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ID Date Author Type Categoryup Subject
  12086   Thu Apr 21 15:12:38 2016 SteveUpdateVACRGA is not working

 

Quote:

Steve pointed out that in the aftermath of the Nitrogen running out a couple of times last week, the RGA had shut itself off thinking that there was a leak and so it was not performing the scheduled scans once a day. So the data files from the scheduled scans were empty in the /opt/rtcds/caltech/c1/scripts/RGA/logs directory. The wiki page for getting it up and running again is up-to-date, but the script RGAset.py did not exist on the c0rga machine, which the RGA is communicating with via serial port. I copied over the script RGAset.py from rossa to c0rga and ran the script on that machine - but the error flags it returned were not all 0 (indicating some error according to the manual) - so I edited the script to send just the initialize command ('IN0') and commented out the other commands, after which I got error flags which were all 0. After this, I ran a manual scan using 'RGAlogger.py', and it appears that the RGA is now able to take scans again - I'm attaching a plot of the scan results. We've saved this scan as a reference to compare against after a few days. 

Our last RGA scan is from February 14, 2016  We had a power outage on the 15th

Gautom has not succeded  reseting it. The old c0rga computer looks dead. Q may resurrect it, if he can?

  12115   Wed May 11 16:39:01 2016 ericqUpdateVACc0rga alive, output wonky
Quote:

Our last RGA scan is from February 14, 2016  We had a power outage on the 15th

Gautom has not succeded  reseting it. The old c0rga computer looks dead. Q may resurrect it, if he can?

The c0rga computer was off, I turned it on via front panel button. After running RGAset.py, RGAlogger.py seems to run. However, there are error messages in the output of the plotrgascan MATLAB script; evidiently there are some negative/bogus values in the output. 

I'll look into it more tomorrow.

  12116   Thu May 12 14:29:58 2016 gautamUpdateVACRGA back up and running

It looks like the hardware reset did the trick. Previously, I had just tried ssh-ing into c0rga and rebooting it. At the time, however, Steve and I noticed that the various LEDs on the RGA unit weren't on, as they are supposed to be in the nominal operating state. Today, Steve reported that all LEDs except the RS232 one were on today, so I just tried following the steps in this elog again, looks like things are back up and running. I'm attaching a plot of the scan generated using plotrgascan MATLAB script, it looks comparable to the plot in elog 11697, which if I remember right, was acceptable.

Unless there is some reason we want to keep this c0rga machine, I will recommission one of the spare Raspberry Pis lying around to interface with the RGA scanner when I get the time...

Quote:
Quote:

Our last RGA scan is from February 14, 2016  We had a power outage on the 15th

Gautom has not succeded  reseting it. The old c0rga computer looks dead. Q may resurrect it, if he can?

The c0rga computer was off, I turned it on via front panel button. After running RGAset.py, RGAlogger.py seems to run. However, there are error messages in the output of the plotrgascan MATLAB script; evidiently there are some negative/bogus values in the output. 

I'll look into it more tomorrow.

This is a cold scan.

Attachment 1: RGAscan_12May2016.png
RGAscan_12May2016.png
  12117   Sun May 15 19:48:08 2016 SteveUpdateVACrun out of N2

3-4 hrs ago we run out of nitrogen. We are back to Vacuum Normal

 

 

Attachment 1: noN2.png
noN2.png
  12119   Tue May 17 14:46:51 2016 SteveUpdateVACRGA scan at day 595

We have good RGA scan now. There was no scan for 3 months.

Attachment 1: RGAscan595d.png
RGAscan595d.png
Attachment 2: pd78-560Hz-d600.png
pd78-560Hz-d600.png
  12174   Tue Jun 14 10:13:34 2016 SteveUpdateVACtemporary N2 supply line

The drill room floor will be retiled Thursday, June 16. Temporary nitrogen line set up will allow emptying the hole area.

 

Ifo room entry will be through control room.

 

Attachment 1: afterN2work.png
afterN2work.png
  12195   Fri Jun 17 15:22:31 2016 gautamUpdateVACN2 supply line restored after retiling
Quote:

The drill room floor will be retiled Thursday, June 16. Temporary nitrogen line set up will allow emptying the hole area.

 

Ifo room entry will be through control room.

 

The retiling work has finished, Steve and I restored the N2 supply configuration to its normal state. The sequence of steps followed was:

  1. Went to the X end and closed the following valves, roughly in this order: VAEE, VAEV, VABS, VABSCI, VASV, VASE, V4, V1.
  2. Checked the RPM on the various turbo pump controllers to make sure they were in their nominal states
  3. Disconnect the electrical connections to V1, V4, V5 and VA6 - just to make sure some spurious signal doesn't unintentionally open any of these valves while we are mucking around with the N2 supply
  4. Close the valves on the N2 cylinders in the drill room. Disconnect the temporary nitrogen line (at this point, the N2 pressure to the IFO valves goes down from ~7-PSI to 0), reconnect the old supply chain, taking care that we aren't unintentionally loosening any of the Swagelock connections while unscrewing stuff
  5. Replaced one of the N2 cylinders that was running low.
  6. Reopen the cylinders, restore N2 pressure to IFO valves to ~70PSI.
  7. Do steps 1-3 in reverse: i.e. reconnect power to all valves, open them in the reverse order we closed them while monitoring the state of the various turbo pumps. 
  8. Acknowledged the error message on the C0VAC medm screen

Note: the valve isolating the RGA automatically shutoff during this work, possibly because it detected a pressure above its threshold - after checking the appropriate pressure gauges, we reopened this valve as well. 

The attached screenshot suggests that everything went as planned and that the vacuum system is back to normal...

 

 

Attachment 1: c0vac_06172016.png
c0vac_06172016.png
  12237   Fri Jul 1 09:20:44 2016 SteveUpdateVACvent 78

  VENT OBJECTIVES:

1, Fix ETMX sus "jump issue"

2, First Contact clean the arms

3, Install new spare cold cathode and convectron gauges: InstruTech-Hornet

4, Install 50 mm apeture beam baffles

5, Check and clean optical quality viewport from inside

 

The following bullets were executed:

  • Closed shutter of PSL-IR and green shutters at the ends 
  • Checked jam nuts are protecting bellows 
  • Check crane functionality & cleanliness last week

  • Particle count must be under 10,000 counts / cf min for 0.5 micron 
  • Checked all metal window covers are on. 
  • Check 5 cylinders (24 cft size) of instrument grade air, called Alfa Gas 1 in stock.
  • Took pictures of medm screens: sus-sum, aligned oplevs pos, alignment values and vac configuration
  • Turned Oplev servos off
  • Closed V1 and VM1, opened VM2
  • Opened VV1 manual valve to Nitrogen cylinder and let the P1 to rise to 25 Torr
  • Switched over to Instrument Grade Air Cylinder and continoed the vent with 8-10 PSI reading at the pressure regulator

We are venting the 40m IFO

     

Quote:

Steve has ordered some teflon parts to take the place of the metal parts in his acetone-soaking jig. They should arrive tomorrow. 

So, we will be begin the venting process tomorrow. Doors to come off on Tuesday.

 

Attachment 1: vent78.png
vent78.png
Attachment 2: vent78at250T.png
vent78at250T.png
  12238   Fri Jul 1 15:48:10 2016 SteveUpdateVACvent 78 at 710 Torr

I just disconnected the 6th instrument grade air cylinder from the vacuum envelope at 720 Torr. Now it will reach equilibrium through a filter as it sucks in lab air.

This is the sure way not to over pressurize the chamber.

 

Attachment 1: pd78at710T.png
pd78at710T.png
  12248   Wed Jul 6 08:34:00 2016 SteveUpdateVACRGA scan at day 639

The last RGA scan of this pumpdown 78

Pressure plot of 640 days long pd 78

CC1 cold cathode gauge was jump started with an accidental pressure glitch, that you can see on P1 plot

 

Attachment 1: RGAscan639d.png
RGAscan639d.png
Attachment 2: pd78d640.png
pd78d640.png
  12250   Wed Jul 6 10:58:07 2016 SteveUpdateVACvent 78 valve configuration

Vacuum Status: Chamber Open

All chamber annuloses are vented.  Vac Monitor screen is not communicating with gauges. The valve position indicator are working.

RGA is pumped by Maglev through VM2

 

Attachment 1: CamberOpen.png
CamberOpen.png
  12293   Tue Jul 12 18:13:19 2016 KojiUpdateVACN2 bottle replaced

Gautam, Koji

We replaced the right N2 bottle as it was empty.

  12314   Wed Jul 20 11:39:07 2016 SteveUpdateVACvent 78 day 20

RGA background scan

Quote:

Vacuum Status: Chamber Open

All chamber annuloses are vented.  Vac Monitor screen is not communicating with gauges. The valve position indicator are working.

RGA is pumped by Maglev through VM2

 

 

Attachment 1: vent78-d20.png
vent78-d20.png
  12337   Tue Jul 26 14:24:38 2016 KojiSummaryVACPurge compressed air system at LHO

I've visited the purge clean air system at LHO Yarm mid-station with John Worden.

The system is described C981637. There is a schematic in C981637-06-V (Vol.6).pdf although the schematic has some differences (or uncorrected mistakes).

This system is intended to provide positive pressure when a soft cover is attached to a chamber door. When the door is open, the purging does not help to keep the chamber clean because the flow is too slow. This protection has to be done with overhead HEPA filters (22x5000cfm). It may be possible that this purge air helps the tube not to allow dusts to come in. But before using this, the chambers and the tubes have to be cleaned, according to John.


- Here at the site, the purge air system is started up a day before the vent. This system is used for the vent air, the purge air, and turbo foreline filling.

- Air intake (attachment 1): At the site, the air is intaken from the VEA. We want to incorporate somewhat clean air instead of dirty, dusty, outside air.

- Initial filter (attachment 2): a high volume filter before the compressors.

- The compressors (attachment 3, 4) are 5x 6 horse power air compressor each goes up to 160 psi. They are turned on and off depending on the demand of the air. Which is turned on is revolved by the controller to equalize the compressor usage hours.

- The compressed air goes through the air cooler (heat exchanger) to remove the heat by the compressor work.

- This air goes through prefilters and accumulated in the air receiver (100psi) (attachment 5). This receiver tank has an automated vent valve for periodical water drainage at the bottom.

- The accumulated air is discharged to twin drier towers (attachment 6, blue). The tower is operated by the controller (attachment 7) alternately with a period of 4min (or 10min by setting). When one of the towers is working, a humid air comes from the bottom and the dry air is discharged from the top. A part of the dry air goes into the other tower from the top to the bottom and dries the tower. There is a vent at the bottom to discharge water periodically.

- The dried air goes through 4 types of filters. After the last filter, all of the plumbing should be made of stainless steel to keep cleanliness.

- The air goes to the pressure reducing regulator (attachment 8, gray). The final flow speed at the chamber side is 50cfm max, according to John.

- The lower pressure air goes through the final filter (attachment 8, blue). As the pressure is low, this filter is big in order to keep the volume of the air flow.

- The purge air is supplied to the chamber side with KF50 (attachment 9). There is a vent valve (attachment 10) for safety and also to run a dry air for at least a day before the use to clean up the supply line. The purge line is disconnected when no in use.

- The entire system (attachment 11) and size comparison (attachment 12).

 

Attachment 1: air_intake.jpg
air_intake.jpg
Attachment 2: initial_filter.jpg
initial_filter.jpg
Attachment 3: compressors1.jpg
compressors1.jpg
Attachment 4: compressors2.jpg
compressors2.jpg
Attachment 5: air_receiver_dryer.jpg
air_receiver_dryer.jpg
Attachment 6: drier.jpg
drier.jpg
Attachment 7: drier_controller2.jpg
drier_controller2.jpg
Attachment 8: pressure_regulator_and_last_filter.jpg
pressure_regulator_and_last_filter.jpg
Attachment 9: chamber_side_supply.jpg
chamber_side_supply.jpg
Attachment 10: vent_valve_for_line_cleaning.jpg
vent_valve_for_line_cleaning.jpg
Attachment 11: the_whole_system.jpg
the_whole_system.jpg
Attachment 12: size_comparison.jpg
size_comparison.jpg
  12338   Tue Jul 26 16:01:32 2016 SteveSummaryVACPurge compressed air system

Thanks for checking this out Koji

The builder in 1996 was Process System International, Inc ( Westborough, MA ) It does not exist any longer or I just could not find them. Flow diagramm at Atm1

Should I be keep looking for a company who could quote us for building a similar smaller unit with 10 - 15 cfm flowrate?

Note: my intension with the two mobile-overhead HEPA filter was the same as John Worden's " clean air overpressured tent " at chamber entrance.

Atm2, Our unit has 650 cfm, velocity 90 fpm at resistance 0.5"    It may be enough to give a little overpressure if we seal it well to the chamber

We use to use them to minimize dirt getting inside the chanbers.

Attachment 1: cleanAirSupl.pdf
cleanAirSupl.pdf
Attachment 2: mobileHEPA.jpg
mobileHEPA.jpg
  12339   Tue Jul 26 17:41:59 2016 KojiSummaryVACPurge compressed air system

We have no number for the CFM without calculation. We can't assume a random number like 10-15

  12483   Mon Sep 12 17:54:24 2016 SteveUpdateVACpumpdown 79

 We are pumping down. The annuloses are below 10 mTorr

The vacuum gauges are not communicating with the medm so there is no plot available.

The main volume pumping is stopped at P1 = 220 Torr  ( New SuperBee 174 Torr ) for overnight.

note: SuperBee was reading 791 Torr at atm and it was not set to 760 !

  12487   Tue Sep 13 16:16:28 2016 ChrisOmnistructureVACvacuum interlock bypassed

(Steve, Chris)

The pumpdown had stalled because of some ancient vacuum interlock code that prevented opening the valve V1 between the turbo pump and the main volume.

This interlock [0] compares the channels C1:Vac-P1_pressure and C1:Vac-PTP1_pressure, neither of which is functioning at the moment. The P1 channel apparently stopped reading sometime during the vent, and contained a value of ~700 torr, while the PTP1 channel contained 0. So the interlock code saw this huge apparent pressure difference and refused to move the valve.

To bypass this check, we used caput to enter a pressure of 0 for P1.

[0] /cvs/cds/caltech/state/from_luna/VacInterlock.st

  12488   Tue Sep 13 17:47:04 2016 SteveUpdateVACpumpdown 79 completed

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is off, not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

Quote:

(Steve, Chris)

The pumpdown had stalled because of some ancient vacuum interlock code that prevented opening the valve V1 between the turbo pump and the main volume.

This interlock [0] compares the channels C1:Vac-P1_pressure and C1:Vac-PTP1_pressure, neither of which is functioning at the moment. The P1 channel apparently stopped reading sometime during the vent, and contained a value of ~700 torr, while the PTP1 channel contained 0. So the interlock code saw this huge apparent pressure difference and refused to move the valve.

To bypass this check, we used caput to enter a pressure of 0 for P1.

[0] /cvs/cds/caltech/state/from_luna/VacInterlock.st

 

  12492   Wed Sep 14 09:44:09 2016 SteveUpdateVACpumpdown 79 completed

The pumpdown started at 9-12-2016

The IFO is at 5e-5 Torr vacuum normal after 73 day at atm.

ITMX needed to be freed and ETMY-UL is still misbehaving occasionally.

New pirani   and cold cathode gauges added at this vent. They were baked at 100 C for 6 hrs under vacuum.

Go to the Vac Rack to read IFO pressure from the gauge itself when Vac. Monitor is blank as it is now !

 

Quote:

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

 

 

Attachment 1: pd79.png
pd79.png
Attachment 2: pd79d2.jpg
pd79d2.jpg
Attachment 3: CCcg.jpg
CCcg.jpg
  12496   Thu Sep 15 10:36:32 2016 SteveUpdateVACpumpdown 79 day 3

IFO pressure 3.7e-5 Torr at new cold cathode InstruTech - Hornet

New items in vacuum:

1, ETMX sus tower with new baked sus wire, EP30-2 epoxied magnets, same at different locations also........ ..........  and 2 ruby wirestandoffs.

2, First Contact cleaned arm test masses only. This technic was a 1st time use in our vacuum system.

3, 50 mm ID green glass baffles at the ends

4, witness mirrors at ETMX and ITMY (old oplev mirrors) We observed a very dusty system: sides of optics, towers and tables were wiped. Hepa tents used at Y arm and BS

5, new pirani, cc gauge and 1.5" right angle valve

 

Quote:

The pumpdown started at 9-12-2016

The IFO is at 5e-5 Torr vacuum normal after 73 day at atm.

ITMX needed to be freed and ETMY-UL is still misbehaving occasionally.

New pirani   and cold cathode gauges added at this vent. They were baked at 100 C for 6 hrs under vacuum.

Go to the Vac Rack to read IFO pressure from the gauge itself when Vac. Monitor is blank as it is now !

 

Quote:

P1 IFO pressure is 1 mTorr, valve configuration: vacuum normal, annulosses are pumped, RGA is not pumped.

THANKS to Chris !

The shutters can be opened with high power.

No communication error message still exist.

I will reboot c1vac1 and c1vac2 to get gauge communication with medm tomorrow.

 

 

 

 

Attachment 1: vent78for73d.png
vent78for73d.png
  12525   Fri Sep 30 10:37:57 2016 SteveUpdateVACvacuum VME machines rebooted

[ Gautam and Steve ]

c1vac1 and c1vac2 were rebooted and the gauges are communicating now. V1, VA6, V5 and V4 were closed and disconnected to avoid unexpected valve switching. All went smoothly.

The new ITcc gauge is at 1e-5 Torr as CC1   This is the gauge that should be logged in slow channel.

TP2 fore line dry pump was replaced this morning after 382 day of operation.

TP3 dry pump is very noisy, but it's pressure still 47 mTorr

Quote:

[ericq, Gautam, Steve]

Following roughly the same procedure as ELOG 11354, c1vac1 and c1vac2 were rebooted. The symptoms were identical to the situation in that ELOG; c1vac1 could be pinged and telneted to, but c1vac2 was totally unresponsive. 

The only change in the linked procedure was that we did not shut down the maglev. Since I unwittingly had it running for days without V4 open while Steve was away, we now know that it can handle shorter periods of time than that...

Upon reboot, many channels were readable again, unfortunately the channels for TP2 and TP3 are still blank. We were able to return to "Vacuum normal state," but because of unknowned communication problems with VM1's interlock, we can't open VM1 for the RGA. Instead we opened VM2 to expose the RGA to the main IFO volumn, but this isn't part of the "Normal" state definite, so things currently read "Undefined state".

 

Attachment 1: rebooted.png
rebooted.png
  12530   Tue Oct 4 11:02:31 2016 SteveUpdateVACRGA is out of order

The last good rga scan at vent 78  day 38

Quote:

 

Quote:

RGA background scan

Quote:

Vacuum Status: Chamber Open

All chamber annuloses are vented.  Vac Monitor screen is not communicating with gauges. The valve position indicator are working.

RGA is pumped by Maglev through VM2

 

 

 

 

Attachment 1: lastBGscan.png
lastBGscan.png
  12537   Fri Oct 7 10:29:57 2016 SteveUpdateVACRGA removed

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

Attachment 1: RGAremoved.png
RGAremoved.png
  12556   Thu Oct 13 00:23:54 2016 ericqUpdateVACPre-vent prep

I have completed the following non-Steve portions of the pre-vent checklist [wiki-40m.ligo.caltech.edu]

  • Center all oplevs, transom QPDs (and IPPOS + IPANG if they are set up)
  • Align the arm cavities for IR and align the green lasers to the arms.
  • Update the SUS Driftmon values
  • Reconcile all SDF differences
  • Reduce input power to no more than 100mW (measured at the PSL shutter) by adjusting wave plate+PBS setup on the PSL table BEFORE the PMC. (Using the WP + PBS that already exist after the laser.)
  • Replace 10% BS before MC REFL PD with Y1 mirror and lock MC at low power.
  • Close shutter of PSL-IR and green shutters at the ends

All shutters are closed. Ready for Steve to check nuts and begin venting!

  12559   Thu Oct 13 16:48:34 2016 SteveUpdateVACvent 79 is completed

IFO is at atmosphere. The MC can be locked in air now.

The doors will be coming off tomorrow 8am sharp.

Do we want to install the ITM baffles?

What about the found OSEM filters?

 

Attachment 1: vent_79.png
vent_79.png
  12574   Thu Oct 20 09:17:08 2016 SteveUpdateVACPumpdown 80 has started

Pumping again after 7 days at atmosphere.

BS, ITMY and OMC chambers were open only.

Checked: jam nuts, viewport covers and beam shutters.

Oplev servo turned off and medm screens shots taken.

New item in vacuum:  green shade 14 glass beam block at IR-input [ from the PSL ] viewport to block green reflection-scatter.

Reminder: viewport is not AR coated for green!

 

 

 

Attachment 1: readyPd80.png
readyPd80.png
Attachment 2: beforePd80.png
beforePd80.png
Attachment 3: pd80at1h.png
pd80at1h.png
Attachment 4: 7d_atm.png
7d_atm.png
  12575   Thu Oct 20 15:59:52 2016 SteveUpdateVACPumpdown 80 has completed

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

Attachment 1: 7hPd80.png
7hPd80.png
Attachment 2: 8hPd80.png
8hPd80.png
Attachment 3: 9hPd80.png
9hPd80.png
  12577   Fri Oct 21 09:28:21 2016 SteveUpdateVACVac Normal reached

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

Attachment 1: VacNormal.png
VacNormal.png
  12589   Mon Oct 31 16:20:50 2016 SteveUpdateVACRGA is reinstalled

Quad rods and  ionizer kit: consisting of repeller cage, anode grid, focus plate and  filament were replaced....... under repair # RGA200/12 ECA 100416-12967

The electronic ECU is not connected. It is beeing pumped at IFO ITcc 9.7E-6 Torr vacNormal

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

  12633   Tue Nov 22 11:31:52 2016 SteveUpdateVACRGA is running again

The Rga was turned on yesterday.

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

Attachment 1: RGAisBack33d.png
RGAisBack33d.png
Attachment 2: pd80-560Hz-d33.png
pd80-560Hz-d33.png
Attachment 3: afterRepair1d.png
afterRepair1d.png
  12636   Wed Nov 23 11:32:13 2016 SteveUpdateVACTP3 drypump replaced again

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

  12642   Mon Nov 28 09:45:44 2016 SteveUpdateVACRGA scan at pumpdown day 40

The vacuum envelope ~1 C warmer today than 7 days ago. Bad peaks are coming down as normal.

 

Attachment 1: RGAscan_d40.png
RGAscan_d40.png
Attachment 2: d2_&_d7scan.png
d2_&_d7scan.png
Attachment 3: RGAd2.png
RGAd2.png
  12681   Thu Dec 22 09:37:20 2016 SteveUpdateVACRGA scan at day 63

Valve configuration: vacuum normal

RGA head temp: 43.5 C

Vac envelope temp: 23 C

 

Attachment 1: pd80-d63.png
pd80-d63.png
Attachment 2: pd80-580Hz-d63.png
pd80-580Hz-d63.png
  12698   Tue Jan 10 14:24:09 2017 SteveUpdateVACRGA scan at day 82

Valve configuration: vacuum normal

Vacuum envelope: 23C

Rga head: 44C

 

Attachment 1: pd80VNd82.png
pd80VNd82.png
  12774   Tue Jan 31 14:14:29 2017 ranaUpdateVACPressure watch script

I think this cron job is running on NODUS (our gateway) instead of our scripts machine:

*/1 * * * * /opt/rtcds/caltech/c1/scripts/Admin/n2Check.sh >> /opt/rtcds/caltech/c1/scripts/Admin/n2Check.log 2>&1

Quote:

Based on Jenne's chiara disk usage monitoring script, I made a script that checks the N2 pressure, which will send an email to myself, Jenne, Rana, Koji, and Steve, should the pressure fall below 60psi. I also updated the chiara disk checking script to work on the new Nodus setup. I tested the two, only emailing myself, and they appear to work as expected. 

The scripts are committed to the svn. Nodus' crontab now includes these two scripts, as well as the crontab backup script. (It occurs to me that the crontab backup script could be a little smarter, only backing it up if a change is made, but the archive is only a few MB, so it's probably not so important...)

moreover this script has a 90MB log file full of not finding its channel

I wish this script was in python instead of BASH and I wish it would run on megatron instead of nodus (why can't megatron send us email too?) and I wish that this log file would get wiped out once in awhile. Currently its been spitting out errors since at least a month ago:

Tue Jan 31 14:10:02 PST 2017 : N2 Pressure:

Channel connect timed out: 'C1:Vac-N2pres' not found.

(standard_in) 1: syntax error

  12853   Mon Feb 27 15:33:10 2017 SteveUpdateVACRGA scan at day 130

Valve configuration: vacuum normal

Vacuum envelope: 23.5 C

RGA head: 46.6 C

 

Attachment 1: rgascan@130d.png
rgascan@130d.png
  13047   Wed Jun 7 11:32:56 2017 SteveUpdateVACsmooth vac reboot

Gautam and Steve,

 

The medm monitor & vac control screens were totally blank since ~ May 24, 2017    Experienced vacuum knowledge is required for this job.

IDENTIFY valve configuration:

                        How to confirm valve configuration when all vac mons are blank?  Each valve has a manual-mechanical position indicator. Look at pressure readings and turbo pump controllers. VAC NORMAL configuration was confirmed based on these information.

Preparation: disconnect valves ( disconnect meaning: valve closes and stays paralized ) in this sequence VC2, VC1 power, VA6, V5, V4 & V1 power,      at ifo pressure 7.3E-6 Torr-it  ( it  = InstruTech cold cathode gauge )

                            This gauge is independent from all other rack  mounted   instrumentation and it is still not logged.

                            Switching to this valve configuration with disconnected valves will insure NOT  venting of the vacuum envelope by accidental glitching voltage drop or computer malfunction.

RESET  v1Vac1 .........in 2-3 minutes........ ( v1Vac1 - 2 )  the vac control screen started reading pressures & position

                    Connected cables to valves (meaning: valve will open if it was open before it was disconnected and it will be control able from computer ) in the following order: V4, V1 power, V5, VA6, VC2 & VC1 power,      at ifo 2E-5 Torr-it.....

                     ....vac configuration is reading VAC NORMAL,

                     ifo 7.4E-6 Torr-it

We have to hook up the it-cold cathode gauge to be monitored - logged !  this should be the substitute for the out of order CC1 pressure gauge.

Attachment 1: vac_reboot.png
vac_reboot.png
  13075   Tue Jun 20 16:28:23 2017 SteveUpdateVACRGA scan
Attachment 1: RGAscan243d.png
RGAscan243d.png
Attachment 2: RGAscan.png
RGAscan.png
  13132   Sun Jul 23 15:00:28 2017 JamieOmnistructureVACstrange sound around X arm vacuum pumps

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

  13134   Mon Jul 24 09:55:29 2017 SteveOmnistructureVACcontroller failer

Ifo pressure was 5.5 mTorr this Monday morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Maglev got warm ~38C but it was still rotating at 560 Hz normal with closed V1

Pressure plots are not available because of computer problems.

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

Attachment 1: TP2controllerFails.png
TP2controllerFails.png
  13142   Tue Jul 25 08:48:57 2017 SteveUpdateVACRGA scan at d278

The RGA did not shut down at the turbo pump controller failing.

Quote:

Ifo pressure was 5.5 mTorr this morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Magelv got warm ~38C but it was still rotating at 560 Hz normal with closed V1

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

 

Attachment 1: RGA278d.png
RGA278d.png
  13143   Tue Jul 25 14:04:06 2017 SteveUpdateVACturbo controller installed and we are running at vac normal

Gautam and Steve,

Spare Varian turbo-V 70 controller, Model 969-9505, sn 21612 was swapped in. It is running the turbo fine @ 50Krpm but it does not allow it's V4 valve to be opened............

It turns out that TP2 @ 75Krpm will allow V4 to open and close. This must be a software issue.

So Vacuum Normal is operational if TP2 is running 75,000 rpm

We want to run at 50,000 rpm on the long term.

Note: the RS232 Dsub connector on the back of this controller is mounted 180 degrees opposite than TP3  and old failed TP2 controller

 

PS: controller is shipping out for repair 7-28-2017

 

Attachment 1: TP2@75Krpm.png
TP2@75Krpm.png
  13171   Tue Aug 8 17:04:26 2017 SteveUpdateVACunintended pump down

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

Attachment 1: pumping_down.png
pumping_down.png
  13172   Tue Aug 8 17:44:11 2017 SteveUpdateVACunintended pump down

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

Attachment 1: stopped_pumping.png
stopped_pumping.png
  13175   Wed Aug 9 11:59:51 2017 SteveUpdateVACunintended pump down at vacuum normal

pd80b has reached Vac Normal. IFO pressure 0.5 mTorr

We need our vauum channels back in dataviewer.

Quote:

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

 

Attachment 1: pdc.png
pdc.png
Attachment 2: pd80b@vacnormal.png
pd80b@vacnormal.png
  13179   Wed Aug 9 16:34:46 2017 ranaUpdateVACVacuum Document recovered

Steve and I found the previous draft of the 40m Vacuum Document. Someone in 2015 had browsed into the Docs history and then saved the old 2013 version as the current one.

We restored the version from 2014 which has all of Steve's edits. I have put that version (which is now the working copy) into the DCC:  https://dcc.ligo.org/E1500239.

The latest version is in our Google Docs place as usual. Steve is going to have a draft ready for us to ready be Tuesday, so please take a look then and we can discuss what needs doing at next Wednesday's 40m meeting.

  13186   Thu Aug 10 15:45:34 2017 SteveUpdateVACaccidental vent to 17 Torr

Finally we got the cold cathode gauge working. IFO pressure 7e-6 Torr-it, vacuum normal valve configuration with all 4 ion pump gate valves closed at ~ 9e-6 Torr.  The cryo pump was also pumped yesterday to remove the accumulated outgassing build up.

The accidental vent was my mistake; made when I was replacing the battery pack of the UPS. The installed pack measured 51 V without any load. The "replace battery" warning light did not go out after the batteries were replaced. 

I then mistakenly and repeatedly pushed the "test" button to reset this, but I did not wait long enough for the batterries to get fully charged. The test put the full load on the new batteries and their charging condition got worse. I made the mistake when trying to put the load from the battery to online and pushed "O" so the power was cut and the computer rebooted to the all off condition. On top of this, I disconnected the wrong V1 cable to close V1.  As the computer rebooted it's interlock closed V1 at 17 Torr.

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

Attachment 1: Mag_UPS.jpg
Mag_UPS.jpg
Attachment 2: UPSbatteryPack.jpg
UPSbatteryPack.jpg
Attachment 3: closing_V1.jpg
closing_V1.jpg
  13233   Mon Aug 21 14:53:32 2017 gautamUpdateVACRGA reset

[gautam, steve]

In the aftermath of the accidental vent, it looks like the RGA was shutdown.

We followed the instructions in this elog to restart the RGA.

Seems to be working now, Steve says we just need to wait for it to warm up before we can collect a reliable scan.

Quote:

We have good RGA scan now. There was no scan for 3 months.

 

  13234   Mon Aug 21 16:35:48 2017 gautamUpdateVACUPS checkup

[steve, gautam]

At Rolf/Rich Abbott's request, we performed a check of the UPS today.

Steve believed that the UPS was functioning as it should, and the recent accidental vent was because the UPS batteries were insufficiently charged when the test was performed. Today, we decided to try testing the UPS.

We first closed V1, VM1 and VA6 using the MEDM screen. We prepared to pull power on all these valves by loosening the power connections (but not detaching them). [During this process, I lost the screw holding the power cord fixed to the gate valve V1 - we are looking for a replacement right now but it seems to be an odd size. It is cable tied for now.]

The battery charge indicator LEDs on the UPS indicated that the batteries were fully charged.

Next, we hit the "Test" button on the UPS - it has to be held down for ~3 seconds for the test to be actually initiated, seems to be a safety feature of the UPS. Once the test is underway, the LED indicators on the UPS will indicate that the loading is on the UPS batteries. The test itself lasts for ~5seconds, after which the UPS automatically reverts to the nominal configuration of supplying power from the main line (no additional user input is required).

In this test, one of the five battery charge indicator LEDs went off (5 ON LEDs indicate full charge).

So on the basis of this test, it would seem that the UPS is functioning as expected. It remains to be investigated if the various hardware/software interlocks in place will initiate the right sequence of valve closures when required.


Quote:
 

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

 

ELOG V3.1.3-