6310.JPG
IMG_6310.JPG
Attachment 4: IMG_6309.JPG
IMG_6309.JPG
  16520   Fri Dec 17 17:50:17 2021 YehonathanUpdateBHDSOS assembly

I threaded a new wire through a different side block with a magnet and clamped it under a microscope. It was hard, but eventually, I was able to do it by holding the wire on both sides of the side block with weights.

The dented wire was discarded and the side block that was mounted on the AS1 adapter was put aside. I mounted the side block with the new wire on the AS1 adapter.

 

Anchal and I hanged the AS1 adapter and clamped the wires on the winches of an SOS tower. I balanced the roll and adjusted the height of the magnet with respect to a side OSEM using a camera (attachments 1 & 2).

I shoot the Hene laser on the optic and look at the reflection. I align the laser beam to be as close as possible to the center of the mirror. The OpLev needs to be realigned.

To my surprise, the ghost beam shoots up above the reflected beam! See attachment 3. I check to see that the arrow which marks the thinnest side of the mirror is horizontal (attachment 4). WTF?!

Also, now I realize that the marking on the Lambda optics are pencil markings 😵😵😵.

Attachment 1: AS1rollbalance.png
AS1rollbalance.png
Attachment 2: AS1Magnet_height.png
AS1Magnet_height.png
Attachment 3: ghostbeam.png
ghostbeam.png
Attachment 4: lambdaopticarrow.jpg
lambdaopticarrow.jpg
  16521   Fri Dec 17 19:16:45 2021 KojiUpdateBHDSOS assembly

We @40m do the convention of the arrow at the thinnest side & pointing the HR side, but nobody says Lambda does the same.

We can just remount the mirror without breaking the wires and adjust the pitching if you do it carefully.

Does this mean that the LO1 also likely to have the wedge pointing up? Or did you rotate the mirror to have the wedge reflection to be as horizontal as possible?

  16523   Fri Dec 17 22:16:07 2021 YehonathanUpdateBHDSOS assembly

I specifically checked the specification before mounting the mirror. It says clearly "Arrow at the thinnest location pointing towards Side 1". I guess they just ignored it.

As for LO1, I mounted it without noticing the location of the arrow. Later, I checked and the ghost beam was horizontal so I left it as it is. Yeah, I guess I will remount the mirror. Also, what do we do with the pencil markings? It's not vacuum-compatible.

Quote:

We @40m do the convention of the arrow at the thinnest side & pointing the HR side, but nobody says Lambda does the same.

We can just remount the mirror without breaking the wires and adjust the pitching if you do it carefully.

Does this mean that the LO1 also likely to have the wedge pointing up? Or did you rotate the mirror to have the wedge reflection to be as horizontal as possible?

 

  16524   Sat Dec 18 00:56:14 2021 KojiUpdateBHDSOS assembly

Sad... We just need to check the wedge direction everytime, unfortunately.

Pencil: can you try to gently wipe it off with solvent & a swab? (IPA / Acetone)
If it does not come off in the end, it's all right to leave. Do we want to scribe the arrow mark? You need a diamond pen.

  16526   Mon Dec 20 13:52:01 2021 KojiUpdateBHDSOS assembly

LO1: No need to remove the pencil mark for the damping test. Until we see serious contamination on the LO1 optic, we don't need to take the optic off from the mount and clean it. If there is a chance of rehanging (because of a broken wire/etc), we do wipe the pencil mark.

Other optics: wipe the pencil mark as much as possible.

  16528   Mon Dec 20 17:26:13 2021 YehonathanUpdateBHDSOS assembly

{Yehonathan, Anchal}

I released the AS1 wires from the winches, removed the adapter from the SOS tower, and removed the Lambda optic from the adapter. Attachment 1 shows the pencil markings on the optic before cleaning. I cleaned the pencil marking from the side of the optic with acetone using swabs until there were no pencil residues on the swab (attachment 2 shows the swab I used next to an unused swab). I was not able to remove the markings completely though (attachment 3).

I remounted the optic with the arrow rotated by 90 degrees counterclockwise.

We hang the adapter on the winches and adjust the height of the magnet and the adapter roll using the winches. We monitor the height of the adapter using a live stream from the Cannon camera. The camera's tilt was adjusted using straight features on the SOS tower. When we ran out of winch travel we adjust the height using the lower EQ stops and pull tight the wires. Attachment 4 shows the alignment of the side magnet with respect to the SOS tower and a side OSEM.

We checked the ghost beam trajectory and it looks much better (attachment 5)

We started realigning the OpLev. We realize that the height of the beam should be 5+14/32" = 5.437 by measuring the height of the screw holding the side OSEM from the table. The real height from the schematics is 5.425 We make the beam parallel with the table first using an iris and then the QPD.

Today, I balanced the counterweight. First using an iris, then by placing a QPD close to the SOS measuring the reflection from AS1. I locked the counterweight's set screw and the QPD Y readout looks good. Attachment 6 shows the QPD y readout near the beat node between pitch and pos. The node comes very close to zero which indicates that the pitch is balanced.

I measured the free-swinging motion using the QPD x and y axes. Attachment 7 shows the spectra of that motion. The major peaks are at 755mHz, 953mHz, and 1.05Hz.

 

Attachment 1: IMG_6312.JPG
IMG_6312.JPG
Attachment 2: IMG_6315.JPG
IMG_6315.JPG
Attachment 3: IMG_6314.JPG
IMG_6314.JPG
Attachment 4: AS1adapterbalancing.png
AS1adapterbalancing.png
Attachment 5: as1ghostbeam2.png
as1ghostbeam2.png
Attachment 6: beat.png
beat.png
Attachment 7: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16531   Tue Dec 21 18:04:46 2021 YehonathanUpdateBHDSOS assembly

I locked the EQ stops while retaining the XY alignment on the QPD and installed 5 green OSEMs. AS1 is ready for transfer into the vacuum chamber.

  16544   Wed Jan 5 19:18:06 2022 YehonathanUpdateBHDSOS assembly -- AS4

{Paco, Yehonathan, Anchal}

Today we suspended AS4 (E2000226-B). Anchal mounted Lambda Optic mirror with an RoC closest to AS4 in a thin optic mount. He noted that this optic as well as AS1 don't have a wedge angle. The specs claim that the wedge angle is 2 degrees what should have been clearly seen by inspecting the optic with a naked eye. All the ghost beam deflections probably come from the curvature of the mirror.

We did all the height and roll balancing using a camera (Attachment 1,2). We balanced that pitch of the adapter using a QPD not before we realigned the OpLev setup.

We measured the motion spectra (attachment 3). Major peaks are found at 755 mHz, 964 mHz, and 1.062Hz. I locked the counterweights setscrew and observed that the pitch balance doesn't change. I locked the EQ stops such that the alignment of the mirror remained the same by monitoring the QPD signals. I clamped the suspensions wires to the suspension block.

The only thing remaining is inserting the OSEMs.

 

Attachment 1: AS4_roll_balance.png
AS4_roll_balance.png
Attachment 2: AS_4_magnet_height.png
AS_4_magnet_height.png
Attachment 3: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16550   Thu Jan 6 17:00:20 2022 YehonathanUpdateBHDSOS assembly -- LO2

{Paco, Yehonathan}

Today we suspended LO2 (E1800089) which Anchal has loaded into the thick optic adapter. Attachments 1,2 show the height and roll balance adjustments.

I realigned the opLev setup and balanced the suspended mass. We figured that if we use 2 counterweights we will be 1 short. We decided to use 1 mass at the back of the adapter. This has the additional advantage that the Viton tip on lower back EQ stop can touch it and act normally. The optic was successfully balanced in this way. Attachment 3 shows the motion spectra on the QPD. There are major peaks at 712 mHz, 854 mHz, 876 mHz, and 996 mHz. As expected using only 1 counterweight raised the center of mass and lowered the pitch resonance frequency. The optic was locked keeping the alignment fixed on the center of the QPD, OSEMs were inserted and the SOS tower was engraved.

We should apply some glue to the counterweight to prevent it from spinning on the setscrew.

Attachment 1: LO2_roll_balance.png
LO2_roll_balance.png
Attachment 2: LO2_magnet_height.png
LO2_magnet_height.png
Attachment 3: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16542   Tue Jan 4 18:27:23 2022 PacoUpdateBHDSOS assembly -- PR3

[yehonathan, paco, anchal]

We continue suspending PR3 today. Yehonathan and Paco suspended the thick optic in its adapter. After fixing some nominal height and undoing any residual roll angle (see Attachments 1,2 for pictures), we noticed a problem with the pitch angle, so we insert the counterweights all the way in. Nevertheless, we soon found out that we needed to shift one of the two counterweights to the back of the adapter side (so one on each side) in order to tare the pitch angle. This is a newly experienced maneuver that may apply for further thick optics.

After taring the pitch angle roughly, we noted another issue. The wedge (~ 1 deg) on the optic made it such that the protruding socket heads on the thick side bumped against the lower clamp (not the earthquake stop tip itself). Attachments #4,5 show the before/after situation which was solved provisionally by replacing the socket head screws with lower profile (flat) head screws in situ. Again, this operation was highly delicate and specific to wedged thick optics, so for future SOS we should keep it in mind.

Another issue that we had with the new thick optic adapters is that for some reason there is a recession in the upper backside of the adapter (attachment coming soon). This makes the upper back EQ stop too short to touch the adapter. We replaced it with a longer screw. When inserted it doesn't really hit the back of the adapter. Rather, it touches the corner of the recession, stoping the optic with friction.

While all this was happening, Anchal started mounting AS4 on its adapter. After one of the magnets broke off, he switched to another one and succeeded. This is the next target for suspension. We still need to check the orientation of the wedge. Furthermore, we started a gluing session in the afternoon to prepare as much as possible for further SOS during the week. 3 side magnets were glued to side blocks. 3 magnets were glued to 3 adapters that were missing 1 magnet each.

In the afternoon, Yehonathan and Paco set up the QPD and did all the usual balancing, and then Anchal took the data of which the result is shown in Attachment #3. The major peaks are located at 723mHz, 953mHz, and 1.05Hz. Very similar to the case of the thin optic adapters.

Anchal progressed with OSEM installation, and engraving and yehonathan glued the counterweight setscrew in place. After securing the EQ stops, and wrapping the wires in foil, we declare PR3 is ready to be installed.

Attachment 1: PR3_roll_balance.png
PR3_roll_balance.png
Attachment 2: PR3_magnet_height.png
PR3_magnet_height.png
Attachment 3: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
Attachment 4: PXL_20220104_231742123.jpg
PXL_20220104_231742123.jpg
Attachment 5: PXL_20220104_232809203.jpg
PXL_20220104_232809203.jpg
  16568   Tue Jan 11 09:53:14 2022 not KojiUpdateBHDSOS assembly -- Peek screws and nuts

I handed the Peek parts we got from McMaster to Jordan for C&B.

  16556   Fri Jan 7 17:59:45 2022 YehonathanUpdateBHDSOS assembly -- SR2

{Yehonathan, Paco}

{Paco, Yehonathan}

Today we suspended SR2 (E1800089) which Anchal has loaded into the thick optic adapter. Attachments 1,2 show the height and roll balance adjustments.

I realigned the opLev setup and balanced the suspended mass. Attachment 3 shows the motion spectra on the QPD. There are major peaks at 723 mHz, 832 mHz, and 996 mHz. I inserted OSEMs and tightened them in place. I adjusted the OSEM plates to make sure the magnets are at the center of the OSEMs, then I tightened the OSEM plates to the SOS tower.

The optic was locked keeping the alignment fixed on the center of the QPD.

Again, we should apply some glue to the counterweight to prevent it from spinning on the setscrew. Is there a glue other than EP30 that we can use?

Related: Peek nuts, screws and washers were ordered from Mcmaster.

Attachment 1: SR2_roll_balance.png
SR2_roll_balance.png
Attachment 2: SR2_magnet_height.png
SR2_magnet_height.png
Attachment 3: FreeSwingingSpectra.pdf
FreeSwingingSpectra.pdf
  16557   Fri Jan 7 18:24:25 2022 KojiUpdateBHDSOS assembly -- SR2

Vacseal in the freezer. It could have been expired sooooo many years ago, We need some cure testing.

Can you release the part numbers of the ordered components (and how/where to use them), so that we can incorporate them into the CAD model?

Quote:

Again, we should apply some glue to the counterweight to prevent it from spinning on the setscrew. Is there a glue other than EP30 that we can use?

Related: Peek nuts, screws and washers were ordered from Mcmaster.

  16561   Mon Jan 10 14:00:44 2022 not KojiUpdateBHDSOS assembly -- SR2

Yes,

For the thin optics adapter design, we want Peek 1/4-20 screw (part # 98885A131) to replace the lower back long EQ stop. On it, we will have a Peek washer (part # 93785A600) fastened between two Peek nuts (part #98886A813).

For the thick optics adapter design, we want Peek 1/4-20 screw (part # 98885A131) to replace both the upper and lower back EQ stop. On the upper stop, we need a single Peek nut (part #98886A813).

I will cure-test the Vacseal.

Quote:

Vacseal in the freezer. It could have been expired sooooo many years ago, We need some cure testing.

Can you release the part numbers of the ordered components (and how/where to use them), so that we can incorporate them into the CAD model?

Quote:

Again, we should apply some glue to the counterweight to prevent it from spinning on the setscrew. Is there a glue other than EP30 that we can use?

Related: Peek nuts, screws and washers were ordered from Mcmaster.

 

  6344   Thu Mar 1 09:26:50 2012 steveUpdateSUSSOS baffle plates are ready

 Green welding glass 7" x 9"   shade #14 with 40 mm hole and mounting fixtures are ready to reduce scatter light on SOS

PEEK 450CA shims and U-shaped clips  will keep these plates damped.

 

Attachment 1: 03011201.PDF
03011201.PDF 03011201.PDF
  14032   Thu Jun 28 16:48:27 2018 gautamUpdateSUSSOS cage towers

For the upcoming vent, we'd like to rotate the SOS towers to correct for the large YAW bias voltages used for DC alignment of the ITMs and ETMs. We could then use a larger series resistance in the DC bias path, and hence, reduce the actuation noise on the TMs. 

Today, I used the calibrated Oplev error signals to estimate what angular correction is needed. I disabled the Oplev loops, and drove a ~0.1 Hz sine wave to the EPICS channel for the DC yaw bias. Then I looked at the peak-to-peak Oplev error signal, which should be in urad, and calibrated the slider counts to urad of yaw alignment, since I know the pk-to-pk counts of the sine wave I was driving. With this calibration, I know how much DC Yaw actuation (in mrad) is being supplied by the DC bias. I also know the directions the ETMs need to be rotated, I want to double check the ITMs because of the multiple steering mirrors in vacuum for the Oplev path. I will post a marked up diagram later. 

Steve is going to come up with a strategy to realize this rotation - we would like to rotate the tower through an axis passing through the CoM of the suspended optic in the vertical direction. I want to test out whatever approach we come up with on the spare cage before touching the actual towers.

Here are the numbers. I've not posted any error analysis, but the way I'm thinking about it, we'd do some in air locking so that we have the cavity axis as a reference and we'd use some fine alignment adjust (with the DC bias voltages at 0) until we are happy with the DC alignment. Then hopefully things change by so little during the pumpdown that we only need small corrections with the bias voltages.

SoS tower DC bias correction
Optic

EPICS excitation

[V pk-pk]

Oplev error signal readback

[urad pk-pk]

Calibration [mrad/V] Current DC bias voltage [V] Required correction [mrad]
ETMX 0.06 110 1.83 -5.5305 -10.14
ITMX 0.02 180 9 -1.4500 -13.05
ITMY 0.02 120 6 -0.3546 -2.13
ETMY 0.06 118 1.97 0.5532 1.09

Some remarks:

  1. Why the apparent difference between ITMs and ETMs? I think it's because the bias path resistors are 400 ohms on the ETMs, but 100 ohms on the ITMs
  2. If we want the series resistance for the bias path to be 10 kohm, we'd only have ~800 urad actuation (for +10V DC), so this would be an ambitious level of accuracy. 
  7331   Fri Aug 31 17:50:41 2012 SteveUpdateSUSSOS centering target

The SOS centering target is 1.9 mm lower than it should be! 

The hole is 10mm for the  ~6 mm beam

 

 

 

  7469   Wed Oct 3 15:58:57 2012 SteveConfigurationIOOSOS coil drivers moved

The SOS coil drivers (Atm2) were moved from 1X1 to 1Y2 location. Is this the best place to locate the  IOO Tip-Tilt steering that will replace the PJ-PZT ?

See 40m wiki T-T

Attachment 1: SOScoildriversTT.jpg
SOScoildriversTT.jpg
Attachment 2: IMG_1680.JPG
IMG_1680.JPG
  6039   Tue Nov 29 17:10:39 2011 DenUpdatedigital noiseSOS creation

One of the possibilities that we see a large low-frequency digital noise is due to Foton. I've checked the SOS coefficients that saves Foton with a Matlab coefficients. I used a 3 order low-pass cheby1 filter cheby1("LowPass",3,0.1,3) 

In matlab I generated SOS model using 3 approaches 


[A,B,C,D]=cheby1(3,0.1,3/1024) % create SS form

[sos,g]=ss2sos(A,B,C,D)  % convert to SOS form


[z, p, k]=cheby1(3,0.1,3/1024) % create ZPK form

[sos,g]=zp2sos(z,p,k)  % convert to SOS form


[b, a]=cheby1(3,0.1,3/1024) % create TF form

[sos,g]=tf2sos(b,a)  % convert to SOS form


As this is a 3 order filter, in the SOS representation we'll get 2 by 6 SOS - matrix. It is presented below. In each matrix place there 4 numbers - from the Foton file and obtained using these 3 methods.

GAIN

1.582261654653329e-07

1.582261654653329e-07

1.582261654653329e-07

1.582261655030947e-07

SOS-MATRIX

1              1.0000000000000000      #           0                                              #       1      #         -0.9911172660954457     #       0

1              1.0005663179617605      #           0                                              #       1      #         -0.9911172660954457     #       0

1              1.0000000000000000      #           0                                              #       1      #         -0.9911172660954457     #       0

1              0.9999894976396830      #           0                                              #       1      #         -0.9911172660997303     #       0

############################################################################################################

1              2.0000000000000000      #          1.0000000000000000         #       1      #        -1.9909750803252266      #      0.9911175825477769

1              1.9994336820732397      #          0.9994340026283055         #      1       #       -1.9909750803252262       #     0.9911175825477765

1              2.0000000000000000      #          1.0000000000000000         #      1       #       -1.9909750803252262       #     0.9911175825477765

1              2.0000105023603174      #          1.0000105024706190         #      1       #       -1.9909750803209423       #     0.9911175825434912

 

It seems that smth analog to zp2sos is used in Foton. We can see that due to representation error we have derivations in the 4 and 6 digits for SS and TF forms. This means that a pretty big mistake can run due to digital transforms even using double precision as in the Matlab test.

Alex Ivanov said that he'll fix that single precision problem and in the 2.5 release we won't have any FLOAT variables. Though we still do not understand how that variables declared as FLOAT can cause filter calculations. 

  12264   Thu Jul 7 09:13:54 2016 SteveUpdateSUSSOS gluing fixture

Atm 1, It's right arm is perfect.

Atm 3-4, The left one has bended (dropped) end.

Atm 2, Our ruby wire stanoffs will fit the jig. Ruby OD 1.27 mm vs. old Aluminum OD 1.0 mm. Length ruby 6.4 mm vs Al 4.8 mm

Atm 5, The fixture translation stages are a bit loooose. Careful use of the micrometer is needed to be precise

Betsy agreed that the 40m will keep SOS fixtures.

Attachment 1: SOSgluingFixRarmWend.jpg
SOSgluingFixRarmWend.jpg
Attachment 2: SOSgluingFixRarm.jpg
SOSgluingFixRarm.jpg
Attachment 3: SOSgluingFixLarm45.jpg
SOSgluingFixLarm45.jpg
Attachment 4: SOSgluingFixLarm.jpg
SOSgluingFixLarm.jpg
Attachment 5: SOSgluingFixture.jpg
SOSgluingFixture.jpg
  16670   Mon Feb 14 18:43:49 2022 PacoSummaryGeneralSOS materials clean room cleared

[Yehonathan, Paco]

We put away most items used / involved in SOS assembly and characterization. Many were stored in the left-most cabinet in the clean area. The OpLev test setup and optics were stored in the upper cabinets above the microscope area, and several screws and other general components were collected in clean bags or wrapped in foil, labeled and put away.

  15267   Wed Mar 11 21:03:57 2020 KojiUpdateBHDSOS packages from Syracuse

I opened the packages send from Syracuse.

- The components are not vacuum clean. We need C&B.
- Some large parts are there, but many parts are missing to build complete SOSs.

- No OSEMs.
- Left and right panels for 6 towers
- 3 base blocks
- 1 suspension block
- 8 OSEM plates. (1 SOS needs 2 plates)

- The parts looks like old versions. The side panels needs insert pins to hold the OSEMs in place. We need to check what needs to be inserted there.

- An unrelated tower was also included.

Attachment 1: P_20200311_203449_vHDR_On.jpg
P_20200311_203449_vHDR_On.jpg
  3581   Fri Sep 17 03:06:06 2010 KojiUpdateSUSSOS sent for baking

Two SOS suspensions for the ETMs were disassembled and packed for cleaning and baking by Bob.

These suspensions have been stored on the X end flow bench long years, and looked quite old.

They have some differences to the modern SOSs.

- The top suspension block is made of aluminum and had dog clamps to fix the wires.
- The side bars are not symmetric: the side OSEM can only be fixed at the right bar (left side in the picture).
- EQ stops were made of Viton.
- One of the tower bases seems to have finger prints (of Mike Zucker?).

I found that the OSEM plates had no play. We know that the arrangement of the OSEMs gets quite difficult
in this situation. Therefore the holes of the screws were drilled with the larger drill.

We decided to replace all of the screws to the new ones as all of the screws are Ag plated and got corroded
by silver sulfide (Ag2S). I checked our stock in the clean room. We have enough screws.

Important note: Use stainless screws in aluminum / Silver-plated screws in stainless
There exists some study about galling: LIGO-G020394-00-D

Attachment 1: IMG_3596.jpg
IMG_3596.jpg
Attachment 2: IMG_3597.jpg
IMG_3597.jpg
  12423   Thu Aug 18 15:16:09 2016 SteveUpdateSUSSOS sus wire is in

 

Stress Relieved 0.0017"  Music Wire  CFW P/N: CFW2035025,   Made 08-17-2016                                

    Old  2003    New  2016  
GBL 358.9 240.610 grams
UTS 357,061 229,603 PSI
YTS 343,211 177,371 PSI
ELONG 2.38 0.8 %
HEAT 10622 10622  

GBL (grams breaking load )         

UTS (ultimate tensile strength)                                 

YTS (yield tensile strength) 

ELONG (elongation)  

Quote:

0.0017" OD., 500ft steel music wire ordered. Pictures of the existing roll are below. It will be on 8" OD. spool too.

 

 

Attachment 1: 0.0017new.jpg
0.0017new.jpg
  12379   Fri Aug 5 09:38:12 2016 SteveUpdateSUSSOS sus wire ordered

0.0017" OD., 500ft steel music wire ordered. Pictures of the existing roll are below. It will be on 8" OD. spool too.

 

Attachment 1: 0.0017.jpg
0.0017.jpg
Attachment 2: 0.0017spec.jpg
0.0017spec.jpg
  12409   Mon Aug 15 14:29:32 2016 SteveUpdateSUSSOS sus wire ordered

The wire will arrive in 1-2 weeks. It is a new production. Brad Snook of Ca Fine Wire was suprised that we are still using the 13 years old wire.  Oxidation is an issue with iron contained steel wire.

He would not give me a shelf life time on it. He recommended to check the strenght of it before usage. It passed with safety factor of 2 just recently.

In the future we'll store the new spool in oxigen free nitrogen environment..

Quote:

0.0017" OD., 500ft steel music wire ordered. Pictures of the existing roll are below. It will on 9" OD. spool too.

 

 

  12410   Mon Aug 15 14:34:33 2016 ericqUpdateSUSSOS sus wire ordered

We have indeed seen numerous tarnished/rusty points along the wires, and just tried to choose lengths free of any of these. I wonder if this can explain the brittleness/ease with which we've been breaking it. My feeling is that we should use the newer wire if feasible.

  12419   Wed Aug 17 22:09:04 2016 ranaUpdateSUSSOS sus wire ordered

Not really true that it passed. That's just an arbitrary margin. Best to throw away all the old wire. We have no quantitative estimate of what the real torque should be. Its just feelings.

Quote:

The wire will arrive in 1-2 weeks. It is a new production. Brad Snook of Ca Fine Wire was suprised that we are still using the 13 years old wire.  Oxidation is an issue with iron contained steel wire.

He would not give me a shelf life time on it. He recommended to check the strenght of it before usage. It passed with safety factor of 2 just recently.

In the future we'll store the new spool in oxigen free nitrogen environment..

 

  10821   Fri Dec 19 18:08:46 2014 JenneUpdateCDSSOS!!! HELP!! EPICS freeze 45min+ so far!

[Jenne, Diego]

The EPICS freeze that we had noticed a few weeks ago (and several times since) has happened again, but this time it has not come back on its own.  It has been down for almost an hour so far. 

 So far, we have reset the Martian network's switch that is in the rack by the printer.  We have also power cycled the NAT router.  We have moved the NAT router from the old GC network switch to the new faster switch, and reset the Martian network's switch again after that.

We have reset the network switch that is in 1X6.

We have reset what we think is the DAQ network switch at the very top of 1X7.

So far, nothing is working.  EPICS is still frozen, we can't ping any computers from the control room, and new terminal windows won't give you the prompt (so perhaps we aren't able to mount the nfs, which is required for the bashrc).

We need help please!

  10822   Fri Dec 19 19:21:04 2014 diegoUpdateCDSSOS!!! HELP!! EPICS freeze 45min+ so far!

Quote:

[Jenne, Diego]

The EPICS freeze that we had noticed a few weeks ago (and several times since) has happened again, but this time it has not come back on its own.  It has been down for almost an hour so far. 

 So far, we have reset the Martian network's switch that is in the rack by the printer.  We have also power cycled the NAT router.  We have moved the NAT router from the old GC network switch to the new faster switch, and reset the Martian network's switch again after that.

We have reset the network switch that is in 1X6.

We have reset what we think is the DAQ network switch at the very top of 1X7.

So far, nothing is working.  EPICS is still frozen, we can't ping any computers from the control room, and new terminal windows won't give you the prompt (so perhaps we aren't able to mount the nfs, which is required for the bashrc).

We need help please!

[EricQ]

 

EricQ suggested it may be some NFS related issue: if something, maybe some computer in the control room, is asking too much to chiara, then all the other machines accessing chiara will slow down, and this could escalate and lead to the Big Bad Freeze. As a matter of fact, chiara's dmesg pointed out its eth0 interface being brought up constantly, as if something is making it go down repeatedly. Anyhow, after the shutdown of all the computers in the control room, a  reboot of chiara, megatron and the fb was performed.

 

[Diego]

Then I rebooted pianosa, and most of the issues seem gone so far; I had to "mxstream restart" all the frontends from medm and everyone of them but c1scy seems to behave properly. I will now bring the other machines back to life and see what happens next.

  10823   Fri Dec 19 20:32:11 2014 diegoUpdateCDSSOS!!! HELP!! EPICS freeze 45min+ so far!

[Diego, Jenne]

 

Everything seems reasonably back to normal:

Notes:

  • the machines in the control room have been rebooted;
  • the c1iscey frontend now behaves;
  • I saw on nodus, which remained up and running the whole time, a bunch of   nfs: server chiara is not responding, timed out  messages, belonging to the freezing time; it may be that the sync option for the nfs share is too resource demanding, or some other network issue;
  • the FSS was doing strange stuff and the MC couldn't recover the lock; the MCautolocker script wasn't running because of the lock loss of the MC and the lack of communication between the machines; so we did a sudo initctl start MCautolocker on megatron and recovered the MC too.
  10961   Fri Jan 30 11:37:20 2015 manasaFrogsTreasureSP table madness ends

SP table has been a mess because Q and I had let our SURF leave without cleaning up.

I cleaned up the SP table, put things back where they belong and did some sorting. I will put back the optomechanics where they belong sometime later.

For now, check out the SP table next time you are looking for a Y1  or lens or BS.

 

 

 

  2485   Fri Jan 8 10:03:04 2010 AlbertoOmnistructureLSCSPOB shutter was closed

This morning I found that there was no light on the SPOB PD. I went looking at the photodetector and I found that the shutter in front of it was closed.

I switched the shutter driver from n.c. to n.o. which had the effect of opening it.

I guess we inadvertently closed the shutter with Rana when last week we were tinkering with the ITMY  camera.

  16610   Fri Jan 21 11:24:42 2022 AnchalSummaryBHDSR2 Input Matrix Diagonalization performed.

The free swinging test was successful. I ran the input matrix diagonalization code (/opt/rtcds/caltech/c1/Git/40m/scripts/SUS/InMAtCalc/sus_diagonalization.py) on theSR2 free-swinging data collected last night. The logfile and results are stored in /opt/rtcds/caltech/c1/Git/40m/scripts/SUS/InMAtCalc/SR2 directory. Attachment 1 shows the power spectral density of the DOF basis data (POS, PIT, YAW, SIDE) before and after the diagonalization. Attachment 2 shows the fitted peaks.


Free Swinging Resonances Peak Fits
  Resonant Frequency [Hz] Q A
POS 0.982 340 3584
PIT 0.727 186 1522
YAW 0.798 252 912
SIDE 1.005 134 3365

SR2 New Input Matrix
  UL UR LR LL SIDE
POS
1.09
0.914
0.622
0.798
-0.977
PIT
1.249
0.143
-1.465
-0.359
0.378
YAW
0.552
-1.314
-0.605
1.261
0.118
SIDE
0.72
0.403
0.217
0.534
3.871

The new matrix was loaded on SR2 input matrix and this resulted in no control loop oscillations at least. I'll compare the performance of the loops in future soon.

 

Attachment 1: SR2_SUS_InpMat_Diagnolization_20220121.pdf
SR2_SUS_InpMat_Diagnolization_20220121.pdf
Attachment 2: SR2_FreeSwingData_PeakFitting_20220121.pdf
SR2_FreeSwingData_PeakFitting_20220121.pdf
  8916   Wed Jul 24 13:41:13 2013 JenneUpdateSUSSR2 flipped

[Jenne, Annalisa]

SR2 is flipped, and reinstalled.  We did that before lunch, and we're about to go in and work on SR3 and PR3.

EDITS / Notes:

I set dog clamps to have a reference position of where the tip tilt was, then I removed SR3 from the chamber.  Once out, I followed the same procedure I used for PR2 during the last vent - I removed the whole suspension (top mount, wires, optic) from the cage, and laid it down flat.  Then I loosened the set screw which pushes on the teflon nudge, removed the mirror, inspected it, and put it back in, with the HR side facing the back side of the ring.  Then I replaced the suspension system in the cage, and put the mirror back into the chamber. 

When I loosened the teflon nudge at the top of the mirror holder ring, the optic seemed to fall down a tiny bit.  I think this implies that the HR surface of the optic did not used to be parallel to the front face of the mirror holder ring.  When I put the suspension back onto the cage, the pitch balancing was very bad.  We checked the level of the table that I had the cage on, and it was miraculously pretty level, so I did the pitch balancing out of the chamber. 

Also, during my quick inspection of the mirror (not thorough, just using room lights), I noticed a small fleck of lint near the edge of the optic on the HR surface.  The HR surface is now on the outside of the SRC, but we should still blow at the optic with the ionized nitrogen to get it off.

I did not think to check the fine-tuning alignment of SR2....Koji did that after lunch (which I will elog about in a separate elog).

 

  8918   Wed Jul 24 15:07:54 2013 KojiUpdateSUSSR2 flipped

After the first flipping, X/Y arms were aligned and locked. Then the ASS aligned the arms.

  16609   Thu Jan 20 18:41:55 2022 AnchalSummaryBHDSR2 set to trigger free swing test

SR2 is set to go through a free swinging test at 3 am tonight. We have used this script (Git/40m/scripts/SUS/InMatCalc/freeSwing.py) reliably in the past so we expect no issues, it has a error catching block to restore all changes at the end of the test or if something goes wrong.

To access the test, on allegra, type:

tmux a -t SR2

Then you can kill the script if required by Ctrl-C, it will restore all changes while exiting.

 

  8924   Thu Jul 25 14:02:53 2013 JenneUpdateSUSSR3, PR3 flipped

Yesterday afternoon, I went back into the BS chamber, and flipped both PR3 and SR3. Now all of the recycling cavity folding mirrors have been flipped.

For PR3, I followed the same procedure as SR2, setting a reference position, removing the optic, flipping it, etc.  When I put it back in, I realized that since this has a 41 degree angle of incidence, the beam going to the BS had translated north by ~1cm.  After some fiddling, Koji pointed out that the 2 degree wedge probably had a more significant effect than just the HR surface having moved back a small amount.  Anyhow, we adjusted PR3 such that we were going through the BS aperture, as well as the ITMY aperture. 

During the flip of PR3, Annalisa and I noticed that the arrow on the barrel of the LaserOptik mirrors also indicates the thickest part of the wedgeThis is opposite of our SOS optics, where the arrow's position on the barrel indicates the thinnest part of the wedge.  For both PR3 and SR3, I kept the arrow on the same side of the optic as it was originally.

I then flipped SR3, following again the same procedure.  PR3 I had done a tiny bit of pitch rebalancing, although I think it was unneccessary, since it is within what we can do with the poking/hysterisis method.  SR3 I did not do any pitch rebalancing.  With PR3 aligned at least to the ITM, Koji and I aligned SR3 and SR2 so that the AS beam was hitting the center of all the SRC optics.  We also adjusted the steering mirrors after the SRM to get the beam centered on PZT3, the last optic on the BS table, which launches the beam over to the OMC chamber.  We scanned around a bit by turning the PZT's knobs, but we were unable to see the AS beam on the camera. 

 

  9376   Wed Nov 13 18:32:04 2013 Nic, EvanUpdateISSSR560 ISS loop

We have implemented an SR560-based ISS loop using the AOM on the PSL table. This is a continuation of the work in 40m:9328.

We dumped the diffracted beam from the AOM onto a stack of razor blades. This beam is not terribly well separated from the main beam, so the razor blades are at a very severe angle. Any alternatives would have involved either moving the AOM or attempting to dump the diffracted beam somewhere on the PMC refl path. We trimmed the RF power potentiometer on the driver so that with 0.5 V dc applied to the AM input, about 10% of the power is diverted from the main beam.

We ran the PMC trans PD into an AC-coupled SR560. To shape the loop, we set SR560 to have a single-pole low- pass at 300 Hz and an overall gain of 5×104. We take the 600 Ω output and send it into a 50 Ω feed-through terminator; this attenuates the voltage by a factor of 10 or so and thereby ensures that the AOM driver is not overdriven.

The AOM driver's AM input accepts 0 to 1 V, so we add an offset to bias the control signal. The output of the 50 Ω feedthrough is sent into the 'A' input of a second SR560 (DC coupled, A − B setting, gain 1, no filtering). Using a DS345 function generator, a 500 mV offset is put into the 'B' input (the function generator reads −0.250 V because it expects 50 Ω input). The 50 Ω output of this SR560 is sent into the AOM driver's AM input.

A measurement of suppressed and unsuppressed RIN is attached. We have achieved a loop with a bandwidth of a few kilohertz and with an in-loop noise suppression factor of 50 from 100 Hz to 1 kHz. This measurement was done using the PMC trans PD, so this spectrum may underestimate the true RIN.

Attachment 1: psl_aom_overhead.jpg
psl_aom_overhead.jpg
Attachment 2: aom_driver.jpg
aom_driver.jpg
Attachment 3: loop_on_settings.jpg
loop_on_settings.jpg
Attachment 4: fxn_gen.jpg
fxn_gen.jpg
Attachment 5: 40m_iss.pdf
40m_iss.pdf
  9380   Wed Nov 13 20:02:12 2013 Nic, EvanUpdateISSSR560 ISS loop

Quote:

We have implemented an SR560-based ISS loop using the AOM on the PSL table. This is a continuation of the work in 40m:9328.

We dumped the diffracted beam from the AOM onto a stack of razor blades. This beam is not terribly well separated from the main beam, so the razor blades are at a very severe angle. Any alternatives would have involved either moving the AOM or attempting to dump the diffracted beam somewhere on the PMC refl path. We trimmed the RF power potentiometer on the driver so that with 0.5 V dc applied to the AM input, about 10% of the power is diverted from the main beam.

We ran the PMC trans PD into an AC-coupled SR560. To shape the loop, we set SR560 to have a single-pole low- pass at 300 Hz and an overall gain of 5×104. We take the 600 Ω output and send it into a 50 Ω feed-through terminator; this attenuates the voltage by a factor of 10 or so and thereby ensures that the AOM driver is not overdriven.

The AOM driver's AM input accepts 0 to 1 V, so we add an offset to bias the control signal. The output of the 50 Ω feedthrough is sent into the 'A' input of a second SR560 (DC coupled, A − B setting, gain 1, no filtering). Using a DS345 function generator, a 500 mV offset is put into the 'B' input (the function generator reads −0.250 V because it expects 50 Ω input). The 50 Ω output of this SR560 is sent into the AOM driver's AM input.

A measurement of suppressed and unsuppressed RIN is attached. We have achieved a loop with a bandwidth of a few kilohertz and with an in-loop noise suppression factor of 50 from 100 Hz to 1 kHz. This measurement was done using the PMC trans PD, so this spectrum may underestimate the true RIN.

 A small followup measurement. Here are spectra of the MC trans diode with and without the ISS on. The DC value of the diode (in counts) changed from 17264.2 (no ISS) to 17504.3 (with ISS), but I didn't account for this change in the plot.

There is a small inkling of benefit between 100Hz and 1kHz. Above about 100Hz, the RIN is suppressed to about the noise level of this measurement. Below 100Hz there is no change, which probably means that power fluctuations are introduced downstream of the AOM, which argues for an outer-loop ISS down the road.

Atm #2 is in units of RIN.

Attachment 1: ISS_560_rot.pdf
ISS_560_rot.pdf
Attachment 2: ISS_560cal.pdf
ISS_560cal.pdf
  9392   Fri Nov 15 10:31:45 2013 SteveUpdateISSSR560 ISS loop connection

Quote:

Quote:

We have implemented an SR560-based ISS loop using the AOM on the PSL table. This is a continuation of the work in 40m:9328.

We dumped the diffracted beam from the AOM onto a stack of razor blades. This beam is not terribly well separated from the main beam, so the razor blades are at a very severe angle. Any alternatives would have involved either moving the AOM or attempting to dump the diffracted beam somewhere on the PMC refl path. We trimmed the RF power potentiometer on the driver so that with 0.5 V dc applied to the AM input, about 10% of the power is diverted from the main beam.

We ran the PMC trans PD into an AC-coupled SR560. To shape the loop, we set SR560 to have a single-pole low- pass at 300 Hz and an overall gain of 5×104. We take the 600 Ω output and send it into a 50 Ω feed-through terminator; this attenuates the voltage by a factor of 10 or so and thereby ensures that the AOM driver is not overdriven.

The AOM driver's AM input accepts 0 to 1 V, so we add an offset to bias the control signal. The output of the 50 Ω feedthrough is sent into the 'A' input of a second SR560 (DC coupled, A − B setting, gain 1, no filtering). Using a DS345 function generator, a 500 mV offset is put into the 'B' input (the function generator reads −0.250 V because it expects 50 Ω input). The 50 Ω output of this SR560 is sent into the AOM driver's AM input.

A measurement of suppressed and unsuppressed RIN is attached. We have achieved a loop with a bandwidth of a few kilohertz and with an in-loop noise suppression factor of 50 from 100 Hz to 1 kHz. This measurement was done using the PMC trans PD, so this spectrum may underestimate the true RIN.

 A small followup measurement. Here are spectra of the MC trans diode with and without the ISS on. The DC value of the diode (in counts) changed from 17264.2 (no ISS) to 17504.3 (with ISS), but I didn't account for this change in the plot.

There is a small inkling of benefit between 100Hz and 1kHz. Above about 100Hz, the RIN is suppressed to about the noise level of this measurement. Below 100Hz there is no change, which probably means that power fluctuations are introduced downstream of the AOM, which argues for an outer-loop ISS down the road.

Atm #2 is in units of RIN.

 I have disconnected the cable from the SR560 to LSC -ch8 for 15minutes this morning. It is moved from the floor to the top of the chambers as preparation for 40m tour. The SR560 seems to be overloading.

The  ISS servo is off according to the MEDM screen. Why MC-T plot showing zero?  The MC was happy yesterday.

 

Attachment 1: ISS.png
ISS.png
  13371   Wed Oct 11 10:29:43 2017 SteveUpdateElectronicsSR560 noise level

Gautam and Steve,

All 3 show the same noise level ~80 nV / rt Hz at 1 kHz as shown. Batteries ordered to be replaced in the top 2

We'll do more measurement to see how can we get to 4 nV / rt Hz  specification level.

Attachment 1: sr560.jpg
sr560.jpg
Attachment 2: sr560noise.jpg
sr560noise.jpg
  13373   Wed Oct 11 17:59:45 2017 ranaUpdateElectronicsSR560 noise level

these are not the SR785 settings that you're looking for

Quote:

Gautam and Steve,

All 3 show the same noise level ~80 nV / rt Hz at 1 kHz as shown. Batteries ordered to be replaced in the top 2

We'll do more measurement to see how can we get to 4 nV / rt Hz  specification level.

To get low noise measurements on the SR785, you have to have the input range set to -50 dB, not +20 dB. Its not within the powers of commercial electronics ADCs to give you a 10 nV noise floor with +10 V input signals. The SR560 has an input referred noise of 5 nV/rHz, so the output noise should be 5e-9 x 500 = 2.5 uV/rHz. Your picture shows it giving 1 uV RMS, so you also need to use the PSD units.

  13456   Tue Nov 28 17:27:57 2017 awadeBureaucracyCalibration-RepairSR560 return, still not charging

I brought a bunch of SR560s over for repair from Bridge labs. This unit, picture attached (SN 49698), appears to still not be retaining charge. I’ve brought it back. 

Attachment 1: 96B6ABE6-CC5C-4636-902A-2E5DF553653D.jpeg
96B6ABE6-CC5C-4636-902A-2E5DF553653D.jpeg
Attachment 2: image.jpg
image.jpg
  13494   Sun Dec 31 12:43:50 2017 ranaSummaryElectronicsSR560: reworking

I have ordered some LSK389A (in both the SOIC-8 and TO-71 packages) to replace the SR560's default front end FET pair (NPD5565).

I'm going to rework s# 00619 once these new FETs come in. Also ordered 100 of the SOIC-8 to DIP-8 adapter boards from Digikey.

This plot shows the current performance compared to the Rai Low Noise box. I expect the FETs should let us get to ~1.5 nV/rHz with the SR560.

Attachment 1: Preamps.pdf
Preamps.pdf
ELOG V3.1.3-