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ID Date Author Type Category Subjectup
  12250   Wed Jul 6 10:58:07 2016 SteveUpdateVACvent 78 valve configuration

Vacuum Status: Chamber Open

All chamber annuloses are vented.  Vac Monitor screen is not communicating with gauges. The valve position indicator are working.

RGA is pumped by Maglev through VM2

 

  12238   Fri Jul 1 15:48:10 2016 SteveUpdateVACvent 78 at 710 Torr

I just disconnected the 6th instrument grade air cylinder from the vacuum envelope at 720 Torr. Now it will reach equilibrium through a filter as it sucks in lab air.

This is the sure way not to over pressurize the chamber.

 

  12559   Thu Oct 13 16:48:34 2016 SteveUpdateVACvent 79 is completed

IFO is at atmosphere. The MC can be locked in air now.

The doors will be coming off tomorrow 8am sharp.

Do we want to install the ITM baffles?

What about the found OSEM filters?

 

  12557   Thu Oct 13 09:30:38 2016 SteveUpdateGeneralvent 79 is happening
Quote:

I have completed the following non-Steve portions of the pre-vent checklist [wiki-40m.ligo.caltech.edu]

  • Center all oplevs, transom QPDs (and IPPOS + IPANG if they are set up)
  • Align the arm cavities for IR and align the green lasers to the arms.
  • Update the SUS Driftmon values
  • Reconcile all SDF differences
  • Reduce input power to no more than 100mW (measured at the PSL shutter) by adjusting wave plate+PBS setup on the PSL table BEFORE the PMC. (Using the WP + PBS that already exist after the laser.)
  • Replace 10% BS before MC REFL PD with Y1 mirror and lock MC at low power.
  • Close shutter of PSL-IR and green shutters at the ends

All shutters are closed. Ready for Steve to check nuts and begin venting!

- checked all jam nuts

- checked all viewports are covered

- turned oplev servos off

- took pictures of medm screens: sus summs, aligned oplev centering, IFO& MC alignment biases and vac configuration

- checked particle counts

- checked crane operational safety

- closed V1, VM1, annuloses

- opened VV1  and vented with Airgas brand, Industrial Grade Nitrogen [ 99.99% ] to 25 Torr

- switched over to Airgas brand compressed air, Alphagas " AI UZ300 "  with Total Hydro Carbon 0.1 PPM

  10536   Thu Sep 25 08:21:15 2014 SteveUpdateVACvent day 1

Quote:

[Steve, EricQ, Jenne]

ITMY and BS heavy doors are off, light doors are on.  Q is aligning the IFO.

 

  10542   Fri Sep 26 09:13:17 2014 SteveUpdateSUSvent day 2

 ITMY in vac table needs leveling.

  7594   Tue Oct 23 08:45:00 2012 SteveUpdateVACvent day 3

Quote:

Quote:

Quote:

Quote:

 

 PSL shutter closed, manual block in place, HV turned off. P1 is at 200 Torr now.  Jenne is taking over here.

 Valves closed, 500 torr.  Steve will finish off Monday morning, then we'll take off doors and get to work.

 We are almost at atm.  P1 750 Torr,  We are slowly reaching equilibrium.

 The access connector was removed, BS and ITMY chambers were opened yesterday.

New one piece aluminum shell access connector installed. Jenne lowered the PSL out put into MC to ~100mW

  10547   Mon Sep 29 09:11:25 2014 SteveUpdateVACvent day 5 RGA scan

 

 

  2635   Tue Feb 23 19:00:45 2010 kiwamuConfigurationVACvent finished

The vent has been finished.

Now the pressure inside the chamber is 760 torr, and it's getting equilibrium with the atmospheric pressure.

Therefore we are ready and can open the door of the chamber tomorrow.

  3259   Wed Jul 21 12:41:31 2010 kiwamuUpdateVACvent finished

The vent has been finished successfully in this morning.

The vent was finished successfully this morning.

  3266   Thu Jul 22 08:07:27 2010 steveUpdateVACvent finished

Quote:

The vent has been finished successfully in this morning.

The vent was finished successfully this morning.

 Thanks to Kiwamu, Alberto and Koji

  6889   Thu Jun 28 20:59:28 2012 yutaBureaucracyLockingvent for PRC check, TOMORROW!

Koji, Jamie and I talked together and I decided to VENT TOMORROW MORNING. Main purpose of this vent is to see if PRM is flipped or not.

Vent schedule:
June 28 (Thu)
  Prepare for the vent tonight

June 29 (Fri)
  Start vent in the morning
  Look into PRC in the evening. If PRM was flipped, we will correct them. We'll use REFL to align the PRM. If PRM was not flipped, look into PR2,PR3 and other related optics.

June 30 (Sat)
July 1 (Sun)
  Thinking time. I can work if needed.

July 2 (Mon)
  If we need something else to do, do it.
  If not, start pumping.
  July 4th is the Independence Day. So, I need IFO working before July 4th.

Check List:
 We will just open the BS chamber.
  - PRM flipping
  - PR2, PR3 flipping
  - PRC suspensions
  - Cipping check in PRC

  6890   Thu Jun 28 22:08:57 2012 JenneBureaucracyLockingvent for PRC check, TOMORROW!

Quote:

Check List:
 We will just open the BS chamber.
  - PRM flipping
  - PR2, PR3 flipping
  - PRC suspensions
  - Cipping check in PRC

 What do you mean by PR2, PR3 flipping?  They are (supposed to be) flat mirrors, so obviously they should be installed correctly, but they won't change the mode matching in a huge way if they're backwards, right?

For the PRM, I recommend checking (a) the arrow inscribed on the thinner side of the optic and (b) that the arrow *actually* points to the HR side.  I'm pretty sure I installed all the optics with the arrow pointing away from the OSEMs, but I never did a thorough check that the arrow always actually pointed to the HR coated side.  I don't remember any optics where I said "hmmm, that's funny, the arrow is pointing backwards", but nor did I write down that I had checked.

Also, hopefully the PRM is correct.  If however it's not, that means that all of the magnets are glued onto the HR side, and we'll have to redo all of the magnet gluing.  The guiderods should be fine, but all 6 magnets would need redoing.  If we were very, very careful and didn't break any of the magnets off of the dumbbells, it's a 24 hour turnaround due to drying time.  Since inevitably we break magnets away from dumbbells, conservatively we should think about a 48 hour turnaround. 

  6891   Fri Jun 29 01:49:36 2012 yutaBureaucracyLockingvent for PRC check, TOMORROW!

Quote:

 What do you mean by PR2, PR3 flipping?  They are (supposed to be) flat mirrors, so obviously they should be installed correctly, but they won't change the mode matching in a huge way if they're backwards, right?

We see some ghost beam spots at POP. This may come from the back of PR2 and PR3. Also, they may change mode matching because of thermal lensing, mirror deformation, and other unexpected reasons. I thought we should check every mirrors in PRC, if PRM is not flipped.

We are going to check PRM just because we spent so much time for the PRC problem, and still don't have the solution or evidence.
PRM flipping is kind of the only idea for the root of all evil -- terrible beam shape, low PR gain, unstable PRMI lock.
So, I want to check with my eye during the stay.

I don't think we have to redo magnet gluing. It's okay to leave them on HR side.

  7849   Tue Dec 18 10:43:20 2012 SteveUpdateVACvent has completed

 The 40m vacuum envelope is at atm    It took 4.5 hours at ~3 Torr/min speed. Atm1

 

What I did:

Turned PZT voltages off: 84.1V at OMC-rack location

                                           -  99V at 1Y3 location as PZT_pitch,

                                             56.6V KEPCO at 1Y3 location as PZT_yaw                                           

Took screen shuts of SUS_SUMMARY, yesterday,  Atm3

Turned off OPLEV _SERVOs, today , Atm2

Closed PSL_SHUTTER and green shutters at the ends

 

Set vacuum valves for vent position and opened VM2 for the RGA

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

 

  7582   Fri Oct 19 16:45:39 2012 SteveUpdateVACvent has started

Quote:

 

 VENT NOW and FIX ALIGNMENT!

 PSL shutter closed, manual block in place, HV turned off. P1 is at 200 Torr now.  Jenne is taking over here.

  7584   Fri Oct 19 19:26:42 2012 JenneUpdateVACvent has started

Quote:

Quote:

 

 PSL shutter closed, manual block in place, HV turned off. P1 is at 200 Torr now.  Jenne is taking over here.

 Valves closed, 500 torr.  Steve will finish off Monday morning, then we'll take off doors and get to work.

  5111   Wed Aug 3 16:18:30 2011 steveUpdateVACvent is almost finished

P1 at 750 Torr,  Vent valve VV1 is left open to atm. It will reach equilibrium in an hour. The PSL power is not turned down yet. The beam path is blocked at two places inside the enclosure.

The low power 20 mW  input  MC can be locked tonight.

 

Next day's - Thursday notes:

We  reached 760 Torr of atm in 8 hrs at  1.7 Torr/ min with 5 cylinders of  instrument grade air.

Used 500 PSI of nitrogen to get to 20 Torr at first.  This flow  and the first cylinder of N2  has to be slower next time.

 

We did the following:

1, oplevs were centered on locked caveties 2 days ago

2, just before vent we rechecked arms  pointing, they wre still locking

3,eloged strain gages  and turned HVs off at PZT-steering   at 1Y3 rack and OMC-PZT ps at 1X2 aux rack. They were actually off.

4,,checked jam nuts 6 places x 3

5, turned oplev servos off

6, eloged SUS summery page

7, checked particle counts at ITMY: 1 micron 300,  0.5 micron 3K,  0.3 micron  30K particles / cft-min. All three cranes were wiped 2 days ago.

8, blocked laser into IFO: main 1064 in 1.25W were blocked by manual 2 blocks on PSL table. The PSL output shutter was left open to be triggered by interlock  at P1 3 mTorr. It did!

    Aux NPRO-AP and green light  input at both ends were blocked.

  2636   Tue Feb 23 19:07:43 2010 kiwamu and steveConfigurationVACvent is completed

Quote:

Kiwamu and Steve have started venting the 40m vacuum envelope.

Preparation:

centered oplevs at resonating cavities,

ITM references were set by green pointer from the ends by Koji,

closed  PSL shutter and placed manual block into beam path,

checked  jamnuts in locked positions on bellows,

turned  HV off at PZT-Jena "steering mirror" power supply and OMC HV ps

checked  particle counts,

switched oplev servos off,

set up N2 cylinder to start vent from 1e-6 Torr to 25 Torr,

have ~ 6 cylinders of instrument grade compressed air to bring envelope from 25 Torr to 760 Torr

 

All three cranes were wiped off today.

 

 Kiwamu has completed the vent.

  10532   Wed Sep 24 13:28:48 2014 SteveUpdateVACvent is completed

 The vent is completed. ITMX was kicked up accidentally. Valve configuration: chamber open, RGA is pumped through VM2  Maglev

  10533   Wed Sep 24 16:02:58 2014 JenneUpdateVACvent is completed

[Steve, EricQ, Jenne]

ITMY and BS heavy doors are off, light doors are on.  Q is aligning the IFO.

  5698   Wed Oct 19 14:03:41 2011 kiwamuUpdateGeneralvent prep : dichroic mirrors

Status update on dichroic mirror:

 I got the specification sheet of an aLIGO 2" dichroic mirror from Lisa.

https://dcc.ligo.org/cgi-bin/private/DocDB/ShowDocument?docid=25232

This is the one from ATF. It has low loss, a high R for 1064 nm and high T for 532 nm. So it matches our needs.

Based on this sheet we may reset some of the parameters in the specification (e.g. incident angle and etc.,) and will get a quote from ATF.

We will buy 3 of them, including 1 spare. First I need to review the specification.

  7249   Wed Aug 22 15:47:34 2012 jamieSummaryGeneralvent prepartion for fast-track vent

We are discussing venting first thing next week, with the goal of
diagnosing what's going on in the PRC.

Reminder of the overall vent plan:

https://wiki-40m.ligo.caltech.edu/vent

Since we won't be prepared for tip-tilt installation (item 2), we should
focus most of the effort on diagnosing what's going on in the PRC.  Of
the other planned activities:

(1) dichroic mirror replacement for PR3 and SR3

  Given that we'll be working on the PRC, we might consider going ahead
  with this replacement, especially if the folding mirror becomes
  suspect for whatever reason.  In any case we should have the new
  mirrors ready to install, which means we should get the phase map
  measurements asap.

(3) black glass beam dumps:

  Install as time and manpower permits.  We need to make sure all needed
  components are baked and ready to install.

(4) OSEM mount screws:

  Delay until next vent.

(5) new periscope plate:

  Delay until next vent.

(6) cavity scattering measurement setup

  Delay until next vent.

  7255   Thu Aug 23 10:38:12 2012 SteveUpdateGeneralvent prepartion for fast-track vent

Quote:

We are discussing venting first thing next week, with the goal of
diagnosing what's going on in the PRC.

Reminder of the overall vent plan:

https://wiki-40m.ligo.caltech.edu/vent

Since we won't be prepared for tip-tilt installation (item 2), we should
focus most of the effort on diagnosing what's going on in the PRC.  Of
the other planned activities:

(1) dichroic mirror replacement for PR3 and SR3

  Given that we'll be working on the PRC, we might consider going ahead
  with this replacement, especially if the folding mirror becomes
  suspect for whatever reason.  In any case we should have the new
  mirrors ready to install, which means we should get the phase map
  measurements asap.

(3) black glass beam dumps:

  Install as time and manpower permits.  We need to make sure all needed
  components are baked and ready to install.

(4) OSEM mount screws:

  Delay until next vent.

(5) new periscope plate:

  Delay until next vent.

(6) cavity scattering measurement setup

  Delay until next vent.

 Bob is back. Cleaning and baking all our posts and clamps. They will be ready for use Tuesday next week. Therefore beam dumps will be available for installation.

  7558   Tue Oct 16 16:46:20 2012 Vent Czar and CzarinaSummaryGeneralvent stuff

We're discussing the plan for the next vent.  Now that we have all the tip-tilt stuff in hand, we should get ready for the big TT installation vent ASAP.  The question is what remains to be done, and when can we be ready

Stuff that needs doing:

* characterize TTs, check electrical connection of quadrupus cables, bake cables and base plates - a week or so (not including baking)

* phase map of LaserOptik mirrors (decide on needed resolution) - a week or so?

* get ready to swap G&H mirrors with LaserOptik mirrors (PR2, PR3, SR2, SR3)

* assembly of black glass beam dumps - one afternoon

* green periscope moving - day or so to make sure greens are resonant in arms, so we have something to align to

* redraw of REFL path?? (rotate 2nd refl mirror to reflect beam to the east, then add mirror to get beam out of IOO chamber viewport), cut hole in BS oplev table's box, install black beam tube

* FI camera mount - make sure it's here, baked

* active TT pitch damping plan

* passive TT weight addition and pitch alignment plan

* camera plan for taking in-chamber photos without touching the tables

* look at layout of ITMY table.  POY pick-off too close to main beam.  Can we move POY pick-off to BS table?

* remount black glass baffles on SOS cages.

 

Stuff to bake:

* Quadrupus cables

* TT base plates

* FI mirror mount for FI camera

* stuff to add to active TTs

* stuff to add to passive TTs

 

  7560   Tue Oct 16 17:13:23 2012 CzarinaSummaryGeneralvent stuff - 4 paths

I see 4+ possible paths for us to take, in terms of a possible vent in the next few weeks:

No Vent - Just do FPPRMI, using AS55

Mini Vent - Fix REFL path, nothing else.  ~1 day at atmosphere

Medium Vent - Fix REFL path, swap G&H mirrors for LaserOptik mirrors (so also resuspend passive TTs, maybe add pitch adjustment option). ~1 week or so at atmosphere - do this rather than Mini if Jan's Finesse calc says the G&H mirrors are too rough

Mega Vent - Fix all the things, do all the things.  Long time at atmosphere

The "+" is to take into account all the possible variations on "medium vent".  The No, Mini and Medium options assume we'll do the Mega option later, just not immediately.

  66   Tue Nov 6 09:45:22 2007 steveSummarySUSvent sus trend
The mc optics dragwippings were done by locking optics by eq stops and rotating-moving
cages so access were good. This technic worked well with mc1 & mc2
MC3 osems were reoriented only.
  2631   Tue Feb 23 13:37:04 2010 kiwamu and steveConfigurationVACventing the 40m vac envelope

Kiwamu and Steve have started venting the 40m vacuum envelope.

Preparation:

centered oplevs at resonating cavities,

ITM references were set by green pointer from the ends by Koji,

closed  PSL shutter and placed manual block into beam path,

checked  jamnuts in locked positions on bellows,

turned  HV off at PZT-Jena "steering mirror" power supply and OMC HV ps

checked  particle counts,

switched oplev servos off,

set up N2 cylinder to start vent from 1e-6 Torr to 25 Torr,

have ~ 6 cylinders of instrument grade compressed air to bring envelope from 25 Torr to 760 Torr

 

All three cranes were wiped off today.

 

  3616   Tue Sep 28 14:12:14 2010 steveUpdateGeneralvertex crane drive is out of order

The vertex crane drive is overheating, it stopped functioning. Service man will be here tomorrow morning.

I crane was just turned  on for for may be  about 5 minutes. The vertical drive was fine for a while, but the horizontal did not worked at all.

The crane is tagged out again and the controller box is cooling down.

  9146   Fri Sep 20 16:37:30 2013 SteveUpdateVACvertex crane folding arm is back on

Quote:

 The folding beam removed as shown. Two man supporting it while I hammering it out. Pin was dry and it gulled into supporting hinges.

The rotating hinge will be machined and bushing will be added with Zerk fitting or similar. This will allow lubrication in the future.

 see elog #9111

Atm1,  The folding arm is back on with 0.1" misalignment at no load in the trolly's way. The other side of the I beam is 0.02" higher than the main beam.. New bushing and pin were greased up  with Krytox before installation.

The axial Zerk 1/8" pipe in the pin upper end can not take any fitting. There is no room. It is taped off.

This gap comes down to ~ 1/16" at fully extended arm with 225 lbs load at the end of it.

The present plan is to grind down the  the misalignment of 0.1"  for a slow-loaded trolly.

Steve Baker of Konacranes will be back to grind down this ridge and load test at 500 lbs on Tuesday,  OCT  1, 2013

 

 

 

  9139   Wed Sep 18 14:57:12 2013 SteveUpdateVACvertex crane folding arm removed

 The folding beam removed as shown. Two man supporting it while I hammering it out. Pin was dry and it gulled into supporting hinges.

The rotating hinge will be machined and bushing will be added with Zerk fitting or similar. This will allow lubrication in the future.

 see elog #9111

  9111   Thu Sep 5 10:47:58 2013 SteveUpdateVACvertex crane folding issue

 

 [Fred Goldbar, Mike Gerfen, Dennis Coyne and Steve]

We inspected the hinge, 1.25" cross pin and I-beams. It is hard to explain what is  causing the folding I-beam corner to jam against the main I-beam.

To limit the motion of the folding I-beam  cross pin bushing will be added. This will take a week to complete.

 

 

 

 

 

  9185   Wed Oct 2 14:25:39 2013 SteveUpdateVACvertex crane is still out of order

 

The smoke alarms were turned off and surrounding areas were covered with plastic.

The folding I-beam was ground down to be in level with the main beam.

Load bearing cable moved into correct position. New folding spring installed.

Crane calibration was done at 500 lbs at the end of the fully extended jib.

Than we realized that the rotating wheel limit switch stopped working.

This means that the crane is still out of order.

 

  9372   Wed Nov 13 08:46:03 2013 SteveUpdateVACvertex crane repair completed

nullQuote:

 

The smoke alarms were turned off and surrounding areas were covered with plastic.

The folding I-beam was ground down to be in level with the main beam.

Load bearing cable moved into correct position. New folding spring installed.

Crane calibration was done at 500 lbs at the end of the fully extended jib.

Than we realized that the rotating wheel limit switch stopped working.

This means that the crane is still out of order.

 

New limit switch installed and tested. The crane is back in full operational mode. Two spare limit switches on hand.

  9117   Mon Sep 9 15:33:06 2013 SteveUpdateVACvertex crane repair is scheduled

Quote:

 

 [Fred Goldbar, Mike Gerfen, Dennis Coyne and Steve]

We inspected the hinge, 1.25" cross pin and I-beams. It is hard to explain what is  causing the folding I-beam corner to jam against the main I-beam.

To limit the motion of the folding I-beam  cross pin bushing will be added. This will take a week to complete.

 

 

 

 

 

 KoneCrane contact John McDaniel (562) 903 - 1371,

Wednesday, September 18,  folding I-beam will be removed.  KoneCrane will start working at 7:30am and they should be out by 12:30pm

 Friday,  September 20, reinstalling machined hinge on the I-beam. Same timing schedule as Wednesday.

  9173   Mon Sep 30 08:53:22 2013 SteveUpdateVACvertex crane repair schedule has changed

Quote:

Quote:

 The folding beam removed as shown. Two man supporting it while I hammering it out. Pin was dry and it gulled into supporting hinges.

The rotating hinge will be machined and bushing will be added with Zerk fitting or similar. This will allow lubrication in the future.

 see elog #9111

Atm1,  The folding arm is back on with 0.1" misalignment at no load in the trolly's way. The other side of the I beam is 0.02" higher than the main beam.. New bushing and pin were greased up  with Krytox before installation.

The axial Zerk 1/8" pipe in the pin upper end can not take any fitting. There is no room. It is taped off.

This gap comes down to ~ 1/16" at fully extended arm with 225 lbs load at the end of it.

The present plan is to grind down the  the misalignment of 0.1"  for a slow-loaded trolly.

Steve Baker of Konecranes will be back to grind down this ridge and load test at 500 lbs on Tuesday,  OCT  1, 2013

 

 

 

 Konecranes rescheduled the completion of the Vertex crane to Wednesday, Oct. 2

  3624   Thu Sep 30 09:34:58 2010 steveUpdateGeneralvertex crane trolly drive fixed

Quote:

The vertex crane drive is overheating, it stopped functioning. Service man will be here tomorrow morning.

I crane was just turned  on for for may be  about 5 minutes. The vertical drive was fine for a while, but the horizontal did not worked at all.

The crane is tagged out again and the controller box is cooling down.

 Atm1, Vertex crane controller unit on horizontal I-beam.

            Module CCES-407 1HP 2.3A 460V/3 phase on the right was replaced. Speed was increased  to 30 Hz

Atm2, See burned insulation on black wire that was shorting to the large suppressor resistor on Atm3 One can see the pit marks on the right end of it.

        This large power dissipater resistor got hot as the malfunctioning controller 407 broke down.   Touching black power wire insulation melted and made a short.

          So the heat was created and finally the fuses were blown. The unnecessary large fuses were replaced by small ones.

Fortunately we had one spare controller on hand that made this repair to be done fast.

We used the new Crane Safety Check list  from LIGO-E1000379-v1 the first time yesterday before doors were removed.

  4165   Tue Jan 18 10:25:23 2011 steveUpdatePEMvertex crane work this week

The crane people are here. The Vertex chambers are covered with plastic. The PSL HEPAs will be running on high during the day.

It is going to be disturbingly noisy and dirty during the day. Please try start working in the evening if it can not wait till next week.

  3492   Tue Aug 31 02:50:45 2010 kiwamuUpdateCDSvertex suspensions controlled by the new CDS

I plugged the new CDS to the vertex suspensions. 

Now PRM, SRM, ITMs, MCs and BS are under the control of the new CDS. 

From now on we will never go back to the old system.

 

Though,  the watchdogs are still running on the old system.

So if you need to turn on/off the watchdogs, you can simply enable/disable them from the usual medm screens.

  3699   Tue Oct 12 17:42:57 2010 yutaUpdateSUSvery first measurement of Q-values for MC1

Background:
 Data aquisition system is fixed, and now we can use the Dataviewer to measure Q-values of the ringdowns for each DOF, each optics.
 First of all, I measured MC1 suspention damping servo for a test.

What I did:
1. Used DAQ channels activated in this entry(#3690) to see and compare the ringdowns when the damping servo is on and off with the Dataviewer.

2. Plotted the data and fitted the ringdown using this formula;
  p[0]*exp(-p[1]*t)*sin(p[2]*t+p[3])+p[4]
 I used python's scipy.optimize.leastsq for the fitting.

3. Calculated the resonant frequency f0 and Q-value using following formulas;
  f0=2*pi*sqrt(p[1]**2+p[2]**2)
  Q=f0/(2*pi)/(2*p[1])

4. For plotting, I subtracted the offset(=p[4]).

All parameters I used for this measurement are automatically saved here;
  /cvs/cds/caltech/burt/autoburt/snapshots/2010/Oct/12/13:07/c1mcs.epics
(-1,0,1 for all matrix elements, GAIN=3,3,3,150 for POS,PIT,YAW,SIDE)

Result:
 Attached is the plot of each 4 DOF ringdown when servo is off and on.
 "servo off" means off for that DOF. Servo for the other 3 DOFs are on.

 As you can see clearly, the damping servo is working.

 The resonant frequencies and Q-values calculated from the fitting are as follows;

  servo off servo on
f0 (Hz) Q f0 (Hz) Q
POS 0.97 large 0.97 16
PIT 0.71 96 0.73 6.9
YAW 0.80 100 0.82 8.9
SIDE 0.99 large 0.99 27


 Resonant frequencies and Q-values have about 1% and 10% error respectively.
 I estimated it from my 2-time measurement of the POS ringdown.

Next work:
 - Find and modify some scripts to optimize the matrix elements
 - Calibrate the displacement
 - Do the same thing for other optics

  3347   Mon Aug 2 10:26:15 2010 steveConfigurationVACvery slow pumpdown completed

Quote:

Bob and Steve closed BS chamber with the help of the manual Genie lift and the pump down started. The PSL shutter was closed and manual block was placed in the beam path. High voltage power supplies were checked to be off.

Pumping speed ~ 1 Torr/min was achieved at  1/8 of a turn opened roughing valve RV1

 3 days pump down #69 completed. Thanks to Koji  and Kiwamu  who did more roughing on Saturday and Sunday.

  7232   Mon Aug 20 09:49:01 2012 SteveUpdateCamerasvideo cameras in the DARK

Quote:

 The problem with the glow on the ETMY face is due to the red light being scattered off of the optical table from the HeNe laser for the OL. Why is the red light hitting the table?

One way to fix the problem for the camera image is to insert a long pass filter (if Steve can find one).

 Edmund Optics: NT62-874

 Edmund Optics: NT65-731

Edmund Optics: NT32-759 

 

 Atm1, condition: all oplev lasers are off or blocked, green shutters are closed at the ends, PSL out put shutter is closed, all outside LED illuminating are off, all room lights are off

                         Only the OSEMs are on. ETMY and ITMX are still look like illuminated.

Atm2, condition: open PSL shutter. ETMY at 11 o'clock  and ETMX 1 o'clock bright scattered spot of 1064 nm are visible

Atm3, condition: closed PSL shutter and restored all oplev He/Ne lasers, it is visible at ETMY

Next: I will disconnect power to OSEMs at ETMY

  7215   Fri Aug 17 08:33:46 2012 SteveUpdateCamerasvideo cameras in the dark

Quote:

 I optimized the TM views with illuminator light on quad1  It actually looks better there.

I'll post a dark-  OSEM light only in jpg tomorrow.  ETMY camera is malfunctioning in dark condition now.

 

ALL  illuminator lighting are off. ITMX and ETMY looks back lighted. I will check on their apertures.

In order to focus on 1064 resonant spots I tried to restore and align the arms  by script. I only got flashes.

  7216   Fri Aug 17 09:34:27 2012 KojiUpdateCamerasvideo cameras in the dark
I used the LED illuminations at ETMX and BS yesterday for a tour.
I am afraid that I left them on.
  7217   Fri Aug 17 10:38:15 2012 SteveUpdateCamerasvideo cameras in the dark
> I used the LED illuminations at ETMX and BS yesterday for a tour.
> I am afraid that I left them on.

It was turned off before the picture was taken.
All LED illuminations were turned off. I checked them a few times.
  7219   Fri Aug 17 14:45:51 2012 ranaUpdateCamerasvideo cameras in the dark

 The problem with the glow on the ETMY face is due to the red light being scattered off of the optical table from the HeNe laser for the OL. Why is the red light hitting the table?

One way to fix the problem for the camera image is to insert a long pass filter (if Steve can find one).

 Edmund Optics: NT62-874

 Edmund Optics: NT65-731

Edmund Optics: NT32-759 

  7236   Mon Aug 20 18:10:44 2012 JenneUpdateCamerasvideo capture script copied over to real scripts directory

The videocapture.py script is now in ...../scripts/general/ , along with the videoswitch. 

Also, there's a button gui on the VIDEO medm screen to capture different camera views.

  10259   Wed Jul 23 10:39:18 2014 SteveUpdateCamerasvideo quad processors replaced

Quad processor 2 & 3 were replaced.

  2120   Mon Oct 19 18:14:28 2009 robUpdateCamerasvideo switch broken

The Chameleon HB (by Knox) video switch that we use for routing video signals into the control room monitors is broken.  Well, either it's broken, or something is wrong with the mv162 EPICS IOC which communicates with it via RS-232.  Multiple reboots/resets of both machines has not yet worked.  The CHHB has two RS-232 inputs--I switched to the second one, and there is now one signal coming through to a monitor but no switching yet. I've been unable to further debug it because we don't have anything in the lab (other than the omega iserver formerly used for the RGA logger) which can communicate with RS-232 ports.  I've been trying to get this thing (the iserver) working again, but can't communicate with it yet.  For now I'm just going to bypass the video switch entirely and use up all the BNC barrel connectors in the lab, so we can at least have the useful video displays back.

  8036   Fri Feb 8 12:43:26 2013 yutaUpdateComputersvideocapture.py now supports movie capturing

I updated /opt/rtcds/caltech/c1/scripts/general/videoscripts.py so that it supports movie capturing. It saves captured images (bmp) and movies (mp4) in /users/sensoray/SensorayCaptures/ directory.
I also updated /opt/rtcds/caltech/c1/scripts/pylibs/pyndslib.py because /usr/bin/lalapps_tconvert is not working and now /usr/bin/tconvert works.
However, tconvert doesn't run on ottavia, so I need Jamie to fix it.

videocapture.py -h:
Usage:
    videocapture.py [cameraname] [options]

Example usage:
    videocapture.py MC2F -s 320x240 -t off
       (Camptures image of MC2F with the size of 320x240, without timestamp on the image. MUST RUN ON PIANOSA!)
    videocapture.py AS -m 10
       (Camptures 10 sec movie of AS with the size of 720x480. MUST RUN ON PIANOSA!)


Options:
  -h, --help          show this help message and exit
  -s SIZE             specify image size [default: 720x480]
  -t TIMESTAMP_ONOFF  timestamp on or off [default: on]
  -m MOVLENGTH        specity movie length (in sec; takes movie if specified) [default: 0]

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