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ID Date Author Type Category Subject
11938   Wed Jan 20 02:53:18 2016 ericqUpdateLSCHopeful signs

[ericq, Gautam]

We gave DRFPMI locking a shot, with the ALS out-of-loop noises as attached. I figured the ALSX noise might be tolerable.

After the usual alignment pains, we got to DRMI holding while buzzing around resonance. Recall that we have not locked since Koji's repair of the LO levels in the IMC loop, so the proper AO gains are a little up in the air right now. There were hopeful indications of arm powers stabilizing, but we were not able to make it stick yet. This is perhaps consistent with the ALSX noise making things harder, but not neccesarily impossible; we assuredly still want to fix the current situation but perhaps we can still lock.

On a brighter note, I've only noticed one brief EPICS freeze all night. In addition, the wall StripTools seem totally contiuous since ~4pm, whereas I'm used to seeing some blocky shapes particularly in the seismic rainbow. Could this possibly mean that the old WiFi router was somehow involved in all this?

Attachment 1: 2016-01-20_ALSOOL.pdf
11937   Tue Jan 19 17:54:39 2016 gautamUpdateLSCALSX Noise still anomalously high

While carrying out my end-table power investigations, I decided to take a quick look at the out-of-loop ALSX noise - see the attached plot. The feature at ~1kHz seems less prominent (factor of 2?) now, though its still present, and the overall noise above a few tens of Hz is still much higher than the reference. The green transmission was maximized to ~0.19 before this spectrum was taken.

EDIT 1130pm:

We managed to access the trends for the green reflected and transmitted powers from a couple of months back when things were in their nominal state - see Attachment #2 for the situation then. For the X arm, the green reflected power has gone down from ~1300 counts (November 2015) to ~600 counts (january 2016) when locked to the arm and alignment is optimized. The corresponding numbers for the green transmitted powers (PSL + End Laser) are 0.47 (November 2015) and ~0.18 (January 2016). This seems to be a pretty dramatic change over just two months. For the Y-arm, the numbers are: ~3500 counts (Green REFL, Nov 2015), ~3500 counts (Green REFL, Jan 2016) ~1.3 (Green Trans, Nov 2015), ~1 (Green Trans, Jan 2016). So it definitely looks like something has changed dramatically with the X-end setup, while the Y-end seems consistent with what we had a couple of months ago...

Attachment 1: 2016_01_19_ALS_OutOfLoop.pdf
Attachment 2: Green_Locking_Trends.png
11936   Tue Jan 19 17:27:58 2016 gautamUpdateGreen LockingAUX X power investigations

Last week, Eric and I noticed that the green transmission levels at the PSL table seem much lower now than they did a month or two ago. To investigate this, I attempted to reproduce a power budget for the X endtable setup - see the attached figure (IR powers measured with calorimeter, green powers measured with Ophir power meter). A summary of my observations:

• The measurements were all made at an AUX-X laser diode current of 1.90A, and laser crystal temperature of 47.41 degrees. The current was chosen on the basis of the AUX-X frequency noise investigations. The temperature was chosen as this is the middle of three end-laser temperatures at wich a beat-note can be found now. Why should this temperature have changed by almost 5 degrees from the value reported here? I checked on the PSL laser controller that the PSL temperature is 33.43 degrees. Turning up the diode current to 2A does not change the situation significantly. Also, on the Innolight datasheet, the tuning geometry graphs' X-axes only runs to 45 degrees. Not sure of what to make of this. I tried looking at the trend of the offset to the slow temperature servo to see if there has been some sort of long-term drift, but was unable to do so...
• The IR power from the laser seems to have halved, compared to the value in Feb 2014. Is this normal deterioration over two years? Changing the laser diode current to 2A and the laser crystal temperature to ~42 degrees (the conditions under which the Feb 2014 measurements were taken) do not alter these numbers radically.
• The green power seems to have become 1/4 its value in Feb 2014, which seems to be consistent with the fact that the IR power has halved.

It is worth noting that two years ago, the IR power from the AUX-Y laser was ~280 mW, so we should still be getting "enough" green power for ALS?

Attachment 1: X_END_POWER_BUDGET.JPG
11935   Tue Jan 19 10:25:53 2016 SteveUpdateSUSEQ 3.6M Ludlow

Just an other local earthquake 3.6 Mag Ludlow, Ca

No obvious sign of damage

Attachment 1: EQ_3.6M_Ludlow.png
11934   Thu Jan 14 18:41:36 2016 ranaUpdateWienerFilteringNoise Subtraction Puzzler

Just not just pedagogical !  Freq domain MISO coherence based subtraction estimation is much faster than calculating MISO WF. And since each bin is independent of each other, this gives us an estimate of how low the noise can go, whereas the Wiener filter is limited by Kramers-Kronig. We should be able to use this on the L1 DARM channel to do the noise hunting as well as estimating the subtraction efficacy of the pseudo channels that you and Rory come up with.

If you can code up a noise hunter example using DARM + a bunch of aux channels, we could implement it in the summary pages code.

11933   Thu Jan 14 15:08:37 2016 ericqUpdateWienerFilteringNoise Subtraction Puzzler

The anticlimatic resolution to my subtraction confusion: Spectral leakage around 1Hz. Increasing the FFT length to 256 sec now shows that the FIR WF pretty much achieves the ideal subtraction.

If nothing else, it's good to have worked out how MISO coherence works.

Attachment 1: subpuzz_resolved.pdf
11932   Thu Jan 14 13:44:05 2016 SteveUpdateSUS earthquake 3.6M

No obvious sign of damage.

Attachment 1: 3.6M_JohannesburgCA.png
Attachment 2: ETMX_3.6_M.png
11931   Thu Jan 14 02:33:37 2016 ericqUpdateLSCALSX Noise still anomalously high

[ericq, Gautam]

We checked the UGF of the AUX X PDH servo, found a ~6kHz UGF with ~45 degree phase margin, with the gain dial maxed out at 10.0. Laser current is at 1.90, direct IR output is ~300mW.

We recovered ALS readout of IR-locked arms. While the GTRX seemed low, after touching up the beam alignment, the DFD was reporting a healthy amount of signal. ALSY was perfectly nominal.

ALSX was a good deal higher than usual. Furthermore, there's a weird shape around ~1kHz that I can't explain at this point. It's present in both the IR and green beats. I don't suspect the DFD electronics, because the Y beat came through fine. The peak has moderate coherence with the AUX X PDH error signal (0.5 or so), but the shape of the PDH error signal is mostly smooth in the band in which the phase tracker output is wonky, but a hint of the bump is present.

Turning the PDH loop gain down increases the power spectrum of the error signal, obviously, but also smoothens out the phase tracker output. The PDH error signal spectrum in the G=10 case via DTT is drowning in ADC noise a bit, so we grabbed it's spectrum with the SR785 (attachment #2, ASD in V/rtHz), to show the smoothness thereof.

Finally, we took the X PDH box to the Y end to see how ALSY would perform, to see if the box was to blame. Right off the bat, when examining the spectrum of error signal with the X box, we see many large peaks in the tens of kHz, which are not present at the same gain with the Y PDH box. Some opamp oscillation shenanigans may be afoot... BUUUUUT: when swapping the Y PDH box into the X PDH setup, the ~1kHz bump is identical. ugh

Attachment 1: 2016-01-14_ALSXspectra.pdf
Attachment 2: PDHsig.pdf
11930   Wed Jan 13 18:36:00 2016 gautamUpdateLSCrestoration of green beat electronics

In preparation for tonight's work, I did the following:

On the PSL table:

• Powered the RF amplifiers for the green beat signal on
• Reconnected the outputs of the Green beat PDs to the RF amplifiers
• Restored wiring in the fiber box such that both IR beats go to the frequency counter.

At the IOO Rack area:

• Restored wiring to the frequency counter module such that the IR beats from both arms go to the respective channels
• Partially cleaned up the setup used for measuring AUX laser frequency noise - moved the SR785 to the X end along with one SR560 so that we can measure the end PDH OLTF
• Brought the HP network analyzer back to the control room so that we can view the green beatnotes.

At the X-end:

• Turned the function generator used for PDH locking back on
• Checked that the AUX laser diode current is 1.90 A, and the crystal temperature is ~47.5 degrees, both of which I think are "good" values from our AUX laser frequency noise measurements
• Did some minor manual alignment of the PZT mirrors

At the Y-end:

• Restored the BNC connection from the PDH box to the laser's "FAST" control input. The long BNC cable used for the PLL is still running along the Y-arm, I will clean this up later.

Having done all this, I checked the green transmission levels for both arms (PSL green shutter closed, after running ASS to maximize IR transmission). GTRY is close to what I remember (~0.40) while the best I could get GTRX to is ~0.12 (I seem to remember it being almost double this value - maybe the alignment onto the beat PD has to be improved?). Also, the amplitudes of the beatnotes on the network analyzer are ~-50dBm, and I seem to remember it being more like -25dBm, so maybe the alignment on the PD is the issue? I will investigate further in the evening. It remains to measure the OLTF of the X-end PDH as well.

11929   Tue Jan 12 19:38:31 2016 gautamUpdateLSCFrequently making noise

EDITS 15Jan:

1. Schematic of test setup added (Attachment #5). Note that the UGF measurements were made with the LPF and gain on the 'wrong' SR560, in a way defeating the purpose of having 2 SR560s in the setup. I only realised this after taking the measuements. But having done the loop algebra, I believe we can extract the necessary information, which is what has been done in subsequent plots...
2. Koji pointed out that UGFs of ~100kHz was probably too high - this is when I took a closer look at the setup and realised the remarks made above in point 1. I realised we were in fact measuring the 'Process' open-loop TF. We can recover the loop TF by measuring the controller TF (which I did, see Attachment #3). The UGF for the PSL+X PLL loop is ~7.5kHz while that for PSL+Y is ~22kHz (both with a 1Hz LP on the SR560 and gain of x200).
3. During the above investigations, I found that the measured TF for a 1Hz LP on the SR560 is weird - there seems to be a zero around 5kHz which gives some phase lead where one would expect a uniformly decaying gain and phase to be -90 degrees. Eric and I confirmed this behavioud on another SR560. Low-pass at 10kHz and high-pass at 1kHz seem to work fine. I will investigate this further when I get the time. Anyhow I don't think this affects anything as long as we measure the correct OLTF. It is still not clear to me why we even need this to lock the PLL...
4. All the spectra (Attachment #4 and #5) are now calibrated taking into account the loop TF. I've added another panel with the spectra in V/rtHz as measured on the SR785, along with the SR560 output noise. I don't think any of the conclusions below are affected by these edits.

Summary:

I took several measurements today using the revised PLL scheme of using the Marconi just as an LO, and actuating on the Laser PZT to keep the PLL locked (I will put up a sketch soon). On the evidence of the attached plots (spectra of PLL control signal), I guess we can conclude the following:

1. The AUX X laser's frequency noise performance is consistent with the levels expected from 'typical' NPRO numbers (and the datasheet), and is more or less consistent across different diode currents/crystal temperatures (? see below...).
2. The diode current should be set to something less than 2.00 A
3. Qualitatively, there is a difference in the shape of the spectra between the PSL+X and PSL+Y combinations above a couple of kHz. I don't know why we see this.

Attachment #2: Measured OLG of PLL for the PSL+X and PSL+Y combinations. The UGF in both cases looks to be above 100 kHz, so I didn't do any calibration for the spectra attached. The gain on the SR560 was set to 200 for all measurements.

Attachment #3: Measured spectra of PLL control signal for various diode currents, with one reading from the PSL+Y combination plotted for comparison. When we took some data last night, Eric noted that there was a factor of ~6 increase in the overall frequency spectrum level at higher currents, I will update the plots with last night's data as well shortly. I found it hardest to keep the PLL locked at a diode current of 2.00 A across all measurements.

Attachment #4: Measured spectra of PLL control signal at two different crystal temperatures. There does not seem to be any significant dependance on temperature, although I did only do the measurement at two temperatures.

Attachment #4 Attachment #1All the data used to make these plots (plus some that have yet to be added to the plots, I will update them).

Misc notes:

• All measurements taken with two free-running lasers (PSL shutter closed)
• The SR560 noise was measured with the input on the SR560 set to ground.
• In order to go from V/rtHz to Hz/rtHz on the plots, I used 1MHz/V for the X-end laser (which I verified by a quick measurement today to be approximately correct) and 4.6 MHz/V for the Y-end laser, based on an earlier measurement.
• I re-routed the long BNC cable to the Y-end, have yet to remove it. The BNC from the PDH setup at the X-end has been re-attached to the X-end NPRO.

Unrelated to this work:

When I came in this afternoon, I noticed that the PMC was unlocked. The usual procedure of turning the servo gain to -10dB and playing around with the DC output adjust slider on the MEDM screen did not work. Eric toggled a few buttons on the MEDM screen after which we were able to relock the PMC using the DC output adjust slider.

Attachment 1: 2016_01_AUXLaser.tar.gz
Attachment 2: OLGs.pdf
Attachment 3: variedCurrent.pdf
Attachment 4: variedTemp.pdf
Attachment 5: PLL_setup.pdf
11928   Tue Jan 12 08:40:06 2016 SteveUpdatePEMAir cond maintenance

Air condition maintenance is happening. It should be done by 10am

11927   Tue Jan 12 07:54:23 2016 SteveUpdateSUSETMX damping restored

PMC locked and ETMX suspension damping restored.

11926   Tue Jan 12 03:03:55 2016 ericqUpdateLSCFrequently making noise

Gautam will soon follow up with detailed analysis, but here is a brief summary of some of our activities and findings.

• Two Marconis were beat together in various ways, we figured the noise added by turning on external modulation didn't make us happy.
• I locked the AUX X laser to the PSL via PZT. I'm more likely to believe we're seeing real broadband laser noise in this configuration; locking the the PSL laser to the IMC brought the noise down in a reasonable way. The PLL bandwidth was a smidge over 100k.
• We saw a factor ~6 increase in noise when changing the diode current from 1.8 to 1.96A. We'll be following this up at more temperatures and currents soon.
• Gautam will verify the AUX X laser PZT calibration tomorrow, and post calibrated spectra of this increase.

Please note that there is a long BNC cable still laid out from the IOO rack area to the X end table; watch your step!

11925   Mon Jan 11 19:01:56 2016 gautamUpdateLSCPLL Marconi Investigation

EDIT 01/12/2016 6PM: I've updated the plots of the in-loop spectra such that they are calibrated throughout the entire domain now. I did so by inferring the closed-loop transfer function (G/(1-G)) from the measured open-loop transfer function (G), and then fitting the inferred TF using vectfit4 (2 poles). The spectra were calibrated by multiplying the measured spectra by the magnitude of the fitted analytic TF at the frequency of interest.

EricQ brought back one of the Marconis that was borrowed by the Cryo lab to the 40m today (it is a 2023B - the Marconi used for all previous measurements in this thread was 2023A). Koji had suggested investigating the frequency noise injected into the PLL by the Marconi, and I spent some time investigating this today. We tried to mimic the measurement setup used for the earlier measurements as closely as possible. One Marconi was used as a signal source, the other as the LO for the PLL loop. All measurements were done with the carrier on the signal Marconi set to 310MHz (since all our previous measurements were done around this value). We synced the two Marconis by means of the "Frequency Standard" BNC connector on the rear panel (having selected the appropriate In/Out configurations digitally first). Two combinations were investigated - with either Marconi as LO and signal source. For each combination, I adjusted the FM gain on the Marconi (D in the plot legends) and the overall control gain on the SR560 (G in the plot legends) such that their product remained approximately constant. I measured the PLL OLG at each pair to make sure the loop shape was the same throughout all trials. Here are the descriptions of the attached plots:

Attachment #1: 2023A as LO, 2023B as source, measured OLGs

Measured OLG for the various combinations of FM gain and SR560 gain tested. The UGF is approximately 30kHz for all combinations - the exceptions being D 1.6MHz, G=1e4 and D=3.2MHz, G=1e4. I took the latter two measurements just because these end up being the limiting values of D for different carrier frequencies on the Marconi.

Attachment #2: 2023A as LO, 2023B as source, measured spectra of control signal (uncalibrated above 30kHz)

I took the spectra down to 2Hz, in two ranges, and these are the stitched versions.

Attachment #3: 2023B as LO, 2023A as source, measured OLGs

Attachment #4: 2023B as LO, 2023A as source, measured spectra of control signal (uncalibrated above 30kHz)

So it appears that there is some difference between the two Marconis? Also, if the frequency noise ASD-frequency product is 10^4 for a healthy NPRO, these plots suggest that we should perhaps operate at a lower value of D than the 3.2MHz/V we have been using thus far?

As a quick trial, I also took quick spectra of the PLL control signals for the PSL+Aux X and PSL+Aux Y beat signals, with the 2023B as the LO (Attachment #5). The other difference is that I have plotted the spectrum down to 1 Hz (they are uncalibrated above 30Hz). The PSL+Y combination actually looks like what I would expect for an NPRO (for example, see page 2 of the datasheet of the Innolight Mephisto) particularly at lower frequencies - not sure what to make of the PSL+X combination. Also, I noticed that the amplitude of the PSL+Y beatnote was going through some large-amplitude (beat-note fluctuates between -8dBm and -20dBm) but low frequency (period ~10mins) oscillations. This has been observed before, not sure why its happening though.

More investigations to be done later tonight.

Attachment 1: 2023ALockedto2023B.pdf
Attachment 2: 2023ALockedto2023B_spectra.pdf
Attachment 3: 2023BLockedto2023A.pdf
Attachment 4: 2023BLockedto2023A_spectra.pdf
Attachment 5: TestSpectra.pdf
Attachment 6: 2016_01_AUXLaser.tar.gz
11924   Sat Jan 9 00:39:15 2016 gautamUpdateLSCAUX Y Freq Noise re-measured
 Quote: With the Y end laser, I was able to lock the PLL with a lower actuation range (1.6MHz/V), and with the PSL in both the free-running and MCL locked configurations.

I took spectra (attached) with the same actuation range (3.2 MHz/V) for the AUX X+PSL and AUX Y+PSL combinations (PSL shutter closed) just to keep things consistent. It looks like there is hardly any difference between the two combinations - could the apparent factor of 3 worse performance of the X end laser have been due to different actuation ranges on the Marconi?

I've not managed to take a spectrum for the proposed replacement Lightwave laser on the PSL table, though with Eric's help, I've managed to find the beatnote (at a temperature of 53.0195 degrees). I had to do some minor alignment tweaking for this purpose on the PSL table - the only optics I touched were the ones in the pink beam path in attachments 1 and 2 in this elog (the setup used to make the measurement is also qualitatively similar to attachment 3 in the same elog, except for the fact that we are feeding back to the Marconi and not the laser - a detailed sketch with specific components used will be put up later). I'll try and measure the frequency noise of this laser as well over the weekend and put up some spectra.

With regards to possibly switching out the Lightwave on the PSL table for the (faulty?) Innolight at the X end, I've verified the following:

• The beam-height from the Lightwave on the mount it is currently sitting on is the same as that from the Innolight on the X end table.
• There is sufficient space on the X end table to house the Lightwave laser+mount

It remains to characterize the beam coming out from the Lightwave laser and do a mode matching calculation to see if we can use the same optics currently in place (with slight rearrangement) to realize a satisfactory mode-matching solution - I've obtained a beam profiler to do this from Liyuan and have the software setup, but have yet to do the beam scan - the plan is to do this on the SP table, but we've put off moving the Lightwave laser off the PSL table until we (i) establish conclusively that the X end laser is malfunctioning and (ii) check the frequency nosie of the Lightwave relative to the Aux lasers currently at the ends.

The area around the Marconi is in a little disarray at the moment with a bunch of cables, SR560s, analyzers etc - I didn't want to disconnect the measurement setup till we're done with it. I have however turned both IR beat PDs on the PSL table off, and have reconnected the Marconi output to the Frequency Generation Unit and have set the carrier back to 11.066209MHz, +13dBm.

Attachment 1: AuxPLL.pdf
11923   Fri Jan 8 22:37:17 2016 KojiUpdateGeneralNew WiFi router

I configured a new wifi bridge for a GPIB Instruments.

The some facts are described on https://wiki-40m.ligo.caltech.edu/Network

The setting up wasn't so straight forward. I added more details there as a linked page.
One thing I had to do with the martian wifi router was that I had to separate the name of SSIDs for 2GHz and 5GHz networks.

The first establishing the connection takes the most of the time, and the data transfer takes literary nothing.

controls@pianosa|netgpibdata > time ./netgpibdata -i 192.168.113.167 -d AG4395A -a 10 -f meas01 Connecting to host 192.168.113.167, GPIB 10... done. Data will be written into meas01.dat. Parameters will be written into meas01.par. Writing measurement data to file... Writing to the parameter file.

real    0m4.056s user    0m0.068s sys    0m0.020s

11922   Fri Jan 8 20:02:49 2016 ranaUpdateLSCAUX Y Freq Noise measured

Unless this is the limit from the way you guys set up the PLL, it seems like there's no difference between the two lasers that's of any import. So then the locking problem has been something else all along - perhaps its noise in the X-PDF lock somehow? PDH box oscillations?

11921   Fri Jan 8 14:47:33 2016 ericqUpdateLSCAUX Y Freq Noise measured

Here are some results from measuring the PSL / AUX Y beat.

With the Y end laser, I was able to lock the PLL with a lower actuation range (1.6MHz/V), and with the PSL in both the free-running and MCL locked configurations. (In the latter, I had to do a bit of human-turning-knob servo to keep the control signal from running away). I also took a spectrum with the marconi detuned from the beat frequency, to estimate the noise from the PD+mixer+SR560.

It looks like the AUX X laser is about 3 times noisier than the Y, though the Y laser looks more like a 10^5 noise-frequency product, whereas I thought we needed 10^4.

Gautam is investigating the PSL / AUX PSL beat with Koji's setup now.

Attachment 1: AUX_freqnoises.pdf
Attachment 2: AUXY_Jan8.zip
11920   Thu Jan 7 19:04:25 2016 KojiUpdateLSCAUX X Freq Noise measured

The next step is to compare this data with the same measurement with the PSL and the AUX laser on the PSL table (or the end Y laser). If these show a lot lower noise level, we can say 1) the x-end laser is malfunctioning and 2) the y-end and AUX laser on the PSL are well low noise.

11919   Thu Jan 7 16:52:32 2016 ericqUpdateLSCAUX X Freq Noise measured

Here is some of the promised data. As mentioned, changing diode current and crystal temperature didn't have much effect on the frequency noise spectrum; but the spectrum itself does seem too high for our needs.

At each temperature, we started measuring the spectrum at 1.8A, and stepped the current up, hoping to reach 2.0 A.

At 47.5 C, we were able to scan the current from 1.8 to 2.0 A without much problem. At 49.0C, the laser mode would hop away above 1.95A. At 50.4C it would hop away above 1.85A. The spectra were not seen to change when physically disconnecting the PZT actuation BNC from the rear of the laser.

The flattening out at the upper end is likely due to the SR560 output noise. I foolishly neglected to record the output spectrum of it, but with the marconi external modulation set to 3.2MHz/V, the few Hz/rtHz above 20k translates to a signal on the order of uV/rtHz, which seems reasonable.

Data and code attached.

Attachment 1: AUXfreqnoise.pdf
Attachment 2: auxXmeasurements.zip
11918   Thu Jan 7 15:29:54 2016 ericqUpdateWienerFilteringNoise Subtraction Puzzler

The puzzle continues...

I found some reference for computing "multicoherence," which should properly estimate the potential MISO subtraction potential in situations where the witness channels themselves have nontrivial coherence. Specifically, I followed the derivations in LIGO-P990002. The underlying math is related to principal component analysis (PCA) or gram-schmidt orthogonalization.

This produced the following results, wherein the Wiener subtraction is still below what the coherences predict.

I've attached the data and code that produced this plot.

Attachment 1: subpuzz2.pdf
Attachment 2: puzzle.zip
11917   Thu Jan 7 04:28:39 2016 ericqUpdateLSCAUX X Freq Noise measured

[ericq, Gautam]

Brief summary of tonights work:

• Locked Marconi to AUX X vs PSL beat at around 320MHz, PSL shutter closed (i.e. both lasers free running)
• Measured control signal spectrum at various laser diode currents, crystal temperatures. Oddly, spectra remained consistent across these variables.
• Measured OLG of PLL to calibrate into open-loop frequency noise of the beat, found UGF ~30kHz

Our "requirement" for the end laser is as follows: We expect to (and have in the past) achieved ALS sensitivity of 1Hz/rtHz at 100 Hz. If the end PDH loop is 1/f from 100Hz-10kHz, then we have 40dB of supression at 100Hz, meaning the free running AUX laser noise should be no more than 100Hz/rtHz at 100Hz.

So, if we expect both the PSL and AUX lasers to have this performance when free running, we would get the green curve below. We do not.

I'll post more details about the exact currents, temperatures and include calibrated plots for the >30kHz range later. Here's the OLG for kicks.

Attachment 1: PLLspec.pdf
Attachment 2: PLL_OLG.pdf
11916   Wed Jan 6 16:40:49 2016 ericqUpdateGeneralNew WiFi router

The new wifi router, a Netgear R6400, has been installed, next to the old one which is disconnected (but not yet removed).

Same SSID, and I've added only the wireless MAC addresses of viviana, paoloa and asia, the three thinkpads inside.

Qualitatively, dataviewer at the X end seems pretty snappy. I'll do some more quantitative comparison of the two routers at some point soon. I will update the wiki, too.

11915   Wed Jan 6 10:58:03 2016 SteveUpdateGeneral projector light bulb is out

Projector light bulb ordered

 Quote: [ Manasa, Ericq and Steve ]  Vivitek D952HD with 186 hours installed.

11914   Wed Jan 6 08:09:04 2016 SteveUpdatePEM4.5 Mag Banning EQ

IFO restored after 4.5 Mag Banning, Ca earthquake.

Attachment 1: 4.5Mag__Banning.png
11913   Tue Jan 5 17:19:57 2016 ranaUpdatesafetyRat trap locations

In the modern times, people use glue traps to catch rats instead of springs. They are less hazardous to people and don't spread rat fluid on the floor.

11912   Tue Jan 5 16:33:45 2016 ericqUpdateLSCAUX X Freq Noise attempt

Turning on the MCL path (in addition to the MCL FF we always have on) let me lock the PLL for multiple seconds, but low frequency excursions still break it in the end. I was able to briefly observe a level of ~50Hz/rtHz at 1kHz, which may or may not be real. Tomorrow we'll send the PLL control signal to MC2, which should lock it up just fine and give us time to twiddle laser diode current, measure the PLL loop shape, etc.

11911   Tue Jan 5 15:48:16 2016 SteveUpdatesafetyRat trap locations

Please look around when working close to these five locations. Use flashlights or leave lights on.

These mechanial traps are HAZARDOUS !

No visitors or tours till Monday, Jan 11  2016

Attachment 1: Control_Room.jpg
Attachment 2: EarmCESdoor.jpg
Attachment 3: 1Y1.jpg
Attachment 4: MC2.jpg
Attachment 5: XarmMaglev.jpg
11910   Tue Jan 5 13:17:06 2016 ranaUpdateLSCAUX X Freq Noise attempt

The problem here is that the MC displacement noise is leading to large frequency excursions of the PSL beam. Options

1. Feed back the low frequency PLL control signal to the MC2 length to suppress the excursion required by the Marconi. This is better than driving the laser, since the drive to the laser would be squashed by the MC locking loop.
2. Put the beat signal through a divider? Don't know if this makes the Marconi more able to handle it.
3. Turn on the MCL path. this will make the low frequency MC error signal go to the MC length, thereby reducing the low frequency feedback to the NPRO.
11909   Tue Jan 5 09:48:52 2016 SteveUpdatePEMRat trap moved

Our janitor confirmed that Q was not hallucinating about this animal. The dropping size indicating a good size one in the IFO room.

One of the mechanical traps moved from the control room to the east arm, close to the " machine shop " door.

I'm going to get more traps.

Quote:

Two mechanical and two sticdky traps were set to catch univited visitor.

Absolutely no food or food remains into inside garbage cans!!!!!!!!!!!!!!!!!!!!!!!!!

 Quote: A small rat / large mouse just ran through the control room. Ugh.

11908   Tue Jan 5 02:54:38 2016 ericqUpdateLSCAUX X Freq Noise attempt

[ericq, Gautam]

We set out to lock a marconi to the IR fiber beat of PSL + AUX X to measure some frequency noise, and failed.

In short, the Marconi's 1.6MHz max external FM isn't enough oomph to stabilize the PLL error signal. It's actually evident on the Agilent that the beat moves around a few times more than that, which I should've noticed sooner... We could briefly "lock" the PLL for a few tenths of a second, but weren't able to get a spectrum from this.

We also tried using the digital phase tracker temperature servo for some help at ~DC; this worked to the extent that we didn't have to twiddle the Marconi carrier frequency to stay on top of the fringes as the beat wandered, but it didn't otherwise stabilize the beat enough to make a difference in locking the PLL.

I suppose one more thing to try is to lock the PSL laser itself to each AUX laser in turn via PLL, and look for different / excess noise.

The Green and IR beat electronics are a in a little bit of disarray at the moment, but it's not like anyone else is going to be using them for the time being...

11907   Mon Jan 4 16:45:11 2016 gautamUpdateGreen LockingY-end AUX PDH noise breakdown

Summary:

I've re-measured the noise breakdown for the Y-end AUX PDH system. Spectra are attached. I've also measured the OLTF of the PDH loop, from which the UGF appears to be ~8.5kHz.

Discussion:

As Eric and Koji pointed out, the spectra uploaded here were clearly wrong as there were breaks in the spectra between decades of frequency. I redid the measurements, this time being extra careful about impedance mismatch effects. All measurements were made from the monitor points on the PDH box, which according to the schematic found here, have an output impedance of 49.9 ohms. So for all measurements made using the SR785 which has an input impedance of 1Mohm, or those which had an SR560 in the measurement chain (also high input impedance), I terminated the input with a 50ohm terminator so as to be able to directly match up spectra measured using the two different analyzers. I'm also using my more recent measurement of the actuator gain of the AUX laser to convert the control signal from V/rtHz to Hz/rtHz in the plotted spectra.

As a further check, I locked the IR to the Y-arm by actuating on MC2, and took the spectrum of the Y-arm mirror motion using the C1CAL model. We expect this to match up well with the in-loop control signal at low frequencies. However, though the shapes seem consistent in Attachment #2 (light orange and brown curves), I seem to be off by a factor of 5- not sure why. In converting the Y-arm mirror motion spectrum from m/rtHz to Hz/rtHz, I multiplied the measured spectrum by $\frac{3.907*10^6}{0.5*532*10^{-9}}$, which I think is the correct conversion factor (FSR/(0.5*wavelength))?

Attachment 1: ErrSigBreakdown.pdf
Attachment 2: controlSigBreakdown.pdf
Attachment 3: YEnd_PDH_OLTF.pdf
11906   Mon Jan 4 16:09:54 2016 gautamUpdateGreen LockingY end laser (Lightwave) PZT calibration

Summary:

I redid this measurement and have now determined the actuator gain to be 4.61 +/- 0.10 MHz/V. This is now pretty consistent with the expected value of ~5MHz/V as reported here.

Details:

I made the following changes to the old methodology:

1. Instead of integrating around the excitation frequency, I am now just taking the ratio of peak heights (phase tracker output / error signal monitor) to determine the actuator gain.
2. I had wrongly assumed that the phase tracker output was calibrated to green Hz and not IR Hz, so I was dividing by two where this was not necessary. I think this explains why my previous measurement yielded an answer approximately half the expected value.

I also took spectra of the phase tracker output and error signal to make sure I was choosing my excitation frequencies in regions where there were no peaks already present (Attachment #1).

The scatter of measured actuator gains at various excitation frequencies is shown in Attachment #2.

Attachment 1: choosingExcFreqs.pdf
Attachment 2: laserPZTcalib.pdf
11905   Mon Jan 4 14:45:41 2016 rana, eq, kojiConfigurationComputer Scripts / Programsnodus pwd change

We changed the password for controls on nodus this afternoon. We also zeroed out the authorized_keys file and then added back in the couple that we want in there for automatic backups / detchar.

Also did the recommended Ubuntu updates on there. Everything seems to be going OK so far. We think nothing on the interferometer side cares about the nodus password.

We also decided to dis-allow personal laptops on the new Martian router (to be installed soon).

11904   Wed Dec 30 11:09:52 2015 SteveUpdateSUS4.4M EQ

Suspensions recovered after 4.4 Mag EQ

Attachment 1: 4.4MeqDevore.png
Attachment 2: free.png
11903   Mon Dec 28 14:12:23 2015 SteveUpdateSUS4.2M EQ

Suspensions are recovered after 4.2 Mag earth quake. No obvoius sign of damage.

Attachment 1: 4.2Meq.png
Attachment 2: recovered4.2M.png
11902   Sat Dec 26 10:34:43 2015 SteveUpdateGeneraltoday

PMC locked manually and PRM sus damping restored.

Attachment 1: 1d.png
11901   Wed Dec 23 16:15:47 2015 ranaOmnistructureALARMfire alarm

Fire alarm went off several minutes ago. Talked to security and they said there was no fire. It beeped twice again just now. No one has been working on the IFO today.

11900   Wed Dec 23 15:43:02 2015 ranaSummaryPSLPMC FSS IMC RF summing box

The EOM upstream of the PMC is used as the phase corrector for the FSS/IMC servo. It is also used to apply the 35.5 MHz PDH RF sidebands for the PMC locking. There is a Pomona box which is used to merge the two signals onto a single cable for the EOM.

Does this circuit make sense to anyone?

Attachment 1: PMCFSSsummingBox.png
11899   Wed Dec 23 03:27:04 2015 ranaUpdateComputer Scripts / ProgramsLHO EPICS slow down

https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=24321

This LHO log indicates that EPICS slow down could be due to NFS activity. Could we make some trend of NFS activity on Chiara and then see if it correlates with EPICS flatlines?

I wonder if our EPICS issues frequency is correlated to the Chiara install.

11898   Tue Dec 22 16:44:03 2015 gautamUpdateGeneralFS725 Rubidium reference - REPAIRED
 Quote: However, the one that was recovered from the ATF lab is no longer locking to the Rubidium reference frequency, although it was locked at the time we disconnected it from the ATF lab. I emailed the support staff at SRS, who seem to think that either the internal oscillator has drifted too far, or the Rb lamp is dead. Either ways, it needs to be repaired. They suggested that I run a check by issuing some serial commands to the unit to determine which of these is actually the problem, but I've been having some trouble setting up the serial link - I will try this again tomorrow.

The Rubidium standard we had sent in for repair and recalibration has come back. I checked the following:

• Powered the unit on - it was locked to the internal rubidium reference within a few minutes as prescribed in the manual.
• After it had locked to the internal reference, I checked that it was able to lock to an external 1pps reference from our GPS timing unit- this too was achieved within a few minutes as prescribed in the manual

However, I am still having trouble setting up a serial communications link with the FS725 with a USB-serial adaptor - I've tried with a Raspberry Pi and my Mac (using screen to try and connect), and also using one of the old Windows laptops lying around on which I was able to install the native software supplied by SRS (still using the USB-serial adaptor to establish connection though). Could it be that the unit is incompatible with the USB-serial adaptor? I had specifically indicated in the repair request that this was also a problem. In any case, this doesn't seem to be crucial, though it would have been nice for diagnostics purposes in the future...

I've stored the repaired FS725 inside the electronics cabinet (marked "Eletronics Modules") for now (the other unit was returned to Antonio in W. Bridge some weeks ago).

Attachment 1: FS725_repaired.jpg
11897   Tue Dec 22 16:39:42 2015 SteveUpdateendtable upgradeETMY optical table enclosure

I think there should be a scientifically based aveluation of the ETMY enclosure so we can make the ETMX better.

Meanwhile I'm counting pieces to move on with the south end table cover.

Attachment 1: IMG_0028.JPG
Attachment 2: IMG_0027.JPG
Attachment 3: ETMY-ISCT_EISOL.jpg
11896   Tue Dec 22 16:23:33 2015 gautamUpdateIOOInput alignment to PMC tweaked

When I came in this afternoon, I saw that the PZT voltage to the PMC had railed. Following the usual procedure of turning the servo gain to zero and adjusting the DC offset, I got the PMC to relock, but the PMCR level was high and the alignment looked poor on the control room monitor. So I tweaked the input alignment on the PSL till I felt it was more reasonable. The view on the control room monitor now looks more like the usual state, and the "REFL (V)" field on the PMC MEDM screen now reads 0.02-0.03 which is the range I remember it being in nominally.

11895   Mon Dec 21 14:31:41 2015 SteveUpdatePEMRat traps set

Two mechanical and two sticdky traps were set to catch univited visitor.

Absolutely no food or food remains into inside garbage cans!!!!!!!!!!!!!!!!!!!!!!!!!

 Quote: A small rat / large mouse just ran through the control room. Ugh.

Attachment 1: ratsNC.jpg
11894   Mon Dec 21 02:29:49 2015 ericqUpdateLSCAUX X RIN measurements

I'll finish up the beat / frequency noise parts of the diagnosis tomorrow later, but I've done some investigation of the AUX X laser RIN.

I placed a PDA255 at one of the rejected beams from the PBS on the downstream side of the IR faraday, making sure the power didn't saturate the PD. I measured the RIN on a SR785, and simultaneously looked at the signal on a 100MHz scope.

The RIN has a very strong dependence on the laser diode current, and no noticable dependence on the crystal temperature or the presence of the PDH modulation / temperature control cables. Here are some traces, note that "nominal" current up until recently was 2.0A.

When adjusting the diode current, a peak beings to appear in the tens of kHz, eventually noticible in the DC power trace on the scope. The point at which this occurs is not fixed.

At all times, I saw a strong intensity fluctuation at around 380-400kHz on the scope whose amplitude fluctuated a fair amount (at least 75mVrms over Vdc=6.5V, but would often be 2 or 3 times that).

I didn't look at the frequency noise while doing this, because the WiFi at the X end was too slow, I'll do more tomorrow in the daytime.

Attachment 1: auxXRIN.pdf
11893   Sun Dec 20 23:23:54 2015 ericqUpdateALARMRats.

A small rat / large mouse just ran through the control room. Ugh.

11892   Fri Dec 18 17:37:04 2015 ranaUpdateLSCUncooperative AUX X

Here's how we should diagnose the EX laser:

1. Compare IR RIN of laser out to 100 kHz with that of another similar NPRO.
2. Look at time series of IR beat signal with a fast scope. Are there any high frequency glitches?
3. Disconnect all of the cables to the EX laser PZT and temperature control. Does the frequency noise change?
4. Change the temperature by +/- 1 deg to move away from mode hop regions. Remeasure RIN and frequency noise and plot.
11891   Thu Dec 17 16:44:03 2015 gautamUpdateCDSALS Slow control MEDM screen updated
 Quote: I've not updated the MEDM screens to reflect the two new paths yet, but will do so soon. It also remains to install appropriate filters for the servo path that takes the frequency readout as the input.

A few more related changes:

1. The couplers that used to sit on the green beat PDs on the PSL table have now been shifted to the IR broadband PDs in the FOL box so that I can get the IR beat frequency over to the frequency counters. The FOL box itself, along with the fibers that bring IR light to the PSL table, have been relocated to the corner of the PSL table where the green beat PDs sit because of cable length constraints.
2. I've updated the ALS slow control MEDM screen to allow for slow control of the beat frequency. The servo shape for now is essentially just an integrator with a zero at 1 Hz. The idea is to set an offset in the new filter module, which is the desired beat frequency, and let the integrator maintain this beat frequency. One thing I've not taken care of yet is automatically turning this loop off when the IMC loses lock. Screenshot of the modified MEDM screen is attached.
3. I checked the performance by using the temperature sliders to introduce an offset. The integrator is able to bring the beat frequency back to the setpoint in a few seconds, provided the step I introduced was not two big (~20 counts, but this is a pretty large shift in beat frequency, nearly 20MHz).

To do:

1. Figure out how to deal with the IMC losing lock. I guess this is important if we want to use the IR beatnote as a diagnostic for the state of the X AUX laser.
2. Optimize the servo gains a little - I still see some ringing when I introduce an offset, this could be avoided...
Attachment 1: ALS_SLOW_17DEC2015.png
11890   Thu Dec 17 14:02:05 2015 gautamUpdateCDSIPC channels for beat frequency control set up

I've set up two IPC channels that take the output from the digital frequency counters and send them to the end front-ends (via the RFM model). A summary of the steps I followed:

1. Set up two Dolphin channels in C1ALS to send the output of the frequency counter blocks to C1RFM (I initially used RFM blocks for these, but eric suggested using Dolphin IPC for the ALS->RFM branch, as they're faster.. Eric's removed the redundant channel names)
2. Set up two RFM channels in C1RFM to send the out put of the frequency counter blocks to C1SCX/Y (along with CDS monitor points to monitor the error rate and a filter module between the ALS->RFM and RFM->SCX/Y IPC blocks - I just followed what seemed to be the convention in the RFM model).
3. Set up the receiving channels in C1SCX and C1SCY
4. Re-compiled and re-started the models in the order C1ALS, C1RFM, C1SCX and C1SCY.

I've set things up such that we can select either the "PZT IN" or the frequency counter as the input to the slow servo, via means of a EPICS variable called "FC_SWITCH" (so C1:ALS-X_FC_SWITCH or C1:ALS-Y_FC_SWITCH). If this is 0, we use the default "PZT IN" signal, while setting it to 1 will change the input to the slow servo to be the frequency readout from the digital frequency counter. I've not updated the MEDM screens to reflect the two new paths yet, but will do so soon. It also remains to install appropriate filters for the servo path that takes the frequency readout as the input.

Tangentially related to this work: I've modified the FC library block so that it outputs frequency in MHz as opposed to Hz, just for convenience..

11889   Thu Dec 17 01:55:16 2015 ericqUpdateLSCUncooperative AUX X

[ericq, Gautam]

We were not able to fix the excess frequency noise of the AUX X laser by the usual laser diode current song and dance. Unfortunately, this level of noise is much too high to have any realistic chance of locking.

We're leaving things back in the IR beat -> phase tracker state with free running AUX lasers, on the off chance that there may be anything interesting to see in the overnight data. This may be limited by our lack of automatic beatnote frequency control. (Gautam will soon implement this via digital frequency counter). I've upped the FINE_PHASE_OUT_HZ_DQ frame rate to 16k from 2k, so we can see more of the spectrum.

For the Y beat, there is the additional weird phenomenon that the beat amplitude slowly oscillates to zero over ~10 minutes, and then back up to its maximum. This makes it hard for the phase tracker servo to stay stable... I don't have a good explanation for this.

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