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Entry  Thu Feb 13 01:47:39 2020, gautam, Update, ALS, Fast ALS - delay line prep delaySlider.pngdelayLineLosses.pdfdelayLineCal.pdf
    Reply  Fri Feb 14 00:53:50 2020, gautam, Update, ALS, Fast ALS - more setup CMSlow_ALSnoise.pdfOLTFmeas.pdf
Message ID: 15209     Entry time: Thu Feb 13 01:47:39 2020     Reply to this: 15212
Author: gautam 
Type: Update 
Category: ALS 
Subject: Fast ALS - delay line prep 

A few years ago, Koji and I setup a delay line phase shifter, which can be used to impart a (switchable) delay to a signal path. Since we talked about reviving the fast (= high bandwidth) ALS control scheme at the meeting, I reminded myself of the infrastructure available.

  • Schematic
  • Comprehensive note on theory of operation / performance.
  • Past elog threads - #11603 and #11604.
  • Attachment #1 - my modification to the ALS screen to add a slider that controls the channel C1:LSC-BO_1_0_SET. The label is a bit misleading for now - elog11604 tells you the conversion between this slider value and the actual delay in nanoseconds, but I couldn't get a soft channel set up that correctly FLNKed to this record. In the process of trying to do so, I edited the C1_ISC-AUX_ALS.db file, and also restarted the modbus and latch processes on c1iscaux a few times.
  • Attachment #2 - frequency dependent loss for some representative delays. At ~200 MHz, I find the measured loss to be > 8dB, which is ~2dB more than what the D. Sigg note tells me to expect. This is rather a lot of loss, but I guess it's okay. Measurement cable loss was calibrated out with the AG4395A.
  • Attachment #3 - confirmation of constantness of delay as a function of frequency, for some representative delays. The "undelayed" setting corresponds to a fixed delay of ~4 nsec, which is consistent with what the D. Sigg note tells me to expect. Once again, I calibrated out the delay of the measurement setup using the AG4395A.

For a beat note in the regime 10-100 MHz, we should have plenty of range in this module to add a delay such that we zero one quadrature of the ALS DFD output (for a linear error signal). 

I then proceeded to connect the single-ended front panel BNC corresponding to the ALS_X_I DFD channel to the IN2 input of the CM board (this would be what we use for high bandwidth ALS feedback). The conventional ALS system uses the differential output from a rear-panel D-sub, so in principle, both systems could run in parallel. I confirmed that I could see a signal when the IN2 path on the CM board was engaged (monitored using ndscope at the CM_Slow output), and that this signal stabilized when the green laser was locked to the X-arm length, which itself was slaved to the PSL frequency using the usual POX locking scheme. I have not yet routed the LO leg of the ALS_X beat through the delay line phase shifter - see next elog for details.

Update about the ALS MEDM screen slider: the trick was to change the OMSL field of the C1:LSC-BO_1_0 channel to "closed_loop" instead of "supervisory". Once this is done, the DOL value of the same channel can be set to the soft channel C1:ALS-DelayCalc, which sets the 16 bit binary string that controls the delay. Because arbitrary delays are not possible, I think it's more natural for the user to interact with this 16-bit binary string rather than the actual delay itself. So the MEDM screen has been slightly modified from what is shown in Attachment #1.

Attachment 1: delaySlider.png  44 kB  | Hide | Hide all
delaySlider.png
Attachment 2: delayLineLosses.pdf  213 kB  | Hide | Hide all
delayLineLosses.pdf
Attachment 3: delayLineCal.pdf  77 kB  | Hide | Hide all
delayLineCal.pdf
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