ID |
Date |
Author |
Type |
Category |
Subject |
11863
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Tue Dec 8 15:40:48 2015 |
Steve | Update | VAC | glitchy RGA scan at day 434 |
The noise floor of the Rga scan is glitching less today
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Attachment 1: lessGlichingToday.png
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11865
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Tue Dec 8 23:24:08 2015 |
gautam | Update | Green Locking | Y end laser (Lightwave) PZT calibration |
Summary:
I measured the PZT actuator gain for the Lightwave NPRO at the Y-end to be 3.6 +/- 0.3 MHz/V. This is somewhat lower than the value of 5 MHz/V reported here, but I think is consistent with that measurement.
Details:
In order to calibrate the Y-axis of my Aux PDH loop noise budget plots, I wanted a measurement of the end laser actuator gain. I proceeded to measure this as follows:
- Use a function generator to add a DC offset to the error point - I did this by taking the output of the RF mixer -> Input A of an SR560, output of the function generator -> input B of the SR560 (via a 20 Ohm attenuator, and with a 50ohm T-eed to the input for impedance matching), and setting the output to A-B, and feeding that to the "Servo Input" on the PDH box.
- I then locked the arm to IR, ran the dither to maximize the green transmission, and set up a beat note at ~39 MHz with the help of the analyzer in the control room.
- Set phase tracker UGF, clear phase history.
- Vary the DC offset to the error point by using the offset on the function generator. I varied the offset until the green TEM00 lock was lost, in steps of 0.1 V. At each step, I averaged the output of the phase tracker for 15 seconds.
- Convert the applied DC offset to the DC offset appearing at the servo output using the transfer function of the servo box (DC gain measured to be ~65 dB), taking into account the 20dB attenuator also.
The attached plot shows the measured data. The X-axis is shown after the conversion mentioned in the last bullet point. The error bars are the standard deviations of the averaging at each DC offset.
To do:
- The value of the DC gain of the servo, 65 dB, is an approximate one based on a rough measurement I did earlier today. I'll take a TF measurement with an SR785 tomorrow, but I think this shouldn't change the number too much.
- Upload the noise budget measurements for the Y-end PDH loop.
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Attachment 1: Ycalib_8Dec.pdf
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11866
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Wed Dec 9 11:25:55 2015 |
Steve | Update | VAC | normal RGA scan at day 435-436 |
Glitches are gone. Rga scan is good
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Attachment 1: glichesGone.png
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Attachment 2: d436.png
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11868
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Wed Dec 9 19:01:45 2015 |
jamie | Update | CDS | back to fb1 |
I spent this afternoon trying to debug fb1, with very little to show for it. We're back to running from fb.
The first thing I did was to recompile EPICS from source, so that all the libraries needed by daqd were compiled for the system at hand. I compiled epics-3.14-12-2_long from source, and installed it at /opt/rtapps/epics on local disk, not on the /opt/rtapps network mount. I then recompiled daqd against that, and the framecpp, gds, etc from the LSCSoft packages. So everything has been compiled for this version of the OS. The compilation goes smoothly.
There are two things that I see while running this new daqd on fb1:
instability with mx_streams
The mx stream connection between the front ends and the daqd is flaky. Everything will run fine for a while, the spontaneously one or all of the mx_stream processes on the front ends will die. It appears more likely that all mx_stream processes will die at the same time. It's unclear if this is some sort of chain reaction thing, or if something in daqd or in the network itself is causing them all to die at the same time. It is independent of whether or not we're using multiple mx "end points" (i.e. a different one for each front end and separate receiver threads in the daqd) or just a single one (all front ends connecting to a single mx receiver thread in daqd).
Frequently daqd will recover from this. The monit processes on the front ends restart the mx_stream processes and all will be recovered. However occaissionally, possibly if the mx_streams do not recover fast enough (which seems to be related to how frequently the receiver threads in daqd can clear themselves), daqd will start to choke and will start spitting out the "empty blocks" messages that are harbirnger of doom:
Aborted 2 send requests due to remote peer 00:30:48:be:11:5d (c1iscex:0) disconnected
00:30:48:d6:11:17 (c1iscey:0) disconnected
mx_wait failed in rcvr eid=005, reqn=182; wait did not complete; status code is Remote endpoint is closed
disconnected from the sender on endpoint 005
mx_wait failed in rcvr eid=001, reqn=24; wait did not complete; status code is Remote endpoint is closed
disconnected from the sender on endpoint 001
[Wed Dec 9 18:40:14 2015] main profiler warning: 1 empty blocks in the buffer
[Wed Dec 9 18:40:15 2015] main profiler warning: 0 empty blocks in the buffer
[Wed Dec 9 18:40:16 2015] main profiler warning: 0 empty blocks in the buffer
My suspicion is that this time of failure is tied to the mx stream failures, so we should be looking at the mx connections and network to solve this problem.
frame writing troubles
There's possibly a separate issue associated with writing the second or minute trend files to disk. With fair regularity daqd will die soon after it starts to write out the trend frames, producing the similar "empty blocks" messages. |
11869
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Wed Dec 9 23:16:13 2015 |
rana | Update | Computer Scripts / Programs | Nodus security |
NDS2 and the usual ports so that we can use optimus as a comsol server.
Quote: |
I don't think there are any other ports we need open, but I could be wrong. Let me know if I broke something you need!
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11870
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Thu Dec 10 12:33:04 2015 |
yutaro | Update | LSC | strange behavior of ASDC |
I did additional tests for the strange behavior of ASCD. ETMY, ETMX and ITMY were misaligned so that only light reflected by ITMX went into AS port. I had done similar measurement before with ITMY YAW varied.
Attachment 1 shows how ASDC level changed when ITMX PIT varied.
Attachment 2 shows how ASDC level changed when ITMX YAW varied.
Attachment 3 shows how the power of light measured by a power meter just after the AS view port varied when ITMX YAW varied.
Comparing 1 & 2, we can say that this behavior is not unique to YAW direction.
From 2 & 3, we can say something strange is happening inside the chamber.
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Attachment 1: 07.png
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Attachment 2: 28.png
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Attachment 3: ASDC.png
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11871
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Thu Dec 10 19:53:22 2015 |
yutaro | Update | LSC | strange behavior of ASDC |
To check if the strange behavior of ASDC is caused by SR2/SR3 or not, I did the following measurement:
ASDC measures the power of the light reflected by ITMX. POXDC measures the power of the light reflected by ITMX and SRM successively. Then I varied the angle of ITMX in YAW direction and compared the behaviors of ASDC and POXDC.
The results are shown in Attachments 1-3.
As you can see in these figures, the strange up-and-down behavior appeared ONLY in ASDC. Therefore, the cause of this behavior exists between AS table and SRM (I had confirmed that the angle of SRM did not affect ASDC).
And this behavior is fringe-like, as can be seen in the figures (there seems to be 3 "peaks" and 2 "valleys"), so the cause could be interference between main path and not good AR reflection at a mirror after SRM before AS table (I suspect a mirror is flipped mistakenly). |
Attachment 1: 30.png
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Attachment 2: 11.png
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Attachment 3: 49.png
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11872
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Fri Dec 11 09:35:44 2015 |
yutaro | Update | LSC | Power recycling gain estimation from arm loss measurement |
I took PR3 AR reflectivity and calculated PRG (PR3 is flipped and so AR surface is inside PRC).
As shown in attached figure, which shows AR specification of the LaserOptik mirror (PR3 is this mirror), AR reflectivity of PR3 is ~0.5 %. Since resonant light in PRC goes through AR surface of PR3 4 times per round trip, round trip loss due to this is ~2 %. Then I got
PRG = 7.8.
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Attachment 1: LaserOptikAR.png
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11873
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Fri Dec 11 13:28:36 2015 |
Koji | Update | LSC | Power recycling gain estimation from arm loss measurement |
Can I ask you to make a plot of the power recycling gain as a function of the average arm loss, indicating the current loss value? |
11874
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Fri Dec 11 15:37:50 2015 |
yutaro | Update | LSC | Power recycling gain estimation from arm loss measurement |
Attached is the plot of relation between the average arm round trip loss and power recycling gain. 2 % loss due to PR3 AR reflection is taken into account. |
Attachment 1: PRG_plot.png
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11875
|
Fri Dec 11 16:16:36 2015 |
yutaro | Update | Optical Levers | Calibration of oplevs for ITMX/ETMX |
Based on calibration measurement I have done (elog 11785, 11831), I updated calibration factors of oplevs on medm screen as follows. Not to change loop gain oplev servo, I also changed oplev servo gain.
C1:SUS-ETMX_OL_PIT_CALIB, C1:SUS-ETMX_OL_PIT_GAIN
(45.1,16) => (200,3.5)
C1:SUS-ETMX_OL_YAW_CALIB, C1:SUS-ETMX_OL_YAW_GAIN
(85.6,8) => (222,3.0)
C1:SUS-ETMY_OL_PIT_CALIB, C1:SUS-ETMY_OL_PIT_GAIN
(26,-16) => (140,-3.0)
C1:SUS-ETMY_OL_YAW_CALIB, C1:SUS-ETMY_OL_YAW_GAIN
(31,-21) => (143,-4.5)
C1:SUS-ITMX_OL_PIT_CALIB, C1:SUS-ITMX_OL_PIT_GAIN
(110,8) => (122,7.2)
C1:SUS-ITMX_OL_YAW_CALIB, C1:SUS-ITMX_OL_YAW_GAIN
(81,-11) => (147,-6)
C1:SUS-ITMY_OL_PIT_CALIB, C1:SUS-ITMY_OL_PIT_GAIN
(159,15) => (239,10)
C1:SUS-ITMY_OL_YAW_CALIB, C1:SUS-ITMY_OL_YAW_GAIN
(174,-21) => (226,-16)
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11877
|
Sun Dec 13 21:55:28 2015 |
gautam | Update | Green Locking | Y end laser (Lightwave) PZT calibration |
Summary:
After the discussions at the Wednesday meeting, I redid this measurement using a sinusoidal excitation summed at the error-point of the PDH servo as opposed to a DC offset. From the data I collected, I measured the actuator gain to be 2.43 +/- 0.04 MHz/V. This is almost half the value we expect, I'm not sure if I'm missing something obvious.
Details:
- Attachment #1 is a sketch of the measurement setup and points at which signals are measured/calculated. Some important changes:
- I am now using the channel C1:ALS-Y_ERR_MON_OUT to directly measure the input signal to the servo. In order to get the calibration constant for this channel from counts to volts, I simply hooked up the input to the channel to an oscilloscope and noted the amplitude of the signal seen on the scope in volts. The number I have used is 52uV/count (note that the signal to the ADC is amplified by a factor of 10 by an SR560).
- I measured the transfer function from the input to the servo (marked "A" in the sketch) to the output of the Pomona box going to the laser PZT (marked "B" on the sketch) using an SR785 - see Attachment #2. This allowed me to convert the amplitude of excitation at A to an amplitude at B, which is what we need, as we want to measure C/B.
- The measurement itself was done by locking the arms to IR, running ASS to maximize IR transmission, setting up a green beat note, and then measuring the two channels of interest with the excitation to the error-point on.
- I was initially trying to use time-series plots to measure these amplitudes - Koji suggested I use the Fourier domain instead, and so I took FFTs of the two channels we are interested in (using a flat-top window with 0.1 Hz BW) and estimated the RMS values at the frequency at which I had injected an excitation. Data+code used is in Attachment #3. In particular, I was integrating the PSD over 1Hz centered at the excitation frequency in order to calculate the RMS power at the excitation frequency - it could be that for C1:ALS-BEATY_FINE_PHASE_OUT_HZ, the spectral leakage into neighbouring bins is more significant than for C1:ALS-Y_ERR_MON_OUT (see Attachment #4)?
- With the amplitudes thus obtained, I took the ratio C/B (see sketch) to determine the MHz/V actuator gain. I had injected excitations at 5 frequencies (916Hz, 933Hz, 977Hz, 1030Hz and 1067Hz, choses in relatively "quiet" parts of the spectrum of C1:ALS-Y_ERR_MON_OUT with no excitations), and the result reported is the average from these five measurements, while the error is the standard deviation in the 5 measurements.
- Unrelated to this meaurement - while I had the SR560 hooked up to the input of the PDH box, I inverted the mixer output to the servo input, as I thought I could use this method to estimate the modulation depth. I did so by locking the Y arm green to the sideband TEM00 mode, and comparing the green transmission in this state to that when the Y arm is locked to a carrier TEM00 mode. I averaged C1:ALS-TRY_OUT for 10 seconds in 3 cases: (i) Carrier TEM00, (ii)sideband TEM00, and (iii) shutter closed - from this measurement, I estimate the modulation depth to be 0.209 +/- 0.006 (errors used to calculate the total error were the standard deviations of the measured transmission).
Next steps:
- Check that I have not missed out anything obvious in estimating the actuator gain - particularly the spectral leakage bit I mentioned above.
- If this methodology and measurement is legitimate, repeat for the X end, and complete the noise budgeting for both AUX PDH loops.
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Attachment 1: IMG_5972.JPG
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Attachment 2: ServoY_TF_13Dec2015.pdf
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Attachment 3: DatanCode.zip
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Attachment 4: PSD_916Hz.pdf
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11878
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Mon Dec 14 14:08:49 2015 |
Steve | Update | SUS | Ruby wire standoffs update |
Two companies are willing to make the ruby grooves and the third one is still working on their quote.
The price is ~$100 each. The cost goes down 10% if we order 50 instead of 30 pieces.
How many should we get ? |
11879
|
Mon Dec 14 16:27:11 2015 |
gautam | Update | Green Locking | Y-end AUX PDH noise breakdown |
Summary:
I've attached the results from my measurements of the noise characteristics of the Y-end auxiliary PDH system.
Details:
The following spectra were measured, in the range DC-1MHz:
- Analyzer noise floor (measured with input terminated)
- Green REFL PD dark noise (measured with the Y-end green shutter closed)
- Mixer noise (measured with input to mixer terminated - measured with an SR560 with a gain of 100)
- Servo noise (measured with input to servo terminated)
- In loop error signal (measured with green locked to Y-arm, LSC off - using monitor point on PDH box)
- In loop control signal (measured with green locked to Y-arm, LSC off - using monitor point on PDH box)
In order to have good spectral resolution, the frequency range was divided into 5 subsections: DC-200Hz, 200Hz-3.4kHz, 3.4kHz-16.2kHz, 10kHz-100kHz, 100kHz-1MHz. The first three are measured using the SR785, while the last two ranges are measured with the Agilent network analyzer. The spectrum of the mixer output with its input terminated was quite close to the analyzer noise floor - hence, this was measured with an S560 preamplifier set to a gain of 100, and subsequently dividing the ASD by 100. To convert the Y-axis from V/rtHz to Hz/rtHz, I used two conversion factors: for the analyzer noise floor, PD dark noise, mixer noise and in-loop error signal, I made an Optickle simulation of a simple FP cavity (all parameters taken from the wiki optics page, except that I put in Yutaro's measured values for the arm loss and a modulation depth of 0.21 which I estimated as detailed here), and played around with the demodulation phase until I got an error signal that had the same qualitative shape as what I observed on an oscilloscope with the arms freely swinging (feedback to the laser PZT disabled). The number I finally used is 45.648 kHz/V (the main horns were 800mV peak-to-peak on an oscilloscope trace, results of the Optickle FP cavity simulation shown in Attachment #2 used to calibrate the X-axis). For the servo noise spectrum and in-loop control signal, I used the value of 2.43 MHz/V as determined here.
I'm not sure what to make of the strong peaks in the mixer noise spectrum between ~60Hz and 10kHz - some of the more prominent peaks are 60Hz harmonics, but there are several peaks in between as well (these have been confusing me for some time now, they were present even when I made the measurement in this frequency range using the Agilent network analyzer. My plan is to repeat these measurements for the Xend now. |
Attachment 1: YAUX_NB_Dec2015.pdf
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Attachment 2: PDH_errSig_Calib.pdf
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11880
|
Mon Dec 14 16:46:42 2015 |
ericq | Update | WienerFiltering | Noise Subtraction Puzzler |
Here's something to ponder.
Our online MCL feedforward uses perpendicular vertex T240 seismometer signals as input. When designing a feedforward filter, whether FIR Wiener or otherwise, we posit that the PSD of the best linear subtraction one can theoretically achieve is given by the coherence, via Psub = P(1-C).
If we have more than one witness input, but they are completely uncorrelated, then this extends to Psub = P(1-C1)(1-C2). However, in reality, there are correlations between the witnesses, which would make this an overestimate of how much noise power can be subtracted.
Now, I present the actual MCL situation. [According to Ignacio's ELOG (11584), the online performance is not far from this offline prediction]

Somehow, we are able to subtract much more noise at ~1Hz than the coherence would lead you to believe. One suspicion of mine is that the noise at 1Hz is quite nonstationary. Using median [C/P]SDs should help with this in principle, but the above was all done with medians, and using the mean is not much different.
Thinking back to one of the metrics that Eve and Koji were talking about this summer, (std(S)/mean(S), where S is the spectrogram of the signal) gives an answer of ~2.3 at that peak at 1.4Hz, which is definitely in the nonstationary regieme, but I don't have much intution into just how severe that value is.
So, what's the point of all this? We generally use coherence as a heuristic to judge whether we should bother attempting any noise subtraction in the first place, so I'm troubled by a circumstance in which there is much more subtraction to be had than coherence leads us to believe. I would like to come up with a way of predicting MISO subtraction results of nonstationary couplings more reliably. |
Attachment 1: subpuzz.pdf
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11881
|
Mon Dec 14 23:49:03 2015 |
ericq | Update | Optical Levers | Calibration of oplevs for ITMX/ETMX |
Quote: |
Based on calibration measurement I have done (elog 11785, 11831), I updated calibration factors of oplevs on medm screen as follows. Not to change loop gain oplev servo, I also changed oplev servo gain.
|
After making sure that the upper UGFs were properly in place, I saved these settings to the SDF files. Thanks Yutaro! |
11882
|
Mon Dec 14 23:56:29 2015 |
ericq | Update | CDS | c1pem reverted |
To get C1PEM data back into the frames, I removed the new BLRMS blocks, recompiled, reinstalled, re-enabled it in daqd, restarted.
We still really want more headroom in our framebuilder situation. |
11883
|
Tue Dec 15 11:22:53 2015 |
gautam | Update | CDS | c1scx and c1asx crashed |
I noticed what I thought was excessive movement of the beam spot on ITMX and ETMX on the control room monitors, and when I checked the CDS FE status overview MEDM screen, I saw that c1scx and c1asx had crashed. I ssh-ed into c1iscex and restarted both models, and then restarted fb as well. However, the DAQ-DCO_C1SCX_STATUS indicator remains red even after restarting fb (see attached screenshot). I am not sure how to fix this so I am leaving it as is for now, and the X arm looks to have settled down. |
Attachment 1: CDS_FE_STATUS_OVERVIEW_15DEC2015.png
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11884
|
Tue Dec 15 18:08:22 2015 |
Max Isi | Update | General | Summary archive cleaning cron job |
I have added a new cron job in pcdev1 at CIT using the 40m shared account. This will run the /home/40m/DetectorChar/bin/cleanarchive script one minute past midnight on the first of every month. The script removes GWsumm archive files older than 1 month old. |
11885
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Wed Dec 16 10:22:14 2015 |
Steve | Update | IOO | this morning |
c1sus and c1ioo were restarted. PMC locked.
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Attachment 1: PMClocked.png
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11886
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Wed Dec 16 10:56:22 2015 |
gautam | Update | CDS | hard reboot of FB |
[ericq,gautam]
Forgot to submit this yesterday...
While we were trying to get the X-arm locked to IR using MC2, frame-builder mysteriously crashed, necessitating us having to go down to the computer and perform a hard reboot (after having closed the PSL shutter and turning all the watchdogs to "shutdown"). All the models restarted by themselves, and everything seems back to normal now.. |
11887
|
Wed Dec 16 18:34:40 2015 |
gautam | Update | Green Locking | Green beat channels temporarily set up as IR beat channels |
Since there are a few hours to go before the locking efforts tonight, I've temporarily borrowed the channels used to read out the green beat frequency, and have hooked them up to the broadband IR PDs in the FOL box on the PSL table. I've used the network analyzer in the control room to roughly position the two beatnotes. I've also turned the green beat PDs back on (since the PSL shutter has to be open for the IR beat, and there is some green light falling on these PDs, but I've terminated the outputs).
So this needs to be switched back before locking efforts tonight... |
11888
|
Wed Dec 16 23:15:28 2015 |
ericq | Update | Green Locking | Green beat channels temporarily set up as IR beat channels |
With the IR beats going to the nominal ALS channels as Gautam left them, we're able to measure the free running frequency noise of the end AUX lasers.
Specifically, the end shutters are closed, leaving the AUX lasers free running. The IR beats then consist of this free running light beating with the PSL light, and the ALS phase trackers give a calibrated frequency noise spectrum. I've stabilized the PSL light by locking the laser to the Y arm via MC2 acutation, so the free running AUX laser noise should dominate by a lot above the suspension resonances. This also has the benefit of giving me the use of the CAL'd Y arm displacement as a sanity check.

At this point in time, it looks like the X laser is close to 10x noisier than the Y laser, though it does seem to be at the rule-of-thumb "10kHz/rtHz at 100Hz" level. |
Attachment 1: 2015-12-16_AUXfreerunning.pdf
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11889
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Thu Dec 17 01:55:16 2015 |
ericq | Update | LSC | Uncooperative AUX X |
[ericq, Gautam]
We were not able to fix the excess frequency noise of the AUX X laser by the usual laser diode current song and dance. Unfortunately, this level of noise is much too high to have any realistic chance of locking. 
We're leaving things back in the IR beat -> phase tracker state with free running AUX lasers, on the off chance that there may be anything interesting to see in the overnight data. This may be limited by our lack of automatic beatnote frequency control. (Gautam will soon implement this via digital frequency counter). I've upped the FINE_PHASE_OUT_HZ_DQ frame rate to 16k from 2k, so we can see more of the spectrum.
For the Y beat, there is the additional weird phenomenon that the beat amplitude slowly oscillates to zero over ~10 minutes, and then back up to its maximum. This makes it hard for the phase tracker servo to stay stable... I don't have a good explanation for this. |
11890
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Thu Dec 17 14:02:05 2015 |
gautam | Update | CDS | IPC channels for beat frequency control set up |
I've set up two IPC channels that take the output from the digital frequency counters and send them to the end front-ends (via the RFM model). A summary of the steps I followed:
- Set up two Dolphin channels in C1ALS to send the output of the frequency counter blocks to C1RFM (I initially used RFM blocks for these, but eric suggested using Dolphin IPC for the ALS->RFM branch, as they're faster.. Eric's removed the redundant channel names)
- Set up two RFM channels in C1RFM to send the out put of the frequency counter blocks to C1SCX/Y (along with CDS monitor points to monitor the error rate and a filter module between the ALS->RFM and RFM->SCX/Y IPC blocks - I just followed what seemed to be the convention in the RFM model).
- Set up the receiving channels in C1SCX and C1SCY
- Re-compiled and re-started the models in the order C1ALS, C1RFM, C1SCX and C1SCY.
I've set things up such that we can select either the "PZT IN" or the frequency counter as the input to the slow servo, via means of a EPICS variable called "FC_SWITCH" (so C1:ALS-X_FC_SWITCH or C1:ALS-Y_FC_SWITCH). If this is 0, we use the default "PZT IN" signal, while setting it to 1 will change the input to the slow servo to be the frequency readout from the digital frequency counter. I've not updated the MEDM screens to reflect the two new paths yet, but will do so soon. It also remains to install appropriate filters for the servo path that takes the frequency readout as the input.
Tangentially related to this work: I've modified the FC library block so that it outputs frequency in MHz as opposed to Hz, just for convenience.. |
11891
|
Thu Dec 17 16:44:03 2015 |
gautam | Update | CDS | ALS Slow control MEDM screen updated |
Quote: |
I've not updated the MEDM screens to reflect the two new paths yet, but will do so soon. It also remains to install appropriate filters for the servo path that takes the frequency readout as the input.
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A few more related changes:
- The couplers that used to sit on the green beat PDs on the PSL table have now been shifted to the IR broadband PDs in the FOL box so that I can get the IR beat frequency over to the frequency counters. The FOL box itself, along with the fibers that bring IR light to the PSL table, have been relocated to the corner of the PSL table where the green beat PDs sit because of cable length constraints.
- I've updated the ALS slow control MEDM screen to allow for slow control of the beat frequency. The servo shape for now is essentially just an integrator with a zero at 1 Hz. The idea is to set an offset in the new filter module, which is the desired beat frequency, and let the integrator maintain this beat frequency. One thing I've not taken care of yet is automatically turning this loop off when the IMC loses lock. Screenshot of the modified MEDM screen is attached.
- I checked the performance by using the temperature sliders to introduce an offset. The integrator is able to bring the beat frequency back to the setpoint in a few seconds, provided the step I introduced was not two big (~20 counts, but this is a pretty large shift in beat frequency, nearly 20MHz).
To do:
- Figure out how to deal with the IMC losing lock. I guess this is important if we want to use the IR beatnote as a diagnostic for the state of the X AUX laser.
- Optimize the servo gains a little - I still see some ringing when I introduce an offset, this could be avoided...
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Attachment 1: ALS_SLOW_17DEC2015.png
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11892
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Fri Dec 18 17:37:04 2015 |
rana | Update | LSC | Uncooperative AUX X |
Here's how we should diagnose the EX laser:
- Compare IR RIN of laser out to 100 kHz with that of another similar NPRO.
- Look at time series of IR beat signal with a fast scope. Are there any high frequency glitches?
- Disconnect all of the cables to the EX laser PZT and temperature control. Does the frequency noise change?
- Change the temperature by +/- 1 deg to move away from mode hop regions. Remeasure RIN and frequency noise and plot.
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11893
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Sun Dec 20 23:23:54 2015 |
ericq | Update | ALARM | Rats. |
A small rat / large mouse just ran through the control room. Ugh. |
11894
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Mon Dec 21 02:29:49 2015 |
ericq | Update | LSC | AUX X RIN measurements |
I'll finish up the beat / frequency noise parts of the diagnosis tomorrow later, but I've done some investigation of the AUX X laser RIN.
I placed a PDA255 at one of the rejected beams from the PBS on the downstream side of the IR faraday, making sure the power didn't saturate the PD. I measured the RIN on a SR785, and simultaneously looked at the signal on a 100MHz scope.
The RIN has a very strong dependence on the laser diode current, and no noticable dependence on the crystal temperature or the presence of the PDH modulation / temperature control cables. Here are some traces, note that "nominal" current up until recently was 2.0A.

When adjusting the diode current, a peak beings to appear in the tens of kHz, eventually noticible in the DC power trace on the scope. The point at which this occurs is not fixed.
At all times, I saw a strong intensity fluctuation at around 380-400kHz on the scope whose amplitude fluctuated a fair amount (at least 75mVrms over Vdc=6.5V, but would often be 2 or 3 times that).
I didn't look at the frequency noise while doing this, because the WiFi at the X end was too slow, I'll do more tomorrow in the daytime. |
Attachment 1: auxXRIN.pdf
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11895
|
Mon Dec 21 14:31:41 2015 |
Steve | Update | PEM | Rat traps set |
Two mechanical and two sticdky traps were set to catch univited visitor.
Absolutely no food or food remains into inside garbage cans!!!!!!!!!!!!!!!!!!!!!!!!!
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A small rat / large mouse just ran through the control room. Ugh.
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Attachment 1: ratsNC.jpg
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Tue Dec 22 16:23:33 2015 |
gautam | Update | IOO | Input alignment to PMC tweaked |
When I came in this afternoon, I saw that the PZT voltage to the PMC had railed. Following the usual procedure of turning the servo gain to zero and adjusting the DC offset, I got the PMC to relock, but the PMCR level was high and the alignment looked poor on the control room monitor. So I tweaked the input alignment on the PSL till I felt it was more reasonable. The view on the control room monitor now looks more like the usual state, and the "REFL (V)" field on the PMC MEDM screen now reads 0.02-0.03 which is the range I remember it being in nominally. |
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Tue Dec 22 16:39:42 2015 |
Steve | Update | endtable upgrade | ETMY optical table enclosure |
I think there should be a scientifically based aveluation of the ETMY enclosure so we can make the ETMX better.
Meanwhile I'm counting pieces to move on with the south end table cover.
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Attachment 1: IMG_0028.JPG
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Attachment 2: IMG_0027.JPG
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Attachment 3: ETMY-ISCT_EISOL.jpg
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Tue Dec 22 16:44:03 2015 |
gautam | Update | General | FS725 Rubidium reference - REPAIRED |
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However, the one that was recovered from the ATF lab is no longer locking to the Rubidium reference frequency, although it was locked at the time we disconnected it from the ATF lab. I emailed the support staff at SRS, who seem to think that either the internal oscillator has drifted too far, or the Rb lamp is dead. Either ways, it needs to be repaired. They suggested that I run a check by issuing some serial commands to the unit to determine which of these is actually the problem, but I've been having some trouble setting up the serial link - I will try this again tomorrow.
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The Rubidium standard we had sent in for repair and recalibration has come back. I checked the following:
- Powered the unit on - it was locked to the internal rubidium reference within a few minutes as prescribed in the manual.
- After it had locked to the internal reference, I checked that it was able to lock to an external 1pps reference from our GPS timing unit- this too was achieved within a few minutes as prescribed in the manual.

However, I am still having trouble setting up a serial communications link with the FS725 with a USB-serial adaptor - I've tried with a Raspberry Pi and my Mac (using screen to try and connect), and also using one of the old Windows laptops lying around on which I was able to install the native software supplied by SRS (still using the USB-serial adaptor to establish connection though). Could it be that the unit is incompatible with the USB-serial adaptor? I had specifically indicated in the repair request that this was also a problem. In any case, this doesn't seem to be crucial, though it would have been nice for diagnostics purposes in the future...
I've stored the repaired FS725 inside the electronics cabinet (marked "Eletronics Modules") for now (the other unit was returned to Antonio in W. Bridge some weeks ago). |
Attachment 1: FS725_repaired.jpg
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Wed Dec 23 03:27:04 2015 |
rana | Update | Computer Scripts / Programs | LHO EPICS slow down |
https://alog.ligo-wa.caltech.edu/aLOG/index.php?callRep=24321
This LHO log indicates that EPICS slow down could be due to NFS activity. Could we make some trend of NFS activity on Chiara and then see if it correlates with EPICS flatlines?
I wonder if our EPICS issues frequency is correlated to the Chiara install. |
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Sat Dec 26 10:34:43 2015 |
Steve | Update | General | today |
PMC locked manually and PRM sus damping restored. |
Attachment 1: 1d.png
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Mon Dec 28 14:12:23 2015 |
Steve | Update | SUS | 4.2M EQ |
Suspensions are recovered after 4.2 Mag earth quake. No obvoius sign of damage.
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Attachment 1: 4.2Meq.png
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Attachment 2: recovered4.2M.png
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Wed Dec 30 11:09:52 2015 |
Steve | Update | SUS | 4.4M EQ |
Suspensions recovered after 4.4 Mag EQ
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Attachment 1: 4.4MeqDevore.png
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Attachment 2: free.png
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Mon Jan 4 16:09:54 2016 |
gautam | Update | Green Locking | Y end laser (Lightwave) PZT calibration |
Summary:
I redid this measurement and have now determined the actuator gain to be 4.61 +/- 0.10 MHz/V. This is now pretty consistent with the expected value of ~5MHz/V as reported here.
Details:
I made the following changes to the old methodology:
- Instead of integrating around the excitation frequency, I am now just taking the ratio of peak heights (phase tracker output / error signal monitor) to determine the actuator gain.
- I had wrongly assumed that the phase tracker output was calibrated to green Hz and not IR Hz, so I was dividing by two where this was not necessary. I think this explains why my previous measurement yielded an answer approximately half the expected value.
I also took spectra of the phase tracker output and error signal to make sure I was choosing my excitation frequencies in regions where there were no peaks already present (Attachment #1).
The scatter of measured actuator gains at various excitation frequencies is shown in Attachment #2. |
Attachment 1: choosingExcFreqs.pdf
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Attachment 2: laserPZTcalib.pdf
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Mon Jan 4 16:45:11 2016 |
gautam | Update | Green Locking | Y-end AUX PDH noise breakdown |
Summary:
I've re-measured the noise breakdown for the Y-end AUX PDH system. Spectra are attached. I've also measured the OLTF of the PDH loop, from which the UGF appears to be ~8.5kHz.
Discussion:
As Eric and Koji pointed out, the spectra uploaded here were clearly wrong as there were breaks in the spectra between decades of frequency. I redid the measurements, this time being extra careful about impedance mismatch effects. All measurements were made from the monitor points on the PDH box, which according to the schematic found here, have an output impedance of 49.9 ohms. So for all measurements made using the SR785 which has an input impedance of 1Mohm, or those which had an SR560 in the measurement chain (also high input impedance), I terminated the input with a 50ohm terminator so as to be able to directly match up spectra measured using the two different analyzers. I'm also using my more recent measurement of the actuator gain of the AUX laser to convert the control signal from V/rtHz to Hz/rtHz in the plotted spectra.
As a further check, I locked the IR to the Y-arm by actuating on MC2, and took the spectrum of the Y-arm mirror motion using the C1CAL model. We expect this to match up well with the in-loop control signal at low frequencies. However, though the shapes seem consistent in Attachment #2 (light orange and brown curves), I seem to be off by a factor of 5- not sure why. In converting the Y-arm mirror motion spectrum from m/rtHz to Hz/rtHz, I multiplied the measured spectrum by , which I think is the correct conversion factor (FSR/(0.5*wavelength))? |
Attachment 1: ErrSigBreakdown.pdf
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Attachment 2: controlSigBreakdown.pdf
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Attachment 3: YEnd_PDH_OLTF.pdf
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Tue Jan 5 02:54:38 2016 |
ericq | Update | LSC | AUX X Freq Noise attempt |
[ericq, Gautam]
We set out to lock a marconi to the IR fiber beat of PSL + AUX X to measure some frequency noise, and failed.
In short, the Marconi's 1.6MHz max external FM isn't enough oomph to stabilize the PLL error signal. It's actually evident on the Agilent that the beat moves around a few times more than that, which I should've noticed sooner... We could briefly "lock" the PLL for a few tenths of a second, but weren't able to get a spectrum from this.
We also tried using the digital phase tracker temperature servo for some help at ~DC; this worked to the extent that we didn't have to twiddle the Marconi carrier frequency to stay on top of the fringes as the beat wandered, but it didn't otherwise stabilize the beat enough to make a difference in locking the PLL.
I suppose one more thing to try is to lock the PSL laser itself to each AUX laser in turn via PLL, and look for different / excess noise.
The Green and IR beat electronics are a in a little bit of disarray at the moment, but it's not like anyone else is going to be using them for the time being... |
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Tue Jan 5 09:48:52 2016 |
Steve | Update | PEM | Rat trap moved |
Our janitor confirmed that Q was not hallucinating about this animal. The dropping size indicating a good size one in the IFO room.
One of the mechanical traps moved from the control room to the east arm, close to the " machine shop " door.
I'm going to get more traps.
Quote: |
Two mechanical and two sticdky traps were set to catch univited visitor.
Absolutely no food or food remains into inside garbage cans!!!!!!!!!!!!!!!!!!!!!!!!!
Quote: |
A small rat / large mouse just ran through the control room. Ugh.
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Tue Jan 5 13:17:06 2016 |
rana | Update | LSC | AUX X Freq Noise attempt |
The problem here is that the MC displacement noise is leading to large frequency excursions of the PSL beam. Options
- Feed back the low frequency PLL control signal to the MC2 length to suppress the excursion required by the Marconi. This is better than driving the laser, since the drive to the laser would be squashed by the MC locking loop.
- Put the beat signal through a divider? Don't know if this makes the Marconi more able to handle it.
- Turn on the MCL path. this will make the low frequency MC error signal go to the MC length, thereby reducing the low frequency feedback to the NPRO.
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Tue Jan 5 15:48:16 2016 |
Steve | Update | safety | Rat trap locations |
Please look around when working close to these five locations. Use flashlights or leave lights on.
These mechanial traps are HAZARDOUS !
No visitors or tours till Monday, Jan 11 2016 |
Attachment 1: Control_Room.jpg
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Attachment 2: EarmCESdoor.jpg
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Attachment 3: 1Y1.jpg
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Attachment 4: MC2.jpg
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Attachment 5: XarmMaglev.jpg
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Tue Jan 5 16:33:45 2016 |
ericq | Update | LSC | AUX X Freq Noise attempt |
Turning on the MCL path (in addition to the MCL FF we always have on) let me lock the PLL for multiple seconds, but low frequency excursions still break it in the end. I was able to briefly observe a level of ~50Hz/rtHz at 1kHz, which may or may not be real. Tomorrow we'll send the PLL control signal to MC2, which should lock it up just fine and give us time to twiddle laser diode current, measure the PLL loop shape, etc. |
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Tue Jan 5 17:19:57 2016 |
rana | Update | safety | Rat trap locations |
In the modern times, people use glue traps to catch rats instead of springs. They are less hazardous to people and don't spread rat fluid on the floor. |
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Wed Jan 6 08:09:04 2016 |
Steve | Update | PEM | 4.5 Mag Banning EQ |
IFO restored after 4.5 Mag Banning, Ca earthquake. |
Attachment 1: 4.5Mag__Banning.png
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Wed Jan 6 10:58:03 2016 |
Steve | Update | General | projector light bulb is out |
Projector light bulb ordered
Quote: |
[ Manasa, Ericq and Steve ]
Vivitek D952HD with 186 hours installed.
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Wed Jan 6 16:40:49 2016 |
ericq | Update | General | New WiFi router |
The new wifi router, a Netgear R6400, has been installed, next to the old one which is disconnected (but not yet removed).
Same SSID, and I've added only the wireless MAC addresses of viviana, paoloa and asia, the three thinkpads inside.
Qualitatively, dataviewer at the X end seems pretty snappy. I'll do some more quantitative comparison of the two routers at some point soon. I will update the wiki, too. |
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Thu Jan 7 04:28:39 2016 |
ericq | Update | LSC | AUX X Freq Noise measured |
[ericq, Gautam]
Brief summary of tonights work:
- Locked Marconi to AUX X vs PSL beat at around 320MHz, PSL shutter closed (i.e. both lasers free running)
- Measured control signal spectrum at various laser diode currents, crystal temperatures. Oddly, spectra remained consistent across these variables.
- Measured OLG of PLL to calibrate into open-loop frequency noise of the beat, found UGF ~30kHz
Our "requirement" for the end laser is as follows: We expect to (and have in the past) achieved ALS sensitivity of 1Hz/rtHz at 100 Hz. If the end PDH loop is 1/f from 100Hz-10kHz, then we have 40dB of supression at 100Hz, meaning the free running AUX laser noise should be no more than 100Hz/rtHz at 100Hz.
So, if we expect both the PSL and AUX lasers to have this performance when free running, we would get the green curve below. We do not. 

I'll post more details about the exact currents, temperatures and include calibrated plots for the >30kHz range later. Here's the OLG for kicks.

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Attachment 1: PLLspec.pdf
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Attachment 2: PLL_OLG.pdf
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Thu Jan 7 15:29:54 2016 |
ericq | Update | WienerFiltering | Noise Subtraction Puzzler |
The puzzle continues...
I found some reference for computing "multicoherence," which should properly estimate the potential MISO subtraction potential in situations where the witness channels themselves have nontrivial coherence. Specifically, I followed the derivations in LIGO-P990002. The underlying math is related to principal component analysis (PCA) or gram-schmidt orthogonalization.
This produced the following results, wherein the Wiener subtraction is still below what the coherences predict.

I've attached the data and code that produced this plot. |
Attachment 1: subpuzz2.pdf
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Attachment 2: puzzle.zip
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