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  OMC elog, Page 5 of 10  Not logged in ELOG logo
ID Date Author Type Category Subjectup
  35   Thu Nov 8 13:24:53 2012 KojiOpticsCharacterizationMore wedge measurement

A1
Horiz Wedge    0.497    +/-    0.004 deg
Vert Wedge      0.024    +/-    0.004 deg

A2
Horiz Wedge    0.549    +/-    0.004 deg
Vert Wedge      0.051    +/-    0.004 deg

A3
Horiz Wedge    0.463    +/-    0.004 deg
Vert Wedge      0.009    +/-    0.004 deg

A4
Horiz Wedge    0.471    +/-    0.004 deg
Vert Wedge      0.019    +/-    0.004 deg

A5
Horiz Wedge    0.458    +/-    0.004 deg
Vert Wedge      0.006    +/-    0.004 deg

  116   Thu Apr 18 11:43:59 2013 KojiGeneralGeneralMounting Glass Bracket Failure

[Jeff, Koji]

- While we were working on the optics alignment, one of the mounting brackets made of glass god tore apart into two when a holding screw was removed.
The glass component had a crack at the very middle of the part.

- We borrowed a setup for photoelastisity measurement from Garilynn. This is a set of polarizer configured to have cross polarization. If there is no photoerastisity
the image is colored in blue (somehow). When the polarization is rotated, the color is changed in red, yellow, or white.

- The cross polarizer was tested with a polycarbonate face shield for the UV protection. It seems doing its job.

- We took a set of photos to see any residual stress in a block. The entire inside of the channel is frosted glass so the technique didn't yield much.
In one orientation we did see stress near the ends but the orientation didn't allow us to see exactly where.

- We had 30 brackets and one OMC requires ten of them. This means that there was no spare and now we don't have enough.
  So we decided to spend more as test pieces.

- We tested three scenarios this afternoon. In all three cases both screws were snugged (estimate 0.5 in*lb) before torquing by a torque wrench with a dial meter.
  The divisions on the dial of the wrench are 1 in*lb. We were not so confident in the exact measurement but we felt good about the repeatability of the values.

  1. Duplicated the original mounting with the chamfers of the PEEK bar facing into the channel. Cracked as the torque wrench read 1 in*lb.
      Crack initiation at the first screw, starting along the longitudinal centerline.

  2. Turned the nut bar over so the flat side faced into the channel. Successfully torqued both screws to 1 in*lb and removed them.

  3. With a razor blade, made fairly large reliefs (countersinks) around the holes in the PEEK. Successfully torqued both screws first to 1 in*lb then 1.5 in*lb.
      The block did crack (again at the screw along the centerline) when the torque was ~1.9 in*lb.

It occurs to us that we need micro-compliance AND structural rigidity to distribute the load. The PEEK bars are small and particularly thin where the #4-40 helicoil holes are.
The load is probably concentrated way too much at the holes because it is too weak. Perhaps a good solution, among others, would be to use an aluminum nut plate
with a thin (.02") kapton or viton layer to give the micro-compliance. Additionally, a kapton layer could be used between the block and the aluminum shim,
though this one is probably to be avoided so as to ensure rigidity of the bolted assembly to the bench. Lastly, the nut bar should be shaped such that the area
around the holes and the end of the channel (pretty much the same area) are less stressed than the center portion. 


After the discussion with Peter and Dennis, we decided to reinforce the bonded glass piece with invar shims.
Each shim will be threaded such that we don't need to stress the glass piece any more. EP30-2 will be used as the glue.

  124   Mon May 13 14:49:35 2013 KojiMechanicsCharacterizationMounting Glass Bracket still broke with tightenin stress

[Koji / Jeff]

This is the elog about the work on May 9th.

We made two glass brackets glue on the junk 2" mirrors with the UV glue a while ago when we used the UV bonding last time.

On May 7th:

We applied EP30-2 to the glass brackets and glued invar shims on them. These test pieces were left untouched for the night
and brought to Bob for heat curing at 94degC for two hours.

On May 9th:

We received the test pieces from Bob.

First, a DCPD mount was attached on one of the test pieces. The fasteners were screwed at the torque of 4 inch lb.
It looked very sturdy and Jeff applied lateral force to break it. It got broken at once side of the bracket.

We also attached the DCPD mount to the other piece. This time we heard cracking sound at 2 inch lb.
We found that the bracket got cracked at around the holes. As the glass is not directly stressed by the screws
we don't understand the mechanism of the failure.

After talking to PeterF and Dennis, we decided to continue to follow the original plan: glue the invar shims to the brackets.

We need to limit the fastening torque to 2 inch lb.

  412   Thu Jun 23 21:03:33 2022 KojiFacilityGeneralMoving the small optical table to CAML (TCS Lab)

I've cleared the small optical table and wondered how to move it out of the room. Fortunately, the north side of the big table had wide enough clearance and let the 36" wide table go through. This was easy without moving other heavy stuff.

From here to the door, a bit of work is required. A possibility is to roll the laser blocking wall to the south side of the big table. This will require moving the shelving in the entrance area but it's not a lot of work compared to disassembling a part of the wall.

If this does not work somehow, we will consider removing the last panel of the wall and it will definitely allow the table to get out from the door.

  353   Tue Apr 23 10:21:12 2019 JoeOpticsConfigurationMoving the spots to the centre of the curved mirrors

[Koji,Philip, Liyuan, Joe]

CM1:

We moved the curved mirrors to these positions:

inner = 0.807mm

outer = 0.983 mm

CM2:

inner = 0.92 mm

outer = 0.85 mm

To do this so that realignment was easier, we moved the screws in steps of 5um. We alternated which mirror we adjusted so that we could monitor with a wincam how well aligned the beam into the cavity was. We only moved the cavity mirrors a small amount so we could still see higher order mode flashes transmitted through the cavity (e.g.TM03 modes). We would then improve the input alignment, and then move the cavity mirrors some more. Once the mirrors were adjusted according to http://nodus.ligo.caltech.edu:8080/OMC_Lab/190422_195450/misalignment4.pdf the spot positions looked near the middle of the curved mirrors (using a beam card). We began beam walking but we ran  out of range of the bottom periscope screws in the yaw dof. We tried using the third screw to move the mirrror in both yaw and pitch, hopefully this will let move the mirror such that we can use the just the yaw screw. This screw also ran out of range, so we decided that the cavity needed a small adjustment.

The curved mirrors were moved slightly (>5um) and then we tried to get alignment. By using the fibre coupler translation stage, we move the beam side ways slightly, and then tried to get the periscope mirrors back to a position where the screws could move the mirrors. Once we had an ok alignment, we checked the beam. It looked like it was pretty close to the centre of the curved mirrors, which is where we wanted it to be.

We then tried locking the cavity, although the error signal was quite small. The adjusted the input offset and gain of the servo (there is apparently some problem to do with the input and output offsets). Once the cavity was locked we could make the final adjustments to aligning. We still ran out of range on the periscope. We decided to move the breadboard with the fibre coupler and mode matching lenses on it. Because we knew that the cavity was aligned such that the beam hits the centres of the curved mirrors, we could regain flashes quite quickly. We saw the error signal go down, but eventually this decrease was just to do with the beam clipping on the periscope mirrors. We moved the spot back to where we ok aligned, and slid the periscope so we were not clipping the mirror. This worked very well, and then optimised the alignment.

We then tried to improve the mode matching. 

We took photos of the spot positions (quite near the center) and made the detuned locking measurement. The fitting of the data (attachment 1) wsa 1.1318m (what error should we put here?).

I think the order we did things in was:

  • turning anti clockwise on the fibre coupler and misalign the diode, we measured the modespacing.
  • returned the alignment for the photodiode, and realign fibre couple.
  • miss align the photodiode horizontally, and then used fibre coupler to maximise the peak higher order mode peak height. We then used the PD again to make the peak height bigger.
  •  
  75   Sat Mar 23 02:32:23 2013 KojiFacilityGeneralN2 cylinder delivered

Preparation for ionized N2 blow

- 99.9998% N2 cylinder delivered (ALPHAGAZ 2 grade by AIR LIQUIDE) ALPHAGAZ 2 [PDF]

- Filter and Arcing module already in the lab

- A brass regulator to be installed (Done - March 24)

- 50 ft air line already in the lab / needs to be wiped/rinsed (Done - March 24)

- Air line and filter installed (Done - March 24)

  304   Tue Aug 7 15:43:12 2018 KojiElectronicsCharacterizationNew LLO EOM stuffed

[Rich, Dean, Koji]

Stuffed all inductors for the new LLO EOM. As the impedances were sensitive to the positions of the inductors in the housing, they were glued with a glue gun.
Also the lid of the housing significantly change the stray capacitance and lowers the resonant frequency (meaning lowers the Q too), we decided to tune the matching circuit without the lid.

The attached plots show the measured impedances. They all look well tuned and matched. We will prepare and perform the optical measurement at the 40m.

  71   Thu Mar 14 22:18:23 2013 KojiGeneralGeneralNew loans for the diode test

ALL returned

Loan from ATF:

2 blue banana cables returned on Jun 4, 2013

BNC cable returned on Mar 21, 2013

TENMA triple power supply returned on July 17, 2015

From 40m:

4x GPIB cables returned on Mar 21, 2013

From EE shop:

red banana cables returned on Jun 4, 2013

  301   Tue Jul 3 12:07:47 2018 Rich AbbottElectronicsCharacterizationNotes on 3rd IFO EOM

Attached please see my notes summarizing the models for the electrodes and inductors within the 3rd IFO EOM

  223   Wed Feb 18 21:51:23 2015 KojiGeneralGeneralNotes on OMC Transportation Fixtures & Pelican

LLO has one empty OMC transportation fixture.

LHO has one empty OMC transportation fixture.

LHO has one OMC transportation fixture with 3IFO OMC in it.

LHO has the Pelican trunk for the OMC transportation. Last time it was in the lab next to the optics lab.

  431   Wed Jul 27 23:52:18 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (1)

Parts check

- D1300052-V3 SN001 is going to be used (Attachment 1)

- This is the PEEK version of the cable bracket (Attachment 2). The side thread holes have no Helicoils inserted. This needs to be done!
 

Connector arrangement check / cable routing check

Attachment 3: Connector Arrangement from the Northside

Attachment 4: Connector Arrangement from the South side

Attachment 5: Cable routing (Northside down)

At this point, the delamination of the V shape beam dumps was visible. This is the subject of bonding reinforcement.

  434   Wed Aug 10 18:42:27 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (4)

[Stephen Koji]

Now we got the C&Bed parts to continue to work on the cable bracket replacement.

1) Helicoil insertion

1/4-20 Helicoils were inserted into the 6 thread holes of D1300052. It went mostly okay. We witnessed that the Helicoil insertion tool delaminated the plating of the Helicoils upon insertion (Attachment 1). Stephen mentioned that this is not usual, but we didn't find anything further such as increased friction, more debris, etc. So we decided to go forward.

2) EP30-2 Kit

The EP30-2 kit was transferred from the 40m clean room to the OMC lab. The EP30-2 kit tracking was updated via C1900343

3) D1300052 reinstallation -> FAIL

Now resumed to the installation of D1300052 bracket. However, the hole size of the bracket is just a bit too small compared with the size of the mighty mouse connectors. It was already quite tight with the metal version. However, this PEEK version seems to have 0.1 mm further small diameter, and then the connectors do not penetrate the holes. The plan could be
1) Use a razor blade to shave the hole inner circle.
2) Use a cleaned drill bit to make the hole size 0.2mm bigger.

  435   Thu Aug 11 15:24:57 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (5)

- The hole size extension is going forwared now.

- Madeline and Chub are cleaning (sonicating) a drill (29/64=0.4531")
- The parts in a bag were brought to the 40m C&B lab.

- The hole is going to be 11mil=0.28mm larger than the recommendation (0.442").
  It's not a D-hole. The connector has a rounded-rectangular flange that fits into the PEEK parts.
  So I don't think it's an issue.

- Chub has a proper spanner to fasten the nuts. We want to use it here and LLO.

 

  436   Mon Aug 15 21:31:56 2022 KojiGeneralGeneralOMC #002 Cable bracket replacement (6)

The cable bracket was successfully replaced.

  • Looking from the QPD side (North side in Attachment 1), the connectors for the DCPDs and PZT are sticking out, and the ones for QPDs are sticking to the other side. So only two rectangular holes (for QPDs) are facing north.
    • Top left is DCPDT
    • Top right is DCPDR
    • Bottom center is PZT
    • Bottom left is QPD (far/long)
    • Bottom right is QPD (near/short)
       
  • First, the cable pegs for the short sides are fastened with the original screws (Vented BHCS 1/4-20).
  • Then, the cables are started to be inserted from the bottom so that the nuts can be rotated with the spanner. The spanner helped a bit but the nut only has two positions to hook the spanner and the clearance is not sufficient to insert the spanner when one of the hook positions is facing the bottom. The enlarged hole (29/64") perfectly worked . The flange of the connector can be held with a rectangular hole, so a bit bigger hole than the connector size was not an issue. Finally, all the cables were attached to the bracket.
  • The bracket has not yet been fixed on the OMC breadboard yet. This was done with the four screws from the top. Along with the assembly document E1300201, the fastening torque was limited to 2 in-lb using a digital torque wrench.
  • Attachment 2 shows the view from the "North" side. Attachment 3 shows the view from the "South" side. The cables were not yet tied on the cable pegs on the long side of the bracket.
  438   Mon Aug 15 22:43:35 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (1)

[Stephen Koji]

Checked the delamination status:

  • The Invar bar on the cable bracket (DCPD side): Almost all delaminated (Attachment 1 left)
  • The invar bar on the cable bracket (QPD side): Rims still intact, center delaminated (Attachment 1 right)
  • The invar bar reinforced in 2016: One of the reinforcement bar half delaminated (Attachment 2)
  439   Mon Aug 15 22:49:03 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (2)

EP30-2 preparation

  • Two Al foil cups + A sheet of Al foil (for test cure)
  • Set a tube on the glue gun
  • Attach an applicator tube
  • Push a couple of times, and dispense the glue for a single stroke on a waste Al cup
  • Pour the 6g of glue to the other cup.
  • Add 0.3g of silica beads powder to the cup
  • Steer. Pick a few drops to the test cure Al foil
  • Bake the test piece for 15min in 200F (95degC) ==> Very good

#1 The Invar bar on the cable bracket (DCPD side)

Added short (frosted) Al bars (Attachment 1) to the short sides of the invar bar. (Attachments 2/3). Some glue was sucked into the delamination gap by capillary action (=good) (Attachment 4)

#2 The Invar bar on the cable bracket (QPD side)

Added short (frosted) Al bars to the short sides of the invar bar. (Attachments 3/5). Maybe some glue was sucked into the delamination gap??? Not so clear. (Attachment 4)

#3 The Invar bar reinforced in 2016

Added a short (frosted) Al bars to a short side of the invar bar (Attachment 6). On both sides of the 2016 reinforcement, rectangular prisms are added (Attachment 6)
Some capillary action is visible beneath the invar bar (Attachment 7)


Leave it as it is for a day

 

  440   Wed Aug 24 02:51:23 2022 KojiGeneralGeneralOMC #002 Delamination repair Part1 (3)

Inspection of the bonding on the suspension interface side. All look good.

  441   Wed Aug 24 02:53:46 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (1)

Inspection of the delaminations in the optics side

  443   Wed Aug 24 03:20:59 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (2)

Bonding

  444   Wed Aug 24 03:26:43 2022 KojiGeneralGeneralOMC #002 Delamination repair Part2 (3)

Inspection

 

  415   Mon Jul 18 14:20:09 2022 KojiGeneralGeneralOMC #002 Plan Portal

== Initial Preparation ==

  • [Done] OMC #002 placement
  • [Done] OMC #002 locking
  • Details OMC ELOG 414

== Measurements ==

  • [Done] Transmission / Power budget before FirstContact OMC ELOG 416
  • [Done] Transmission / Power budget after FirstContact OMC ELOG 417
  • [Done] Backscatter measurement with a new deflection optics
    • [Done] Optics bonding done waiting for cure OMC ELOG 420 -> Returned the bond to Madeline OMC ELOG 424
    • [Done] Backscatter measurement
      • Measurement: 0.6 ppm OMC ELOG 422
      • (Transmission is 10~60mW. If the backscatter is the order of 1ppm or less, we expect the light level is ~10nW. Can we really detect it? How? ... OK... last time the measurement has been done with the stick PD type powermeter with baffles and the room light turned off (OMC ELOG 209). So it's not totally crazy.)
  • [Done] High QE PD preparation / install / QE check
    • [Done] High QE PD inventory check
      • A1-23    LLO OMC#001
      • A1-25    LLO OMC#001
      • B1-01    LHO OMC#003
      • B1-16    LHO OMC#003
      • B1-22    @CIT Cage B1 Cleaned/Installed
      • B1-23    @CIT Cage B2 Cleaned/Installed
      • C1-03    @CIT Cage B3 Cleaned
      • C1-05    Dead / CIT contamination test cav
      • C1-07    Dead / CIT contamination test cav
      • C1-08    @CIT Cage C2
      • C1-09    @CIT Cage C3
      • C1-10    @CIT Cage C4
      • C1-11    @CIT Cage D1
      • C1-12    @CIT Cage D2
      • C1-14    @CIT Cage D3
      • C1-15    Dead / CIT Cage D4
      • C1-17    LHO Spare
      • C1-21    LHO Spare
      • D1-08    not @CIT, maybe LLO Spare?
      • D1-10    not @CIT, maybe LLO Spare?
    • [Done] Install & QE check
  • [Done] Fiber input beam characterization OMC ELOG 421

== Repair / Preparation ==


== Shipping ==

  • [Done] Tools to ship to LLO OMC ELOG 448
    • CLASS B special tool kit (Allens / Pliers / Mighty-Mouse spanner / Spatula / etc)
    • FC kit
    • Electronic kit (PD connector / trans-impedance amp)
    • Spare High QE PDs
    • Power meters
    • Glass Beamdumps (for optical testing)
    • Cable bracket replacement kit (PEEK cable bracket / cable pegs / fastners / spare fasteners / kapton sheet / cable ties)
    • Emergency EP30-2 kit (excluding the bond)
       
  • [Done] OMC Pelican Filling (Stephen) / OMC Outerbox/insulation (Stephen/Downs) / OMC Shipment Aug 29, 2022 OMC ELOG 445

 

  417   Thu Jul 21 02:55:06 2022 KojiGeneralGeneralOMC #002 Power Budget after mirror cleaning

o Power Budget after FirstContact cleaning (2022/07/20)
NPRO ADJ -50 (min)
Fiber incident --.-mW
Fiber output --.-mW
Matching to the fiber ??%



DCPD T =  8.62  +/- 0.01  mW
REFPD  =  3.549  +/- 0.001 V

DCPD R =  9.46  +/- 0.01  V
REFPD  =  3.562 +/- 0.001 V

CM1    =  74.5  +/- 0.1   uW
REFPD  =  3.585 +/- 0.001 V

CM2    =  81.7  +/- 0.1   uW
REFPD  =  3.585 +/- 0.001 V

REFLPD
vOFS    = -6.197 +/- 0.001 mV (beam blocked)
vOFS_REF= +4.58mV

LOCKED =  47.6  +/- 0.2   mV
REFPD  =  3.596 +/- 0.003 V

UNLOCK =  2.700 +/- 0.003 V
REFPD  =  3.590 +/- 0.001 V

P_Inc  =  19.36 +/- 0.001  mW
REFPD  =  3.594 +/- 0.001 V


Analysis Result

- Cavity coupling 0.980 (2.0% junk&sidebands)

- Cavity R&T: R=229ppm, T=0.970 (previous T=0.946, 2.4% UP!)
- OMC Throughput (Cavity T x First BS R): T=0.963
- Cavity loss per mirror 42.8 ppm / Round Trip Loss 238ppm

  416   Tue Jul 19 03:17:56 2022 KojiGeneralGeneralOMC #002 Power Budget before mirror cleaning

o Power Budget (2022/07/18)
NPRO ADJ -50 (min)
Fiber incident 62.8mW
Fiber output 45.1mW
Matching to the fiber 72%


DCPD T =  8.90  +/- 0.01  mW
REFPD  =  3.760  +/- 0.001 V

DCPD R =  8.82  +/- 0.01  V
REFPD  =  3.760 +/- 0.001 V

CM1    =  81.4  +/- 0.1   uW
REFPD  =  3.767 +/- 0.001 V

CM2    =  86.6  +/- 0.1   uW
REFPD  =  3.767 +/- 0.001 V

REFLPD
OFS    = -6.214 +/- 0.001 mV (beam blocked)
OFS_REF= +4.587mV

LOCKED =  57.5  +/- 0.5   mV
REFPD  =  3.970 +/- 0.003 V

UNLOCK =  2.816 +/- 0.003 V
REFPD  =  3.943 +/- 0.001 V

P_Inc  =  20.04 +/- 0.01  mW
REFPD  =  3.946 +/- 0.001 V
 


Analysis Result

- Cavity coupling 0.989 (1.1% junk&sidebands)

- Cavity R&T: R=756ppm, T=0.946
- OMC Throughput (Cavity T x First BS R): T=0.939
- Cavity loss per mirror 90 ppm / Round Trip Loss 432ppm

 

  430   Wed Jul 27 10:34:30 2022 KojiGeneralGeneralOMC #002 Protective FirstContact Paint

The optical surfaces were coated with FirstContact to keep them clean / somewhat protected during the transportation.
The PD aperture was sealed with FirstContact "caps" (made by Kate in 2016?).

  281   Fri Jun 23 01:58:11 2017 KojiOpticsGeneralOMC #002 Repair - CM1 gluing

[Alena, Koji]

Jun 21: Alena and Koji worked on gluing of the CM1 mirror on the OMC breadboard #002. This is an irregular procedure. Usually, the PZT mirror subassembly is prepared before the mounting prism is glued on the breadboard. In this occasion, however, a PZT and a mirror are bonded on an existing prism because only the damaged mirror and still functional PZT were debonded from the mouting prism.

For this purpose, the mirror and the PZT were fixed on the mounting prism with the modified fixture set (D1600338). The original PZT was reused, and the new mirror #8 was used. The alignment of the mirror was checked OK using the cavity beam before any glue was applied. The arrow of the CM mirror is facing up.

We mixed 8g EP30-2 (it was almost like 3~4 pushes) and 0.4g glass sphere bond lining. Along with EP30-2 procedure, the bond was mixed in an Al pot and tested with 200degF (~93degC) preheated the oven for 15min. The cured bond showed perfect dryness and crispness. The bond was painted on the PZT and the PZT was placed on the fixture. Then more bond was painted on the other side of the PZT. The mirror was placed in the fixture. The spring-loaded front plate was fixed, and the breadboard was left for a day. (Attachment 1~3)

Jun 22: The fixture was removed without causing any visible delamination or void. The attachment 4~6 show how wet the joint is (before baking). There were some excess of EP30-2, which bonded the fixture and the mounting prism as usual. The fixture was detached by prying the front piece against the rear piece with a thin allen key. Some of the excess bond on the mounting prism was removed by scratching.

The alignment of the cavity was checked with the cavity beam and it is still fine.

More photos can be found here: Link to Google Photos Album "OMC #002 Repair - CM1 gluing"

  422   Fri Jul 22 00:31:17 2022 KojiGeneralGeneralOMC #002 backscatter measurement

Measure the power ratio between the forward-propagating and reverse-propagating beams.

  1. Place a small deflecting mirror at the transmission.
  2. Place a flat mirror at the deflected transmission. When the alignment of this mirror is adjusted to retroreflect this beam, the DC of the cavity reflection PD increases, and also the CCD shows spurious fringes.
  3. This condition allows us to locate the power meter at the reverse-propagating spot of the transmission (Attachment 1)
  4. Place a black glass beam dump for the main (bright) transmission (Attachment 2)
  5. Now the power meter is receiving the counter-propagating beam. Turn off the room light and place an anodized Al baffle as shown in Attachment 2. Move the baffle to block only the counter-propagating. Move the baffle out. => Record the power meter reading with/without the baffle in the counter-propagating path. The difference is the power of the reverse-propagating beam.
  6. Now measure the power of the reflected main transmission. This tells us the power ratio between the foward- and back-propagating beams.
  7. Remove the small deflecting mirror and measure the power of the main transmission.
  8. Now the back-propagating power can be estimated from 6 and 7. The same amount is going back to the IFO path.
  9. The reflectivity can be calculated from the 7 and the transmission

- To increase the incident laser power, NPRO Current ADJ was set to be 0 (increased from -50)

- 1st:  Without the baffle 0.373 +/- 0.001 uW / With the baffle 0.318 +/- 0.001 uW
- 2nd: Without the baffle 0.370 +/- 0.001 uW / With the baffle 0.318 +/- 0.001 uW
- 3rd: Without the baffle 0.370 +/- 0.001 uW / With the baffle 0.317 +/- 0.001 uW

==> 53.3 +/- 0.6 nW

- The main transmission was 84.0mW
==> Backpropagation ratio was 0.634+/-0.007 ppm

- Direct measurement of the OMC was  after BS 96.6mW
==> Backpropagation power from the cavity: 61.3 +/- 0.7 nW

- Cavity transmission for the matched beam is Tcav RinputBS = 0.963
==> Incident resonant TEM00 power 100.3mW

- Reflection 61.3+/-0.7 nW x RinputBS = 60.8+/-0.7 nW
-> The effective reflectivity for the mode-matched resonant TEM00 beam incident on the OMC (1st steering mirror) is 0.606+/-0.007 ppm

  426   Tue Jul 26 00:01:59 2022 KojiGeneralGeneralOMC #002 delamination check 2

More epoxy delamination check:

DCPD R (Attachment 1): Found half delaminated

DCPD T (Attachment 2): Found half delaminated

QPD1/QPD2 (Attachment 3): Looks fine

------

In total we need to fix bonding of three invar bases (including the one for the cable bracket)

  437   Mon Aug 15 22:06:18 2022 KojiGeneralGeneralOMC #002 new cable tie installed

[Stephen Koji]

New cable ties were installed on the cable pegs attached to the long sides of the cable bracket.

 

  445   Wed Aug 24 11:29:47 2022 KojiGeneralGeneralOMC #002 ready for shipment

[Stephen Koji]

The OMC #002 is ready for shipment.

Attachment 1: Work done on Sept 19, 2022

Other attachments: Putting the OMC in the pelican case.

  478   Sat Jan 28 00:38:56 2023 KojiMechanicsGeneralOMC #1 cable bracket replacement / OMC #1 repair completed

The AL metal bracket was replaced with a PEEK version.

Attachments 1/2: Before the replacement. The photos show how the cables are arranged.

Attachment 3: How the replacement work is going. The 1/4-20 screws were super tight. Once the connectors were removed, an Allen key was inserted to a hole so that the 1/4-20 on the short sides were removed by closing Allen key arms. For the screws on the longer sides, the same technique can be applied by using three Allen keys. This time none of the screws/cable pegs were wasted. The clothes were used to protect the breadboard from any impact of the action.

Attachments 4/5: Final state.

OMC #1 repair has been 100% done

---------

We still have 4 correct cable pegs and many 1/4-20 BHSCs for OMC #4.

  464   Fri Dec 2 11:42:03 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants
[Camille, Koji] Log of the work on Nov 30, 2022
 
The following is the notes from GariLynn

Cleaning for water-soluble contaminants:
It uses deionized water instead of acetone.
Note:
  • The first contact must go on the mirror before the water can dry,  so you will need a bigger brush. We have some that are 1cm, I think they are in the back wall cabinet of B119.
  • For the bigger brush, you will need a beaker and perhaps a bigger bottle of First Contact.  There is one in the mini-fridge in the back corner of B110
  • You use an alpha swab instead of a cotton bud
  • For this effort, I encourage you to get a bottle of DI water from stores.
  • I also encourage you to rehearse the motions beforehand - timing is critical, and your mirrors are in a tight spacing

(Attachment 1)
We obtained Regent grade DI water. It was poured into a smaller cup.
FC liquid was also poured into a small beaker.
Wash the mirror with a swab. We should have used a smaller swab that GariLynn has in her lab.

As soon as the mirror was wiped with the water, the FC was applied with a large brush. Don't let the water away!
Then more layer of the FC was added as usual.


The quick painting of FC made a mess around the mirrors due to excess liquid (Attachment 2). So, we decided to remove the FC remnants (on non-optic surfaces) with cotton swabs and then applied FC as usual.

This made the mess removed, however, we found the OMC loss was increased to >10%(!) (Attachment 3). We decided to continue tomorrow (Thu) with more weapons loaded consulting with GariLynn.

 

  465   Fri Dec 2 12:38:15 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants

Another set of FC cleaning was applied to FM1/FM2/CM1/CM2 and SM2. Some FC strings are visible on SM2. So I decided to clean SM2 as well as the cavity mirrors close to SM2 (i.e. FM2 and CM2)

As a result, the bright scattering spot on CM1 is now very dim. And the loss was reduced to 4.0%. This is 0.4% better than the value before the water cleaning.

It'd be interesting to repeat the water cleaning, at least on FM1. FM1 is the closest cavity mirror to the beam dump damaged by the high-power laser pulse.
Maybe we should also clean the AR side of FM1 and BS1, as they were right next to the damaged beam dump. It is not for the loss but for reducing the scattering.

  466   Fri Dec 2 23:58:33 2022 KojiOpticsCharacterizationOMC #1 cleaning for water soluble contaminants

The second trial of the water scrub

A bright scatter is visible on FM1, so I tried water scrub on FM1. This time, both surfaces of FM1 and both surfaces of BS1 were cleaned.

Smaller Vectra swabs were used for the scrub. Then the water was purged by IPA splashed from a syringe. Right after that FC was applied.
This was a bit messy process as the mixture of water/IPA/FC was splattered on the breadboard.
Nevertheless, all the mess was cleaned by FC in the end.

The transmission measurements are shown in Attachment 1, and the analyzed result is shown together with the past results.

The 2nd water scrub didn't improve the transmission and it is equivalent to the one after the two times of deep cleaning.
I concluded that the water scrub didn't change the transmission much (or at all). We reached the cleaning limit.

  457   Tue Nov 15 10:58:53 2022 KojiOpticsGeneralOMC #1 damaged black glass removal

[Camille, Koji]

The damaged black glass was removed from the OMC breadboard leaving the glass base.
The black glass pieces were bonded very tightly on the FS base with EP30-2. The apparent amount of the bond was not so much but it was such hard that removal by hand was not possible.
We decided to give drips of Acetone on the base hoping the gradual dissolving of EP30-2. Using a knife edge, the "filets" of the bonds were removed, but the BD was still tight.

By wedging the black glass-black glass bonding with the nife edge, the left side (the directly damaged one) was taken off from the structure leaving a tiny fragment of the glass on the base.

The remaining one was even stronger. We patiently kept dripping Acetone on the base and finally, the black glass piece was knocked off and removed from the base.

Attachment 1: The base right after the black glass removal.

Attachment 2: The black glass pieces were stored in a container with Al foil + clean cloth bed. The damaged and fogged surfaces faced up.

Attachment 3: The zoom-in shot of the black glass pieces.

Attachment 4: The base was wiped with Acetone and cleaned with FC. We will bond another BD assembly on the base, presumably using the UV epoxy.

  458   Tue Nov 15 11:12:24 2022 KojiOpticsGeneralOMC #1 fogging on the AR side of BS1 cleaned

[Camille, Koji]

Photo of the BS1 AR cleaning process

Attachment 1: Before cleaning. Foggy surface is visible.

Attachment 2: After FC cleaning. The structure of the deposited material is still quite visible.

Attachment 3: Acetone scrubbing. Cotton Q-tip was used so that the stick does not melt with acetone.

Attachment 4: After acetone scrubbing. Nicely clean!

Acetone scrubbing was applied to HR/AR of BS1, FM1, FM2, BS2, and HR of CM1 and CM2. (total 10 surfaces)
Then final FC paint was applied to these 10 surfaces.

We'll come back to the setup on Thu for FC peeling and loss measurement.

  477   Thu Jan 26 23:46:13 2023 KojiOpticsGeneralOMC #1 input beam dump bonding

A beam dump was stacked on the base of the previous beam dump. The angle was determined so that the main transmission goes through while the stray OMC reflection is blocked without clipping at the edge.

The resulting alignment of the beam dump is shown in Attachment 1.

The beam dump tended to slip on the base. To prevent that a couple of weights were placed around the bonding area. (Attachment 2)

 

  475   Thu Jan 26 23:07:14 2023 KojiOpticsGeneralOMC #4: Input beam dump bonding

[Camille, Koji]

During the second UV epoxy session, we did not bond the input beam dump. This is because this beam dump was not the one planned from the beginning and if it was bonded in place, it would have created difficulties when removing the template.

First, we aligned a couple of Allen wrenches to define the location of the beam dump. We've checked that the main transmission is not blocked at all while the stray beam from the OMC reflection is properly dumped.

After the confirmation, the UV epoxy + UV alight were applied.

The resulting position of the beam dump is shown in the attachment.

  474   Thu Jan 26 22:57:19 2023 KojiOpticsGeneralOMC #4: One Invar block bonded with tilt

[Camille, Koji]

The bottom side template was separated into two pieces and successfully removed from the breadboard. The template was assembled together again and bagged to store it in a cabinet.

We found that the invar block for DCPD(R) was bonded with some air gap (Attachment2 1/2).

 

The Allen key used as a weight was too small, which caused it to get under one of the screws used as hooks and lift the block.

 

We've investigated the impact of this tilt.

- Bonding strength: The bonding area is ~60% of the nominal. So this is weak, but we can reinforce the bonding with an aluminum bar.
- Misalignment of the DCPD housing: The tilt will laterally move the position of the DCPD. However, the displacement is small and it can be absorbed by the adjustment range of the DCPD housing.
- Removal: From the experience with the removal of the beam dump glass, this requires a long time of acetone soaking.

Conclusion:

- We don't need to remove the invar block.
- Action Item: Reinforcement of the bonding

  479   Sat Jan 28 00:46:21 2023 KojiMechanicsGeneralOMC #4: Replaced the locks of the transport fixture

Yesterday, we noticed that we could not close the transport fixture for OMC #4. We could not fully rotate the knobs of the locks. Today, I took the hooks from the functioning locks of the spare transport fixture.

It turned out that the default dimension of the lock seemed too tight. The functioning one has the through holes elongated by a file or something. This modification will be necessary for future transport fixtures.

  476   Thu Jan 26 23:16:35 2023 KojiOpticsConfigurationOMC #4: Top side bonding.

[Camille, Koji]

1. Flipping the OMC

It turned out that the transport fixture for this OMC could not be closed. The locks are too short, and the knobs could not be turned. We temporarily fastened the long 1/4-20 screws to secure the box and flipped it to make the top side face up.

2. Setting up the top-side template

The top side template was attached to the breadboard. We took care that the lock nuts on the positioning screws were not touched. The margins between the template and the glass edges were checked with a caliper. The long sides seemed very much parallel and symmetric, while the short sides were not symmetric. The lock nut on the short side was loosened, and the template was shifted to be symmetric w.r.t. the breadboard.

3. UV epoxy work

The cylindrical glass pieces were wiped, and the bonding surfaces were cleaned so that the visible fringes were <5 fringes. We confirmed the hooking side is properly facing up. The UV epoxy and UV curing were applied without any trouble. (Attachment 1)

4. EP30-2 bonding of the invar mounting blocks

Six invar blocks were bonded. This time the Allen key weights were properly arranged, so they didn't raise the blocks. The bond properly wetted the mating surfaces.

---

The final step of the bonding is to remove the template.
And replace the locks of the transport fixture.

 

  471   Thu Jan 19 23:45:44 2023 KojiOpticsGeneralOMC #4: cavity mirror bonding

[Koji, Camille]

We worked on the bonding of the flat mirrors for the OMC cavity with UV epoxy.

- Prepared the UV illumination setup. Cleaned up the table a bit to spare some space for the illuminator.
- Checked the output power of the illuminator. The foot pedal worked fine. The timer was set to be 10s. The UV output from the fiber was nominally 6W. This is after some warming up for ~1min. (Checked the output power continuously with the UV power meter.)

- Checked the cavity alignment / FSR / TMS - it looked good at this moment

- We confirmed that the UV epoxy has an expiration of July 3, 2023. The bond capsule was brought from Downs right before the work started, and thawed at the lab.

FM1 bonding

- The bottom of FM1 and the breadboard were cleaned. Cleaning with lens cleaning paper + IPA remained a few specks of dust on the surface. We decided to use Vectra swabs to wipe the breadboard surface. This worked pretty well.
- Applied a tap of UV epoxy to FM1 and placed it on the template. The optic was constrained by a retainer clip.
- We found that the spot positions were significantly moved. Probably FM1 was not well touching the template before. We tried to recover the previous optical axis by aligning CM1 and CM2.
- Here is the tip: align the beam on CM1 at the desired spot. Move CM1 to bring the spot on CM2 to the desired spot. CM2 is aligned to have TEM00 as much as possible.

- We recovered reasonable spots on the mirrors. Measured the FSR and TMS (vertical and horizontal) to be 264.73MHz, 58.18MHz, and 58.37MHz, respectively. This makes the 9th-order modes well separated from TEM00. Very good.

- Gave UV illumination 10s x 2. Confirmed that the mirror is rigidly bonded.

 

FM2 bonding

- Continued to bond the other flat mirror. The same process was repeated.
- The bottom of FM2 and the breadboard were cleaned.
- Applied a tap of UV epoxy to FM2 and placed it on the template. The optic was constrained by a retainer clip.
- Measured the FSR and TMS (vertical and horizontal) to be 264.7925MHz, 58.15MHz, and 58.3725MHz, respectively. This makes the 9th-order modes well separated from TEM00. Very good.

- Gave UV illumination 10s x 2. Confirmed that the mirror is rigidly bonded.

SM1/BS2/BS3 bonding

- Continued to bond some less important mirrors.
- SM1 was placed on the template with the same step as above. BS2 (for QPD) and a dummy QPD housing were also placed just to check if the optical axis has any inconsistency. The good beam alignment on the QPD housing was confirmed.
- Applied a bond to SM1 and blasted the UV (20s)
- Applied a bond to BS2. Checked the alignment on QPD1 again. It looked good. UV illumination was applied.

- Placed BS3 to the cavity transmission. A dummy DCPD housing was placed at the reflection side of BS3. There was no inconsistency with the beam alignment.
- The UV illumination was applied (20s).


Optic Inventory

Breadboard: #6
BS1: E6
FM1: A1
FM2: A3
CM1: PZT ASSY #8 (M7+PZT11+C11)
CM2: PZT ASSY #11 (M14+PZT13+C13)
SM1: E9
BS2: B8
SM2:
SM3:
BS3: B6

  472   Mon Jan 23 19:51:20 2023 KojiOpticsGeneralOMC #4: cavity mirror bonding

[Camille, Koji]

We continued to bond two CM mirrors and the other two steering mirrors for QPD2.

Before the bonding work, the FSR and TMSs were checked again.

FSR: 264.7925 MHz
TMS_V: 58.15125 MHz
TMS_H: 58.33375 MHz

Checked the transmission: The OMC loss was 4.3 +/- 0.2 %.

This does not make the HOMs coincidently resonant until the 18th-order (+9MHz). Looks good.


CM1/CM2/SM2/SM3 bonding

- Applied the bond to CM1 and the UV illuminated.
- Applied the bond to CM2 and the UV illuminated.
==> The cavity bonding is completed.

Removed the micrometer for CM2 to allow us to bond SM2/SM3
- Checked the spot at QPD2: The spot was a couple of mm too left. This was too much off compared to the QPD adjustment range. ==> Decided to shim the SM3 position with a piece of Al foil.
- Otherwise everything looked good. SM2/SM3 were bonded.


Invar block bonding

Prepared EP30-2
- There are three tubes of EP30-2 that expires on 2/22, 2023.
- A tube was almost empty. Used this tube to fill/purge the applicator. The 2nd tube was then attached to squeeze out 8g of glue mixture. 
- 0.4g of fused silica beads were added to the glue mixture.
- Mixed the bond and a test piece was baked by the oven. (200F=95C, 5min preheat, bakeing 15min).
- The glue test piece was "dry" and crisp. Looked good.
- Applied the glue on the invar blocks. Confirmed that the bonding surfaces were made completely "wet".
- 4-40 screws were inserted to the blocks so that the blocks were pushed toward the template. See Attachments 3 and 4.

 

Optic Inventory

Breadboard: #6
BS1: E6
FM1: A1
FM2: A3
CM1: PZT ASSY #8 (M7+PZT11+C11)
CM2: PZT ASSY #11 (M14+PZT13+C13)
SM1: E9
BS2: B8
SM2: E11
SM3: E14
BS3: B6

  319   Tue Mar 19 17:30:25 2019 KojiGeneralCharacterizationOMC (002) Test items

OMC #002 Optical tests

  • FSR measurement (done, 2019/1/8-9, 2019/4/1)
  • TMS measurement (done, 2019/1/9)
  • TMS measurement (with DC voltage on PZTs) (done, 2019/1/10)
  • Cleaning (done, 2019/3/19)
  • Power Budget (done, 2019/3/19, 2019/4/1)
  • PZT DC response (done, 2019/3/27)
  • PZT AC response (done, 2019/3/27)
  • QPD alignment (done, 2019/4/5)
  • DCPD alignment (done, 2019/4/4)
  • Beam quality check (done, 2019/4/4)

(Backscattering test)

(Cabling / Wiring)

  • (Attaching cable/mass platforms)
  • (PZT cabling)
  • (DCPD cabling)
  • (QPD cabling)

(Baking)
(First Contact)
(Packing / Shipping)

  325   Fri Apr 5 23:30:20 2019 KojiGeneralGeneralOMC (002) repair completed

OMC(002) repair completed

When the cable harness of OMC(004) is going to be assembled, the cable harness of OMC(002) will be replaced with the PEEK one. Otherwise, the work has been done.

Note that there are no DCPDs installed to the unit. (Each site has two in the OMC and two more as the spares)

More photos: https://photos.app.goo.gl/XdU1NPcmaXhATMXw6

  127   Tue May 14 19:06:00 2013 KojiCleanGeneralOMC Baking

The OMC is in the air bake oven now.

 

  387   Fri Dec 13 14:59:18 2019 StephenGeneralGeneralOMC Beam Dump Production Cure Bake

[Koji, Jordan, Stephen]

The beam dumps, bonded on Fri 06 Dec 2019, were placed in the newly tuned and configured small dirty ABO at the Bake Lab on Fri 13 Dec 2019.

Images are shared and references are linked below

Bonding log entry - https://nodus.ligo.caltech.edu:8081/OMC_Lab/386

Bake ticket - https://services.ligo-wa.caltech.edu/clean_and_bake/request/992/

OMC Beam Dump - https://dcc.ligo.org/LIGO-D1201285

  388   Wed Dec 18 21:54:53 2019 KojiGeneralGeneralOMC Beam Dump Production Cure Bake

The beamdumps were taken out from the oven and packed in bags.

The bottom of the V are completely "wet" for 17 BDs among 20 (Attachment 1/2).

3 BDs showed insufficient glue or delamination although there is no sign of lack of rigidity. They were separated from the others in the pack.

  393   Mon Sep 28 16:03:13 2020 ranaGeneralGeneralOMC Beam Dump Production Cure Bake
are there any measurements of the BRDF of these things? I'm curious how much light is backscattered into the incoming beam and how much goes out into the world.

Maybe we can take some camera images of the cleaned ones or send 1-2 samples to Josh. No urgency, just curiosity.

I saw that ANU and also some labs in India use this kind of blue/green glass for beam dumps. I don't know much about it, but I am curious about its micro-roughness and how it compares to our usual black glass. For the BRDF, I think the roughnesss matters more for the blackness than the absorption.

  394   Mon Sep 28 16:13:08 2020 KojiGeneralGeneralOMC Beam Dump Production Cure Bake

According to the past backscatter test of the OMC (and the black glass beamdump: not V type but triangular type on a hexagonal-mount), the upper limit of the back reflection was 0.13ppm. https://nodus.ligo.caltech.edu:8081/OMC_Lab/209

I don't have a BRDF measurement. We can send a few black glass pieces to Josh.

  110   Sat Apr 13 21:06:02 2013 KojiOpticsGeneralOMC Bottom-side: cavity glued

[Jeff, Zach, Lisa, Koji]

Gluing of the cavity mirrors went very well!!!

Preparation

- Checked if the cavity is still resonating. => Yes.

- Checked the FSR: 264.251MHz => 1.1345m
  2.5mm too long => Move each micrometer by 0.625mm backward

- FSR&TMS (I)
  Aligned the cavity again and checked the FSR: 264.8485MHz => 1.13194m
  TMS(V): 58.0875MHz => gamma_V = 0.219324
  TMS(H): 58.1413MHz => gamma_H = 0.219526
  the 9th modes of the carrier is 9.7-10.4 line width (LW) away from the carrier resonance
  the 13th modes of the lower f2 sideband are 9.2-10.2 LW away
  the 19th modes of the upper f2 sideband are 0.3-1.8 LW away
  We found that this coincidence of the resonance can be corrected by shortening the cavity round-trip by 0.5mm

- Spot positions (I)
 
The spots on the curved mirrors were ~1mm too much inside (FM side). In order to translate the cavity axis,
  MM2 and MM4 were pushed by θ
  θ/2.575 = 1mm ==> θ = 2.6 mrad
  The separation of the micrometers are ~20mm
  d/20mm = 2.6mrad ==> d = 52um

  1div of the micrometer corresponds to 10um => 5div = 50um

- Move the micrometers and adjusted the input steering to recover the alignment.

- In any case we were confident to adjust the FSR/TMS/spot positions only with the micrometers

BS1/FM1/FM2 gluing

- Aligned the cavity

- Glued BS1/FM1/FM2 one by one while the cavity resonance was maintained.
  FM2 was slipping as the table is not leveled well and the fixture was not supporting the optic.

- FSR&TMS (II)
  FSR: 264.964875MHz => 1.13144m (Exactly 0.5mm shorter!)
  TMS(V): 58.0225MHz => gamma_V = 0.218982
  TMS(H): 58.1225MHz => gamma_H = 0.219359
  the 9th modes of the carrier is 10.3~11.7 LW away
  the 13th modes of the lower f2 sideband are 7.4~9.3 LW away
  the 19th modes of the upper f2 sideband are 1.5~4.4 LW away

- Spot positions (II)
  Looked OK.

CM2 gluing

- Glued CM2. The mirror was supported from the back with allen keys.

- FSR&TMS (III)
 
FSR: 264.9665625MHz => 1.13144m
  TMS(V): 58.1275MHz => gamma_V = 0.219377
  TMS(H): 58.0813MHz => gamma_H = 0.219202
  the 9th modes of the carrier is 10.2~10.9 LW away
  the 13th modes of the lower f2 sideband are 8.5~9.4 LW away
  the 19th modes of the upper f2 sideband are 1.4~2.7 LW away

- Spot positions (III)
  Looked slightly off at CM2. Pushed MM2 by 4um.

CM1 gluing

- Glued CM1.

- FSR&TMS (IV)
 
FSR: 264.964875MHz => 1.13144m
  TMS(V): 58.06625MHz => gamma_V = 0.219145
  TMS(H): 58.08625MHz => gamma_H = 0.219220
  the 9th modes of the carrier is 10.8~11.1 LW away
  the 13th modes of the lower f2 sideband are 8.2~8.6 LW away
  the 19th modes of the upper f2 sideband are 2.6~3.2 LW away

- Spot positions (final confirmation)
  Looked OK. 

Final measurement

- After everything was finished, more detailed measurement has been done.

- FSR&TMS (final)
 
FSR: 264.963MHz => 1.13145m
  TMS(V): 58.0177MHz => gamma_V = 0.218966
  TMS(H): 58.0857MHz => gamma_H = 0.219221
  the 9th modes of the carrier is 10.8~11.7 LW away
  the 13th modes of the lower f2 sideband are 7.3~8.6 LW away
  the 19th modes of the upper f2 sideband are 2.6~4.5 LW away

Final values for the micrometers

  • MM1: The one closest to the input mirror (CM1) 0.78mm
  • MM2: The other one on CM1 0.89
  • MM3: The one closest to the output mirror (CM2) 0.90
  • MM4: The other one on CM2 0.90
/------------\

0.90         0.78
\------------/
0.90         0.89

 

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