ID |
Date |
Author |
Type |
Category |
Subject |
113
|
Tue Apr 16 09:43:58 2013 |
Koji | Optics | Configuration | Mirror list for L1OMC |
L1 OMC
Cavity Mirrors
FM1 (input coupler): A8
FM2 (output coupler): A7
CM1 (curved mirror close to FM1): C6
CM2 (curved mirror close to FM2): C5
DCPD path
BS3 (BS for DCPDs): B5 B7
QPD path
BS1 (input steering): E10
SM1 (steering mirror next to BS1): E12
BS2 (BS for QPD path): B3
SM2 (steering mirror next to BS2): E4
SM3 (steering mirror next to SM2): E16

|
114
|
Tue Apr 16 23:26:51 2013 |
Koji | Optics | Characterization | Further More Mirror T measurement |
Since the previous measurement showed too high loss, the optical setup was checked.
It seemed that a PBS right before the T&R measurement setup was creating a lot of scattering (halo) visible with a sensor card.
This PBS was placed to confirm the output polarization from the fiber, so it was ok to remove it.
After the removal, the R&T measurement was redone.
This time the loss distributed from 0.2% to 0.8% except for the one with 1.3%. Basically 0.25% is the quantization unit due to the lack of resolution.
At least B7, B10, B12 seems the good candidate for the DCPD BS.
The AR reflection was also measured. There was a strong halo from the main reflection with an iris and sense the power at ~.5mm distance to separate the AR reflection from anything else. Now they are all somewhat realistic. I'll elog the measurement tonight.
33.6 +/- 0.2 uW out of 39.10+/-0.05 mW was observed. The offset was -0.236uW.
This gives us the AR reflectivity of 865+/-5ppm . This meets the spec R<0.1%
Mirror | P_Incident P_Trans P_Refl | T R loss |
| [mW] [mW] [mW] | |
---------------------------------------------------------------------------------------------
B1 | 39.10+/-0.05 19.65+/-0.05 19.25+/-0.05 | 0.503+/-0.001 0.492+/-0.001 0.005+/-0.002 |
B2 | 39.80+/-0.05 19.90+/-0.05 19.70+/-0.05 | 0.500+/-0.001 0.495+/-0.001 0.005+/-0.002 |
B4 | 39.50+/-0.05 19.70+/-0.05 19.30+/-0.05 | 0.499+/-0.001 0.489+/-0.001 0.013+/-0.002 |
B5 | 39.50+/-0.05 19.70+/-0.05 19.50+/-0.05 | 0.499+/-0.001 0.494+/-0.001 0.008+/-0.002 |
B6 | 39.55+/-0.05 19.50+/-0.05 19.95+/-0.05 | 0.493+/-0.001 0.504+/-0.001 0.003+/-0.002 |
B7 | 40.10+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.494+/-0.001 0.504+/-0.001 0.002+/-0.002 |
B8 | 40.15+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.493+/-0.001 0.503+/-0.001 0.004+/-0.002 |
B9 | 40.10+/-0.05 19.90+/-0.05 19.90+/-0.05 | 0.496+/-0.001 0.496+/-0.001 0.008+/-0.002 |
B10 | 40.10+/-0.05 19.70+/-0.05 20.30+/-0.05 | 0.491+/-0.001 0.506+/-0.001 0.002+/-0.002 |
B11 | 40.20+/-0.05 19.80+/-0.05 20.20+/-0.05 | 0.493+/-0.001 0.502+/-0.001 0.005+/-0.002 |
B12 | 40.20+/-0.05 19.90+/-0.05 20.20+/-0.05 | 0.495+/-0.001 0.502+/-0.001 0.002+/-0.002 |
---------------------------------------------------------------------------------------------
|
115
|
Wed Apr 17 07:30:04 2013 |
Koji | Optics | General | QPD path glued |
Yesterday, all of the glass components for the QPD path were glued.
- Check the alignment of the beam with the cavity.
- Placed the prisms
- Placed the QPD mount for the gluing test. An alignment disk instead of a diode was placed on the mount.
- Checked the spot positions at the QPDs. A CCD camera with a lens was used to find the spot.
The spots were ~0.5mm lower on the QPD1, and ~1mm lower on the QPD2.
- Glued the first steering mirror while the spot position was continuously monitored.
- Glued the BS in the QPD path while the spot position was monitored.
- FInally a glass bracket was glued.
- The spot on QPD2 was too low to absorb by the QPD shim.
- Once the steering mirror was clamped by a cantilever spring (to prevent slipping), the spot moved up a bit.
(Or, we should say, the cantilever misaligned the optics a bit in pitch in a preferrable direction.)
- The other steering mirror is clamped by a cantilever spring (to prevent slipping), the spot moved up a bit.
Or, we should say, the cantilever misaligned the optics a bit in pitch in a preferrable direction.)
- The last steering mirrors was also glued in a same way. As a result the spot is 0.5mm below the center of the alignment disk.
- Once the PD mounting brackets were glued, we can't place the QPD mount on it as the PEEK bar can't be inserted without moving the gluing template.
- The QPD mount with out the glass bracket was used to check the alignment of the beam dumps.
As the beam dumps have a wide aperture and the yaw alignment of the QPD is big, we could accommodate the beams in the dumps easily.
- The dumps were glued. |
116
|
Thu Apr 18 11:43:59 2013 |
Koji | General | General | Mounting Glass Bracket Failure |
[Jeff, Koji]
- While we were working on the optics alignment, one of the mounting brackets made of glass god tore apart into two when a holding screw was removed.
The glass component had a crack at the very middle of the part.
- We borrowed a setup for photoelastisity measurement from Garilynn. This is a set of polarizer configured to have cross polarization. If there is no photoerastisity
the image is colored in blue (somehow). When the polarization is rotated, the color is changed in red, yellow, or white.
- The cross polarizer was tested with a polycarbonate face shield for the UV protection. It seems doing its job.
- We took a set of photos to see any residual stress in a block. The entire inside of the channel is frosted glass so the technique didn't yield much.
In one orientation we did see stress near the ends but the orientation didn't allow us to see exactly where.
- We had 30 brackets and one OMC requires ten of them. This means that there was no spare and now we don't have enough.
So we decided to spend more as test pieces.
- We tested three scenarios this afternoon. In all three cases both screws were snugged (estimate 0.5 in*lb) before torquing by a torque wrench with a dial meter.
The divisions on the dial of the wrench are 1 in*lb. We were not so confident in the exact measurement but we felt good about the repeatability of the values.
1. Duplicated the original mounting with the chamfers of the PEEK bar facing into the channel. Cracked as the torque wrench read 1 in*lb.
Crack initiation at the first screw, starting along the longitudinal centerline.
2. Turned the nut bar over so the flat side faced into the channel. Successfully torqued both screws to 1 in*lb and removed them.
3. With a razor blade, made fairly large reliefs (countersinks) around the holes in the PEEK. Successfully torqued both screws first to 1 in*lb then 1.5 in*lb.
The block did crack (again at the screw along the centerline) when the torque was ~1.9 in*lb.
It occurs to us that we need micro-compliance AND structural rigidity to distribute the load. The PEEK bars are small and particularly thin where the #4-40 helicoil holes are.
The load is probably concentrated way too much at the holes because it is too weak. Perhaps a good solution, among others, would be to use an aluminum nut plate
with a thin (.02") kapton or viton layer to give the micro-compliance. Additionally, a kapton layer could be used between the block and the aluminum shim,
though this one is probably to be avoided so as to ensure rigidity of the bolted assembly to the bench. Lastly, the nut bar should be shaped such that the area
around the holes and the end of the channel (pretty much the same area) are less stressed than the center portion.
After the discussion with Peter and Dennis, we decided to reinforce the bonded glass piece with invar shims.
Each shim will be threaded such that we don't need to stress the glass piece any more. EP30-2 will be used as the glue.
|
118
|
Thu Apr 18 11:59:02 2013 |
Koji | General | General | DCPD path gluing |
[Jeff, Koji]
DCPD path gluing
Usual preparation
- Locked the cavity.
- Aligned the input beam to the cavity
DCPD BS gluing
- Placed the DCPD BS on the breadboard
- Placed the dummy DCPD mount on the reflection side of the BS. Check the height and position of the spot.
- Placed the dummy DCPD mount on the transmission side of the BS. Check the height and position of the spot.
- The spot positions looked fine.
- Added a dub of UV glue on the BS. Placed it along the fixture.
- Checked the reflection spot again with the CCD. Kept monitored the spot position through out the gluing process
of the BS.
- Blasted the UV illumination
Reflection side beam dump gluing
- Replaced the alignment disk of the dummy DCPD with a photodiode with the cap removed.
- Put the dummy DCPD mount and the beam dump in place
- Checked the reflection spot from the diode on the beam dump. It looked fine.
- Applied 2~3 dubs of the glue on the beam dump. Slid in the dump to the fixture.
- Applied UV illumination. As the beam dump shadows the illumination 3 times of 10sec blasts were applied.
Transmission side beam dump gluing
- Put the dummy DCPD mount with the diode in place
- Put the beam dump in place. The template needed to be lifted up a bit to accomplish this action.
This should be fixed by the modification of the template.
- Checked the transmission spot on the diode and the spot reflected from the diode on the beam dump.
- Actually the spot was too much close to the vertex of the "V" on the beam dump. We determined that
this was mainly caused by the misalignment of the diode element, and can be compensated by the tilt of the diode mount.
- Removed the beam dump from the template once. Applied 2~3 dubs of the glue on the beam dump.
Slid in the dump to the fixture by lifting up the template again.
- Applied UV illumination. As the beam dump shadows the illumination 3 times of 10sec blasts were applied.
Mounting bracket gluing
- Glued the mounting brackets for the DCPD mounts based on the positions specified by the template.
Removing the templates
- Removed the connection bars between the two templates.
- Removed the template at the QPD side. The screws at all of the three sides were needed to be released in order to accomplish this action.
Once the screws are released, the template was slid on the breadboard so that the pads did not scratch the optical surface.
Keep one side of the template use as a pivot, lifted up another side until the pads clear the optic. Then lifted up the other side.
- Removed the other template. This time, the screws at the two DCPD sides are released. The template was slid and lifted in a same way.
Last beam dump gluing
- Once the QPD side template was removed, the last beam dump at the transmission side of the first steering mirror was glued.
- This has been done without any gluing fixture, we held the beam dump with clean Allen keys on the breadboard.
- The paths for the main and stray beams were confirmed by an IR sensor card, and blasted the UV.
Closing the transport fixture
- Removed the constraining pins for the breadboard.
- Made sure all of the constraining pins/screws are released for the other side of the transport fixture were released.
- Put the lid on.
- Fastened the constraining pins/screws of the transport fixture.
- Wrapped the fixture with sheets of the Al foil.
- Pack the fixture in anti-static bags.
|
119
|
Fri May 3 21:09:08 2013 |
Koji | General | General | OMC is back |
L1 OMC is back on the table for the action next week. |
120
|
Mon May 6 19:31:51 2013 |
Koji | Optics | Characterization | Spot position measurement on the diode mounts |
Measurement Order: DCPD2->DCPD1->QPD1->QPD2
DCPD1: 1.50mm+0.085mm => Beam 0.027mm too low
DCPD2: 1.75mm+0.085mm => Beam 0.051mm too high (...less confident)
QPD1: 1.25mm+0.085mm => Beam 0.077mm too low
QPD2: 1.25mm+0.085mm => Beam 0.134mm too low
or 1.00mm+0.085mm => Beam 0.116mm too high
|
121
|
Wed May 8 15:08:57 2013 |
Koji | Optics | Characterization | Spot position measurement on the diode mounts |
Remeasured the spot positions:
DCPD1: 1.50mm+0.085mm => Beam 0.084mm too high
DCPD2: 1.50mm+0.085mm => Beam 0.023mm too high
QPD1: 1.25mm+0.085mm => Beam 0.001mm too low
QPD2: 1.25mm+0.085mm => Beam 0.155mm too low
|
122
|
Wed May 8 15:36:50 2013 |
Koji | General | General | Latest OMC schedule |
May
(done) Mon 6th: Invar plate arrival / Spot position measurement
(done) Tue 7th: Invar plate cleaning / Spot position measurement / EP30-2 arrival / Invar plate gluing to the test mounting brackets
(done) Wed 8th: Invar plate cleaning done / Baking of the test pieces (with Bob's oven)
Thu 9th: ***After bake torque/force test***
***If the invar plate passes the test***
Thu 9th Light side invar plate gluing
Fri 10th Cable side invar plate gluing
Mon 13th The OMC given to Bob (Air bake & Vac bake)
Mon 20th The OMC received from Bob
Apply First contact
Diode mount adjustment / Electronic tests
Tue 21st Diode mount adjustment / Electronic tests / Optical tests
Wed 22nd Final cabling (***Chub***)
Thu 23rd Final cabling / Packing
Fri 24th Packing / Shipping
Mon 27th? Arrival to LLO / Koji fly to LLO
Tue 28th Test on the optical bench
Wed 29th Test on the optical bench
Thu 30th Suspension test? (***Jeff B***)
June
Tue 4th Suspension test done? |
123
|
Fri May 10 09:33:22 2013 |
Koji | Supply | General | COMSOL simulation on the glass bracket stress |

|
124
|
Mon May 13 14:49:35 2013 |
Koji | Mechanics | Characterization | Mounting Glass Bracket still broke with tightenin stress |
[Koji / Jeff]
This is the elog about the work on May 9th.
We made two glass brackets glue on the junk 2" mirrors with the UV glue a while ago when we used the UV bonding last time.
On May 7th:
We applied EP30-2 to the glass brackets and glued invar shims on them. These test pieces were left untouched for the night
and brought to Bob for heat curing at 94degC for two hours.
On May 9th:
We received the test pieces from Bob.
First, a DCPD mount was attached on one of the test pieces. The fasteners were screwed at the torque of 4 inch lb.
It looked very sturdy and Jeff applied lateral force to break it. It got broken at once side of the bracket.
We also attached the DCPD mount to the other piece. This time we heard cracking sound at 2 inch lb.
We found that the bracket got cracked at around the holes. As the glass is not directly stressed by the screws
we don't understand the mechanism of the failure.
After talking to PeterF and Dennis, we decided to continue to follow the original plan: glue the invar shims to the brackets.
We need to limit the fastening torque to 2 inch lb.
|
125
|
Mon May 13 14:59:16 2013 |
Koji | Mechanics | General | Invar shim gluing |
The invar reinforcement shims were glued on the glass brackets on the breadboard.
We worked on the light side on May 10th and did on the dark side on May 13rd.
U-shaped holding pieces are used to prevent each invar shim to be slipped from the right place.
We are going to bring the OMC breadboard to the bake oven tomorrow to cure the epoxies and promote the outgasing.
|
126
|
Mon May 13 15:00:23 2013 |
Koji | General | General | Current most reliable OMC schedule |
May
Tue 14th The OMC given to Bob (Air bake & Vac bake)
Mon 20th The OMC received from Bob
Apply First contact
Diode mount adjustment / Electronic tests
Tue 21st Diode mount adjustment / Electronic tests / Optical tests
Wed 22nd Final cabling (***Chub***)
Thu 23rd Final cabling / Packing
Fri 24th Packing / Shipping
Mon 27th? Arrival to LLO / Koji fly to LLO
Tue 28th Test on the optical bench
Wed 29th Test on the optical bench
Thu 30th Suspension test? (***Jeff B***)
June
Tue 4th Suspension test done? |
127
|
Tue May 14 19:06:00 2013 |
Koji | Clean | General | OMC Baking |
The OMC is in the air bake oven now.
|
128
|
Mon May 20 14:59:21 2013 |
Koji | General | General | OMC is out from the oven |
The OMC came back to the table again.
No obvious change is visible: no crack, no delamination
The OMC was fixed on the table and the beam was aligned to the cavity |
129
|
Tue May 21 18:28:08 2013 |
Koji | General | General | Current most reliable OMC schedule |
- The wrong Mighty Mouse connectors for the PZT wires were prepared. The correct ones are in the vacuum oven till Tuesday morning.
- The thread holes for the cable pegs are 1/4-20 rather than 10-24. This requires re-machining of the cable pegs & the C&B.
- We are waiting for the fast shipment of the from LHO
May
Thu 23rd Diode mount adjustment / Optical tests
Fri 24th Optical tests
Tue 28th Mighty mouse connector available / Diode mounting finalization
Wed 29th final check
Thu 30th shipment
Fri 31th
June
Mon 3rd ? Arrival to LLO / Koji fly to LLO
Tue 4th Suspension test done? |
130
|
Thu May 23 23:41:48 2013 |
Koji | Mechanics | General | DCPD/QPD Mount |
DCPD mounts and QPD mounts were attached on the breadboard. They are not aligned yet and loosely fastened.
DCPD (mounting 4-40x5/16 BHCS Qty4)
Face plates fatsened by 4-40x5/16 BHCS (24 out of 40)
Housing Face plate Destination PD
002 002 L1OMC DCPD1 #10
003 003 L1OMC DCPD2 #11
004 004 H1OMC DCPD1
008
005 H1OMC DCPD2
009
006 I1OMC DCPD1
010
007 I1OMC DCPD2
QPD (mounting 4-40x5/16 BHCS Qty4)
Face plates fatsened by 4-40x1/4 BHCS (24 out of 80)
Housing Face plate Destination QPD
002 002 L1OMC QPD1 #38 #43 swapped on 29th May.
003 003 L1OMC QPD2 #43 #38
swapped on 29th May.
004
004
H1OMC QPD1
005
005
H1OMC QPD2
006
006
I1OMC QPD1
007
007 I1OMC QPD2
* 4-40x5/16 BHCS Qty 8 left
* 4-40x5/16 BHCS Qty 56 left
Cut the diode legs by 3mm
|
131
|
Thu May 30 14:38:42 2013 |
Koji | Electronics | General | Cable fitting |
Yesterday Jeff and Chub worked on the cabling of the OMC. It turned out that the gender of the cable connectors
going from the cavity side to the connector bracket on top of the OMC were opposite from what is needed.
This way, the connectors can't fixed on the cable harness, thus they are free during the shipping.
We considered several ideas to mitigate this issue and decided to swap the gender of the Mighty Mouse connectors.
In order to check this operation may cause the shortage of the cable length, we made the fitting of the cables.
They seem all long enough for Chub to replace the Mighty Mouse connectors with the proper gender.
We also checked the polarity of the PZT wires. We marked the positive side of the PZT by a knot at the wire end.
|
132
|
Thu May 30 15:00:28 2013 |
Koji | Optics | General | QPD alignment |
The QPD alignment was adjusted using the aligned beam to the cavity and the 4ch transimpedance amplifier.
As I have a test cable for the QPD, I attached a DB9 connector on it so that I can use the QPD transimpedance
amplifier to read the photocurrent. The transimpedance of the circuit is 1kV/A.
As this board (D1001974) does not have X/Y/SUM output, I quickly made the summing circuit on a universal
board I took from Japan a while ago.
The spot on the QPD1 (shorter arm side) seems too low by ~0.64mm. It seems that the QPD is linearly responding
to the input misalignment, so there is no optical or electrical problem.
As I wonder how much I can improve the situation by replacing the diodes, I swapped the diodes between QPD1 and QPD2.
Now QPD1 and QPD2 have the diode #43 and #38, respectively. It improved the situation a llitle (about 60um).
But the beam is still 0.58mm too low. 95% of the power is on the upper two elements.
Of course this is at the edge of the linear range.
I confirmed we still can observe the cavity is fringing even with the beam is aligned on this QPD. So this may be
sufficient for the initial alignment.
The QPD2 was in a better situation. The spot is about 100um too low but this is still well with in the linear range.
The incident powers on the diodes were also measured. The estimated responsivities and Q.E.s are listed below.
The reflection from the diode is adjusted to hit the beam dump properly.
Here are the raw numbers
QPD# QPD1 QPD2
Diode# #43 #38
-------------------------------------
Power Incident 118.8 uW 115.7uW
Sum Out 78.8 mV 84.6 mV
Vertical Out 69.1 mV 11.9 mV
Horizontal Out 9.8 mV -1.6 mV
SEG1 -1.90 mV -17.8 mV
SEG2 -2.18 mV -17.5 mV
SEG3 -32.0 mV -25.3 mV
SEG4 -42.0 mV -23.8 mV
-------------------------------------
Responsivity[A/W] 0.66 0.73
Q.E. 0.77 0.85
-------------------------------------
Arrangement of the segments
View from the beam
/ 2 | 1 X
|---+---|
\ 3 | 4 /
|
133
|
Fri May 31 05:46:54 2013 |
Koji | Optics | General | QPD alignment |
Peter F suggested to check the bottom surface of the PD housings if there is any protrusion/interference/whatever.
And that was true! It was found that the front side of QPD1 (Left) was lifted by a machining burr.
It seems that this burr consistently exists as the other one also have it (see QPD2 picture (right)) although it is not too terrible compared to the one in QPD1.

Once these burrs were removed, the spots were found on the right position of each diode.
From the measurement of the power on each segment, the positions of the spots were estimated. (listed in the table)
They indicate that the spots are within 0.1mm from the center. This is good enough.
The quantum efficiency was measured from the incident power and the sum output. It seems that there are
some difference between the diodes. The numbers are consistent with the measurement the other day.
QPD# QPD1 QPD2
Diode# #43 #38
-------------------------------------
Power Incident 84.7 uW 86.2 uW
Sum Out 56 mV 61 mV
Vertical Out -6.8 mV 10 mV
Horizontal Out 4.2 mV 8.8 mV
SEG1 -17 mV -15 mV
SEG2 -14.5 mV -11 mV
SEG3 -11 mV -15 mV
SEG4 -13 mV -20 mV
-------------------------------------
Spot position X +25 um +46 um (positive = more power on SEG1 and SEG4)
Spot position Y -42 um +46 um (positive = more power on SEG3 and SEG4)
-------------------------------------
Responsivity[A/W] 0.66 0.71
Q.E. 0.77 0.82
-------------------------------------
Arrangement of the segments
View from the beam
/ 2 | 1 X
|---+---|
\ 3 | 4 /
---------------
I(w,x,y) = Exp[-2 (x^2 + y^2)/w^2]/(Pi w^2/2)
(SEG_A+SEG_B-SEG_C-SEG_D)/(SEG_A+SEG_B+SEG_C+SEG_D) = Erf[sqrt(2) d/w]
d: distance of the spot from the center
w: beam width
|
134
|
Fri May 31 14:07:54 2013 |
Koji | Optics | Characterization | Transverse Mode Spacing measurement afte the baking |
Measurement for pitch
Free Spectral Range (FSR): 264.9703 +/− 0.0007 MHz
Cavity roundtrip length: 1.131419 +/− 0.000003 m
Transverse mode spacing (TMS): 57.9396 +/− 0.0002 MHz
TMS/FSR: 0.218664 +/− 0.000001
Assuming the line width of the cavity 1/400 of the FSR...
- the 9th modes of the carrier is 12.8 line width (LW) away from the carrier resonance
- the 13th modes of the lower f2 sideband are 5.7 LW away
- the 19th modes of the upper f2 sideband are -6.8 LW away
Measurement for yaw
Free Spectral Range (FSR): 264.9696 +/− 0.0004 MHz
Cavity roundtrip length: 1.131422 +/− 0.000002 m
Transverse mode spacing (TMS): 58.0479 +/− 0.0002 MHz
TMS/FSR: 0.219074 +/− 0.000001
- the 9th modes of the carrier is 11.3 line width (LW) away from the carrier resonance
- the 13th modes of the lower f2 sideband are 7.8 LW away
- the 19th modes of the upper f2 sideband are -3.7 LW away
The followings are the previous values before the bake
[from this entry]
- After everything was finished, more detailed measurement has been done.
- FSR&TMS (final)
FSR: 264.963MHz => 1.13145m
TMS(V): 58.0177MHz => gamma_V = 0.218966
TMS(H): 58.0857MHz => gamma_H = 0.219221
the 9th modes of the carrier is 10.8~11.7 LW away
the 13th modes of the lower f2 sideband are 7.3~8.6 LW away
the 19th modes of the upper f2 sideband are 2.6~4.5 LW away |
135
|
Mon Jun 3 18:58:08 2013 |
Koji | Optics | Configuration | OMC final tests |
- QPD mount aligned, QPD output checked
The spots are with 100um from the center of the diodes. [ELOG Entry (2nd photo)]
- TMS/FSR dependence on the PZT V
Shows significant dependence on the PZT voltages
It seems that the curvartures get longer when the voltages are applied to the PZTs.
The effect on these two PZTs are very similar. The dependence is something like
(TMS/FSR) ~ 0.219 - 1e-5 V
May cause resonance of the higher-order modes (like 13th order of the 45MHz sidebands) at a specific range of the PZTs.
We can't change anything any more, but the impact needs to be assessed
- DC response of the PZTs [ELOG Entry]
PZT voltages were swept. Observed multiple fringes during the sweep.
The data to be analyzed.
- AC response of the PZTs [ELOG Entry]
PZT1 and PZT2 well matched. The first resonance at 10kHz.
- Open loop TF of the servo
The UGF more than ~30kHz.
- Cleaning of the main optics with First Contact
Done. Visible scattering seen with an IR was reduced, but still exist.
All four cavity mirrors have about the same level of scattering.
Each scattering is a group of large or small bright spots.
It's actually a bit difficult to resolve the bright spots with the IR viewer.
- Raw transmission: i.e. Ratio between the sum of the DCPD paths and the incident power
May 8th (before the baking): 0.918
May 8th (First Contact applied): 0.940 (improved)
Jun 2nd (after the baking): 0.927 (worse)
Jun 2nd (First Cotact applied): 0.964 (improved)
Date |
2013/6/2 |
2013/6/2 |
2013/6/2 |
Condition |
Before the cleaning |
After the FC cleaning |
After drag wiping |
Input Power [mW] |
39.8 |
38.4 |
38.4 |
REFLPD dark offset [V] |
-0.0080 |
-0.0080 |
-0.0080 |
REFLPD locked [V] |
0.048 |
0.0437 |
0.046 |
REFLPD unlocked [V] |
6.41 |
6.39 |
6.37 |
|
|
|
|
Transmitted Power to DCPD1 (T) [mW] |
18.8 |
18.8 |
18.8 |
Transmitted Power to DCPD2 (R) [mW] |
18.1 |
18.2 |
18.2 |
FM2 transmission [mW] |
- |
- |
- |
CM1 transmission [mW] |
0.200 |
0.193 |
0.198 |
CM2 transmission [mW] |
0.204 |
0.204 |
0.205 |
Input BS transmission [mW] |
0.260 |
0.228 |
0.245 |
|
|
|
|
Cavity Finesse |
396.9 |
403.79 |
403.79 |
|
|
|
|
Junk Light Power (Pjunk) [mW] |
0.303 |
0.302 |
0.317 |
Coupled beam power (Pcouple) [mW] |
39.50 |
38.10 |
38.08 |
Mode Matching (Pcouple/Pin) [mW] |
0.992 |
0.992 |
0.992 |
Cavity reflectivity in power |
0.00112 |
0.000211 |
0.000206 |
Loss per mirror [ppm] |
111 |
35.9 |
34.8 |
Cavity transmission for TEM00 carrier
|
0.934 |
0.971 |
0.972 |
- TMS/FSR/Finesse change before/after cleaning [ELOG Entry]
Just a small change from the parameters before the bake.
No quantitative difference.
Method:
BB EOM produces the AM sidebands together with the PM sidebands.
Ideally, the PM sidebands does not produce the signal at the transmission, the output is dominated by the AM component.
This is only true when there is no lock offset. In reality the curve is contaminated by the PM-AM conversion by the
static offset or dynamic deviation of the locking point. So I had to take the central part of the TF and check the
dependence of the fit region and the finesse.
Before the cleaning: Finesse 396.9
After the cleaning: Finesse 403.8
To Do
- Placement of the DCPD housings
- Through-put test with DCPDs
- Transmission dependence on the incident power
(although the max incident is limited to ~35mW)
- Application of the first contact for the surface protection |
136
|
Mon Jun 3 21:19:03 2013 |
Koji | General | General | Planning |
Monday - Evening
(Koji)
[done] - DCPD alignment
[done] - DCPD test & through-put measurement
[done] - Power dependence test
[done] - Apply Protective First Contact Layer on the optic surfaces
[done] - Wiping the OMC
Tuesday - Morning
(Chub)
[done] - Bring the cable from the oven
Tuesday - Afternoon
(Chub/Jeff)
[done] - Cabling of the OMC
Wednesday - Morning
(Jeff/Koji)
[done] - Cable tying down
[done] - Screw tightening for the PDs
[done] - Wrapping / Packing
[done] - Weighting? (65lb for everything)
(Jeff/George)
[done] - Shipping? (or Wednesday)
Items to be shipped together
v - OMC cables between the cable harness to the suspension
v - 1 PZT cable pin
v - DCPD preamp kit
v - toruqe driver & bits
v - kapton sheet/tube
v - Test PD cables
v - Spare diodes
v - QPD amp circuits (just in case)
v - 1GHz PD / Power supply banana-PD cable / 1GHz PD cables
[done] - Installation scheduling with Peter/Brian/(Mike?)
- Travel plan
[done] Koji goes LLO immediately (possible?) 6/6-6/22
Jeff goes LLO next week?
(Koji)
[done] - Room cleaning
--------------------------
Optical testing plan
Day 0
- Freight and Koji moving
Day 1 Arrival (Thursday or Friday)
- Inspect the shock detector
- Unpacking
- Check the condition of the breadboard
- Place the transportation fixture on the table
- Removing the First Contact layers
- Locking
- Mode matching
Day 2
- Transmission measurement
- Power dependence test
- PD installation / (diode can opening, optional)
- (PD realign, optional)
- diode test
Day 3
- Power dependence test
---------------------------
OMC installation plan
TBD
---------------------------
OMCS installation plan
TBD
---------------------------
Documents
- OMC Hazard analysis (done)
- OMCS Hazard analysis (done)
- OMC instllation procedure
- OMCS instllation procedure
- Work permits
cf. previous documents: E080024, E1300201
---------------------------
---------------------------
Misc
- LIGO access card
controls@lloisc0-work:~$ 2.23-5mW T
2.23-5mW: command not found
controls@lloisc0-work:~$ 2.17 \pm 0.01 R
2.17: command not found
controls@lloisc0-work:~$ 67-68mV inlock
67-68mV: command not found
controls@lloisc0-work:~$ 973mV unlock
973mV: command not found
controls@lloisc0-work:~$ Pin 5.47+-0.014.4
No command 'Pin' found, did you mean:
|
138
|
Wed Jun 5 18:19:51 2013 |
Koji | General | General | Some recent photos from the OMC final test at CIT |
Applying First Contact for the optics cleaning
PD alignment / scattering photos
Cabling
Cabling (final)
|
139
|
Wed Jun 5 18:51:31 2013 |
Koji | General | General | L1 OMC shipped out |
[Koji, Jeff]
The L1 OMC finally sent out from Caltech!
 |
140
|
Fri Jun 7 16:04:44 2013 |
Koji | General | General | [LLO] OMC arrived |
[Koji Zach Suresh]
The OMC arrived at LLO without any destruction!
- We found that one shock sensor on the box turned red, the other stayed white.
- We brought the Perican case to the changing room and the wrapping was opened in the optics lab.
- The OMC was discovered without any obvious damage. Successful shipment!
- The inspection with a halogen light indicated some amount of particules on the breadboard.
The both sides of the breadboard were wiped with the cleanroom cloth.
- The First Contact layers on the optics were removed while the ionized nitrogen gas was brew.
|
141
|
Mon Jun 10 10:04:37 2013 |
Koji | General | General | [LLO] OMC Test |
[Koji Zach]
We worked on the OMC test over the weekend.
- At the beginning, the measured OMC transmission was ~85% even after subtracting the junk light and sidebands from the calculation.
- A pretty visible (by eye) dust were on CM1. Also a small residue of First Contact was found on the same mirror.
- We applied FC only on CM1 to remove these.
- The measued transmission went up to the level of 96%.
- We swept the incident power from 0.3mW to 30mW in order to see the dependence of the transmission against the incident power.
- The variation of the transmission ~10% was observed (attached figure 1, Red). This was compared with the similar dependence measured at Caltech (Magenta)
- So, the reduction of the transmission was observed as in eLIGO, although the measurements at Caltech and LLO are not consistent.
- Can this be attributed to the dependence of the PD efficiency? We measured the incident power on the PDs together with the preamp DC output. (Figure.2)
This gives us how the responsivity changes with the incident power.
- Nevertheless, the dependence remains. We'll make more accurate measurement today. |
142
|
Thu Jun 13 12:04:57 2013 |
Koji | General | General | [LLO] OMC Optical Test - completed |
https://alog.ligo-la.caltech.edu/aLOG/index.php?callRep=7373 |
145
|
Tue Jun 18 10:01:11 2013 |
Koji | Optics | Characterization | Cavity Finesse analysis |
This is the analysis of the cavity finesse data taken on Apr/13/2013 (before baking), May/30/2013 (after baking), and Jun/02/2013 (after cleaning).
If we believe this result, baking contaminated the cavity, and the first contact removed it. That agrees with the power measurement of the transmitted light. |
146
|
Tue Jun 18 15:45:38 2013 |
Koji | General | General | [LLO] OMC installation in HAM6 |
OMC installed in HAM6!
https://alog.ligo-la.caltech.edu/aLOG/index.php?callRep=7486
|
147
|
Fri Jun 28 12:20:49 2013 |
Koji | General | General | Dmass's loan of Thorlabs HV amp |
http://nodus.ligo.caltech.edu:8080/Cryo_Lab/799
(KA: Returned upon H1OMC building) |
148
|
Sat Jul 6 17:10:07 2013 |
Koji | Mechanics | Characterization | PZT Response analysis |
Analysis of the PZT scan / TF data taken on May 31st and Jun 1st.
[DC scan]
Each PZT was shaken with 10Vpp 1Hz triangular voltage to the thorlabs amp.
The amp gain was x15. Abut 4 TEM00 peaks were seen on a sweep between 0 and 10V.
The input voltage where the peaks were seen was marked. Each peak was mapped on the
corresponding fringe among four. Then the each slope (up and down) was fitted by a iiner slope.
Of course, the PZTs show hystersis. Therefore the result is only an approximation.
PZT1: PZT #26, Mirror C6 (CM1)
PZT2: PZT #23, Mirror C5 (CM2)
PZT arrangement [ELOG Entry]
PZT1:
Ramp Up 13.21nm/V
Ramp Down 13.25nm/V
Ramp Up 13.23nm/V
Ramp Down 13.29nm/V
=> 13.24+/-0.02 nm/V
PZT2:
Ramp Up 13.27nm/V
Ramp Down 12.94nm/V
Ramp Up 12.67nm/V
Ramp Down 12.82nm/V
=> 12.9+/-0.1 nm/V
[AC scan]
The OMC cavity was locked with the fast laser actuation. Each PZT was shaken with a FFT analyzer for transfer function measurments.
(No bias voltage was given)
The displacement data was readout from the laser fast feedback. Since the UGF of the control was above 30kHz, the data was
valid at least up to 30kHz. The over all calibration of the each curve was adjusted so that it agrees with the DC response of the PZTs (as shown above).
The response is pretty similar for these two PZTs. The first series resonance is seen at 10kHz. It is fairly high Q (~30). |
149
|
Fri Aug 9 10:09:56 2013 |
Koji | General | General | PZT Assembly #3/#4 |
Yesterday, Jeff and I bonded the PZT assemblies (#3/#4).
The attached is the arrangement of the components |
150
|
Mon Aug 12 20:22:19 2013 |
Koji | General | General | PZT Assembly #5/#6 |
PZT Assembly #5/#6 were glued on Fri Aug 9th
They are removed from the fixture on Mon Aug 12th.
All of the four PZT assemblies were moved to the OMC lab. |
151
|
Fri Aug 16 15:31:17 2013 |
Koji | Optics | Configuration | Mirror list for OMC(002) |
OMC(002)
Cavity Mirrors
FM1 (input coupler): A9
FM2 (output coupler): A13
CM1 (curved mirror close to FM1): C9 (PZT ASSY #6 / M6 /PZT21/C9)
CM2 (curved mirror close to FM2): C4 (PZT ASSY #4 / M11/PZT25/C4)
DCPD path
BS3 (BS for DCPDs): B10
QPD path
BS1 (input steering): E3
SM1 (steering mirror next to BS1): E5
BS2 (BS for QPD path): B9
SM2 (steering mirror next to BS2): E1
SM3 (steering mirror next to SM2): E2

|
152
|
Fri Aug 16 16:36:19 2013 |
Koji | Optics | General | Optics List |
Link to the "Mirror/PZT Characterization links"
Breadboard
BB1 OMC(001) OMC
BB2 OMC(002) OMC
BB3 -
BB4 OMC(003) OMC
BB5 -
BB6 -
Mounting Prisms:
M01
M02
M06 OMC(002) CM1 (PZT ASSY #6)
M07
M10 OMC(003) CM1 (PZT ASSY #5)
M11 OMC(002) CM2 (PZT ASSY #4)
M12
M13 OMC(003) CM2 (PZT ASSY #3)
M14
M15
M16 OMC(001) CM1 (PZT ASSY #1)
M17
M20 OMC(001) CM2 (PZT ASSY #2)
M21
M22
Mirror A:
A1 fOMC FM1
A2 Fullerton for the scattering measurement
A3 fOMC FM2
A4
A5
A6 OMC(003) FM2
A7 OMC(001) FM2
A8 OMC(001) FM1
A9 OMC(002) FM1
A10
A11
A12 OMC(003) FM1
A13 OMC(002) FM2
A14
Mirror B:
B1
B2
B3 OMC(001) BS2 (QPD)
B4
B5 OMC(003) BS2 (QPD)
B6
B7 OMC(001) BS3 (DCPD)
B8
B9 OMC(002) BS2 (QPD)
B10 OMC(002) BS3 (DCPD)
B11
B12 OMC(003) BS3 (DCPD)
Mirror C:
C1 OMC(003) CM1 (PZT ASSY #5)
C2 Fullerton for the scattering measurement
C3 OMC(003) CM2 (PZT ASSY #3)
C4 OMC(002) CM2 (PZT ASSY #4)
C5 OMC(001) CM2 (PZT ASSY #2)
C6 OMC(001)
CM1 (PZT ASSY #1)
C7 fOMC CM1
C8 fOMC CM2 -> OMC(002) CM1 (PZT ASSY #6)
C9 OMC(002) CM1 (PZT ASSY #6) -> BURNT
C10 (Liyuan tested)
C11 (Liyuan tested)
C12 curvature untested, faux OMC CM2
C13 curvature untested
Mirror E:
E1 OMC(002) SM2
E2 OMC(002) SM3
E3 OMC(002) BS1
E4 OMC(001) SM2
E5 OMC(002) SM1
E6
E7 OMC(003) BS1
E8 OMC(003) SM1
E9
E10 OMC(001) BS1
E11
E12 OMC(001) SM1
E13 OMC(003) SM2
E14
E15
E16 OMC(001) SM3
E17 OMC(003) SM3
E18
PZT:
PZT11
PZT12
PZT13
PZT14 OMC(003) CM1 (PZT ASSY #5)
PZT15 OMC(003) CM2 (PZT ASSY #3)
PZT21 OMC(002) CM1 (PZT ASSY #6)
PZT22
PZT23 OMC(001) CM2 (PZT ASSY #2)
PZT24
PZT25 OMC(002) CM2 (PZT ASSY #4)
PZT26 OMC(001) CM1 (PZT ASSY #1)
|
153
|
Fri Aug 16 17:21:38 2013 |
Koji | General | General | [OMC002] Build started |
[Jeff Koji]
The breadboard (SN2) was loaded on the transportation fixture.
The laser side template was installed and the cavity mirrors were placed.
The laser beam will be resonated in the cavity next week. |
154
|
Wed Aug 21 08:31:21 2013 |
Koji | Optics | Characterization | H1 OMC cavity alignment |
Alignment of the H1 OMC cavity mirrors
- The cavity mirrors as well as the first steering mirror were aligned on the cavity side template.
- The locking of the cavity was not so stable as before. Some high freq (several hundreds Hz) disturbance makes the cavity
deviate from the linear range. This can be mitigated by turning off the HEPA units but this is not an ideal condition.
- FSR and TMS were measured.
FSR: 264.305MHz
TMS(V): 58.057MHz
TMS(H): 58.275MHz
These suggest the cavity length L and f_TMS/f_FSR (say gamma, = gouy phase / (2 pi) ) as
L=1.1343 m (1.132m nominal)
gamma_V = 0.219659 (0.21879 nominal)
gamma_H = 0.220484 (0.21939 nominal)
- the 9th modes of the carrier is away from the resonance 6-9 times of the line width (LW)
- the 13th modes of the lower f2 sideband are 11-15 LW away
- the 19th modes of the upper f2 sideband are 0.6-7 LW away
We still need precise adjustment of the gouy phase / cavity length, this was enough for the gluing of the flat mirrors |
155
|
Thu Aug 22 15:34:03 2013 |
Koji | Optics | General | OMC Cavity side gluing |
[Koji Jeff]
o BS1, FM1, FM2 prisms were glued
=> This fixed the unstability of the OMC locking
o Checked the spot position on the curved mirrors.
The height of the template was measured to be 6.16mm.
Using a sensor card, the heights of the spots on the curved mirrors were measured to be 7.4mm (CM1) and 7.9mm (CM2).
This means that the beam is ~1.5mm too low.
When the post clamps were applied to the PZT assemblies, the spot positions moved up a little bit (7.9mm - CM1, 8.2mm - CM2).
This is still ~1mm too low.
We can accommodate this level of shift by the curved mirror and the prisms.
We'll try other PZT assemblies to see if we can raise the beam height. |
156
|
Thu Aug 22 15:40:15 2013 |
Koji | Electronics | Configuration | PZT endurance test |
[Koji, Jeff]
Background
In response to the failure of one of the PZTs on L1OMC (LLO:8366), we have been taking place an endurance test of
the four PZT sub-assemblies in prior to their being glued on the glass breadboard.
According to the technical note by Noliac, the common mode of PZT failure is degradation of the impedance
due to cyclic actuation (like 10^7 times) with over voltage. Therefore our procedure of the test to actuate the PZTs
at least 10^7 times with half voltage of the nominal operating voltage (i.e. nominal 200V) and check the degradation
of the impedance.
Driving signal
For the driving of the PZT, a thorlabs HV amp is used. A source signal of 3.5Vpp with an offset of 1.7V is produced
by DS345 function generator. This signal turns to a sinusoidal signal between 0 and 100V in conjunction with the gain
of 15 at the HV amp.
The maximum driving frequency is determined by the current supply limit of the HV amp (60mA). The capacitance
of each PZT is 0.47uF. If we decide to cycle the signal for 4 PZTs in parallel, the maximum frequency achievable
without inducing voltage drop is 100Hz. This yields the test period of 28hours in order to achive 10^7 cycles.

Initial impedance diagnosis
To check the initial state of the PZTs, a DC voltage of 100V was applied via 1kOhm output resistance.
(Note that this output resistance is used only for the impedance test.)
For each PZTs, both side of the resister showed 99.1V for all measurement by a digital multimeter.
Assuming the minimum resolution (0.1V) of the multimeter, the resistance of each PZT was more than 1MOhm before
the cycling test.
Failure detection
In order to detect any impedance drop of the PZTs, the driving signal is monitored on the oscilloscope via a 1:10 probe.
If there is any significant impedance drop, the driver can't provide the driving current correctly. This can be found
by the deviation of the driving voltage from the reference trace on the oscilloscope (below).

Temperature rise
Because of the loss angle of the PZT capacitance, heating of the PZTs is expected. In order to check the temperature rise,
an IR Viewer (FLIR) was used. We did not take care of careful calibration for the PZT emissibity as what we want was a
rough estimation of the temperature.
Before the driving (LEFT) and at the equilibrium (RIGHT)
 
The temperature change of the PZT was tracked for an hour (below). Fitting of the points indicated that the temperature rise is 2.3degC and the
time constant of 446 sec. This level of temperature rise is totally OK. (Note that the fitting function was T = 27.55 - 2.31 Exp[-t/446.])

Results
DAY1:
Start driving
20:27 25.2 degC, status OK
20:33 26.7 degC, status OK
20:41 26.9 degC, status OK
20:48 27.6 degC, status OK
20:54 27.4 degC, status OK
21:10 27.4 degC, status OK
21:37 status OK
Stop driving
70 minutes of driving (i.e. 4.2x10^5 cycles) => no sign of degradation
DAY2:
Start driving
14:15, 24.5 degC, status OK
14:17, 26.0 degC, status OK
14:24, 27.0 degC, status OK
14:40, 26.8 degC, status OK
14:50, 26.8 degC, status OK
15:30, 26.8 degC, status OK
15:55 status OK
17:40 status OK
21:00 status OK (2.43Mcycles + 0.42Mcycles = 2.85Mcycles)
1d+12:00 status OK (7.83Mcycles + 0.42Mcycles = 8.25Mcycles)
1d+15:00 status OK (8.91Mcycles + 0.42Mcycles = 9.33Mcycles)
1d+18:40 status OK (10.23Mcycles + 0.42Mcycles = 10.65Mcycles)
Stop Driving
After 10.65Mcycles no sign of degradationwas found.
|
157
|
Fri Aug 23 19:24:32 2013 |
Koji | Electronics | Configuration | PZT endurance test (II) |
The PZT tests were finished with the conclusion that the PZT won't be damaged with our expected usage.
This is another test of the PZTs to make sure small (~10V) reverse voltage does not break the PZTs.
Background
At the site, we decided to use one of the PZT, which is still alive, for the HV and LV actuation.
The HV actuation is limited to 0 to 100V while the LV actuation is 10Vdc with 1Vpp fast dithering.
This means that a reverse voltage upto 10.5V will be applied to the PZT at the worst case.
From the technical note this level of reverse voltage does not induce polarization of the PZT.
The test is to ensure the PZT is not damaged or degraded by this small reverse voltage.
Method
HV drive: Thorlabs HV amp (G=15) driven with DS345 function generator (3.5Vpp+1.7Vdc, 0.1Hz)
=> 0-100V @0.1Hz
=> The hot side of the potential is connected to the positive side of the PZT
LV drive: Phillips function generator (1Vpp+9.5Vdc@1kHz)
The driving frequency is limited by the current output of the function generator.
=> The hot side of the potential is connected to the negative side of the PZT
These drives shares the common ground.
Tests
Testing with spare PZTs
Started @19:23 (Aug 23)
Stopped @20:15+2d (Aug 25, duration 48h52m)
17600cycles for the 0.1Hz drive.
176Mcycles for the 1kHz drive.
Checked the impedances of PZT1 and PZT2.
Apply 100Vdc via a 1kOhm resister, 0V detected across the 1kOhm resister
This is equivalent to the resistance of 1MOhm.
Testing with the PZT subassemblies
Started shaking of the four PZT assemblies @20:20 (Aug 25)
No impedance change observed @11:10+1d
No impedance change observed @15:30+1d
Stopped shaking of the four PZT assemblies @XXXX (Aug 26)
Wiring for the test

|
158
|
Tue Aug 27 17:02:31 2013 |
Koji | Mechanics | Characterization | Spot position measurement on the diode mounts |
After the PZT test, the curved mirrors were aligned to the cavity again.
In order to check the height of the cavity beam, the test DCPD mount was assembled with 2mm shim (D1201467-3)
The spot position was checked with a CCD camera.
According to the analysis of the picture, the spot height is about 0.71mm lower than the center of the mount. |
159
|
Thu Aug 29 02:52:50 2013 |
Koji | Optics | Characterization | H1OMC Curved Mirror Alignment |
Cavity parameter was measured with 50V bias on PZT1 (CM1)
- PZT combination was changed: PZT1 #21 (PZT ASSY#6) / PZT2 #25 (PZT ASSY #4)
- 19th HOMs of the USB makes accidental resonance with the nominal cavity length.
Because of the mirror astigmatism, HOMs spreads more than the design.
In order to avoid these modes, the cavity length had to be moved from the nominal value (1.134m).
- The clearance between the fixture and the prism was limited. This prevents to shorten the cav length.
The cavity length was made longer about 10mm.
-----
Cavity parameter obtained from the pitch misalignment
Free Spectral Range (FSR): 261.777947 +/− 0.000299 MHz
Cavity roundtrip length: 1.145217 +/− 0.000001 m
Lock offset: 1.636183 +/− 0.238442 kHz
Transverse mode spacing (TMS): 57.581950 +/− 0.000163 MHz
TMS/FSR: 0.219965 +/− 0.000001
Cavity pole (1st order modes, avg and stddev): 353.465396 +/− 0.657630 kHz
Finesse (1st order modes, avg and stddev): 370.302940 +/− 0.688585
Carrier 9th-order HOM: -8.1 line width away
Upper Sideband 13th-order HOM: 13.3 LW away
Lower Sideband 19th-order HOM: 2.2 LW away
-----
Cavity parameter obtained from the pitch misalignment
Free Spectral Range (FSR): 261.777106 +/− 0.000226 MHz
Cavity roundtrip length: 1.145220 +/− 0.000001 m
Lock offset: 0.215937 +/− 0.183434 kHz
Transverse mode spacing (TMS): 57.875622 +/− 0.000116 MHz
TMS/FSR: 0.221087 +/− 0.000000
Cavity pole (1st order modes, avg and stddev): 356.862001 +/− 0.448102 kHz
Finesse (1st order modes, avg and stddev): 366.776766 +/− 0.460598
Carrier 9th-order HOM: -4.1 line width away
Upper Sideband 13th-order HOM: 19.1 LW away
Lower Sideband 19th-order HOM: 10.8 LW away
-----
We could avoid hitting the 19th modes of the 45MHz sidebands.
First accidental hit is the 28th order modes of the lower sideband.
Red: Carrier
Blue: Upper sideband (45MHz)
Green: Lower sideband (45MHz)

|
160
|
Thu Aug 29 18:55:36 2013 |
Koji | Mechanics | General | I1 OMC top side gluing (UV) |
The glass components for the I1 OMC top side were glued by the UV glue.
Breadboard SN#4
Wire bracket SN#5/6/7/8 |
161
|
Fri Aug 30 12:14:50 2013 |
Koji | Optics | General | H1 OMC Cavity length adjustment |
Short conclusion:
The roundtrip cavity length for the H1 OMC was adjusted to be 1.145m
instead of 1.132m such that the 19th HOMs of the lower sideband do not get resonant together with the carrier.
Background:
The purpose of the OMC is to transmit the carrier TEM00 mode while anything else is rejected.
As the optical cavity has infinite numbers of resonant modes, what we practically do is to select
the roundtrip accumulated gouy phase so that low order higher order modes for the carrier
as well as the sidebands (including the TEM00 modes).
The nominal round trip length of the OMC is 1.132m. The curvature of the mirror is 2.575m.
The nominal ratio between the TMS and FSR is 0.218791 and 0.219385 (TMS_V/TMS_H= 0.9973)
for the vertical and horizontal modes. This split comes from the non-zero angle (~4deg) of incidence on the curved mirrors.
In reality, the TMS/FSR ratio depends on the true curvature of the mirror. More importantly, astigmatism
of the mirror changes the difference of the ratios for the vertical and horizontal modes.
The mirror astigmatism can either reduce or increase the split. between the TMSs. For example,
the L1 OMC showed the TMS/FSR ratio of (0.218822, 0.219218) for the vertical and horizontal modes.
TMS_V/TMS_H is 0.9982 which is 0.18% from the unity. This suggests, roughly to say, that 0.27% of the
astigmatism coming from the AOI of 4deg was partially compensated by the mirror astigmatism. This was lucky.
Something unlucky happened to the case for the first choice of the H1OMC curved mirrors.
TMS_V/TMS_H is 0.990 which is indeed 1% away from the unity. This actually caused some problem:
As the modes spreads too wide, the 19th modes became unavoidable. (see the picture below)

Red - carrier, Blue - upper sideband (+45MHz), Green - lower sideband
After the replacing one of the PZT assembly with another one, 1-TMS_V/TMS_H went down to 6%.
But still the 19th mode is on resonance. In order to shift the 19th mode from the resonance, the cavity length
had to be changed more than the range of the micrometer.
Simple simulation:
Attached Mathematica file calculates expected mode structure when the curved mirror position is
moved by DL (then the total roudtrip length changes 4*DL). This tells us that the 19th mode is
moved from the resonance by giving DL=-0.003 or DL=0.0025.
It was impossible to make the cavity short enough as the gluing fixture interferes with the curved mirror.
In fact, it was also impossible to make the cavity long enough as it was. Therefore PEEK shims with
the thickness of 1.5mm was inserted.

Result:
The FSR and TMS were measured with the longer cavity. 50V was applied to PZT1.
FSR: 261.775MHz
TMS_V: 57.575MHz
TMS_H: 57.880MHz
=> Cavity round trip length of 1.1452m
=> TMS/FSR = {0.219941, 0.221106}
The 19th modes for the lower sidebands are successfully moved from the carrier resonance.
The first accidental resonance is the lower sideband at the 28th order modes.

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Fri Aug 30 12:22:56 2013 |
Koji | Optics | General | H1 OMC Cavity side UV gluing |
H1 OMC Cavity side optics was glued on the breadboard
Curved mirror gluing
- Applied the UV glues to CM1/CM2 prisms.
- Checked the spot positions on the curved mirrors
- Apply 50V to CM1
- Measure the FSR and TMS while the cavity was locked.
FSR: 261.70925MHz
TMS_V: 57.60500MHz
TMS_H: 57.94125MHz
=> Cavity round trip length of 1.1455m
=> TMS/FSR = {0.220111, 0.221395}
First accidental resonance is the lower sideband at 28th order modes.

Carrier 9th-order HOM: 2.9~7.6 line width away
Upper Sideband 13th-order HOM: 14.1-20.7 LW away
Lower Sideband 19th-order HOM: 3.3-13.1 LW away
- As this result was satisfactory, the UV illumination was zapped. It did not change the alignment. The cavity was kept locked during the illumination.
Peripheral optics gluing
- QPD path BS/Steering Mirrors were glued
- DCPD path BS was glued
The UV glue was applied to the optics.
Then the optics were placed on the breadboard along with the fixture.
Placed the dummy QPD/DCPD mount with the alignment disks.
The horizontal positions of the spots were well with in the horizontal range of the mounts.
The UV illumination was zapped. Checked the alignment again and no problem was found. |
163
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Fri Aug 30 12:24:28 2013 |
Koji | Optics | Characterization | H1OMC Spot positions |
Beam heights on the diodes
DCPD1: 14.459mm -> With 1.5mm shim, the beam will be 0.038mm too low.
DCPD2: 14.221mm -> With 1.25mm shim, the beam will be 0.026mm too low.
QPD1: 14.691mm -> With 1.75mm shim, the beam will be 0.056mm too low.
QPD2: 14.379mm -> With 1.5mm shim, the beam will be 0.118mm too low. |
164
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Fri Aug 30 12:25:29 2013 |
Koji | General | General | H1 OMC Invar mount gluing |
The Invar Mounting Blocks were glued on the breadboard.
Serial number #1/2/5/6/7/8 -> I1 OMC cable side
Serial number #9/10/11/12 -> H1 OMC cavity side |
165
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Tue Sep 3 17:03:25 2013 |
Koji | General | General | H1 OMC gluing completed |
[Koji Jeff]
H1 OMC All Gluing completed
5 Glue H1 beam dumps (UV)
4 glass wire brackets glued on the H1 topside (UV) SN: #9/10/11/12
6 Invar blocks glued on the H1 topside (EP30) SN: #13/14/15/16/18/19 |
166
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Wed Sep 4 22:22:54 2013 |
Koji | General | General | H1 OMC wrapped and moved to the bake lab. |
[Koji, Jeff]
We moved the H1OMC to the bake lab.
Chub set up the vacuum bake oven (Oven F) and running without the actual OMC.
We use low temperature (55degC) for the baking.
The actual OMC will be baked from tomorrow afternooon. |