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ID Date Author Type Categoryup Subject
  253   Sun Mar 13 21:22:27 2016 KojiElectronicsCharacterizationDark current measurement of the HQE PD and other PDs

Transfered for RGA scan

B4 (C1-05) -> F1
C1 (C1-07) -> F2

 

  254   Sun Mar 13 22:02:09 2016 KojiOpticsCharacterizationHQEPD QE measurement (direct comaprison)

Direct comparison of the PD responsibities

We can expect 5% increase of the QE with the new PD.


P-pol 10deg incident

Power meter Ophir RM9C (Systematic error +/-5%)
Vbias = 6V

C30665GH (#07)
Incident: 7.12mW
Reflection: 0.413mW (=> R=5.8%)
PD output: 5.690+/-0.006V
=> Responsibity 0.799+/-0.001 A/W
=> QE = 0.931+/-0.001

HQE PD (A1-23)
Incident: 7.15mW
Reflection: 0.020+/-0.1mW (=> R=0.28%)
PD output: 6.017+/-0.007V
=> Responsibity 0.842+/-0.001 A/W
=> QE = 0.981+/-0.001

Note that there is a 5% systematic error with the power meter.

  255   Sat Mar 26 01:49:48 2016 KojiOpticsCharacterizationHQEPD QE

Calibration of the transimpedance

Use KEITHLEY 2450 as a calibrated current source. Model 2450 has the current source accuracy of 0.020%+1.5uA at 10mA range. For 6mA current output, the error is 3uA (0.05%).

The output of the current amp at 103 Ohm setting was 6.0023V when -6.000mA current was applied. i.e R_trans = 1000.4 +/- 0.5 Ohm. This is a negligible level.

QE of the diodes (As of 07/30/2016)

Refer E1800372

Attachment 1: QE1.png
QE1.png
Attachment 2: QE2.png
QE2.png
  256   Sat Mar 26 17:39:50 2016 KojiElectronicsCharacterizationHQEPD dark noise

Dark noise measurement for 6 HQEPDs and 1 C30665. All of these showed sufficiently low dark current noise levels compared with the noise level of the DCPD preamp. The measurement was limited by the input noise (ADC) noise of the FFT analyzer as the line noises were too big.

The measurement has been done with the transimpedance of 1e7. The bandwidth of the measurement was 50kHz.

Attachment 1: PD_dark_current.pdf
PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf
  257   Sat Mar 26 18:22:24 2016 KojiElectronicsCharacterizationBaking / Contamination tests of the PDs

For the production of the aLIGO PDs, the following transfer of the PDs were carried out
A1-23 Cage A1 -> G1
A1-25 Cage A2 -> G2

The cage A will be baked at 75degC to see if this improves AMU=64 emission.

At the same time, we will put C1-05 (F1) and C1-07 (F2) into the contamination test cavity.

  259   Tue Apr 5 18:22:40 2016 KojiElectronicsCharacterizationBaking / Contamination tests of the PDs

Possible reduction of the QE was observed after air-bake at 75degC.


Yesterday I received Cage G from Bob for intermediate test of the PD performance after air bake but before vacuum bake.
This cage was prepared to be the production pair.

According to the ICS, https://ics-redux.ligo-la.caltech.edu/JIRA/browse/Bake-8047
the PDs were air baked at 75degC for 48 hours.

I took the PDs to my lab to check if there is any issue in terms of the performance.
- Dark current: No change observed
- Dark noise: No noise increase observed
- QE: Probably reduced by ~0.5%.

Here I attached the result of the QE measurement. I have measured the QEs of the baked ones (A1-23 and A1-25) and the reference. Since the reference PD has not been baked, this gives us the measure of the systematic effect. The reference showed the reduction of ~0.1%. Assuming this reduction came from the systematic effect of the measurement system, I observed at least 0.5% QE reduction (A1-23). Note that the previous measurement of 99.8% for A1-25 was too high and dubious. But both A1-23 and A1-25 showed ~0.4% lower QEs.

So I believe the air-baking process reduced the QE.

Another evidence was that now I could clearly see the beam spots on these air-baked-PDs with an IR viewer when the PDs were illuminated with a 1064nm beam. Usually it is difficult to see the spot on the PD. The spot on the reference PD was still dark. So this difference was very obvious. I was afraid that something has been deposited on the surface of the photosensitive element. The surface of the diodes looked still very clean when they were checked with a green LED flash light.

Attachment 1: QE_after_air_bake.pdf
QE_after_air_bake.pdf
  260   Tue Apr 5 21:20:15 2016 KojiElectronicsCharacterizationMore dark noise measurement

All survived PDs have been measured.

Attachment 1: PD_dark_current.pdf
PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf PD_dark_current.pdf
  266   Tue Aug 23 23:36:54 2016 KojiOpticsCharacterizationInspection of the damaged CM1 (prev H1OMC)

1. Calum and GariLynn checking the CM1 defect from the front side.
2. Same as above
3. Close up of the defect
4. Using dino-lite microscope to get a close up view of the defect from the front surface.
5. Same as 4
6. Finished for the day and setting up a safefy clamp
7. Finally a tefron cover was attached.

Attachment 1: P8238983.jpg
P8238983.jpg
Attachment 2: P8238986.jpg
P8238986.jpg
Attachment 3: P8238987.jpg
P8238987.jpg
Attachment 4: P8238989.jpg
P8238989.jpg
Attachment 5: P8238990.jpg
P8238990.jpg
Attachment 6: P8238994.jpg
P8238994.jpg
Attachment 7: P8238996.jpg
P8238996.jpg
  267   Thu Aug 25 02:17:09 2016 KojiOpticsCharacterizationInspection of the damaged CM1 (prev H1OMC)

Initial inspection results by Calum, et al.
https://dcc.ligo.org/LIGO-E1600268

  276   Tue Mar 28 21:04:27 2017 KojiElectronicsCharacterizationPDH amp

Attachment 1: PDH amp RF part (before the preamp was installed)

Attachment 2: RF-AF transmission

Attachment 3: Attachment 3: LO dependence

Attachment 4: RF amp gain (saturation)

Attachment 5: Input/output noise level

Attachment 6: Attachment 6: Preamp/DCPD out buffer AF circuit

Attachment 1: DSC_0269.JPG
DSC_0269.JPG
Attachment 2: RF_to_AF_conversion.pdf
RF_to_AF_conversion.pdf
Attachment 3: LO_dependence.pdf
LO_dependence.pdf
Attachment 4: RFamp_gain.pdf
RFamp_gain.pdf
Attachment 5: PreampNoise.pdf
PreampNoise.pdf
Attachment 6: preamp.png
preamp.png
  286   Sat Jul 29 18:44:38 2017 ranaElectronicsCharacterizationPDH amp

attachment 6: DCPD preamp looks like the opamp is wired for positive feedback?

  287   Sat Jul 29 21:42:51 2017 KojiElectronicsCharacterizationPDH amp

The polarities indicated in the right circuits were opposite, obviously.

  291   Thu Feb 22 20:21:02 2018 KojiOpticsCharacterizationaLIGO EOM test

POSTED to 40m ELOG

  292   Mon Apr 2 17:27:04 2018 KojiOpticsCharacterizationaLIGO EOM test

2nd optical test http://nodus.ligo.caltech.edu:8080/40m/13725

  296   Wed May 30 16:40:38 2018 KojiMechanicsCharacterizationEOM mount stability test

https://awiki.ligo-wa.caltech.edu/wiki/EOM_Mount_Stability

  297   Wed May 30 17:44:23 2018 KojiOpticsCharacterization3IFO EOM surface check

3IFO EOM dark microscope images courtesy by GariLynn and Rich

Attachment1/2: Hole #1
Attachment3/4: Hole #2
Attachment5: Hole #2

Attachment 1: IMG_5756.JPG
IMG_5756.JPG
Attachment 2: IMG_5757.JPG
IMG_5757.JPG
Attachment 3: IMG_5758.JPG
IMG_5758.JPG
Attachment 4: IMG_5759.JPG
IMG_5759.JPG
Attachment 5: Looking_at_Hole2.png
Looking_at_Hole2.png
  298   Mon Jul 2 11:30:22 2018 KojiElectronicsCharacterization3IFO EOM impedance measurement

[Rich Koji]

3IFO EOM (before any modification) was tested to measure the impedance of each port.

The impedance plot and the impedance data (triplets of freq, reZ, imZ) were attached to this entry.

Attachment 1: impedance_eom.pdf
impedance_eom.pdf
Attachment 2: EOM_Z_DATA.zip
  299   Mon Jul 2 12:29:01 2018 KojiElectronicsCharacterizationImpedances of individual components (3IFO EOM)

[Rich Koji]

The impedances of the individual components from the 3IFO EOM (before modification) were tested.
Each component was modeled by LISO. The LISO model (in PDF and txt) are attached at the end of the entry.

Coils
There are three inductors taken from the EOM unit. They showed the Q ranging from 150~300.
Their impedances are compared with the coil taken from the 9MHz port of the spare EOM (=current LHO EOM).
The inductance of the 8.7MHz inductor indicated higher L but still higher Q.

Todd made a replica of the 45.3MHz coil. He used a silver plated wire and it actually showed highest Q of ~400.

Crystal capacitance
The crystal capacitances were measured by attaching a test rig on the DB15 connector of the crystal housing. The rig was calibrated such that the impedances of the attched components on the rig were measured. They showed somewhat similar feature with parasitic resonances at ~50MHz. Above this frequnecy the capacitance went down (i.e. Abs(Z) went up). This indicates there are stray series LCR in pararrel to the crystal. Not sure what is the cause of this.

The central (24.1MHz) port showed smaller capacitance. This probably means the plates for the central port is smaller. Not sure the actual dimensions of the plates for this unit.
 

Attachment 1: impedance_coils.pdf
impedance_coils.pdf
Attachment 2: impedance_xtals.pdf
impedance_xtals.pdf
Attachment 3: q_coils.pdf
q_coils.pdf
Attachment 4: component_models.pdf
component_models.pdf component_models.pdf component_models.pdf component_models.pdf component_models.pdf component_models.pdf component_models.pdf component_models.pdf
Attachment 5: liso_models.zip
  301   Tue Jul 3 12:07:47 2018 Rich AbbottElectronicsCharacterizationNotes on 3rd IFO EOM

Attached please see my notes summarizing the models for the electrodes and inductors within the 3rd IFO EOM

Attachment 1: EOM_Analysis2.pdf
EOM_Analysis2.pdf EOM_Analysis2.pdf
  302   Wed Jul 4 18:30:51 2018 KojiElectronicsCharacterizationEOM circuit models

The circuit models for the 3IFO EOM (before mods) were made using LISO.
Then the modification plan was made to make it a new LLO EOM.

Impedance data, LISO model, Mathematica files are zipped and attached at the end.

Attachment 1: eom_models.pdf
eom_models.pdf eom_models.pdf eom_models.pdf
Attachment 2: eom9.pdf
eom9.pdf
Attachment 3: eom24.pdf
eom24.pdf
Attachment 4: eom45.pdf
eom45.pdf
Attachment 5: 180704_3IFO_EOM_model.zip
  303   Thu Jul 26 20:57:07 2018 KojiElectronicsCharacterization9MHz port tuned impedance

[Rich Koji]

The 9MHz port was tuned and the impedance was measured.

Attachment 1: impedance_eom.pdf
impedance_eom.pdf
Attachment 2: eom9.pdf
eom9.pdf
Attachment 3: eom_models_9MHz.pdf
eom_models_9MHz.pdf
  304   Tue Aug 7 15:43:12 2018 KojiElectronicsCharacterizationNew LLO EOM stuffed

[Rich, Dean, Koji]

Stuffed all inductors for the new LLO EOM. As the impedances were sensitive to the positions of the inductors in the housing, they were glued with a glue gun.
Also the lid of the housing significantly change the stray capacitance and lowers the resonant frequency (meaning lowers the Q too), we decided to tune the matching circuit without the lid.

The attached plots show the measured impedances. They all look well tuned and matched. We will prepare and perform the optical measurement at the 40m.

Attachment 1: P_20180806_154457.jpg
P_20180806_154457.jpg
Attachment 2: impedance_eom.pdf
impedance_eom.pdf
Attachment 3: impedance_eom_zoom.pdf
impedance_eom_zoom.pdf
  305   Wed Aug 8 17:32:56 2018 Rich AbbottGeneralCharacterizationModulation Index Test Setup at 40m Lab

Attached is a block diagram of the test setup used in the 40m lab to measure the modulation index of the IO modulator

Attachment 1: 40mLabModIndexSetup.pdf
40mLabModIndexSetup.pdf
  306   Thu Aug 9 11:24:29 2018 KojiGeneralCharacterizationModulation Index Test Setup at 40m Lab

[Rich Koji]

The impedances of the new LLO EOM were measured with the beat note setup at the 40m PSL (as described in the previous ELOG entry.

At the target frequencies (9.1MHz, 24.1MHz, 45.5MHz, 118.3MHz), the modulation responses were (0.09, 2.9e-3, 0.053, 0.021) rad/V.

This corresponds to the requirement for the driving power as follows.

Frequency
[MHz]
Response
[rad/V]
modulation depth 
required (LHO) [rad]
Required
drive [Vpk]
Required
drive [dBm]
    9.1 0.09 0.22 2.4 17.8
  24.1 2.9e-3   0.014 4.8 23.7
  45.5   0.053 0.28 5.3 24.5
118.3   0.021   0.010   0.48   3.6

 

Attachment 1: modulation_depth.pdf
modulation_depth.pdf
Attachment 2: modulation_depth_zoom.pdf
modulation_depth_zoom.pdf
  311   Thu Jan 10 20:42:54 2019 KojiOpticsCharacterizationFSR / HOM Test of OMC SN002

OMC SN002 = Former LHO OMC which CM1 was destroyed by the lock loss pulse in 2016. This OMC needs to be optically tested before storage.

The test items:

  • [done] FSR measurement with offset PDH locking (FM->AM conversion)
  • [done] FSR/finesse measurement with the EOM RFAM injection
  • [done] TMS measurement with input miaslignment and the trans RFPD misalignment: with no PZT offset
  • [done] TMS measurement with input miaslignment and the trans RFPD misalignment: with PZT offsets
     
  • PZT response
  • Mirror cleaning
  • Power budget
  • Diode alignment: shim height
  • PD/QPD alignment
  312   Thu Jan 10 20:45:00 2019 KojiOpticsCharacterizationPZT test cable

As OMC SN002 already has the PZTs connected to the Mighty-Mouse connector, a test cable with a female mighty-mouse connector was made.

A small imperfection: When the cable was inserted to the connector shell, I forgot to mirror the pin out. Therefore the color and pin number do not match.

Attachment 1: OMC_PZT_wiring.pdf
OMC_PZT_wiring.pdf
  313   Sat Jan 12 22:49:11 2019 KojiOpticsCharacterizationPM-SM patch cable mode cleaning effect

Mode cleaning capability of an optical fiber was measured. The conclusion is that the leakage of the non-fiber mode to the fiber output is insignificant and also practically negligible.

The tested fiber was Thorlabs 5-m Polarization Maintaining Single-Mode fiber (P3-1064PM-FC-5, PM Patch Cable, PANDA, 1064 nm, FC/APC, 5m).

The output mode cleaner was used as a mode analyzer. The fiber input was aligned and the misaligned so that the amount of higher order mode for the fiber is changed. The fiber output has been mode matched to an output mode cleaner. Therefore excess mode mismatch when the fiber input was misaligned, was accounted as the leakage higher order mode.

For each alignment state, the OMC transmission (in V), the OMC reflection (in V), and the OMC reflection with the OMC unlocked were measured. The voltages were measured with a digital multimeter (non-portable unit). With the fiber input beam aligned to the fiber, the fiber input and output powers were measured with a power meter.

With the input beam aligned
- Fiber input: 52.5 +/- 0.2 [mW]
- Fiber output: 35.5 +/- 0.2 [mW] (~68% coupling)
- Reflection PD offset: -0.00677 +/- 0.00001 [V]

- Refl PD reading with the OMC unlocked: 6.32 +/- 0.01 [V]
- Refl PD reading with the OMC locked: 0.133 +/- 0.002 [V]
- OMC Trans PD with the OMC locked: -1.72 +/- 0.01 [V] 

With the input beam misaligned
- Refl PD reading with the OMC unlocked: 3.63 +/- 0.01 [V]
- Refl PD reading with the OMC locked: 0.0752 +/- 0.001 [V]
- OMC Trans PD with the OMC locked: -1.00 +/- 0.01 [V] 

The naive mode matching was 0.9779 +/- 0.0003 and 0.9775 +/- 0.0003 without and with misalignment. We initially had roughly 17mW of non-fiber mode incident. And it was increased by roughly 15mW. For the misaligned case, the amount of the OMC-matched carrier was also reduced due to the misalignment. So the actual fiber mode cleaning effect needs more careful quantitative analysis.


The power budget at each part of the setup was modeled as shown in Attachment 1. The blue numbers are the measured values.
The factor a is the ratio of the leakage non-fiber mode into the fiber transmission.
The factor (1-b) is the mode matching of the fiber mode into the OMC mode.

\begin{align} P_{\rm omcrefl} & = a P_{\rm nofib} + b P_{\rm fib} \nonumber \\ P_{\rm fibout} & = P_{\rm omcrefl} + (1-b) P_{\rm fib} \nonumber \\ P_{\rm tot} & = P_{\rm nofib} + P_{\rm fib} \nonumber \end{align}

and

\begin{align} P'_{\rm omcrefl} &= a P'_{\rm nofib} + b P'_{\rm fib} \nonumber \\ P'_{\rm fibout} &= P'_{\rm omcrefl} + (1-b) P'_{\rm fib} \nonumber \\ P_{\rm tot} &= P'_{\rm nofib} + P'_{\rm fib} \nonumber \end{align}

With the calibration between the refl PD and the power meter measurement,
  \begin{align} P_{\rm tot} &= 52.5 \pm 0.2 {[mW]} \nonumber \\ P_{\rm fibout} &= 35.5 \pm 0.2 {\rm [mW]} \nonumber \end{align}
\begin{align} P_{\rm omcrefl} &= 0.78 \pm 0.01\,\,{\rm [mW]} \nonumber \\ P'_{\rm omcrefl} &= 0.460 \pm 0.006\,\,{\rm [mW]} \nonumber \\ P'_{\rm fibout} &= 20.4 \pm 0.13 \,\,{\rm [mW]} \nonumber \end{align}

The solution of the equations is
\begin{align} a &= (4 \pm 4) \times 10^{-4} \nonumber \\ b &= 0.0219 \pm 0.0005 \nonumber \end{align}

So, the leakage of the non-fiber mode to the fiber output is insignificant. Moreover, the number is practically negligible because the mismatching between the fiber and OMC modes is of the order of percent and dominated by the aberration of the collimator (i.e. the OMC reflection looks like concentric higher-order LG modes) with the order of 1~2%.
 

Attachment 1: fiber_mode_cleaning.pdf
fiber_mode_cleaning.pdf
  315   Sat Feb 2 16:17:13 2019 KojiOpticsCharacterizationSummary: OMC(001) HOM structure recalculation

Each peak of the transfer function measurement was fitted again with a complex function:

\begin{align} h(f;a_{\rm r}, a_{\rm i}, f_0, dT, \Gamma, a_0, b_0, a_1, b_1) & \nonumber\\ = (a_{\rm r} + i a_{\rm i}) e^{-i 2 \pi f dT} \frac{1}{1 + i (f - f_0)/\Gamma} &+ (a_0 + i b_0) + (a_1 + i b_1)f \nonumber \end{align}


OMC (001)
History:
Measurement date 2013/5/31, Installed to L1 2013/6/10~

Attachment 1: OMC_HOM_130531.pdf
OMC_HOM_130531.pdf
Attachment 2: HOM_PZTV.pdf
HOM_PZTV.pdf
Attachment 3: HOM_plot_PZT0_0.pdf
HOM_plot_PZT0_0.pdf
Attachment 4: Cav_scan_response_HOM.pdf
Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf Cav_scan_response_HOM.pdf
  316   Sat Feb 2 20:03:19 2019 KojiOpticsCharacterizationSummary: OMC(002) HOM structure recalculation (before mirror replacement)

OMC (002)
History:
Measurement date 2013/10/11, Installed to L1 2013/XX

Attachment 1: OMC_HOM_131011.pdf
OMC_HOM_131011.pdf
Attachment 2: HOM_PZTV.pdf
HOM_PZTV.pdf
Attachment 3: HOM_plot_PZT0_0.pdf
HOM_plot_PZT0_0.pdf
Attachment 4: Cav_scan_response_PZT_HOM.pdf
Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf
  317   Sat Feb 2 20:28:21 2019 KojiOpticsCharacterizationSummary: OMC(003) HOM structure recalculation

OMC (003)
History:
Measurement date 2014/7/5, Stored for I1, Installed to H1 2016/8 upon damage on 002

Attachment 1: OMC_HOM_140705.pdf
OMC_HOM_140705.pdf
Attachment 2: HOM_PZTV_PZT1_0V.pdf
HOM_PZTV_PZT1_0V.pdf
Attachment 3: HOM_plot_PZT0_0.pdf
HOM_plot_PZT0_0.pdf
Attachment 4: Cav_scan_response_PZT_HOM.pdf
Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf Cav_scan_response_PZT_HOM.pdf
  318   Sat Feb 2 20:35:02 2019 KojiOpticsCharacterization Summary: OMC(002) HOM structure recalculation (after mirror replacement)

OMC (002) after repair
History:
Mirror replacement after the damage at H1. Measurement date 2019/1/10

Attachment 1: OMC_HOM_190110.pdf
OMC_HOM_190110.pdf
Attachment 2: HOM_PZTV.pdf
HOM_PZTV.pdf
Attachment 3: HOM_plot_PZT0_0.pdf
HOM_plot_PZT0_0.pdf
Attachment 4: Cav_scan_response_PZT.pdf
Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf Cav_scan_response_PZT.pdf
  319   Tue Mar 19 17:30:25 2019 KojiGeneralCharacterizationOMC (002) Test items

OMC #002 Optical tests

  • FSR measurement (done, 2019/1/8-9, 2019/4/1)
  • TMS measurement (done, 2019/1/9)
  • TMS measurement (with DC voltage on PZTs) (done, 2019/1/10)
  • Cleaning (done, 2019/3/19)
  • Power Budget (done, 2019/3/19, 2019/4/1)
  • PZT DC response (done, 2019/3/27)
  • PZT AC response (done, 2019/3/27)
  • QPD alignment (done, 2019/4/5)
  • DCPD alignment (done, 2019/4/4)
  • Beam quality check (done, 2019/4/4)

(Backscattering test)

(Cabling / Wiring)

  • (Attaching cable/mass platforms)
  • (PZT cabling)
  • (DCPD cabling)
  • (QPD cabling)

(Baking)
(First Contact)
(Packing / Shipping)

  320   Thu Mar 28 16:36:52 2019 KojiMechanicsCharacterizationOMC(002) PZT characterization

As performed in the ELOG 202, the PZTs of the OMC 002 were tested.

DC response was measured by sweeping each PZT with 0-150V triangular voltage at 11Hz. Acquire 0.2sec of the tie series using an oscilloscope to get the PDH error, cavity transmission, and the sweep signal.

The voltage where the tranmission peaks were observed were fitted were recorded. One fringe corresponds to the displacement of 532nm. So the displacement and the applied volatagewere fitted witha linear function.

This gave the PZT response for PZT1 and PZT2 to be 14.9nm/V and 14.4nm/V.

 

AC response was measured with SR785. The PZT was shaken with 1~50mVpp signal with the DC offset of 5V while the OMC was locked with the feedback to the laser fast PZT. The transfer function from the applied PZT voltage to the servo output were measured. The closed loop TF was also measured to remove the effect of the servo control.  The DC levels of the responses were calibrated using the values above.

Attachment 1: PZT_Scan.pdf
PZT_Scan.pdf
Attachment 2: OMC_PZT_Response.pdf
OMC_PZT_Response.pdf
  322   Fri Apr 5 01:07:18 2019 KojiOpticsCharacterizationOMC(002): transmitted beam images

There was a concern that the transmission from CM1 has additional fringes. The shape of the transmitted beams from CM1, CM2, and FM2 (main) werecaptured with WinCamD.
Indeed CM1 and CM2 have the fringes, but it does not exist in the main transmission. So it seems that the fringes are associated with the curved mirrors. But how???

Attachment 1: CM1trasns.png
CM1trasns.png
Attachment 2: CM2trasns.png
CM2trasns.png
Attachment 3: FM2trans2.png
FM2trans2.png
  323   Fri Apr 5 01:08:17 2019 KojiOpticsCharacterizationOMC(002): DCPD / QPD alignment

The beam height in the cavity became totally different from the previous one and the shims needed to be much thicker than before. This is probably because of the alignment of the newly-glue curved mirror.

As the beam height is 2~2.5mm higher, two shims need to be stacked. The preliminary check of the heights using the alignment disks (dummy PDs) suggested the following combinations.

QPD1(SHORT)  D1201467-03 (SN 007) + D1201467-03 (SN 008) (2.0 mm + 2.0 mm = 4 mm)
QPD2(LONG)   D1201467-01 (SN 001) + D1201467-01 (SN 002) (1.5 mm + 1.5 mm = 3 mm)
DCPD1(TRANS) D1201467-02 (SN 006) + D1201467-03 (SN 005) (1.75mm + 2.0 mm = 3.75 mm)
DCPD2(REFL)  D1201467-02 (SN 002) + D1201467-03 (SN 006) (1.75mm + 2.0 mm = 3.75 mm)

This resulted that the fixing button head socket screws for the PD housings to be replaced from 5/16" to 7/16". Stephen kept CLASS A spare screws from Jeff's time.

For the DCPD alignment, a cap-removed Excelitas 3mm InGaAs PD is used. -> This needs to be returned to the PD stock next time.

- DCPD1 was aligned using the zoomed CCD image (Attachment 1). Once the beam is aligned, the angle was tweaked to have the reflection nicely dumped by the glass beam dump (Attachment 2).

- DCPD2 was aligned too. (Attachment 2/3)

- The two housings were fastened by a torque wrench at 2 inch lb.

Next step:

Continue with the QPDs. The QPD amp was already set.

Notes:
The cable of the CCD monitor has a problem -> need to check what's wrong
The servo box probably have large offset at the output stage or somewhere (but not input stages).

Attachment 1: IMG_7521.JPG
IMG_7521.JPG
Attachment 2: IMG_7529.JPG
IMG_7529.JPG
Attachment 3: IMG_7539.JPG
IMG_7539.JPG
Attachment 4: IMG_7541.JPG
IMG_7541.JPG
  324   Fri Apr 5 20:50:54 2019 KojiOpticsCharacterizationOMC(002): QPD alignment

QPD#              QPD1       QPD2
Housing#          #004       #008
Diode#            #44        #46
Shim              (see OMC ELOG 323)

-------------------------------------
Power Incident    252.3 uW  266.0 uW
Sum Out           174.2 mV  176.0 mV   +0.3
Vertical Out      + 4.7 mV  +19.0 mV   +0.2
Horizontal Out    -16.1 mV  - 8.0 mV   +0.0
SEG1              -52.4 mV  -53.  mV   -0.1
SEG2              -37.6 mV  -47.  mV   -0.1
SEG3              -41.8 mV  -34.  mV   -0.1
SEG4              -43.7 mV  -36.  mV   -0.1

-------------------------------------
Spot position X   +39   um  +15. um  (positive = more power on SEG1 and SEG4)
Spot position Y   - 8.1 um  -56. um  (positive = more power on SEG3 and SEG4)
-------------------------------------

Responsivity[A/W] 0.69      0.66
Q.E.              0.80      0.77
-------------------------------------

Arrangement of the segments
View from the beam
/ 2 | 1 X
|---+---|
\ 3 | 4 /


---------------

I(w,x,y) = Exp[-2 (x^2 + y^2)/w^2]/(Pi w^2/2)

(SEG_A+SEG_B-SEG_C-SEG_D)/(SEG_A+SEG_B+SEG_C+SEG_D) = Erf[sqrt(2) d/w]

d: distance of the spot from the center
w: beam width

Attachment 1: P_20190405_215906.jpg
P_20190405_215906.jpg
Attachment 2: P_20190405_215927.jpg
P_20190405_215927.jpg
  336   Mon Apr 15 21:11:49 2019 PhilipOpticsCharacterizationOMC(004): PZT testing for spare OMC

[Koji, Philip]

Today we tested the functionality of the four remaining PZTs (11,12,13 and 22) .  Each PZT was placed within a collimated 500um beam.
Roughly half of the beam was blocked by the PZT. The PZT and a PD then acted as shadow sensor. Each PZT was tested with 0 and
150 V. The resulting power change then could be converted into a displacement of the PZT using the beam diameter.

The open light value for each of these tests was 3.25 V.

PZT 11:
0 V supply voltage     --> 1.717 V on PD
150 V supply voltage --> 1.709 V on PD
delta = 0.008 V

PZT 12:
0 V supply voltage     --> 1.716 V on PD
150 V supply voltage --> 1.709 V on PD
delta = 0.007 V

PZT 13:
0 V supply voltage     --> 1.702 V on PD
150 V supply voltage --> 1.694 V on PD
delta = 0.008 V

PZT 22:
0 V supply voltage     --> 1.770 V on PD
150 V supply voltage --> 1.762 V on PD
delta = 0.008 V

0.008 V --> 0.24% change in power on PD --> about  3.8 um displacement assuming no light which is blocked
by the PZT is hitting the PD.

 

We further started to drive all four PZTs over night with 100 V (half of their range) at 100 Hz.
We additionally display the impedance to ensure none of them degrades.

All four PZTs seem to be connected to Teflon coated wires. It needs to be checked if these
fulfill the vacuum compatibility requirements.

  337   Tue Apr 16 11:36:36 2019 KojiOpticsCharacterizationOMC(004): PZT testing for spare OMC

Attachment 1: Shadow sensor setup for the PZT displacement test

Attachment 2: PZT endurance test. 4 PZTs were shaken at once.

Attachment 3~5: Function generator setup 100Hz, 3.5Vpp 1.75Voffset (meant be displayed for 50Ohm load)

Attachment 6: The above setting yields 7Vpp unipolar signal @Hi-Z load

Attachment 7: The output was monitored with a 1/10 probe with the PZTs connected. This shows 10Vmax 0Vin -> Good. This photo was taken at 17:35.

Attachment 8: The test is going well @9:15 next day. (t=15.7hours = 5.6Mcycles)

Attachment 9: The test went well. The modulation was stopped @15:35. (t=21hours = 7.6Mcycles)

Attachment 1: IMG_7620.jpg
IMG_7620.jpg
Attachment 2: IMG_7623.jpg
IMG_7623.jpg
Attachment 3: IMG_7629.jpg
IMG_7629.jpg
Attachment 4: IMG_7630.jpg
IMG_7630.jpg
Attachment 5: IMG_7631.jpg
IMG_7631.jpg
Attachment 6: IMG_7632.jpg
IMG_7632.jpg
Attachment 7: IMG_7633.jpg
IMG_7633.jpg
Attachment 8: P_20190416_091537.jpg
P_20190416_091537.jpg
Attachment 9: IMG_7634.JPG
IMG_7634.JPG
  342   Tue Apr 16 21:16:11 2019 KojiOpticsCharacterizationOMC(004): PZT testing for spare OMC

After having dug into the past email, it turned out that these wires were the ones already replaced from the original teflonwires. The length of them were confirmed to be ~19" (480mm). 

Quote:

All four PZTs seem to be connected to Teflon coated wires. It needs to be checked if these
fulfill the vacuum compatibility requirements.

 

  350   Sat Apr 20 00:50:12 2019 KojiOpticsCharacterizationOMC(004): Spot positions

Similarly to OMC ELOG 349 the spot positions after the replacement of CM2 were measured (Attachment 1)
Also, the spot positions after the realignment were measured. (Attachment 2)

Attachment 1: misalignment2.pdf
misalignment2.pdf
Attachment 2: misalignment3.pdf
misalignment3.pdf
  354   Wed Apr 24 13:58:51 2019 JoeOpticsCharacterizationOMC power budget and UV Epoxy Bonding of BS1

[koji,philip,joe,liyuan,stephen]

need to add spot positions.

Mirrors: PZT11,PZT22, A14, A5

Measurement postion Power P_normalise
P_in 15.66+-0.01mV 3.251+-0.001
V_ref,lock 64+-2mV 3.22+-0.001
V_ref,unlock 2.808+-0.001 V 3.253+-0.001
P_qpd 99.5+-0.5 uW 3.24+-0.002
P_cm1 79.0+-0.5 uW 3.22+-0.002
P_cm2 76.2+-0.03 uW 3.22+-0.01
P_trans 14.55+-0.05 mW 3.22+-0.01
Vref,dark -6.286 mV +-0.01mV  

Mode matching = 97.72%

15.66-> 15.30mW coupled.

~100uW for QPD

->15.2mW in cavity

Trans = 14.55mW -> 95.7% transmission

The flat mirrors were the ones with the most scattering, so we thought about how to improve it. We tried to move the first flat mirror by pushing it with our finger so that he beam would move along the optic. We tried this a couple of times, however the second time we moved it we lost our alignment and could not retrieve it. We looked at the mirror and we could see quite a lot of newtonian rings. We could see a small fibre on the glass bread board. We cleaned the optics base and the gbb, and we could get the alignment back. The beam was aligned to the cavity, the spots no longer hit the centre of the CM2. 

We measured the power budget again.

Measurement position Power P_normalise
V_ref,lock 47mV 3.24V
P_trans 14.45+-0.005mW 3.24 +-0.003 V
V_ref,unlock 2.68+-0.001 V 3.25+-.003
     

mode matching = 1-47/2680 = 0.9824, 98.2% mode matching

same p_normalise so

15.66-> 15.34mW coupled.

~15.24mW in cavity

transmission = 14.45, so 94.8% transmission.

Koji noticed that FM1 wasn't touching the template correctly, so he re-aligned the cavity.

Afternoon session - UV Bonding (E1300201-v1 procedure 6.4.4 "Gluing" using procedure in section 7.2 "UV Gluing")

Wiped down UV PPE, UV Illuminator, and UV Power Meter

Applied Optocast 3553-LV Epoxy to sample fused silica optics, to test quantity of glue needed and to become familiar with the process and tools. Philip and Joe each created a successful bond. Joe's had 3 visible spots in the bulk of the bond. Acetone was used to scrub some residue of epoxy from the surface near the OD, which was likely cured. Short duration exposure (seconds) to acetone at the perimeter of the bond did not yield any weakening of bond.

While test pieces were bonded, Koji was making some adjustments to the cavity alignment in preparation for gluing of the steering mirror BS1.

Koji noticed that the spring clamp was causing pitch in the BS1 mirror, so he recommended that we utilize the "restrain by allen key" technique to load the mirror during curing.

Once aligned, we tried taking the BS1 mirror out of the template and then putting it back. We did this twice and both times the cavity needed realigning (with the curved mirrors as well as the input steering periscope). Why is this? Since the mirror was touching the template it should not have become misaligned right? Maybe the template moves slightly? I think before glueing in the cavity mirrors we should find out why probably? Koji took a look and claimed that a few optics may have been unconstrained. 

Planning between Koji and Joe led to placement of 5 drops of epoxy on the BS1 surface, to match the bonding area. At this point we noticed that the template was not secured very well, by poking down on it we could see it move. This might explain why we are becoming misaligned very easily. Once the prism was back on the board, Koji used allen keys to move around the prism. This was done until we could align it again (i.t looked too pitched). The beam was aligned back into the cavity, and the UV light was used to cure the bond. The reflected DC when locked was

  • pre-cured = 47mV
  • cured = 55 mV

so it looks ok still.

 

 

 

  355   Thu Apr 25 15:05:19 2019 JoeOpticsCharacterizationLooking at PZT HOM spacing dependance and thinking about workflow

[koji, joe]

The template or glass breadboard was wobbling, and we noticed that the caivty alignment became worse/better when it was pressed down. We saw that it was the glass breadboard, so it was fixed into the transport fixture more securely. Now its alignement didn't change when it was pressed down. We took a pzt mirror out and replaced it, the alignment din't change much so that was good. We set up posts to hold the pzt wires.

We noticed that the bottom of the mirrors were dirty, so we cleaned them, and once we were happy with the newton rings, we aligned the cavity

Took a photo of CM2, the spot is maybe 1 beam diameter vertically and horizontally from the centre, and quite a bright spot could be seen. The same problem with CM1. We thought it would be good to see a measurement of higher order mode spacing dependence on PZT DC voltage rather than doing the full characterisation since the alignment seems to change quite a lot when ever we do anything, and this cavity arrangement probably isn't very good anyway (can see scattering on both curved mirrors with the IR camera). 

did measurements of FSR, = 2.64835MHz

did HOM spacing for 0,75,150V on CM1 in pitch and yaw.

we want to come up with a work flow for how to do these measurements, and make automate parts of the analysis?

 

  356   Wed May 1 15:40:46 2019 KojiOpticsCharacterizationOMC(004): Spot positions and the scattering

Tried a few things.

1. Replaced CM1 (PZT ASSY #10=M21+PZT#22+C12) with PZT ASSY #7 (=M1+PZT#13+C13)

We tried PZT ASSY #7 at the beginning and had the spots at almost at the top edge of the curved mirrors. As we found a particle on the bottom of the M1 prism (and removed it), I gave it a try again. Resulting spots are again very high. This results in rejecting PZT ASSY #7 and we set the combination of the PZT ASSYs as #8 (M7+P11+C11) and #10 (M21+P22+C12). This combination nominally gives the spot ~1mm above the center of the curved mirrors.

2. Swapped FM1 and FM2. Now FM1=A5 and FM2=A14.

No significant change of the scattering features on the FMs. The transmitted power was 14.85mW (Ref PD Vin = 3.42V), Reflection PD Vrefl,lock = 54.3mV and Vrefl,unlock = 2.89V (Vin=3.45V), Vrefl,offset = -6.39mV. The incident power was 17.43mW (Vin 3.69V).

==> Coupling 0.979 , OMC transmission 0.939 (This includes 0.6% loss to the QPD path) ...Not so great number

3. Built better camera setups to check the spot position and the scattering from the cavity mirrors.

Now the spot heights are fixed and safe to move the camera up for inches to obtain better views of the mirror faces. The camera was set 15" away from the mirrors with 1.5" height from the beam elevation. This is 0.1rad (~ 5 deg) and Cos(0.1)~0.995 so the distortion (compression) of the view is negligible. (Attachment) The spot photo were taken with the fixed CCD gain, the focus on the glass, and  lens aperture F=8.0. Later the focus and aperture were adjusted to have clear view of the scattring points.

The intensity of each scattering was constant at different views. I suppose this is because the scattering is coming from a spot smaller than the wavelength. The bright spots does not show any visible feature on the mirror surfaces when they were inspected with a green flash light.

CM2 has the excellent darkness and we want to keep this spot position. FM1, FM2, and CM1 showed bright scattering.

The spot at CM1 is not well centered on the mirror. And this is the way to avoid this scattering point. So let's think about to move the spot on CM1 by 1.3mm towards the center while the spot on the CM2 is fixed. Note that this is going to be done by the micrometers for CM1 and CM2.

By turning right micrometer of CM1 forward (50um = 5div = 1/10 turn) and the left micrometer of CM2 backward (60um = 6div) moves the spots on FM1, FM2, CM1, and CM2 by (0.43, 0.87, 1.3, 0)mm. This basically moves the spots toward the center of each mirror. Let's give it a try.

 

Attachment 1: misalignment.pdf
misalignment.pdf misalignment.pdf
  357   Fri May 3 11:06:28 2019 KojiOpticsCharacterizationOMC(004): Spot positions and the scattering

Experiment on 5/1
- CM1 right knob was moved 1div (10um) backward such that the spots were better centered on the mirrors 

FM1 (A5): h=-0.2mm -> 0.4mm made the spot much darker but still it has a few scattering spots.
FM2 (A14): h=-0.8mm -> 0.2mm reduced the number of spots from 2 to 1. And it is darker. The remaining spot at the center.
CM1 (C11): h=-1.3mm -> +1.0mm made the spot much darker.
CM2 (C12): h=-0.7mm -> +0.2mm remains dark.

Note: CM1 h=1mm and CM2 h~0mm are good locations. h+ is the good direction to move. Avoid h-.
FM1 and FM2 has the scat spots at the center. Want to go h+ more.

Uniformly go h+ is the good move. => This can be done by rotate CM1 positive => CM1 right knob CCW.

2019/5/1 CM1 right micrometer 1div backward
         
    Unit   V_RefPD [V]
P_TRANS 13.53 [mW]   3.09
V_REFL_LOCKED 53.4 [mV]   3.09
V_REFL_UNLOCK 2.52 [V]   3.065
P_IN 14.45 [mW]   3.07
V_REFL_OFFSET -6.35 [mV]    
         
Coupling 0.977      
OMC_Trans 0.953      

Improvement of the transmission from 93.9%->95.3%


- Further moved CM1 right knob 0.5div (0.5um) backward such that the spots were moved to h+ directions.
FM1 (A5): h=0.4mm -> 1.1mm (there is only one spot rather than multiple spots)
FM2 (A14): h=0.2mm -> 1.1mm (darker but multiple spots)
CM1 (C11): h=1.0mm -> 1.8mm (brighter but single spot)
CM2 (C12): h=0.2mm -> 1.5mm (dark multiple spots)

2019/5/1 CM1 right micrometer 0.5div backward
         
    Unit   V_RefPD [V]
P_TRANS 14.55 [mW]   3.28
V_REFL_LOCKED 49 [mV]   3.28
V_REFL_UNLOCK 2.755 [V]   3.299
P_IN 15.64 [mW]   3.3
V_REFL_OFFSET -6.316 [mV]    
         
Coupling 0.980      
OMC_Trans 0.955      

Not much improvement of the transmission but kept 95% level.

- Replaced FM1 (A5) with A1 mirror (No photo)

Good news: This did not change the cavity alignment at all.

Transmission 95.4%

- Tweaked the CM1 angle

Transmission 95.3%

=> A1 mirror does not improve the transmission much.


Next Plan: Use A5 (or something else) as FM2 and see if A14 caused the dominant loss.

Attachment 1: misalignment.pdf
misalignment.pdf misalignment.pdf misalignment.pdf
  360   Thu May 9 18:10:24 2019 KojiOpticsCharacterizationOMC(004): Spot position scan / power budget

(Now the CCD image is captured as a movie and the screen capture is easier!)

Various spot positions on CM1 and CM2 were tried to test how the transmission is dependent on the spot positions. CM1 has a few bright spots while CM2 shows very dark scattering most of the case. Attachment 1 is the example images of one of the best alignment that realized the transmission of ~96%. FM1 and FM2 also showed bright spots. The replacement of the FM mirrors does not improve nor degrade the transmission significantly. The transmission is still sensitive to the spot positions on the alignment. This indicates that the loss is likely to be limited by CM1.

Attachment 2 shows the distribution of the (known) scattering spots on CM1. The bright spots are distributed every ~1mm on the spot height and the beam (with beam radius of .5mmm) can't find a place where there is no prominent spots.

We will be able to examine if the transmission can be improved or not by replacing this CM1 mirror.

Attachment 1: 190508.png
190508.png
Attachment 2: scattering_spots_CM1.png
scattering_spots_CM1.png
  365   Thu May 23 01:42:46 2019 KojiOpticsCharacterizationC30665 high power test

An Excelitas C30665 PD with the cap removed (SN07 in Case H slot #2) was exposed to the beam with the optical power of 1.4mW to 334mW.
After each illumination, the dark current and the dark noise level were tested. Also the photo image of the PD surface was taken each time.

- No significant change of the dark current after each illumination.

- No significant change of the dark noise after each illumination.

- No visible change of the surface observed.

 

Attachment 1: C30665_high_power_test.pdf
C30665_high_power_test.pdf
Attachment 2: pd_surface.jpg
pd_surface.jpg
  366   Thu May 23 23:27:38 2019 KojiOpticsCharacterizationIGHQEX3000 high power test

LaserComponents IGHQEX3000 (Cage B2: Serial# B1-23) was exposed to the beam with the optical power from 1.6mW to 332mW.
After each illumination, the dark current and the dark noise level were measured. Also the photo image of the PD surface was taken each time.

- No significant change of the dark current after each illumination.

- No significant change of the dark noise after each illumination.

- No visible change of the surface observed.

(During this dark noise measurement, the current amp gain was set to be 1e8 V/A, instead of 1e7 for the measurements yesterday.)

Attachment 1: HQEPD_high_power_test.pdf
HQEPD_high_power_test.pdf
Attachment 2: pd_images.png
pd_images.png
  369   Mon Jul 1 12:38:49 2019 KojiOpticsCharacterizationA and M prisms perpendicularity measurement

[Stephen, Koji]

The perpendicularity of some of the A and M prisms were tested.

Results

- The measurement results are listed as Attachment 1 and 2 together with the comparisons to the measurement in 2013 and the spec provided from the vendor.
- Here, the positive number means that the front side of the prism has larger angle than 90deg for the air side. (i.e. positive number = facing up)
- The RoC of the curved mirrors is 2.5m. Therefore, roughly speaking, 83arcsec corresponds to ~1mm beam spot shift. The requirement is 30 arcsec.
- The A prisms tend to have positive and small angle deviations while the M prisms to have negative and large (~50arcsec) angle deviations.
- The consistency: The measurements in 2013 and 2019 have some descrepancy but not too big. This variation tells us the reliability of the measurements, say +/-30arcsec.

Setup

- The photos of the setup is shown as Attachments 3/4/5. Basically this follows the procedure described in Sec 2.2.2 of T1500060.
- The autocollimator (AC) is held with the V holders + posts.
- The periscope post for the turning Al mirror was brought from Downs by Stephen.
- The turning mirror is a 2" Al mirror. The alignment of the turning mirror was initially aligned using the retroreflection to the AC. Then the pitching of the holder was rotated by 22.5deg so that the AC beam goes down to the prism.
- The prism is held on a Al mirror using the post taken from a prism mount.
- If the maximum illumination (8V) is used, the greenish light becomes visible and the alignment becomes easier.
- There are two reflections 1) The beam which hits the prism first, and then the bottom mirror second, 2) The beam which hits the bottom mirror first and then the prism second. Each beam gains 2 theta compared to the perfect retroreflection case. Therefore the two beams have 4 theta of their relative angle difference. The AC is calibrated to detect 2 theta and tells you theta (1div = 1 arcmin = 60 arcsec). So just read the angle defferencein the AC and divide the number by 2 (not 4).

Attachment 1: A_prism.png
A_prism.png
Attachment 2: M_prism.png
M_prism.png
Attachment 3: P_20190627_222658.jpg
P_20190627_222658.jpg
Attachment 4: setup2.JPG
setup2.JPG
Attachment 5: M01_1_id.JPG
M01_1_id.JPG
Attachment 6: A14_meas.JPG
A14_meas.JPG
  370   Mon Jul 1 12:49:42 2019 KojiOpticsCharacterizationScattering measurement of A and C mirrors

Liyuan's scattering measurement for the A and C mirrors.

Attachment 1: omc_cm_tis_062419.pdf
omc_cm_tis_062419.pdf omc_cm_tis_062419.pdf
Attachment 2: omc_prism_tis_062419.pdf
omc_prism_tis_062419.pdf omc_prism_tis_062419.pdf omc_prism_tis_062419.pdf
  371   Thu Aug 22 12:35:53 2019 StephenOpticsCharacterizationWedging of the debonded PZTs 2019 August

Wedge and thickness measurements of PZTs 12 and 13 took place after debonding and cleaning - results are shown in the first image (handwritten post-it format).

These thickness measurements seem to have come back thinner than previous measurements. It is possible that I have removed some PZT material while mechanically removing glue. It is also possible that there is systematic error between the two sets of measurements. I did not run any calculations of wedge ange or orientation on these data.

Note that cleaning of debonded PZTs involved mechanically separating glue from the planar faces of PZTs. The second image shows the razer blade used to scrape the glue away.

There were thick rings of glue where there had been excess squeezed out of the bond region, and there was also a difficult-to-remove bond layer that was thinner. I observed the presence of the thin layer by its reflectivity. The thick glue came off in patches, while the thin glue came off with a bit of a powdery appearance. It was hard to be certain that all of the thin bond layer came off, but I made many passes on each of the faces of the 2 PZTs that had been in the bonded CM assemblies. I found it was easiest to remove the glue in the bonded

I was anticipating that the expected 75-90 micron bond layer would affect the micrometer thickness measurements if it was still present, but I did not notice any irregularities (and certainly not at the 10 micron level), indicating that the glue was removed successfully (at least to the ~1 micron level).

 

Quote:

Yesterday I measured the thickness of the PZTs in order to get an idea how much the PZTs are wedged.

For each PZT, the thickness at six points along the ring was measured with a micrometer gauge.
The orientation of the PZT was recognized by the wire direction and a black marking to indicate the polarity.

A least square fitting of these six points determines the most likely PZT plane.
Note that the measured numbers are assumed to be the thickness at the inner rim of the ring
as the micrometer can only measure the maximum thickness of a region and the inner rim has the largest effect on the wedge angle.
The inner diameter of the ring is 9mm.



The measurements show all PZTs have thickness variation of 3um maximum.

The estimated wedge angles are distributed from 8 to 26 arcsec. The directions of the wedges seem to be random
(i.e. not associated with the wires)



As wedging of 30 arcsec causes at most ~0.3mm spot shift of the cavity (easy to remember),
the wedging of the PZTs is not critical by itself. Also, this number can be reduced by choosing the PZT orientations
based on the estimated wedge directions --- as long as we can believe the measurements.



Next step is to locate the minima of each curved mirror. Do you have any idea how to measure them?

 

Attachment 1: IMG_4775.JPG
IMG_4775.JPG
Attachment 2: IMG_4770.JPG
IMG_4770.JPG
ELOG V3.1.3-