ID |
Date |
Author |
Type |
Category |
Subject |
196
|
Sun Jul 6 02:45:56 2014 |
Koji | Optics | General | FSR Measurement |
3rd OMC FSR / Finesse measurement
RF AM was injected by detuning a HWP. |
617
|
Thu Aug 24 12:30:58 2023 |
Camille Makarem, Thejas | Optics | Characterization | FSR and TMS analysis |
Attached are the analysis results from the measurements in 616.
FSR: 264.657354 +/- 0.003444 MHz
Pitch TMS: 58.45691858660249 MHz
Yaw TMS: 58.55821902092523 MHz
The attached plot shows the HOM spectrum with their sidebands. We see that there is overlap between TEM00 and one of the 9th-order modes which means this higher order mode will resonate with the TEM00 carrier.
We estimate that by increasing the FSR to ~266.7 MHz, we will avoid this as shown in the next attached plot (HOM_scan.pdf).
This will require us to decrease the cavity length by 16mm (4 mm each mirror). We plan begin adjusting the micrometers this afternoon. |
616
|
Wed Aug 23 07:48:14 2023 |
Camille Makarem, Tejas | Optics | Characterization | FSR and TMS measuarement of A+ build |
[Camille, Thejas]
22 August 2023
We used the network analyzer to measure the FSR of the cavity using the method described in section 3.2.1 of T1500060. We locked the OMC cavity and maximized transmission the TEM00 mode. (REFL PD signal was ~45-50mV and REFL CCD looked the same as in 610). We adjusted to input offset on the servo module (REFL PD signal ~95mV) and recorded the transfer function between the modulation signal (channel R) and the transmission PD signal (channel A). (See attached picture of transfer function and phase.) We fit the FSR data to the code to get a value of 264.658982 MHz.
We also recorded the TMS of the cavity (with 0V to the PZTs). We measured the horizontal and vertical mode spacing separately. After maximizing transmission of TEM00, we then used the fiber coupler to misalign in the vertical direction first (REFL PD signal ~100). Using the network analyzer, we observed the peak at ~58 MHz. We then misaligned the mirror that steers the transmited beam to the PD. We clipped the transmitted beam so as to maximize the peak at ~58 MHz. (See attached spectrum.)
We recoved vertical alignment and then repeated this process for the horizontal direction. (See attached spectrum.)
Analysis in the next elog entry.
File names:
test_22-08-2023_160812 --> FSR
test_22-08-2022_165728 --> TMS vertical
test_22-08-2022_170543 --> TMS horizontal
https://gla-my.sharepoint.com/personal/t_seetharamu_1_research_gla_ac_uk/_layouts/15/onedrive.aspx?id=%2Fpersonal%2Ft%5Fseetharamu%5F1%5Fresearch%5Fgla%5Fac%5Fuk%2FDocuments%2FA%2B%20OMC%20%231%2F22%5F08%5F2023&view=0 |
468
|
Fri Dec 9 13:13:13 2022 |
Koji | Optics | Characterization | FSR/TMS/Spot Positions/Transmission |
[Camille Koji]
We quickly measured the basic parameters of the OMC as is.
=== FSR ===
Used the technique to find a dip in the transmission transfer function (TF) with offset locking + phase modulation. The FSR was 264.79003MHz = The cavity length of 1.13219 [m] (requirement 1.132+/-0.005 [m])
=== TMS ===
Used the technique to find the peaks in the trans TF with phase modulation + input misalignment + trans PD clipping.
TMS_V: 58.0727 / TMS_H: 58.3070 => TMS/FSR V:0.219316 H:0.220201
This makes the 9th-order modes nicely avoided (Attachment 1). A slightly longer FSR may makes the numbers close to the nominal.
=== Spot positions ===
The image/video capture board turned out not functional with the new Apple silicon mac. We decided to use a small CCD monitor and took a photo of the display.
All the spots are within the acceptable range. The scattering on CM2 was particularly bright on the CCD image and also in the image with the IR viewr.
The spot on FM1/2 are right at the expected location. The spot on CM1 is 0.5mm low and 0.7mm inside (left). The spot on CM2 is ~0.25mm too high and 0.3mm outside.
(Attachment 2, a small grid is 1 mm/div)
== Transmission ==
We made a quick simplified measurement (Attachment 3).
Assuming the reflectivity of the matched beam to be ~0, the mode matching is M=1-(59.2e-3-(-6.5e-3))/(3.074-(-6.5e-3))=0.979
==> The power of the coupled mode is M x 21.28mW = 20.83 mW
The measued transmission was 19.88 mW
==> The OMC transmission (total) was 0.954 (4.5% loss)
This number is not too bad. But the spot on CM2 has too bright scattering. Next week, we want to check if swapping CM2 may improve the situation or not. |
469
|
Mon Dec 12 19:04:40 2022 |
Koji | Optics | Characterization | FSR/TMS/Spot Positions/Transmission 2nd trial |
[Camille Koji]
We replaced CM2 with a PZT mirror subassembly serialized by PZT "13" (Attachment 1).
This made the transmission increase to 96.x%. Therefore the quick measurement of FSR and TSM were done. Also more careful measurement of the transmission was done.
Next time
== Alignment ==
- CM2 was replaced from PZT "12" to PZT "13".
- The resulting position of the cavity spot were all over 1mm too "+" (convention T1500060 Appendix C).
- So we decided to rotate CM2 by 1mrad in CW. This was done with (-) micrometer of CM2 "pushed" by 20um (2 rotational div).
- The resulting spot positions were checked with CCD. (Attachment 2). The spot positions seemed to be within +/-1mm from the center as far as we can see from the images. (good)
- CM2 spot looks much darker. CM1 spot is almost invisible with a CCD and also an IR viewer. FM1/2 spots were nominal bright level. (Looks OK)
== Quick measurement of the transmission ==
Transmission: 20.30 mW
Reflection Voltage (locked): 65.0 mV
Reflection Voltage (unlocked): 3.094 V
Reflection Voltage (dark): -6.5 mV
Incident Power: 21.64 mW
---> Mode matching 1-0.023 / Pcoupled = 21.14 / OMC Transmission 0.96
96% transmission is not the best but OK level. We decided to proceed with this mirror combination.
== Quick measurement of FSR/TMS ==
FSR: 264.7837MHz
TMS_V = 58.2105MHz
TMS_H = 58.1080MHz
The HOM structure (with PZT Vs = 0) is shown in Attachment 3. 9th order modes look just fine. The excplicit coincidence is 19th order 45MHz lower sideband. (Looks good)
== Transmission measurement ==
The raw measurements are shown in Attachment 4. The processed result is shown in Attachment 5.
We found that data set 2 has exceptionally low transmission. So we decided to run the 4th measurement excluding the set 2.
Over all OMC loss
Set1: 0.029 +/- 0.014
Set3: 0.041 +/- 0.0014
Set4: 0.038 +/- 0.001
--> 0.036 +/- 0.004
(0.964 Transmission)
|
184
|
Wed May 14 02:15:15 2014 |
Koji | Optics | Characterization | FSR/TSM adjustment of the OMC cavity |
1. FSR was adjusted and measured with "the golden arches" technique again.
FSR = 264.8412 MHz +/- 1400Hz => Lcav = 1.13197 m. (nominal 1.132m)
2. Transverse mode spacings for the vertical and horizontal modes were measured.
TMS/FSR = 0.218144 (V) / 0.219748 (H)
This is almost perfect!
The 19th-order lower sideband hit the resonance. Next step is to glue some of the flat mirrors.

|
88
|
Mon Apr 1 03:13:41 2013 |
Koji | Optics | General | Failure of PZT-glass joints |
[Koji, Jeff, Zach, Lisa]
We glued a test PZT-mirror assembly last week in order to make sure the heat cure of the epoxy does not make any problem
on the glass-PZT joints. The assembly was sent to Bob for the heat treatment. We received the assembly back from Bob on Wednesday.
We noticed that the assembly after the heat cure at 100degC had some voids in the epoxy layer
(looking like the fused silica surface was only 70% "wetted" by the epoxy).
The comparison of the assembly before and after the heat treatment is found in the slideshow at the bottom of the entry.
Initially our main concern was the impact to the control and noise performance.
An unexpected series resonance on the PZT transfer function and unwanted noise creation by the imperfect bonding may terribly ruin the IFO sensitivity.
In reality, after repeated poking by fingers, the PZT-prism joint was detached. This isn't good at all.
Note that there is no sign of degradation on the glass-glass joint.
We investigated the cause of this like:
- Difference of thermal expansion (3ppm/C PZT vs 0.55ppm/C fused silica)
- Insufficient curing of epoxy by UV (but this is the motivation of the heat cure)
Our resolution up to this point is to switch the glue to EP30-2. This means we will go through the heat cure test again.
Unfortunately there is no EP30-2 in stock at Caltech. We asked MIT to send us some packets of EP30-2.
Hardness of the epoxies is another concern. Through the epoxy investigation, we learned from Noliac that the glue for the PZT
should not be too hard (stiff) so as not to constrain the deformation of the PZT. EP30-2 has Shore D Hardness of 75 or more,
while Optocast UV epoxy has 88, and EPOTEK Epoxies, which Noliac suggested for gluing, has ~65. This should also be
confirmed by some measurement. We will also ask Master Bond if they have information regarding the effect of curing
temperature on the hardness of the epoxy. EP30-2 can be cured anywhere between RT and 200F (it's service range is up to 300F).
However, the entire breadboard, with the curved mirror sub-assemblies, will need to be baked at 110C to cure the UV Bond epoxy.
We hope that exposure to relatively higher temps doesn't harden the EP30-2. The EP30-2 data sheet recommends an epoxy
thickness of 80-120 microns which is much thicker than we would like.
We also don't have a way tocontrol the thickness; though we could add glass spheres to the epoxy to control the thickness.
The thickness of the EP30-2 used to bond the metal wire guide prism on the core optics is much thinner at 15-25 microns.
|
105
|
Mon Apr 8 23:42:33 2013 |
Koji | Optics | Configuration | Fake OMC roughly aligned |
Mode matching:
|
372
|
Fri Aug 23 11:11:44 2019 |
shruti | Optics | Characterization | Finding the curvature bottom |
I attempted to fit the data taken by Koji of the beam spot precession at the CCD in order to find the location of the curvature bottom in terms of its distance (d) and angle ( ) from the centre of the mirror. This was done using the method described in a previous similar measurement and Section 2.1.3 of T1500060.
Initially, I attempted doing a circle_fit on python as seen in Attachment 1, and even though more points seem to coincide with the circle, Koji pointed out that the more appropriate way of doing it would be to fit the following function:
![f(i, \theta, r, \phi) = \delta_{i,0} [r \cos(\theta+\phi) + x_c] + \delta_{i,1} [r \sin(\theta+\phi) +y_c]](https://latex.codecogs.com/gif.latex?f%28i%2C%20%5Ctheta%2C%20r%2C%20%5Cphi%29%20%3D%20%5Cdelta_%7Bi%2C0%7D%20%5Br%20%5Ccos%28%5Ctheta+%5Cphi%29%20+%20x_c%5D%20+%20%5Cdelta_%7Bi%2C1%7D%20%5Br%20%5Csin%28%5Ctheta+%5Cphi%29%20+y_c%5D)
since that would allow us to measure the angle more accurately; is the anti-clockwise measured angle that the curvature bottom makes with the positive x direction.
As seen on the face of the CCD, x is positive up and y is positive right, thus, plotting it as the reflection (ref. Attachment 2) would make sure that is measured anti-clockwise from the positive x direction.
The distance from the curvature bottom is calculated as

r: radius of precession on CCD screen (value obtained from fit parameters, uncertainty in this taken from the std dev provided by fit function)
R: radius of curvature of the mirror
L: Distance between mirror and CCD
R = 2.575 0.005 m (taken from testing procedure doc referenced earlier) and L = 0.644 0.005 m (value taken from testing doc, uncertainty from Koji)
|
d (mm) |
(deg) |
C7 |
0.554 0.004 |
-80.028 0.005 |
C10 |
0.257 0.002 |
-135.55 0.02 |
C13 |
0.161 0.001 |
-79.31 0.06 |
|
45
|
Wed Dec 19 18:47:03 2012 |
Koji | Clean | General | First Contact Training with Margot |
Steve and I visited Margot to have a training session for application of First Contact on optics.
- Make "thick" layer of first contact. It becomes thin when it gets dried.
- Apply more FC once a peek sheet is placed on the FC
- Wait for drying (~15min)
- Rip off the FC layer by pulling a peek tab. Make sure the ionized N2 is applied during ripping.
- Margot has a Dark Field Microscope. We checked how the dusts are removed from the surface.
There are many dusts on the mirror even if they are invisible. First Contact actually removes
these dusts very efficiently. Margot told us that even carbonhydrates (like finger prints) can be removed by FC.
|
51
|
Wed Jan 2 07:45:39 2013 |
Koji | Optics | Characterization | First Contact test |
Conclusion: Good. First contact did not damage the coating surface, and reduced the loss
- Construct a cavity with A1 and C2
- Measure the transmission and FWHM (of TEM10 mode)
- Apply First Contact on both mirrors
- Measure the values again
Transmission:
2.66 +/- 0.01 V -> 2.83 +/- 0.01 V
==> 6.3% +/- 0.5 % increase
FWHM of TEM10:
Before: (66.1067, 65.4257, 66.1746) +/- (0.40178, 0.38366, 0.47213) [kHz]
After: (60.846, 63.4461, 63.7906) +/- (0.43905, 0.56538, 0.51756) [kHz]
==> 5.1% +/- 2.7% decrease
Question: What is the best way to measure the finesse of the cavity? |
517
|
Mon Apr 3 11:06:47 2023 |
Thejas | Optics | Characterization | Flat mirror flatness |
Data can be found in DCC document T2300050.
On Friday. Camille and I measured the flatness of the flat mirror. Tilt values (without subtracting tilt) were less than 100 nm and PV across the surface was about 50 nm.
This checks that the flat mirror surface distortions are not contributing to the systematic deviations in our measurement of curvature minimum with varying the fiducial clocking angle. The deviations in the data show a far more disagreement between Y-Tilt of different clocking angles than the X-Tilt.
|
14
|
Wed Aug 1 19:35:00 2012 |
Koji | Facility | General | Floor cleaned / Workbench being built / Table top defect |
- The floor of the room was cleaned and waxed!
- Sticky mats are placed! Now we require shoe covers!

- Work benches are being built. One unit is done.

- The other is half done because the table top has chippings.

|
112
|
Tue Apr 16 08:12:14 2013 |
Koji | Optics | Characterization | Further More Mirror T measurement |
T&Rs of the B mirrors and some of the E mirrors are measured.
I found that these BSs have high loss (1%~3%) . As this loss will impact the performance of the squeezer
we should pick the best ones for the DCPD path. B5, B6, and B12 seems the best ones.
Mirror | P_Incident P_Trans P_Refl | T R loss |
| [mW] [mW] [mW] | |
-------+--------------------------------------+-------------------------------------------+
B1 | 13.80+/-0.05 7.10+/-0.05 6.30+/-0.05 | 0.514+/-0.004 0.457+/-0.004 0.029+/-0.005 |
B2 | 14.10+/-0.05 6.50+/-0.05 7.15+/-0.05 | 0.461+/-0.004 0.507+/-0.004 0.032+/-0.005 |
B3 | 13.87+/-0.05 7.05+/-0.05 6.55+/-0.05 | 0.508+/-0.004 0.472+/-0.004 0.019+/-0.005 |
B4 | 13.85+/-0.05 6.78+/-0.05 6.70+/-0.05 | 0.490+/-0.004 0.484+/-0.004 0.027+/-0.005 |
B5 | 13.65+/-0.05 6.93+/-0.05 6.67+/-0.05 | 0.508+/-0.004 0.489+/-0.004 0.004+/-0.005 |
B6 | 13.75+/-0.05 6.70+/-0.05 6.92+/-0.05 | 0.487+/-0.004 0.503+/-0.004 0.009+/-0.005 |
B7 | 13.83+/-0.05 7.00+/-0.05 6.60+/-0.05 | 0.506+/-0.004 0.477+/-0.004 0.017+/-0.005 |
B8 | 13.90+/-0.05 6.95+/-0.05 6.68+/-0.05 | 0.500+/-0.004 0.481+/-0.004 0.019+/-0.005 |
B9 | 13.84+/-0.05 6.95+/-0.05 6.70+/-0.05 | 0.502+/-0.004 0.484+/-0.004 0.014+/-0.005 |
B10 | 13.97+/-0.05 6.98+/-0.05 6.72+/-0.05 | 0.500+/-0.004 0.481+/-0.004 0.019+/-0.005 |
B11 | 13.90+/-0.05 7.05+/-0.05 6.70+/-0.05 | 0.507+/-0.004 0.482+/-0.004 0.011+/-0.005 |
B12 | 13.90+/-0.05 6.98+/-0.05 6.78+/-0.05 | 0.502+/-0.004 0.488+/-0.004 0.010+/-0.005 |
-------+--------------------------------------+-------------------------------------------+
Mirror | P_Incident P_Trans P_Refl | T R loss |
| [mW] [uW] [mW] | [ppm] |
-------+-------------------------------------------+------------------------------------------+
E4 | 13.65+/-0.05 0.0915+/-0.0005 13.50+/-0.05 | 6703+/-44ppm 0.989+/-0.005 0.004+/-0.005 |
E12 | 13.75+/-0.05 0.0978+/-0.0005 13.65+/-0.05 | 7113+/-45 0.993+/-0.005 0.000+/-0.005 |
E16 | 13.90+/-0.05 0.0975+/-0.0005 13.30+/-0.05 | 7014+/-44 0.957+/-0.005 0.036+/-0.005 |
-------+-------------------------------------------+------------------------------------------+
|
114
|
Tue Apr 16 23:26:51 2013 |
Koji | Optics | Characterization | Further More Mirror T measurement |
Since the previous measurement showed too high loss, the optical setup was checked.
It seemed that a PBS right before the T&R measurement setup was creating a lot of scattering (halo) visible with a sensor card.
This PBS was placed to confirm the output polarization from the fiber, so it was ok to remove it.
After the removal, the R&T measurement was redone.
This time the loss distributed from 0.2% to 0.8% except for the one with 1.3%. Basically 0.25% is the quantization unit due to the lack of resolution.
At least B7, B10, B12 seems the good candidate for the DCPD BS.
The AR reflection was also measured. There was a strong halo from the main reflection with an iris and sense the power at ~.5mm distance to separate the AR reflection from anything else. Now they are all somewhat realistic. I'll elog the measurement tonight.
33.6 +/- 0.2 uW out of 39.10+/-0.05 mW was observed. The offset was -0.236uW.
This gives us the AR reflectivity of 865+/-5ppm . This meets the spec R<0.1%
Mirror | P_Incident P_Trans P_Refl | T R loss |
| [mW] [mW] [mW] | |
---------------------------------------------------------------------------------------------
B1 | 39.10+/-0.05 19.65+/-0.05 19.25+/-0.05 | 0.503+/-0.001 0.492+/-0.001 0.005+/-0.002 |
B2 | 39.80+/-0.05 19.90+/-0.05 19.70+/-0.05 | 0.500+/-0.001 0.495+/-0.001 0.005+/-0.002 |
B4 | 39.50+/-0.05 19.70+/-0.05 19.30+/-0.05 | 0.499+/-0.001 0.489+/-0.001 0.013+/-0.002 |
B5 | 39.50+/-0.05 19.70+/-0.05 19.50+/-0.05 | 0.499+/-0.001 0.494+/-0.001 0.008+/-0.002 |
B6 | 39.55+/-0.05 19.50+/-0.05 19.95+/-0.05 | 0.493+/-0.001 0.504+/-0.001 0.003+/-0.002 |
B7 | 40.10+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.494+/-0.001 0.504+/-0.001 0.002+/-0.002 |
B8 | 40.15+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.493+/-0.001 0.503+/-0.001 0.004+/-0.002 |
B9 | 40.10+/-0.05 19.90+/-0.05 19.90+/-0.05 | 0.496+/-0.001 0.496+/-0.001 0.008+/-0.002 |
B10 | 40.10+/-0.05 19.70+/-0.05 20.30+/-0.05 | 0.491+/-0.001 0.506+/-0.001 0.002+/-0.002 |
B11 | 40.20+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.493+/-0.001 0.502+/-0.001 0.005+/-0.002 |
B12 | 40.20+/-0.05 19.90+/-0.05 20.20+/-0.05 | 0.495+/-0.001 0.502+/-0.001 0.002+/-0.002 |
---------------------------------------------------------------------------------------------
|
49
|
Mon Dec 31 03:11:45 2012 |
Koji | Optics | Characterization | Further more RoC measurement |
Total (excluding C2, C7, C8): 2.575 +/- 0.005 [m]
New results
C6: RoC: 2.57321 +/− 4.2e-05m
C7: RoC: 2.56244 +/− 4.0e−05m ==> Polaris mount
C8: RoC: 2.56291 +/− 4.7e-05m ==> Ultima mount
C9: RoC: 2.57051 +/− 6.7e-05m
Previous results
C1: RoC: 2.57845 +/− 4.2e−05m
C2: RoC: 2.54363 +/− 4.9e−05m ==> Josh Smith @Fullerton for scattering measurement
C3: RoC: 2.57130 +/− 6.3e−05m
C4: RoC: 2.58176 +/− 6.8e−05m
C5: RoC 2.57369 +/− 9.1e−05m |
39
|
Fri Nov 9 00:43:32 2012 |
Koji | Optics | Characterization | Further more wedge measurement |
Now it's enough for the first OMC (or even second one too).
Today's measurements all distributed in theta>0.5deg. Is this some systematic effect???
I should check some of the compeled mirrors again to see the reproducibility...
A1 Horiz Wedge 0.497039 +/- 0.00420005 deg / Vert Wedge 0.02405210 +/- 0.00420061 deg
A2 Horiz Wedge 0.548849 +/- 0.00419993 deg / Vert Wedge 0.05087730 +/- 0.00420061 deg
A3 Horiz Wedge 0.463261 +/- 0.00420013 deg / Vert Wedge 0.00874441 +/- 0.00420061 deg
A4 Horiz Wedge 0.471536 +/- 0.00420011 deg / Vert Wedge 0.01900840 +/- 0.00420061 deg
A5 Horiz Wedge 0.458305 +/- 0.00420014 deg / Vert Wedge 0.00628961 +/- 0.00420062 deg
B1 Horiz Wedge 0.568260 +/- 0.00419988 deg / Vert Wedge -0.00442885 +/- 0.00420062 deg
B2 Horiz Wedge 0.556195 +/- 0.00419991 deg / Vert Wedge -0.00136749 +/- 0.00420062 deg
B3 Horiz Wedge 0.571045 +/- 0.00419987 deg / Vert Wedge 0.00897185 +/- 0.00420061 deg
B4 Horiz Wedge 0.563724 +/- 0.00419989 deg / Vert Wedge -0.01139000 +/- 0.00420061 deg
B5 Horiz Wedge 0.574745 +/- 0.00419986 deg / Vert Wedge 0.01718030 +/- 0.00420061 deg
E1 Horiz Wedge 0.600147 +/- 0.00419980 deg / Vert Wedge 0.00317778 +/- 0.00420062 deg
E2 Horiz Wedge 0.582597 +/- 0.00419984 deg / Vert Wedge -0.00537131 +/- 0.00420062 deg
E3 Horiz Wedge 0.592933 +/- 0.00419982 deg / Vert Wedge -0.01082830 +/- 0.00420061 deg
-------
To check the systematic effect, A1 and B1 were tested with different alignment setup.
A1 Horiz Wedge 0.547056 +/- 0.00419994 deg / Vert Wedge 0.0517442 +/- 0.00420061 deg
A1 Horiz Wedge 0.546993 +/- 0.00419994 deg / Vert Wedge 0.0469938 +/- 0.00420061 deg
A1 Horiz Wedge 0.509079 +/- 0.00420003 deg / Vert Wedge 0.0240255 +/- 0.00420061 deg
B1 Horiz Wedge 0.547139 +/- 0.00419994 deg / Vert Wedge 0.0191204 +/- 0.00420061 deg
|
249
|
Tue Dec 29 12:15:46 2015 |
Koji | General | General | Glasgow polarizer passed to Kate |
The Glasgow polarizer was passed to Kate on Dec 17, 2015. |
391
|
Mon Aug 10 15:34:04 2020 |
Koji | Facility | Loan / Lending | Glue bake oven |
Black and Decker Glue Baking Oven came back to the OMC lab on Aug 10, 2020, Georgia had lent the unit for the SAMS assembly/testing. |
161
|
Fri Aug 30 12:14:50 2013 |
Koji | Optics | General | H1 OMC Cavity length adjustment |
Short conclusion:
The roundtrip cavity length for the H1 OMC was adjusted to be 1.145m
instead of 1.132m such that the 19th HOMs of the lower sideband do not get resonant together with the carrier.
Background:
The purpose of the OMC is to transmit the carrier TEM00 mode while anything else is rejected.
As the optical cavity has infinite numbers of resonant modes, what we practically do is to select
the roundtrip accumulated gouy phase so that low order higher order modes for the carrier
as well as the sidebands (including the TEM00 modes).
The nominal round trip length of the OMC is 1.132m. The curvature of the mirror is 2.575m.
The nominal ratio between the TMS and FSR is 0.218791 and 0.219385 (TMS_V/TMS_H= 0.9973)
for the vertical and horizontal modes. This split comes from the non-zero angle (~4deg) of incidence on the curved mirrors.
In reality, the TMS/FSR ratio depends on the true curvature of the mirror. More importantly, astigmatism
of the mirror changes the difference of the ratios for the vertical and horizontal modes.
The mirror astigmatism can either reduce or increase the split. between the TMSs. For example,
the L1 OMC showed the TMS/FSR ratio of (0.218822, 0.219218) for the vertical and horizontal modes.
TMS_V/TMS_H is 0.9982 which is 0.18% from the unity. This suggests, roughly to say, that 0.27% of the
astigmatism coming from the AOI of 4deg was partially compensated by the mirror astigmatism. This was lucky.
Something unlucky happened to the case for the first choice of the H1OMC curved mirrors.
TMS_V/TMS_H is 0.990 which is indeed 1% away from the unity. This actually caused some problem:
As the modes spreads too wide, the 19th modes became unavoidable. (see the picture below)

Red - carrier, Blue - upper sideband (+45MHz), Green - lower sideband
After the replacing one of the PZT assembly with another one, 1-TMS_V/TMS_H went down to 6%.
But still the 19th mode is on resonance. In order to shift the 19th mode from the resonance, the cavity length
had to be changed more than the range of the micrometer.
Simple simulation:
Attached Mathematica file calculates expected mode structure when the curved mirror position is
moved by DL (then the total roudtrip length changes 4*DL). This tells us that the 19th mode is
moved from the resonance by giving DL=-0.003 or DL=0.0025.
It was impossible to make the cavity short enough as the gluing fixture interferes with the curved mirror.
In fact, it was also impossible to make the cavity long enough as it was. Therefore PEEK shims with
the thickness of 1.5mm was inserted.

Result:
The FSR and TMS were measured with the longer cavity. 50V was applied to PZT1.
FSR: 261.775MHz
TMS_V: 57.575MHz
TMS_H: 57.880MHz
=> Cavity round trip length of 1.1452m
=> TMS/FSR = {0.219941, 0.221106}
The 19th modes for the lower sidebands are successfully moved from the carrier resonance.
The first accidental resonance is the lower sideband at the 28th order modes.

|
162
|
Fri Aug 30 12:22:56 2013 |
Koji | Optics | General | H1 OMC Cavity side UV gluing |
H1 OMC Cavity side optics was glued on the breadboard
Curved mirror gluing
- Applied the UV glues to CM1/CM2 prisms.
- Checked the spot positions on the curved mirrors
- Apply 50V to CM1
- Measure the FSR and TMS while the cavity was locked.
FSR: 261.70925MHz
TMS_V: 57.60500MHz
TMS_H: 57.94125MHz
=> Cavity round trip length of 1.1455m
=> TMS/FSR = {0.220111, 0.221395}
First accidental resonance is the lower sideband at 28th order modes.

Carrier 9th-order HOM: 2.9~7.6 line width away
Upper Sideband 13th-order HOM: 14.1-20.7 LW away
Lower Sideband 19th-order HOM: 3.3-13.1 LW away
- As this result was satisfactory, the UV illumination was zapped. It did not change the alignment. The cavity was kept locked during the illumination.
Peripheral optics gluing
- QPD path BS/Steering Mirrors were glued
- DCPD path BS was glued
The UV glue was applied to the optics.
Then the optics were placed on the breadboard along with the fixture.
Placed the dummy QPD/DCPD mount with the alignment disks.
The horizontal positions of the spots were well with in the horizontal range of the mounts.
The UV illumination was zapped. Checked the alignment again and no problem was found. |
263
|
Fri Aug 12 14:58:17 2016 |
Koji | General | Configuration | H1 OMC DCPD replacement |
Preparation of 3rd OMC for the use in H1
New DCPD(T) = B1-01
DCPD(T) = DCPDA: extracted and accomodated in CAGE-A SLOT1
New DCPD(R) = B1-16
DCPD(R) = DCPDB: extracted and accomodated in CAGE-A SLOT2 |
164
|
Fri Aug 30 12:25:29 2013 |
Koji | General | General | H1 OMC Invar mount gluing |
The Invar Mounting Blocks were glued on the breadboard.
Serial number #1/2/5/6/7/8 -> I1 OMC cable side
Serial number #9/10/11/12 -> H1 OMC cavity side |
169
|
Mon Oct 14 13:40:16 2013 |
Koji | Optics | Characterization | H1 OMC Optical testing |
Since the middle of September, the optical tests of H1 OMC were took place.
Here is summary of the progress.
TEST1: FSR/FINESSE measurement before applying First Contact
TEST2: Power budget
MIrror cleaning with First Contact
TEST3: FSR/FINESSE measurement after First Contact application
TEST4: Power budget
TEST5: N/A
TEST6: HOM measurement @PZT V=0
TEST7: HOM measurement @PZT V=0-200
TEST8: DC response of the PZT
TEST9: AC response of the PZT
TEST10: PD/QPD alignment / output check
|
170
|
Mon Oct 14 15:50:55 2013 |
Koji | Optics | Characterization | H1 OMC Power budget |
LHO OMC power budget
Date |
2013/9/17 |
2013/9/17 |
2013/10/16 |
2013/10/22 |
Condition |
Before the cleaning |
After the cleaning |
Confirmation |
Confirmation |
Input Power [mW] |
35.2 |
35.4 |
34.54 |
34.9 |
REFLPD dark offset [V] |
-0.00763 |
-0.00763 |
-0.00772 |
-0.000759 |
REFLPD unlocked [V] |
0.0749 +/- 0.0005 |
0.067+/- 0.0005 |
0.0640+/-0.0005 |
0.0530+/-0.0001 |
REFLPD locked [V] |
5.49 +/- 0.01 |
5.55+/-0.01 |
5.28+/-0.01 |
5.26+/-0.01 |
|
|
|
|
|
Transmitted Power to DCPD1 (T) [mW] |
16.5 |
16.4 |
16.1 |
16.0 |
Transmitted Power to DCPD2 (R) [mW] |
15.9 |
16.2 |
15.55 |
15.55 |
FM2 transmission [mW] |
32.4 |
32.9+/-0.1 |
- |
- |
CM1 transmission [mW] |
0.166 |
0.169 |
0.164 |
0.165 |
CM2 transmission [mW] |
0.165 |
0.169 |
0.158 |
0.162 |
Input BS transmission [mW] |
0.234 |
0.218 |
0.230 |
0.227 |
|
|
|
|
|
Cavity Finesse |
373.114 |
373.114 |
373.114 |
373.114 |
|
|
|
|
|
Junk Light Power (Pjunk) [mW] |
0.489 |
0.434 |
0.422 |
0.332 |
Coupled beam power (Pcouple) [mW] |
34.71 |
34.97 |
34.12 |
34.57 |
Mode Matching (Pcouple/Pin) [mW] |
0.986 |
0.988 |
0.988 |
0.990 |
Cavity reflectivity in power |
0.00115 |
0.00119 |
0.00136 |
0.00199 |
Loss per mirror [ppm] |
122 |
124 |
134 |
167 |
Cavity transmission for TEM00 carrier
|
0.933 |
0.932 |
0.927 |
0.913 |
|
154
|
Wed Aug 21 08:31:21 2013 |
Koji | Optics | Characterization | H1 OMC cavity alignment |
Alignment of the H1 OMC cavity mirrors
- The cavity mirrors as well as the first steering mirror were aligned on the cavity side template.
- The locking of the cavity was not so stable as before. Some high freq (several hundreds Hz) disturbance makes the cavity
deviate from the linear range. This can be mitigated by turning off the HEPA units but this is not an ideal condition.
- FSR and TMS were measured.
FSR: 264.305MHz
TMS(V): 58.057MHz
TMS(H): 58.275MHz
These suggest the cavity length L and f_TMS/f_FSR (say gamma, = gouy phase / (2 pi) ) as
L=1.1343 m (1.132m nominal)
gamma_V = 0.219659 (0.21879 nominal)
gamma_H = 0.220484 (0.21939 nominal)
- the 9th modes of the carrier is away from the resonance 6-9 times of the line width (LW)
- the 13th modes of the lower f2 sideband are 11-15 LW away
- the 19th modes of the upper f2 sideband are 0.6-7 LW away
We still need precise adjustment of the gouy phase / cavity length, this was enough for the gluing of the flat mirrors |
165
|
Tue Sep 3 17:03:25 2013 |
Koji | General | General | H1 OMC gluing completed |
[Koji Jeff]
H1 OMC All Gluing completed
5 Glue H1 beam dumps (UV)
4 glass wire brackets glued on the H1 topside (UV) SN: #9/10/11/12
6 Invar blocks glued on the H1 topside (EP30) SN: #13/14/15/16/18/19 |
166
|
Wed Sep 4 22:22:54 2013 |
Koji | General | General | H1 OMC wrapped and moved to the bake lab. |
[Koji, Jeff]
We moved the H1OMC to the bake lab.
Chub set up the vacuum bake oven (Oven F) and running without the actual OMC.
We use low temperature (55degC) for the baking.
The actual OMC will be baked from tomorrow afternooon. |
159
|
Thu Aug 29 02:52:50 2013 |
Koji | Optics | Characterization | H1OMC Curved Mirror Alignment |
Cavity parameter was measured with 50V bias on PZT1 (CM1)
- PZT combination was changed: PZT1 #21 (PZT ASSY#6) / PZT2 #25 (PZT ASSY #4)
- 19th HOMs of the USB makes accidental resonance with the nominal cavity length.
Because of the mirror astigmatism, HOMs spreads more than the design.
In order to avoid these modes, the cavity length had to be moved from the nominal value (1.134m).
- The clearance between the fixture and the prism was limited. This prevents to shorten the cav length.
The cavity length was made longer about 10mm.
-----
Cavity parameter obtained from the pitch misalignment
Free Spectral Range (FSR): 261.777947 +/− 0.000299 MHz
Cavity roundtrip length: 1.145217 +/− 0.000001 m
Lock offset: 1.636183 +/− 0.238442 kHz
Transverse mode spacing (TMS): 57.581950 +/− 0.000163 MHz
TMS/FSR: 0.219965 +/− 0.000001
Cavity pole (1st order modes, avg and stddev): 353.465396 +/− 0.657630 kHz
Finesse (1st order modes, avg and stddev): 370.302940 +/− 0.688585
Carrier 9th-order HOM: -8.1 line width away
Upper Sideband 13th-order HOM: 13.3 LW away
Lower Sideband 19th-order HOM: 2.2 LW away
-----
Cavity parameter obtained from the pitch misalignment
Free Spectral Range (FSR): 261.777106 +/− 0.000226 MHz
Cavity roundtrip length: 1.145220 +/− 0.000001 m
Lock offset: 0.215937 +/− 0.183434 kHz
Transverse mode spacing (TMS): 57.875622 +/− 0.000116 MHz
TMS/FSR: 0.221087 +/− 0.000000
Cavity pole (1st order modes, avg and stddev): 356.862001 +/− 0.448102 kHz
Finesse (1st order modes, avg and stddev): 366.776766 +/− 0.460598
Carrier 9th-order HOM: -4.1 line width away
Upper Sideband 13th-order HOM: 19.1 LW away
Lower Sideband 19th-order HOM: 10.8 LW away
-----
We could avoid hitting the 19th modes of the 45MHz sidebands.
First accidental hit is the 28th order modes of the lower sideband.
Red: Carrier
Blue: Upper sideband (45MHz)
Green: Lower sideband (45MHz)

|
175
|
Mon Nov 4 19:43:56 2013 |
Koji | General | General | H1OMC Packed |
H1OMC PZT connector was replaced with the correct one. This was the final step for H1OMC.
Jeff and I packed the OMC and put it in the perikan case. It will be shipped tomorrow.
The other tools are also packed in the other box. Here is the list of the items
- Spare PD/QPDs (2 cages)
- Test PD/QPD cables
- Torque driver / bits
- Low noise transimpedance amp
- Kapton sheets
- First Contact kit
- 1/4-20 Screws for the balance weights
- OMC-Structure cables
- Preamp adapter plate
- Screws for the cable mounts
- Clean tools
(scissors, tweezers, forceps, Diagonal pliers, long nose prier)
- Spare Peek cable ties
|
163
|
Fri Aug 30 12:24:28 2013 |
Koji | Optics | Characterization | H1OMC Spot positions |
Beam heights on the diodes
DCPD1: 14.459mm -> With 1.5mm shim, the beam will be 0.038mm too low.
DCPD2: 14.221mm -> With 1.25mm shim, the beam will be 0.026mm too low.
QPD1: 14.691mm -> With 1.75mm shim, the beam will be 0.056mm too low.
QPD2: 14.379mm -> With 1.5mm shim, the beam will be 0.118mm too low. |
173
|
Tue Oct 22 17:17:59 2013 |
Koji | General | General | H1OMC cabling |
[Chub, Jeff, Koji]
We worked on the wiring and routing of the cables.
- The cables for the PZT was installed first.
- Pins for the mighty mouse connector were crimped on the PZT wires
- Checked the wiring diagram (D1300589) to find the pinouts.
Pin1 of the mighty mouse is connected to PZT2+, Pin2 to PZT2-, PIn3 to PZT1+, and Pin4 to PZT1-
- Then QPD and PD cables are fixed on the cable harness.
- The QPD/PD cables are attached on the diode housings.
During this process one of the DCPD mounts moved. The fixing screws were not torqued enough.
This means that all of the FC layers need to be removed and the DCPD housing should be aligned again.
- We continued on the cabling. The cables were routed on the top (cable) side.
- Some of the cable pegs were tightened by PEEK cable ties.
- We found that Pin1 and Pin2 of the PZT cables were not intact anymore.
- We ask Chub to work on the PZT pins tomorrow. The PD alignment will be taken tonight or tomorrow. |
176
|
Thu Nov 21 00:05:35 2013 |
Koji | General | General | H1OMC electronics arrangement |
Checked the PZT arrangement: Mighty Mouse Pin1&2 -> PZT2 (DCPD side), Mighty Mouse Pin3&4 -> PZT1 (QPD side)
DCPD response:
Illuminate DCPD1 (T) -> DCPD B responded in MEDM
Illuminate DCPD2 (R) -> DCPD A responded in MEDM
QPD response:
Illuminate QPD1 -> QPD A responded in MEDM
Illuminate QPD2 -> QPD B responded in MEDM
--------
DCPD1 (T) is marked as "A". This PD is SN"0288"
DCPD2 (R) is marked as "B". This PD is SN"0721"
Corresponding iLOG for the performance
|
368
|
Mon Jun 24 12:54:58 2019 |
Koji | Clean | General | HEPA BOOTH |
https://www.airscience.com/purair-flow-laminar-flow-cabinets |
519
|
Wed Apr 5 22:09:30 2023 |
Koji | Facility | General | HEPA Enclosure extension |
Chub finished the HEPA enclosure extension project. |
500
|
Mon Mar 6 12:25:08 2023 |
Koji | Facility | General | HEPA Enclosure improvement |
Chub, JC, and co worked on the HEPA enclosure improvement. |
198
|
Sun Jul 6 03:56:40 2014 |
Koji | Optics | Characterization | HOM measurement with PZT vol swept |
Cavity FSR/TMS measurement (2014/7/5) with PZT voltages swept from 0V to 200V (50V step) |
199
|
Sun Jul 6 08:31:14 2014 |
Koji | Optics | Characterization | HOM measurement with PZT vol swept |
3rd OMC, HOM diagram at PZT1=0V and PZT2=50V.
First coincidence with the carrier is the 32nd-order carrier mode. Very good. |
255
|
Sat Mar 26 01:49:48 2016 |
Koji | Optics | Characterization | HQEPD QE |
Calibration of the transimpedance
Use KEITHLEY 2450 as a calibrated current source. Model 2450 has the current source accuracy of 0.020%+1.5uA at 10mA range. For 6mA current output, the error is 3uA (0.05%).
The output of the current amp at 103 Ohm setting was 6.0023V when -6.000mA current was applied. i.e R_trans = 1000.4 +/- 0.5 Ohm. This is a negligible level.
QE of the diodes (As of 07/30/2016)
Refer E1800372 |
254
|
Sun Mar 13 22:02:09 2016 |
Koji | Optics | Characterization | HQEPD QE measurement (direct comaprison) |
Direct comparison of the PD responsibities
We can expect 5% increase of the QE with the new PD.
P-pol 10deg incident
Power meter Ophir RM9C (Systematic error +/-5%)
Vbias = 6V
C30665GH (#07)
Incident: 7.12mW
Reflection: 0.413mW (=> R=5.8%)
PD output: 5.690+/-0.006V
=> Responsibity 0.799+/-0.001 A/W
=> QE = 0.931+/-0.001
HQE PD (A1-23)
Incident: 7.15mW
Reflection: 0.020+/-0.1mW (=> R=0.28%)
PD output: 6.017+/-0.007V
=> Responsibity 0.842+/-0.001 A/W
=> QE = 0.981+/-0.001
Note that there is a 5% systematic error with the power meter. |
256
|
Sat Mar 26 17:39:50 2016 |
Koji | Electronics | Characterization | HQEPD dark noise |
Dark noise measurement for 6 HQEPDs and 1 C30665. All of these showed sufficiently low dark current noise levels compared with the noise level of the DCPD preamp. The measurement was limited by the input noise (ADC) noise of the FFT analyzer as the line noises were too big.
The measurement has been done with the transimpedance of 1e7. The bandwidth of the measurement was 50kHz. |
262
|
Fri Jul 22 22:24:05 2016 |
Koji | General | General | HQEPD inventory |
As of Jul 22, 2016
As of Aug 11, 2016
As of Aug 16, 2016
A1-23 in Cage G https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-A1-23
-> Shipped to LLO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8181
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-1
= Replaced C30665 eLIGO PD (SN 01 in Cage G now) ICS: C30665GH-0-00-0001
-> Removed PD@LLO, Waiting for the shipment to CIT
A1-25 in Cage G https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-A1-25
-> Shipped to LLO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8181
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-1
= Replaced C30665 eLIGO PD (SN 02 in Cage G now) ICS: C30665GH-0-00-0002
-> Removed@LLO, Waiting for the shipment to CIT
B1-01 in Cage A https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-B1-01
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-3_2
= replaced C30665 eLIGO PD (SN 11 in Cage A now) ICS: C30665GH-0-00-0011
-> Removed PD@LHO
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8187
B1-16 in Cage A https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-B1-16
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Now in https://ics-redux.ligo-la.caltech.edu/JIRA/browse/ASSY-D1201439-3_2
= replaced C30665 eLIGO PD (SN 12 in Cage A now) ICS: C30665GH-0-00-0012
-> Removed PD@LHO
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8187
C1-05 in Cage F https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-05
-> @CIT contamination test cavity
C1-07 in Cage F https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-07
-> @CIT contamination test cavity
C1-17 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-17
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Left @LHO as a spare
C1-21 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-C1-21
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Left @LHO as a spare
D1-08 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-D1-08
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Moved to Cage A3
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8186
-> Arrived at CIT (Aug 16)
D1-10 in Cage E https://ics-redux.ligo-la.caltech.edu/JIRA/browse/IHGQEX3000-0-00-D1-10
-> Shipped to LHO https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8182
-> Moved to Cage A4
-> Shipped from LHO to CIT https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Shipment-8186
-> Arrived at CIT (Aug 16) |
427
|
Tue Jul 26 00:12:58 2022 |
Koji | General | General | High QE PD: QE measurements |
- Installed the High QE PDs to OMC #002
- B1-22@Cage B1 was installed to the transmission DCPD
- B1-23@Cage B1 was installed to the reflection DCPD
Upon the installation, the legs of the PDs were cut by 3mm. Also, the tab of the PD could not be embedded in the DCPD housing. Therefore, the tabs were cut.
The alignment looked just fine. The weak reflections are directed to the black glass beam dumps.
- After the installation, the QEs were measured.
- With Thorlabs S130C power meter, the QE was estimated to be ~95%. (Accuracy +/-7%)
- With Thorlabs S401C power meter, the QE was estimated to be ~100%. (Accuracy +/-3%)
It is so confusing. So I decided to make the QE test setup.
Ophir RM9 with chopper (+/-5%): 8.97mW
Thorlabs S140C integrating sphere (+/-7%): 9.11mW
Thorlabs S130C PD power meter (+/-7%): 9.15mW
Thorlabs S401C thermal power meter (+/-3%): 8.90mW
So there looks ~3% discrepancy between S130C and S401C
Then tried to measure the QE of C1-03@Cage B3 with Ophir RM9
- Initial state: QE=0.95
- First FirstContact application: QE went up to 0.973
- Second FirstContact application: QE = 0.974, basically no change
To Do:
- Calibrate the trans-impedance amp with Keithley
- Apply FC to B1-22 and B1-23 to see if there is an improvement
- The power should be measured with S401C because the accuracy seems better (+/-3%).
- Take photos of the PD FC process
General To Do:
- Backscatter test 2nd trial
- Start applying the first contact to the optical surfaces
- Beam dump cleaning
- Apply FC cap to the PDs
- Delamination repair (light side)
- Delamination repair (dark side)
- Cable bracket replace (dark side)
|
429
|
Wed Jul 27 10:34:09 2022 |
Koji | General | General | High QE PD: QE measurements 2 |
- DLPCA-200 trans-impedance amplifier was calibrated.
Keithley source meter 2450 was connected to the amp. Provide current and read the output voltage with the precision digital voltage meter (Agilent/Keysight).
Gain: 999.7V/A@7mA, 999.6V/A@8mA
- From the power meter spec, Thorlabs S401C seemed the best (+/-3%). So the QEs of the 9 PDs were checked with this power meter again.
- All PDs exhibited the QE of 0.95~0.96. It's all relative as the power meter has a systematic error.
- Tried to clean B1-22 and B1-23 PDs. They didn't show significant improvement after the cleaning. To avoid the unnecessary risk of damaging the PDs, further cleaning was not performed. (Some photos were attached)
- What we can do is use this result as the relative measurements.
- For OMC#2, B1-22 is the DCPD(T) and B1-23 is the DCPD(R). C1-03 and C1-12 are the spares, according to this latest result.
- At LLO, we track down the source of the throughput reduction (-10%). The QEs of the PDs are going to be tested in the same setup at once to compare their PDs and our PDs.
PD Type |
SN |
Case |
DCV1 |
Pin [mW] |
dPin [mW] |
Power Meter |
DCV2 |
Avg(DCV) |
Std(DCV) |
DCVOFS (mV) |
Responsivity [A/W] |
dR |
QE |
dQE |
Date |
Note |
IGHQEX3000 |
B1-22 |
B1 |
7.734 |
9.43 |
0.02 |
TL 401C |
7.745 |
7.7395 |
0.006 |
-0.0260 |
0.821 |
0.002 |
0.957 |
0.002 |
July 26, 2022 |
clean1 / installed (T) |
IGHQEX3000 |
B1-23 |
B2 |
7.679 |
9.26 |
0.02 |
TL 401C |
7.709 |
7.6940 |
0.015 |
-0.0220 |
0.831 |
0.002 |
0.969 |
0.003 |
July 26, 2022 |
clean1 / installed (R) |
IGHQEX3000 |
C1-03 |
B3 |
7.775 |
9.40 |
0.02 |
TL 401C |
7.770 |
7.7725 |
0.003 |
-0.0450 |
0.827 |
0.002 |
0.964 |
0.002 |
July 26, 2022 |
clean3 |
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
IGHQEX3000 |
C1-08 |
C2 |
7.717 |
9.45 |
0.02 |
TL 401C |
7.750 |
7.7335 |
0.017 |
-0.0430 |
0.819 |
0.002 |
0.954 |
0.003 |
July 26, 2022 |
initial |
IGHQEX3000 |
C1-09 |
C3 |
7.737 |
9.50 |
0.05 |
TL 401C |
7.776 |
7.7565 |
0.019 |
-0.0580 |
0.817 |
0.005 |
0.952 |
0.006 |
July 26, 2022 |
initial |
IGHQEX3000 |
C1-10 |
C4 |
7.757 |
9.50 |
0.03 |
TL 401C |
7.774 |
7.7655 |
0.009 |
-0.0650 |
0.818 |
0.003 |
0.953 |
0.003 |
July 26, 2022 |
initial |
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
IGHQEX3000 |
C1-11 |
D1 |
7.826 |
9.66 |
0.01 |
TL 401C |
7.828 |
7.8270 |
0.001 |
-0.0570 |
0.810 |
0.001 |
0.945 |
0.001 |
July 26, 2022 |
initial |
IGHQEX3000 |
C1-12 |
D2 |
7.841 |
9.51 |
0.02 |
TL 401C |
7.841 |
7.8410 |
0.000 |
-0.0410 |
0.825 |
0.002 |
0.961 |
0.002 |
July 26, 2022 |
initial |
IGHQEX3000 |
C1-14 |
D3 |
7.769 |
9.55 |
0.01 |
TL 401C |
7.789 |
7.7790 |
0.010 |
-0.0520 |
0.815 |
0.001 |
0.950 |
0.002 |
July 26, 2022 |
initial |
|
3
|
Wed Jun 20 00:10:53 2012 |
Koji | Facility | General | Hole on the wall was patched |

|
38
|
Thu Nov 8 20:12:10 2012 |
Koji | Optics | Configuration | How many glass components we need for a plate |
Optical prisms 50pcs (A14+B12+C6+E18)
Curved Mirrors 25pcs (C13+D12)
|
Qty |
Prisms
|
Curved |
No BS OMC |
Wedge tested |
Coating A: IO coupler |
|
14 |
0 |
2 prisms |
5/5 |
Coating B: BS 45deg |
|
12 |
0 |
2 prisms |
0/5 |
Coating C: HR |
|
6 |
13 |
2 curved |
|
Coating D: Asym. output coupler |
|
0 |
12 |
- |
|
Coating E: HR 45deg |
|
18 |
0 |
4 prism (1 trans + 3 refl) |
0/3 |
D1102209 Wire Mount Bracket |
25 |
|
|
4 |
|
D1102211 PD Mount Bracket |
30 |
|
|
8 |
|
|
37
|
Thu Nov 8 19:52:57 2012 |
Koji | Optics | General | How to apply UV epoxy |
KA's question:
Do you know how to apply this epoxy?
Do we need a plunger and a needle for this purpose?
Nic saids:
When we did it with Sam, I seem to remember just squirting some on some foil then dabbing it on with the needle. |
160
|
Thu Aug 29 18:55:36 2013 |
Koji | Mechanics | General | I1 OMC top side gluing (UV) |
The glass components for the I1 OMC top side were glued by the UV glue.
Breadboard SN#4
Wire bracket SN#5/6/7/8 |
206
|
Fri Jul 11 00:06:33 2014 |
Koji | Optics | Characterization | I1OMC PD |
DCPD# DCPD1 DCPD2
Housing# #009 #010
Diode# #07 #10
Shim 1.00mm 01 1.00mm 02 (1.00mm = D1201467-09)
-------------------------------------
Power Incident 11.1 mW 10.6 mW
Vout 7.65 V 7.33 V
Responsivity[A/W] 0.69 0.69
Q.E. 0.80 0.81
-------------------------------------
photo 2nd 1st
PD alignment confirmation
|
205
|
Thu Jul 10 23:22:28 2014 |
Koji | Optics | Characterization | I1OMC QPD |
QPD# QPD1 QPD2
Housing# #006 #007
Diode# #50 #51
Shim 1.25mm 03 1.25mm 02 (1.25mm = D1201467-10)
-------------------------------------
Power Incident 123.1-13.0 uW 124.5-8.0 uW
Sum Out 77.0 mV 82.5 mV
Vertical Out -24.0 mV - 8.8 mV
Horizontal Out 4.2 mV 9.0 mV
SEG1 -11.6 mV -16.0 mV
SEG2 -12.6 mV -18.0 mV
SEG3 -25.2 mV -24.4 mV
SEG4 -21.4 mV -21.4 mV
-------------------------------------
Spot position X -21 um -19 um (positive = more power on SEG1 and SEG4)
Spot position Y +102 um +47 um (positive = more power on SEG3 and SEG4)
-------------------------------------
Responsivity[A/W] 0.70 0.71
Q.E. 0.82 0.83
-------------------------------------
Arrangement of the segments
View from the beam
/ 2 | 1 X
|---+---|
\ 3 | 4 /
---------------
I(w,x,y) = Exp[-2 (x^2 + y^2)/w^2]/(Pi w^2/2)
(SEG_A+SEG_B-SEG_C-SEG_D)/(SEG_A+SEG_B+SEG_C+SEG_D) = Erf[sqrt(2) d/w]
d: distance of the spot from the center
w: beam width
|