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New entries since:Wed Dec 31 16:00:00 1969
ID Date Authorup Type Category Subject
  443   Wed Aug 24 03:20:59 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (2)

Bonding

  444   Wed Aug 24 03:26:43 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (3)

Inspection

 

  445   Wed Aug 24 11:29:47 2022 KojiGeneralGeneralOMC #002 ready for shipment

[Stephen Koji]

The OMC #002 is ready for shipment.

Attachment 1: Work done on Sept 19, 2022

Other attachments: Putting the OMC in the pelican case.

  446   Thu Aug 25 14:22:08 2022 KojiGeneralGeneralLLO OMC #001 Ballast Mass investigation

Inspected the past LLO add-on mass configuration.

There are unknown masses at the DCPD side. It looks like a small SS mass with an estimated mass of 5g. But the DCC number is unknown.

We are going to add 10g on each corner as well as the damping aterial. We should be able to figure out the fastener / mass configuration.

  447   Thu Aug 25 20:05:00 2022 KojiGeneralGeneralLLO OMC #001 Ballast Mass investigation

Here is the balance mass info for the LLO OMC#001 analyzed from the photographs

  • Added masses are: 50+10g, 50+20, 10+20+5, and 20+20+10 for the mass right above FM1/CM1/FM2 and CM2, respectively.
  • The length of the 1/4-20 screws seem L=3/4"~1"

If we attach the additional mass, longer 1/4-20 screws (1", 1" 1/8, 1" 1/4) are going to be used.

  448   Fri Aug 26 22:29:02 2022 KojiGeneralGeneralTool Shipping Prep

Shipping preparation for the LLO trip

Started July 15, 2022 and finished Aug 30. So it took ~1.5 months (with a couple weeks of break)


Class B special tools

  • Screw Drivers 1
    • https://www.steritool.com/
    • https://www.steritool.com/precision-screwdrivers-mini.aspx
  • Screw Drivers 2
    • What I have seems S555Z-7
    • https://www.starrett.com/
    • https://www.starrett.com/dms/flipbooks/Cat-33/index.html?page=354
  • Allen Wrenches
    • Bondhus: These are not made of SS, but of so called protanium steel. I have a chrome finish one (BriteGuard) and K14 gold finish one (goldguard).
    • https://intl.bondhus.com/pages/goldguard-ball-end
    • https://intl.bondhus.com/pages/briteguard-ball-end
  • Scissors
    • VWR - Stainless Steel
    • Unknown PN /  probably this?
    • https://us.vwr.com/store/product/4527635/vwr-dissecting-scissors-sharp-blunt-tip
  • Forceps
    • VWR - Stainless Steel
    • https://us.vwr.com/store/product/4531765/vwr-hemostatic-forceps
  • Wire cutters
    • Looks like they are orthodontic wire cutters. One has the marking "Orthomechanic Stainless Steel" but the company does not sell cutters anymore. The other has a marking "333" but the company is unknown. Similar products can be found on Amazon
  • Long nose pliers - straight stainless steel
    • https://www.aventools.com/
    • https://www.aventools.com/long-nose-pliers-stainless-steel-6-2
  • Bent nose pliers - stainless steel
    • unknown 
  • Tweezers
    • Excelta 
    • The short one is 20A-S-SE. The longer one is 24-SA-PI, maybe?
    • https://www.excelta.com/
    • https://www.excelta.com/straight-laboratory-instruments-forceps
    • https://www.excelta.com/style-24-24-6-sa
  • Mighty-Mouse spanner
  • 2x driver bits for the digital torque wrench

First Contact Kit

  • FC bottole / PEEK mesh

Bonding kit (excl EP30-2 bond)

  • reinforcement bars (4 types)
  • bonding liner powder
  • tools: spatula / bond applying rod

Power meters (excl Power meter controller)

  • Thorlabs Thermal
  • Thorlabs Photodiode
  • Thorlabs Integrating Sphere

Electronics

  • preamp + power cable
  • PD testing kit (PD connector / DB9 break out / grabber-BNC)
  • Nitrile gloves

Cable bracket replacement kit

  • PEEK cable bracket (Helicoiled)
  • Cable pegs (x4 salvaged / spare)
  • fastners
  • kapton sheet
  • cable ties

Optics / Optomechanics

  • Optical fiber / spare fiber
  • OMC transport feet
  • OMC backscatter inspection prisms

Misc tools

  • digital torque wrench

=== Action done on Aug 30 ===

Fiber MM setup / Fiber coupler mount
Glass Beamdumps (for optical testing)
Flipper mirror
Thorlabs fiber coupler tool
General bent nose plier for fiber
Thorlabs collimator tiny allen
Spare High QE PDs

Spare OMC bags / Zip bags

Balance Mass 10g Qty 8 (Different Type D11*** 1.25" dia), 20g Qty 10 / Mass damper D1700301 -04 / Mass damper screws SHCS 1/4-20 x 1.25 Qty 25 / 1" screws and 1 1/8" screws

Shipping request: https://services1.ligo-la.caltech.edu/FRS/show_bug.cgi?id=25002


=== Low supply! ===

  • Masks
  • 7.0 gloves supply low
  • 7.5 glove completely gone
  • Wet vectra cloth
  • Dry vectra cloth
  449   Tue Sep 20 08:54:33 2022 KojiGeneralGeneralPD cage arrangement

Upon the LLO work, the current PD arrangement in the cages are:
CAGE B
B1 OMC1 PDT (A1-23)
B2 OMC1 PDR (A1-25)
B3 original (C1-03)
B4 OMC2 PDT (B1-22)

CAGE C
C1 OMC2 PDR (B1-23)
C2 original (C1-08)
C3 original (C1-09)
C4 original (C1-10)

  450   Mon Sep 26 14:27:49 2022 KojiGeneralGeneralLLO OMC ICS work

OMC #001

OMC #002

  452   Mon Nov 7 22:00:33 2022 KojiOpticsConfigurationSetting up the fiber couplers

Fiber matching: 43.2/56.7 = 76%
S/P-pol ratio 0.7/43.2 = 1.6%

 

  453   Fri Nov 11 19:07:48 2022 KojiSupplyGeneralSupply Order

Clean Supply Ordered

  • TexWipe TX8410 AlphaSat Vectra Alpha 10 50 sheets x 12 pk  (VWR TWTX8410)
  • Mask KIMTECH PURE® M3 Pleat-Style Face Masks 50 masks x 10 pk (VWR 15628-213)
  • Stainless Pan x3 (VWR 10193-562)
  • Ansell Accutech Latex Gloves 6.5 25*8pk (Fisher 19162026)
  • Ansell Accutech Latex Gloves 7.0 25*8pk (Fisher 19162027)
  455   Mon Nov 14 09:27:13 2022 KojiOpticsCharacterizationtransmission measurements through OMC #1 (before cleaning)

The measured total optical loss of the OMC was

1st:   0.015 +/- 0.003
2nd: 0.085  +/- 0.005
3rd:  0.0585+/- 0.0008
4th:  0.047  +/- 0.002

In avegrage the estimated loss is
Loss = 0.055 +/- 0.014

This is unchanged from the measurement at LLO after the FC cleaning
Loss = 0.053 +/- 0.010

  457   Tue Nov 15 10:58:53 2022 KojiOpticsGeneralOMC #1 damaged black glass removal

[Camille, Koji]

The damaged black glass was removed from the OMC breadboard leaving the glass base.
The black glass pieces were bonded very tightly on the FS base with EP30-2. The apparent amount of the bond was not so much but it was such hard that removal by hand was not possible.
We decided to give drips of Acetone on the base hoping the gradual dissolving of EP30-2. Using a knife edge, the "filets" of the bonds were removed, but the BD was still tight.

By wedging the black glass-black glass bonding with the nife edge, the left side (the directly damaged one) was taken off from the structure leaving a tiny fragment of the glass on the base.

The remaining one was even stronger. We patiently kept dripping Acetone on the base and finally, the black glass piece was knocked off and removed from the base.

Attachment 1: The base right after the black glass removal.

Attachment 2: The black glass pieces were stored in a container with Al foil + clean cloth bed. The damaged and fogged surfaces faced up.

Attachment 3: The zoom-in shot of the black glass pieces.

Attachment 4: The base was wiped with Acetone and cleaned with FC. We will bond another BD assembly on the base, presumably using the UV epoxy.

  458   Tue Nov 15 11:12:24 2022 KojiOpticsGeneralOMC #1 fogging on the AR side of BS1 cleaned

[Camille, Koji]

Photo of the BS1 AR cleaning process

Attachment 1: Before cleaning. Foggy surface is visible.

Attachment 2: After FC cleaning. The structure of the deposited material is still quite visible.

Attachment 3: Acetone scrubbing. Cotton Q-tip was used so that the stick does not melt with acetone.

Attachment 4: After acetone scrubbing. Nicely clean!

Acetone scrubbing was applied to HR/AR of BS1, FM1, FM2, BS2, and HR of CM1 and CM2. (total 10 surfaces)
Then final FC paint was applied to these 10 surfaces.

We'll come back to the setup on Thu for FC peeling and loss measurement.

  459   Thu Nov 17 18:56:22 2022 KojiOpticsGeneral Transmission measurements of OMC #1 after deep cleaning

[Camille, Koji]

- Removed the first contact we left on Monday.

- Measured transmission (Set1) Very high loss! Total optical loss of 18.5%! Observation with the IR viewer indicated that CM1 has bright scattering. We suspencted a remnant of FC.

- Applied the second FC on the four cavity mirrors. This made the CM1 sport darker.

- Measured the transmission (Set1~Set3). We had consistent loss of 4.2~5.0%. We concluded that this is the limitation of this OMC even with the cleaning.

  460   Thu Nov 17 19:50:00 2022 KojiOpticsCharacterizationConclusion on the cleaning of OMC #001

Conclusion on the cleaning of OMC #001

- After a couple of first contact cleaning trials and deep cleaning, the total loss was measured to be 0.045+/-0.004.
  This indicated a slight improvement from the loss measured at LLO before any cleaning (0.064+/-0.004).
  However, the number did not improve to the level we marked in 2013 (0.028+/-0.004).

- This loss level of 4.5% is comparable to the loss level of OMC #3, which is currently used at LHO.
  Therefore, this OMC #1 is still a useful spare for the site use.

- Some notes / to-do regarding this unit:
  1) The beam dump with melted black glass was removed. A new beam dump needs to be bonded on the base.
  2) The connector bracket still needs to be replaced with the PEEK version.
  3) The PZT of CM1 has been defunct since 2013. Combining LV and HV drivers is necessary upon use at the site. (LLO used to do it).

  462   Mon Nov 21 19:13:35 2022 KojiGeneralGeneralTransmission measurement (2nd deep cleaning of OMC #1)

OMC Transmission measurement after the 2nd deep cleaning

The 2nd deep cleaning didn't improve the transmission. (See Attachment 2)
The measured loss was 0.044+/-0.002

 

  463   Tue Nov 29 15:54:47 2022 KojiGeneralConfigurationWindows laptop for WincamD Beam'R2 recovery

Aaron took the set to Cryo lab

 

  464   Fri Dec 2 11:42:03 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants
[Camille, Koji] Log of the work on Nov 30, 2022
 
The following is the notes from GariLynn

Cleaning for water-soluble contaminants:
It uses deionized water instead of acetone.
Note:
  • The first contact must go on the mirror before the water can dry,  so you will need a bigger brush. We have some that are 1cm, I think they are in the back wall cabinet of B119.
  • For the bigger brush, you will need a beaker and perhaps a bigger bottle of First Contact.  There is one in the mini-fridge in the back corner of B110
  • You use an alpha swab instead of a cotton bud
  • For this effort, I encourage you to get a bottle of DI water from stores.
  • I also encourage you to rehearse the motions beforehand - timing is critical, and your mirrors are in a tight spacing

(Attachment 1)
We obtained Regent grade DI water. It was poured into a smaller cup.
FC liquid was also poured into a small beaker.
Wash the mirror with a swab. We should have used a smaller swab that GariLynn has in her lab.

As soon as the mirror was wiped with the water, the FC was applied with a large brush. Don't let the water away!
Then more layer of the FC was added as usual.


The quick painting of FC made a mess around the mirrors due to excess liquid (Attachment 2). So, we decided to remove the FC remnants (on non-optic surfaces) with cotton swabs and then applied FC as usual.

This made the mess removed, however, we found the OMC loss was increased to >10%(!) (Attachment 3). We decided to continue tomorrow (Thu) with more weapons loaded consulting with GariLynn.

 

  465   Fri Dec 2 12:38:15 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants

Another set of FC cleaning was applied to FM1/FM2/CM1/CM2 and SM2. Some FC strings are visible on SM2. So I decided to clean SM2 as well as the cavity mirrors close to SM2 (i.e. FM2 and CM2)

As a result, the bright scattering spot on CM1 is now very dim. And the loss was reduced to 4.0%. This is 0.4% better than the value before the water cleaning.

It'd be interesting to repeat the water cleaning, at least on FM1. FM1 is the closest cavity mirror to the beam dump damaged by the high-power laser pulse.
Maybe we should also clean the AR side of FM1 and BS1, as they were right next to the damaged beam dump. It is not for the loss but for reducing the scattering.

  466   Fri Dec 2 23:58:33 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants

The second trial of the water scrub

A bright scatter is visible on FM1, so I tried water scrub on FM1. This time, both surfaces of FM1 and both surfaces of BS1 were cleaned.

Smaller Vectra swabs were used for the scrub. Then the water was purged by IPA splashed from a syringe. Right after that FC was applied.
This was a bit messy process as the mixture of water/IPA/FC was splattered on the breadboard.
Nevertheless, all the mess was cleaned by FC in the end.

The transmission measurements are shown in Attachment 1, and the analyzed result is shown together with the past results.

The 2nd water scrub didn't improve the transmission and it is equivalent to the one after the two times of deep cleaning.
I concluded that the water scrub didn't change the transmission much (or at all). We reached the cleaning limit.

  467   Mon Dec 5 20:09:39 2022 KojiOpticsGeneral(re)starting the OMC #4 build

[Camille Koji]

We started buikding the OMC #4.

  • Removed OMC #1 from the optical setup and placed it at a safe side on the optical table/
  • Fixed OMC #4 in the optical setup
  • Cleaned the OMC cavity mirrors
  • Placed the OMC cavity mirrors
    • FM1: A1
    • FM2: A3
    • CM1: PZT #11
    • CM2: PZT #12
  • Aligned the beam to the cavity
  • Locked the cavity on TEM00
  • Finely aligned the beam to the cavity
  468   Fri Dec 9 13:13:13 2022 KojiOpticsCharacterizationFSR/TMS/Spot Positions/Transmission

[Camille Koji]

We quickly measured the basic parameters of the OMC as is.

=== FSR ===
Used the technique to find a dip in the transmission transfer function (TF) with offset locking + phase modulation. The FSR was 264.79003MHz = The cavity length of 1.13219 [m] (requirement 1.132+/-0.005 [m])

=== TMS ===

Used the technique to find the peaks in the trans TF with phase modulation + input misalignment + trans PD clipping.
TMS_V: 58.0727 / TMS_H: 58.3070 => TMS/FSR V:0.219316 H:0.220201

This makes the 9th-order modes nicely avoided (Attachment 1). A slightly longer FSR may makes the numbers close to the nominal.

=== Spot positions ===

The image/video capture board turned out not functional with the new Apple silicon mac. We decided to use a small CCD monitor and took a photo of the display.

All the spots are within the acceptable range. The scattering on CM2 was particularly bright on the CCD image and also in the image with the IR viewr.

The spot on FM1/2 are right at the expected location. The spot on CM1 is 0.5mm low and 0.7mm inside (left). The spot on CM2 is ~0.25mm too high and 0.3mm outside.
(Attachment 2, a small grid is 1 mm/div)

== Transmission ==

We made a quick simplified measurement (Attachment 3).

Assuming the reflectivity of the matched beam to be ~0, the mode matching is M=1-(59.2e-3-(-6.5e-3))/(3.074-(-6.5e-3))=0.979
==> The power of the coupled mode is M x 21.28mW = 20.83 mW
The measued transmission was 19.88 mW

==> The OMC transmission (total) was 0.954 (4.5% loss)

This number is not too bad. But the spot on CM2 has too bright scattering. Next week, we want to check if swapping CM2 may improve the situation or not.

  469   Mon Dec 12 19:04:40 2022 KojiOpticsCharacterizationFSR/TMS/Spot Positions/Transmission 2nd trial

[Camille Koji]

We replaced CM2 with a PZT mirror subassembly serialized by PZT "13" (Attachment 1).
This made the transmission increase to 96.x%. Therefore the quick measurement of FSR and TSM were done. Also more careful measurement of the transmission was done.

Next time


== Alignment ==

  • CM2 was replaced from PZT "12" to PZT "13".
  • The resulting position of the cavity spot were all over 1mm too "+" (convention T1500060 Appendix C).
  • So we decided to rotate CM2 by 1mrad in CW. This was done with (-) micrometer of CM2 "pushed" by 20um (2 rotational div).
  • The resulting spot positions were checked with CCD. (Attachment 2). The spot positions seemed to be within +/-1mm from the center as far as we can see from the images. (good)
  • CM2 spot looks much darker. CM1 spot is almost invisible with a CCD and also an IR viewer. FM1/2 spots were nominal bright level. (Looks OK)

== Quick measurement of the transmission ==

Transmission: 20.30 mW
Reflection Voltage (locked): 65.0 mV
Reflection Voltage (unlocked): 3.094 V
Reflection Voltage (dark): -6.5 mV
Incident Power: 21.64 mW

---> Mode matching 1-0.023 / Pcoupled = 21.14 / OMC Transmission 0.96

96% transmission is not the best but OK level. We decided to proceed with this mirror combination.

== Quick measurement of FSR/TMS ==

FSR: 264.7837MHz
TMS_V = 58.2105MHz
TMS_H = 58.1080MHz

The HOM structure (with PZT Vs = 0) is shown in Attachment 3. 9th order modes look just fine. The excplicit coincidence is 19th order 45MHz lower sideband. (Looks good)

== Transmission measurement ==

The raw measurements are shown in Attachment 4. The processed result is shown in Attachment 5.
We found that data set 2 has exceptionally low transmission. So we decided to run the 4th measurement excluding the set 2.

Over all OMC loss
Set1: 0.029 +/- 0.014
Set3: 0.041 +/- 0.0014
Set4: 0.038 +/- 0.001

--> 0.036 +/- 0.004
(0.964 Transmission)

 

  470   Mon Dec 19 18:51:50 2022 KojiOpticsCharacterizationTMS measurement with the PZT voltages altered

[Camille, Koji] Log of the work on Dec 15, 2023

The vertical and horizontal TMSs for OMC #4 were measured with the PZT voltages scanned from 0V to 200V.

We concluded that this alignment nicely avoids the higher-order mode structure up to ~19th order. We are ready for the cavity mirror bonding.


The RF transfer functions to the trans RF PD from the modulation on the BB EOM were taken with the presence of the vertical misalignment of the incident beam and the vertical clipping of the beam on the RFPD.

The typical measurement results and the fitting results are shown in Attachments 1/2.

The TFs were taken with the voltage 0, 50, 100, 150, and 200V applied to PZT1 while PZT2 were left open. The measurement was repeated with the role of PZT1 and PZT2 swapped.


The ratio between the TMS and FSR was evaluated for each PZT voltage setting. (Attachment 3)

When the PZTs are open, the first coincident resonance is the 19th-order mode of the 45MHz lower sideband. (Attachment 4)

When the PZT2 voltage is scanned with PZT1 kept at ~0V, no low-order sidebands come into the resonance (Attachment 5) until the PZT1 voltage is above 100V.

We found that the high voltage on PZT1 misaligns the cavity in yaw and the spot (presumably) moves to an undesirable area regarding the cavity loss.
This does not happen to PZT2. Therefore the recommendation here is that the PZT2 is used as the high voltage PTZ, while PZT1 is for the low voltage actuation.

 

  471   Thu Jan 19 23:45:44 2023 KojiOpticsGeneralOMC #4: cavity mirror bonding

[Koji, Camille]

We worked on the bonding of the flat mirrors for the OMC cavity with UV epoxy.

- Prepared the UV illumination setup. Cleaned up the table a bit to spare some space for the illuminator.
- Checked the output power of the illuminator. The foot pedal worked fine. The timer was set to be 10s. The UV output from the fiber was nominally 6W. This is after some warming up for ~1min. (Checked the output power continuously with the UV power meter.)

- Checked the cavity alignment / FSR / TMS - it looked good at this moment

- We confirmed that the UV epoxy has an expiration of July 3, 2023. The bond capsule was brought from Downs right before the work started, and thawed at the lab.

FM1 bonding

- The bottom of FM1 and the breadboard were cleaned. Cleaning with lens cleaning paper + IPA remained a few specks of dust on the surface. We decided to use Vectra swabs to wipe the breadboard surface. This worked pretty well.
- Applied a tap of UV epoxy to FM1 and placed it on the template. The optic was constrained by a retainer clip.
- We found that the spot positions were significantly moved. Probably FM1 was not well touching the template before. We tried to recover the previous optical axis by aligning CM1 and CM2.
- Here is the tip: align the beam on CM1 at the desired spot. Move CM1 to bring the spot on CM2 to the desired spot. CM2 is aligned to have TEM00 as much as possible.

- We recovered reasonable spots on the mirrors. Measured the FSR and TMS (vertical and horizontal) to be 264.73MHz, 58.18MHz, and 58.37MHz, respectively. This makes the 9th-order modes well separated from TEM00. Very good.

- Gave UV illumination 10s x 2. Confirmed that the mirror is rigidly bonded.

 

FM2 bonding

- Continued to bond the other flat mirror. The same process was repeated.
- The bottom of FM2 and the breadboard were cleaned.
- Applied a tap of UV epoxy to FM2 and placed it on the template. The optic was constrained by a retainer clip.
- Measured the FSR and TMS (vertical and horizontal) to be 264.7925MHz, 58.15MHz, and 58.3725MHz, respectively. This makes the 9th-order modes well separated from TEM00. Very good.

- Gave UV illumination 10s x 2. Confirmed that the mirror is rigidly bonded.

SM1/BS2/BS3 bonding

- Continued to bond some less important mirrors.
- SM1 was placed on the template with the same step as above. BS2 (for QPD) and a dummy QPD housing were also placed just to check if the optical axis has any inconsistency. The good beam alignment on the QPD housing was confirmed.
- Applied a bond to SM1 and blasted the UV (20s)
- Applied a bond to BS2. Checked the alignment on QPD1 again. It looked good. UV illumination was applied.

- Placed BS3 to the cavity transmission. A dummy DCPD housing was placed at the reflection side of BS3. There was no inconsistency with the beam alignment.
- The UV illumination was applied (20s).


Optic Inventory

Breadboard: #6
BS1: E6
FM1: A1
FM2: A3
CM1: PZT ASSY #8 (M7+PZT11+C11)
CM2: PZT ASSY #11 (M14+PZT13+C13)
SM1: E9
BS2: B8
SM2:
SM3:
BS3: B6

  472   Mon Jan 23 19:51:20 2023 KojiOpticsGeneralOMC #4: cavity mirror bonding

[Camille, Koji]

We continued to bond two CM mirrors and the other two steering mirrors for QPD2.

Before the bonding work, the FSR and TMSs were checked again.

FSR: 264.7925 MHz
TMS_V: 58.15125 MHz
TMS_H: 58.33375 MHz

Checked the transmission: The OMC loss was 4.3 +/- 0.2 %.

This does not make the HOMs coincidently resonant until the 18th-order (+9MHz). Looks good.


CM1/CM2/SM2/SM3 bonding

- Applied the bond to CM1 and the UV illuminated.
- Applied the bond to CM2 and the UV illuminated.
==> The cavity bonding is completed.

Removed the micrometer for CM2 to allow us to bond SM2/SM3
- Checked the spot at QPD2: The spot was a couple of mm too left. This was too much off compared to the QPD adjustment range. ==> Decided to shim the SM3 position with a piece of Al foil.
- Otherwise everything looked good. SM2/SM3 were bonded.


Invar block bonding

Prepared EP30-2
- There are three tubes of EP30-2 that expires on 2/22, 2023.
- A tube was almost empty. Used this tube to fill/purge the applicator. The 2nd tube was then attached to squeeze out 8g of glue mixture. 
- 0.4g of fused silica beads were added to the glue mixture.
- Mixed the bond and a test piece was baked by the oven. (200F=95C, 5min preheat, bakeing 15min).
- The glue test piece was "dry" and crisp. Looked good.
- Applied the glue on the invar blocks. Confirmed that the bonding surfaces were made completely "wet".
- 4-40 screws were inserted to the blocks so that the blocks were pushed toward the template. See Attachments 3 and 4.

 

Optic Inventory

Breadboard: #6
BS1: E6
FM1: A1
FM2: A3
CM1: PZT ASSY #8 (M7+PZT11+C11)
CM2: PZT ASSY #11 (M14+PZT13+C13)
SM1: E9
BS2: B8
SM2: E11
SM3: E14
BS3: B6

  473   Wed Jan 25 23:51:04 2023 KojiGeneralGeneralThe items packed for Downs

Qty1 1/2 mounts
Qty2 prism mounts
Qty6 gluing fixures
Qty1 Rotary stage
Qty1 2" AL mirror
Qty1 Base for the AL mirror

=> Handed to Stephen -> Camille on Jan 27, 2023.

  474   Thu Jan 26 22:57:19 2023 KojiOpticsGeneralOMC #4: One Invar block bonded with tilt

[Camille, Koji]

The bottom side template was separated into two pieces and successfully removed from the breadboard. The template was assembled together again and bagged to store it in a cabinet.

We found that the invar block for DCPD(R) was bonded with some air gap (Attachment2 1/2).

 

The Allen key used as a weight was too small, which caused it to get under one of the screws used as hooks and lift the block.

 

We've investigated the impact of this tilt.

- Bonding strength: The bonding area is ~60% of the nominal. So this is weak, but we can reinforce the bonding with an aluminum bar.
- Misalignment of the DCPD housing: The tilt will laterally move the position of the DCPD. However, the displacement is small and it can be absorbed by the adjustment range of the DCPD housing.
- Removal: From the experience with the removal of the beam dump glass, this requires a long time of acetone soaking.

Conclusion:

- We don't need to remove the invar block.
- Action Item: Reinforcement of the bonding

  475   Thu Jan 26 23:07:14 2023 KojiOpticsGeneralOMC #4: Input beam dump bonding

[Camille, Koji]

During the second UV epoxy session, we did not bond the input beam dump. This is because this beam dump was not the one planned from the beginning and if it was bonded in place, it would have created difficulties when removing the template.

First, we aligned a couple of Allen wrenches to define the location of the beam dump. We've checked that the main transmission is not blocked at all while the stray beam from the OMC reflection is properly dumped.

After the confirmation, the UV epoxy + UV alight were applied.

The resulting position of the beam dump is shown in the attachment.

  476   Thu Jan 26 23:16:35 2023 KojiOpticsConfigurationOMC #4: Top side bonding.

[Camille, Koji]

1. Flipping the OMC

It turned out that the transport fixture for this OMC could not be closed. The locks are too short, and the knobs could not be turned. We temporarily fastened the long 1/4-20 screws to secure the box and flipped it to make the top side face up.

2. Setting up the top-side template

The top side template was attached to the breadboard. We took care that the lock nuts on the positioning screws were not touched. The margins between the template and the glass edges were checked with a caliper. The long sides seemed very much parallel and symmetric, while the short sides were not symmetric. The lock nut on the short side was loosened, and the template was shifted to be symmetric w.r.t. the breadboard.

3. UV epoxy work

The cylindrical glass pieces were wiped, and the bonding surfaces were cleaned so that the visible fringes were <5 fringes. We confirmed the hooking side is properly facing up. The UV epoxy and UV curing were applied without any trouble. (Attachment 1)

4. EP30-2 bonding of the invar mounting blocks

Six invar blocks were bonded. This time the Allen key weights were properly arranged, so they didn't raise the blocks. The bond properly wetted the mating surfaces.

---

The final step of the bonding is to remove the template.
And replace the locks of the transport fixture.

 

  477   Thu Jan 26 23:46:13 2023 KojiOpticsGeneralOMC #1 input beam dump bonding

A beam dump was stacked on the base of the previous beam dump. The angle was determined so that the main transmission goes through while the stray OMC reflection is blocked without clipping at the edge.

The resulting alignment of the beam dump is shown in Attachment 1.

The beam dump tended to slip on the base. To prevent that a couple of weights were placed around the bonding area. (Attachment 2)

 

  478   Sat Jan 28 00:38:56 2023 KojiMechanicsGeneralOMC #1 cable bracket replacement / OMC #1 repair completed

The AL metal bracket was replaced with a PEEK version.

Attachments 1/2: Before the replacement. The photos show how the cables are arranged.

Attachment 3: How the replacement work is going. The 1/4-20 screws were super tight. Once the connectors were removed, an Allen key was inserted to a hole so that the 1/4-20 on the short sides were removed by closing Allen key arms. For the screws on the longer sides, the same technique can be applied by using three Allen keys. This time none of the screws/cable pegs were wasted. The clothes were used to protect the breadboard from any impact of the action.

Attachments 4/5: Final state.

OMC #1 repair has been 100% done

---------

We still have 4 correct cable pegs and many 1/4-20 BHSCs for OMC #4.

  479   Sat Jan 28 00:46:21 2023 KojiMechanicsGeneralOMC #4: Replaced the locks of the transport fixture

Yesterday, we noticed that we could not close the transport fixture for OMC #4. We could not fully rotate the knobs of the locks. Today, I took the hooks from the functioning locks of the spare transport fixture.

It turned out that the default dimension of the lock seemed too tight. The functioning one has the through holes elongated by a file or something. This modification will be necessary for future transport fixtures.

  336   Mon Apr 15 21:11:49 2019 PhilipOpticsCharacterizationOMC(004): PZT testing for spare OMC

[Koji, Philip]

Today we tested the functionality of the four remaining PZTs (11,12,13 and 22) .  Each PZT was placed within a collimated 500um beam.
Roughly half of the beam was blocked by the PZT. The PZT and a PD then acted as shadow sensor. Each PZT was tested with 0 and
150 V. The resulting power change then could be converted into a displacement of the PZT using the beam diameter.

The open light value for each of these tests was 3.25 V.

PZT 11:
0 V supply voltage     --> 1.717 V on PD
150 V supply voltage --> 1.709 V on PD
delta = 0.008 V

PZT 12:
0 V supply voltage     --> 1.716 V on PD
150 V supply voltage --> 1.709 V on PD
delta = 0.007 V

PZT 13:
0 V supply voltage     --> 1.702 V on PD
150 V supply voltage --> 1.694 V on PD
delta = 0.008 V

PZT 22:
0 V supply voltage     --> 1.770 V on PD
150 V supply voltage --> 1.762 V on PD
delta = 0.008 V

0.008 V --> 0.24% change in power on PD --> about  3.8 um displacement assuming no light which is blocked
by the PZT is hitting the PD.

 

We further started to drive all four PZTs over night with 100 V (half of their range) at 100 Hz.
We additionally display the impedance to ensure none of them degrades.

All four PZTs seem to be connected to Teflon coated wires. It needs to be checked if these
fulfill the vacuum compatibility requirements.

  345   Wed Apr 17 10:30:37 2019 PhilipOpticsGeneralOMC optical set-up day 1

[Joe, Koji, Liyuan, Philip, Stephen]
Work done on 16.04.2019

Finishing assembly of transport box
Assembly worked fine except for the clamping structure to clamp the lid of the transport box to the bottom part.
It seemed that some of the plastic of these clamps became brittle during the baking. The plastic was removed and the
clamps where wiped clean. It appears that the clamps can't be locked as they should. Still the transport box should be fine
as the long screws will mainly clamp the two parts together.

Preparing the transport box to mount the breadboard
The lid of the the transport box was placed upside down and clamped to the table. All peak clamping structures where pulled back as far as possible.

Preparation and cleaning of the breadboard
We unpacked the breadboard and found lots of dust particles on it (most likely from the soft paper cover which was used). We used the ionized nitrogen gun
at 25 psi to get rid of the majority of particles and cross-checked with a bright green flash light before and after blowing. The second stage of cleaning was done
below the clean room tent and included the wiping of all surfaces. The breadboard was then placed into the prepared lid of the transport box and clamped with peak
screws.

Unpacking of the template
The previously cleaned template was unpacked while the last layer of coverage was removed below the cleanroom tent.

Template adjustment on the breadboard
All peak screws of the clamping structure of the template where removed. The template was placed onto the breadboard only seperated by peak spacers.
All peak screws have been inserted for horizontal clapming. A calipper was used to measure the distance of each edge of the template to the edge of the
breadboard. For documentation the labeled side of the bradboard (facing away from the persons on the pictures) of the upside down breadboard is defined to 
be the south side, continuing clockwise with west, north and east. First rough alignment was done by shifting the template on the breadboard and then the 
peak screws where used for fine tuning. The caliper values measured where:
North   C 8.32mm     E 8.52 mm     W 8.41 mm
East     C 8.08 mm
South   C 8.32 mm
West    C 8.02 mm
(E indicating east side position, W indicating west side position and C indicating center position)

  347   Fri Apr 19 09:21:07 2019 PhilipOptics Cleaning of OMC optics

ach[Joe, Phillip, Koji, Stephen]

Work from 17.04.2019

First contact cleaning of OMC optics
We cleaned the OMC optic with first contact. After a first cleaning run all mirrors except for two looked
fine. One had some first contact residuals on the left at center height and another had some particle sitting
near the center area. As the ionized nitrogen gun didn't help we applied another round of first contact which resolved
the two issues. Unfortutanely the second run of cleaning again left some residuals of first contact at the edges.
We were able to peal these off with tweezers.

Placement of Optics at the breadboard
We cleaned the contact surfaces for the bonds using optic wipes and pure isopropanol. The placement wen't well for 3 of the 5 optics (low number of newtonian rings).
One was recleaned and placed on the breadboard again which seemed fine. For the 5th no newtonian rings could be seen (either verry ood or bad) we planed on trying it in the current set-up. Mirrors used can be seen in attachment 3.

 

  300   Mon Jul 2 15:27:31 2018 Rich AbbottElectronicsGeneralWork on EOM (3rd IFO unit)

Koji, Rich

We took apart the unit removed from the 3rd IFO (Unit serial number aLIGO #3, XTAL 10252004) to see what makes it tick.  Koji has done a fine job of adding the plots of the impedance data to this log book.  Attached are some details of the physical construction showing the capacitor values used in shunt before the coils.

  301   Tue Jul 3 12:07:47 2018 Rich AbbottElectronicsCharacterizationNotes on 3rd IFO EOM

Attached please see my notes summarizing the models for the electrodes and inductors within the 3rd IFO EOM

  305   Wed Aug 8 17:32:56 2018 Rich AbbottGeneralCharacterizationModulation Index Test Setup at 40m Lab

Attached is a block diagram of the test setup used in the 40m lab to measure the modulation index of the IO modulator

  290   Thu Nov 30 12:18:41 2017 StephenGeneralGeneralPreparation for Modal Testing on 4 December

Norna Robertson, Stephen Appert ||  29 Nov 2017, 2 pm to 4 pm  ||  227 Downs, CIT

We made some preparations for modal testing, but did not have enough time to make measurements. Below is an after-the-fact log, including some observations and photos of the current state of the OMC bench.

  1. Previous testing results at T1700471 (technical note in progress as of 30 Nov 2017).
    1. One goal of the next round: add damping material to equate with damping material of T1600494.
    2. Second goal of the next round: use a more localized sweep to better resolve the body mode around 1080 Hz -1100 Hz
  2. Transport Fixture was opened without issue, revealing the "Top" (suspending and cable routing) surface of the bench. Damping stacks were still in place from previous testing
  3. We removed the bolts from the damper stacks, but found that all masses with metal-viton interfaces had adhered to viton washers, causing the stacks to stick together.
    1. By using an allen key as a lever to wedge apart bottom mass and the bracket where they were joined by a viton washer, we separated the masses from the bracket.
    2. An allen key was used as a lever to push apart the two masses, which were also joined by a viton washer
    3. Once exposed, viton washers were pried from metal surfaces.
  4. After the damper stacks had been detached from the  No viton washer appeared to leave any residue or particulate - the separated parts all appeared as clean as they had been at the onset.
  327   Thu Apr 11 10:54:38 2019 StephenGeneralGeneralOMC(004): preparation for the PZT subassembly bonding
Quote:

Preparation for the PZT subassembly bonding (Section 6.2 and 7.3 of T1500060 (aLIGO OMC optical testing procedure)
- Gluing FIxture (Qty4)
- Silica Sphere Powder
- Electric scale
- Toaster Oven for epoxy mixture qualification

- M prisms
- C prisms
- Noliac PZTs

- Cleaning tools (forceps, tweezers)
- Bonding kits (copper wires, steering sticks)
- Thorlabs BA-2 bases Qty2
- Razor Blades

 

Also brought to the 40m on 10 April, in preparation for PZT subassembly bonding:

- new EP30-2 epoxy (purchased Jan 2019, expiring Jul 2019 - as documented on documents attached to glue, also documented at C1900052.

- EP30-2 tool kit (maintained by Calum, consisting of mixing nozzles, various spatulas, etc)

 

Already at the 40m for use within PZT subassembly bonding:

- "dirty" ABO A with temperature controller (for controlled ramping of curing bake)

- clean work areas on laminar flow benches

- Class B tools, packaging supplies, IPA "red wipes", etc.

 

Upon reviewing EP30-2 procedure T1300322 (current revision v6) and OMC assembly procedure E1300201 (current revision v1) it appears that we have gathered everything required.

  344   Wed Apr 17 09:08:47 2019 StephenGeneralGeneralOMC(004): Unwrapping and preparing breadboard

[Stephen, Philip, Koji, Joe]

Breadboard D1200105 SN06 was selected as described in eLOG 338. This log describes unwrapping and preparation of the breadboard.

Relevant procedure section: E1300201 section 6.1.5

Breadboard was unwrapped. No issues observed during unwrapping.

  • Attachment 1: packaging of SN06.

Visual inspection showed no issues observed in breadboard - no large scratches, no cracks, no chipping, polished area (1 cm margin) looks good.

  • Attachment 2: engraving of SN06.

Initially the breadboard has a large amount of dust and fiber from the paper wrapping. Images were gathered using a green flashlight at grazing incidence (technique typical of optic inspection).

PROCEDURE IMPROVEMENT: Flashlight inspection and Top Gun use should be described (materials, steps) in E1300201.

  • Attachment 3: particulate before Top Gun, large face.
  • Attachment 4: particulate before Top Gun, small face.

Top gun was used (with medium flow rate) to remove large particulate. Breadboard was placed on Ameristat sheet during this operation.

  • Attachment 5: particulate after Top Gun

Next, a clean surface within the cleanroom was protected with Vectra Alpha 10 wipes. The breadboard, with reduced particulate after Top Gun, was then placed inside the cleanroom on top of these wipes. Wiping with IPA Pre-wetted Vectra Alpha 10 wipes proceeded until the particulate levels were acceptable.

Joe and Koji then proceeded with placing the breadboard into the transport fixture.

 

  358   Thu May 9 16:07:18 2019 StephenMechanicsGeneralImprovements to OMC Bonding Fixture

[Stephen, Koji]

As mentioned in eLOG 331, either increased thermal cycling or apparent improvements in cured EP30-2 strength led to fracture of curved mirrors at unintended locations of bonding to the PEEK fixture parts.

The issue and intended resolution is summarized in the attached images (2 different visualizations of the same item).

Redline has been posted to D1600336-v3.

Drawing update will be processed shortly, and parts will be modified to D1600336-v4.

 

  367   Tue May 28 12:14:20 2019 StephenOpticsGeneralCM PZT Assembly Debonding of EP30-2 in Acetone

[LiyuanZ, StephenA]

Downs B119

Summary: Beginning on 20 May 2019, two CM PZT assemblies were soaked in Acetone in an effort to debond the EP30-2 bonds between tombstone-PZT and between PZT-optic. Debonding was straightforward after 8 days of soaking. 24 hours of additional acetone soaking will now be conducted in an attempt to remove remnant EP30-2 from bonding surfaces.

Procedure: The assemblies were allowed to soak in acetone for 8 days, with acetone level below the HR surface of the optic. No agitation of the solution, mechanical abrasion of the bond, or other disturbance was needed for the bond to soften.

GariLynn contributed the glassware and fume hood, and advised on the process (similar to debonding of CM and PZT from OMC SN002 after damaging event). The equipment list was (WIP, more detail / part numbers will be gathered today and tomorrow):

  • crystallizing dish (no spout, like a deep petri dish)
  • curved lid
  • wax sheet (to seal)
  • acetone
  • fume hood

Results: Today, 28 May 2019, I went to the lab to check on the optics after 8 days of soaking. Liyuan had monitored the acetone level during the first 4 days, topping up once on 24 May. All bonds were fully submerged for 8 days.

There were 2 assemblies soaked in one crystallizing dish. Debonded assemblies - ref OMC eLOG 328 for specified orientations and components:

PZT Assy #9 - ref. OMC eLOG 334 - M17+PZT#12+C10

PZT Assy #7 - ref. OMC eLOG 332 - M1+PZT#13+C13

PZT Assy #7 was investigated first.

  • C13 was removed with no force required.
  • PZT#13 was removed with no force required.
  • EP30-2 remained at the bond surfaces and tracing the diameters of each bond on each of the 3 bonding surfaces of the PZT and tombstone - these components were returned to the dish to soak.
  • No EP30-2 remained on the surface of the curved mirror - C13 was removed and stored.

A video of removal of C10 and PZT#12 from PZT Assy #9 was collected (See Attachment 8), showing the ease with which the debonded components could be separated.

  • C10 was removed with no force required.
  • A slight force - applied by gripping the barrel of the PZT and pushing with the index finger on the surface of the tombstone - was required to separate PZT#12 from M17,
    • likely due to excess glue at the barrel of the PZT
  • EP30-2 remained at the bond surfaces and tracing the diameters of each bond on each of the 3 bonding surfaces of the PZT and tombstone - these components were returned to the dish to soak.
  • No EP30-2 remained on the surface of the curved mirror - C13 was removed and stored.

Photos and video have been be added to supplement this report (edit 2019/07/08).

 

  371   Thu Aug 22 12:35:53 2019 StephenOpticsCharacterizationWedging of the debonded PZTs 2019 August

Wedge and thickness measurements of PZTs 12 and 13 took place after debonding and cleaning - results are shown in the first image (handwritten post-it format).

These thickness measurements seem to have come back thinner than previous measurements. It is possible that I have removed some PZT material while mechanically removing glue. It is also possible that there is systematic error between the two sets of measurements. I did not run any calculations of wedge ange or orientation on these data.

Note that cleaning of debonded PZTs involved mechanically separating glue from the planar faces of PZTs. The second image shows the razer blade used to scrape the glue away.

There were thick rings of glue where there had been excess squeezed out of the bond region, and there was also a difficult-to-remove bond layer that was thinner. I observed the presence of the thin layer by its reflectivity. The thick glue came off in patches, while the thin glue came off with a bit of a powdery appearance. It was hard to be certain that all of the thin bond layer came off, but I made many passes on each of the faces of the 2 PZTs that had been in the bonded CM assemblies. I found it was easiest to remove the glue in the bonded

I was anticipating that the expected 75-90 micron bond layer would affect the micrometer thickness measurements if it was still present, but I did not notice any irregularities (and certainly not at the 10 micron level), indicating that the glue was removed successfully (at least to the ~1 micron level).

 

Quote:

Yesterday I measured the thickness of the PZTs in order to get an idea how much the PZTs are wedged.

For each PZT, the thickness at six points along the ring was measured with a micrometer gauge.
The orientation of the PZT was recognized by the wire direction and a black marking to indicate the polarity.

A least square fitting of these six points determines the most likely PZT plane.
Note that the measured numbers are assumed to be the thickness at the inner rim of the ring
as the micrometer can only measure the maximum thickness of a region and the inner rim has the largest effect on the wedge angle.
The inner diameter of the ring is 9mm.



The measurements show all PZTs have thickness variation of 3um maximum.

The estimated wedge angles are distributed from 8 to 26 arcsec. The directions of the wedges seem to be random
(i.e. not associated with the wires)



As wedging of 30 arcsec causes at most ~0.3mm spot shift of the cavity (easy to remember),
the wedging of the PZTs is not critical by itself. Also, this number can be reduced by choosing the PZT orientations
based on the estimated wedge directions --- as long as we can believe the measurements.



Next step is to locate the minima of each curved mirror. Do you have any idea how to measure them?

 

  375   Wed Sep 18 22:30:11 2019 StephenSupplyGeneralEP30-2 Location and Status

Here is a summary of the events of the last week, as they relate to EP30-2.

1) I lost the EP30-2 syringes that had been ordered for the OMC, along with the rest of the kit.

  • Corrective action: Found in the 40m Bake Lab garbing area.
  • Preventative action: log material moves and locations in the OMC elog
  • Preventative action: log EP30-2 moves and locations in PCS via location update [LINK]
  • Preventative action: keep EP30-2 kit on home shelf in Modal Lab unless kit is in use

2) The EP30-2 syringes ordered for the OMC Unit 4 build from January had already expired, without me noticing.

  • Corrective action: Requested LHO ship recently-purchased EP30-2 overnight
  • Preventative action: log expiration dates in OMC elog
  • Preventative action: begin purchasing program supported by logistics, where 1 syringe is maintained on hand and replaced as it expires

3) LHO shipped expired epoxy on Thursday. Package not opened until Monday.

  • Corrective action: Requested LHO ship current EP30-2 overnight, this time with much greater scrutiny (including confirming label indicates not expired)
  • Preventative action: Packages should be opened, inspected, and received in ICS or Techmart on day of receipt whenever possible.

4) Current, unopened syringe of EP30-2 has been received from LHO. Expiration date is 22 Jan 2020. Syringe storage has been improved. Kit has been docked at its home in Downs 303 (Modal Lab) (see attached photo, taken before receipt of new epoxy).

Current Status: Epoxy is ready for PZT + CM subassembly bonding on Monday afternoon 23 September.

  376   Wed Sep 18 23:16:06 2019 StephenSupplyGeneralItems staged at 40m Bake Lab for PZT Subassembly Bonding

The following items are presently staged at the 40m Bake Lab (see photo indicating current location) (noting items broght by Koji as well):

  1. Bonding fixtures, now modified with larger washers to constrain springs, and with modification from OMC elog 358.
  2. Curved Mirrors and Tombstones as selected by Shruti in OMC elog 374.
  3. PZTs as debonded from first iteration subassemblies (SN 12 and SN 13)
  4. Epoxy-cure-testing toaster oven
  5. Other items I can't think of but will populate later  =D

The following item is in its home in Downs 303 (Modal Lab)

  1. EP30-2 epoxy (expiration 2020 Jan 22) with full kit (tracked in PCS via location update [LINK])

 

  377   Wed Sep 18 23:38:52 2019 StephenGeneralGeneralDirty ABO ready for PZT Subassembly Bonding

The 40m Bake Lab's Dirty ABO's OMEGA PID controller was borrowed for another oven in the Bake Lab, so I have had to play with the tuning and parameters to recover a suitable bake profile. This bake is pictured below (please excuse the default excel formatting).

I have increased the ramp time, temperature offset, and thermal mass within the oven; after retuning and applying the parameters indicated, the rate of heating/cooling never exceeds .5°C/min.

Expected parameters:  Ramp 2.5 hours Setpoint 1 (soak temperature) 94 °C no additional thermal mass
Current parameters:    Ramp 4 hours Setpoint 1 (soak temperature) 84 °C Thermal mass added in the form of SSTL spacers (see photo)


The ABO is controlled by a different temperature readout from the data logger used to collect data; the ABO readout is a small bead in contact with the shelf, while the data logger is a lug sandwiched between two stainless steel masses upon the shelf. I take the data logger profile to be more physically similar to the heating experienced by an optic in a gluing fixture, so I feel happy about the results of the above bake.

I plan to add the data source file to this post at my earliest convenience.

  379   Tue Sep 24 12:19:20 2019 StephenGeneralGeneral Dirty ABO test run prior to PZT Subassembly Bonding

The 40m Bake Lab's Dirty ABO's OMEGA PID controller was borrowed for another oven in the Bake Lab (sound familiar? OMC elog 377), so I have had to play with the tuning and parameters to recover. This bake seemed to inadequately match the intended temperature profile for some reason (intended profile is shown by plotting prior qualifying bake for comparison).

The parameters utilized here are exactly matching the prior qualifying bake, except that the autotuning may have settled on different parameters.

Options to proceed, as I see them, are as follows:

  1. reposition the oven's driving thermocouple closer to the load and attempt to qualify the oven again overnight
  2. retune the controller and attempt to qualify the oven again overnight
  3. proceed with current bake profile, except monitor the soak temperature via data logger thermocouple and intervene if temperature is too high by manually changing the setpoint.

 

  380   Thu Sep 26 17:33:52 2019 StephenGeneralGeneralDirty ABO test run prior to PZT Subassembly Bonding - ABO is Ready!

Follow up on OMC elog 379

I was able to obtain the following (dark blue) bake profile, which I believe is adequate for our needs.

The primary change was a remounting of the thermocouple to sandwich it between two stainless steel masses. The thermocouple bead previously was 1) in air and 2) close to the oven skin.

ELOG V3.1.3-