attached plot shows MC_IN1/MC_IN2. needs work.
This is supposed to be a measurement of the relative gain of the MCL and AO paths in the CM servo. We expect there to
be a more steep slope (ideally 1/f). Somehow the magnitude is very shallow and so the crossover is not stable. Possible
causes? Saturations in the measurement, broken whitening filters, extremely bad delay in the digital system? needs work.