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ID Date Author Type Categoryup Subject
  12577   Fri Oct 21 09:28:21 2016 SteveUpdateVACVac Normal reached

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

Attachment 1: VacNormal.png
VacNormal.png
  12589   Mon Oct 31 16:20:50 2016 SteveUpdateVACRGA is reinstalled

Quad rods and  ionizer kit: consisting of repeller cage, anode grid, focus plate and  filament were replaced....... under repair # RGA200/12 ECA 100416-12967

The electronic ECU is not connected. It is beeing pumped at IFO ITcc 9.7E-6 Torr vacNormal

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

  12633   Tue Nov 22 11:31:52 2016 SteveUpdateVACRGA is running again

The Rga was turned on yesterday.

Quote:

The RGA is removed for repaire. It's volume at atmophere and sealed.. P4 reading of 38 Torr is not correct.

 

 

Attachment 1: RGAisBack33d.png
RGAisBack33d.png
Attachment 2: pd80-560Hz-d33.png
pd80-560Hz-d33.png
Attachment 3: afterRepair1d.png
afterRepair1d.png
  12636   Wed Nov 23 11:32:13 2016 SteveUpdateVACTP3 drypump replaced again

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

  12642   Mon Nov 28 09:45:44 2016 SteveUpdateVACRGA scan at pumpdown day 40

The vacuum envelope ~1 C warmer today than 7 days ago. Bad peaks are coming down as normal.

 

Attachment 1: RGAscan_d40.png
RGAscan_d40.png
Attachment 2: d2_&_d7scan.png
d2_&_d7scan.png
Attachment 3: RGAd2.png
RGAd2.png
  12681   Thu Dec 22 09:37:20 2016 SteveUpdateVACRGA scan at day 63

Valve configuration: vacuum normal

RGA head temp: 43.5 C

Vac envelope temp: 23 C

 

Attachment 1: pd80-d63.png
pd80-d63.png
Attachment 2: pd80-580Hz-d63.png
pd80-580Hz-d63.png
  12698   Tue Jan 10 14:24:09 2017 SteveUpdateVACRGA scan at day 82

Valve configuration: vacuum normal

Vacuum envelope: 23C

Rga head: 44C

 

Attachment 1: pd80VNd82.png
pd80VNd82.png
  12774   Tue Jan 31 14:14:29 2017 ranaUpdateVACPressure watch script

I think this cron job is running on NODUS (our gateway) instead of our scripts machine:

*/1 * * * * /opt/rtcds/caltech/c1/scripts/Admin/n2Check.sh >> /opt/rtcds/caltech/c1/scripts/Admin/n2Check.log 2>&1

Quote:

Based on Jenne's chiara disk usage monitoring script, I made a script that checks the N2 pressure, which will send an email to myself, Jenne, Rana, Koji, and Steve, should the pressure fall below 60psi. I also updated the chiara disk checking script to work on the new Nodus setup. I tested the two, only emailing myself, and they appear to work as expected. 

The scripts are committed to the svn. Nodus' crontab now includes these two scripts, as well as the crontab backup script. (It occurs to me that the crontab backup script could be a little smarter, only backing it up if a change is made, but the archive is only a few MB, so it's probably not so important...)

moreover this script has a 90MB log file full of not finding its channel

I wish this script was in python instead of BASH and I wish it would run on megatron instead of nodus (why can't megatron send us email too?) and I wish that this log file would get wiped out once in awhile. Currently its been spitting out errors since at least a month ago:

Tue Jan 31 14:10:02 PST 2017 : N2 Pressure:

Channel connect timed out: 'C1:Vac-N2pres' not found.

(standard_in) 1: syntax error

  12853   Mon Feb 27 15:33:10 2017 SteveUpdateVACRGA scan at day 130

Valve configuration: vacuum normal

Vacuum envelope: 23.5 C

RGA head: 46.6 C

 

Attachment 1: rgascan@130d.png
rgascan@130d.png
  13047   Wed Jun 7 11:32:56 2017 SteveUpdateVACsmooth vac reboot

Gautam and Steve,

 

The medm monitor & vac control screens were totally blank since ~ May 24, 2017    Experienced vacuum knowledge is required for this job.

IDENTIFY valve configuration:

                        How to confirm valve configuration when all vac mons are blank?  Each valve has a manual-mechanical position indicator. Look at pressure readings and turbo pump controllers. VAC NORMAL configuration was confirmed based on these information.

Preparation: disconnect valves ( disconnect meaning: valve closes and stays paralized ) in this sequence VC2, VC1 power, VA6, V5, V4 & V1 power,      at ifo pressure 7.3E-6 Torr-it  ( it  = InstruTech cold cathode gauge )

                            This gauge is independent from all other rack  mounted   instrumentation and it is still not logged.

                            Switching to this valve configuration with disconnected valves will insure NOT  venting of the vacuum envelope by accidental glitching voltage drop or computer malfunction.

RESET  v1Vac1 .........in 2-3 minutes........ ( v1Vac1 - 2 )  the vac control screen started reading pressures & position

                    Connected cables to valves (meaning: valve will open if it was open before it was disconnected and it will be control able from computer ) in the following order: V4, V1 power, V5, VA6, VC2 & VC1 power,      at ifo 2E-5 Torr-it.....

                     ....vac configuration is reading VAC NORMAL,

                     ifo 7.4E-6 Torr-it

We have to hook up the it-cold cathode gauge to be monitored - logged !  this should be the substitute for the out of order CC1 pressure gauge.

Attachment 1: vac_reboot.png
vac_reboot.png
  13075   Tue Jun 20 16:28:23 2017 SteveUpdateVACRGA scan
Attachment 1: RGAscan243d.png
RGAscan243d.png
Attachment 2: RGAscan.png
RGAscan.png
  13132   Sun Jul 23 15:00:28 2017 JamieOmnistructureVACstrange sound around X arm vacuum pumps

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

  13134   Mon Jul 24 09:55:29 2017 SteveOmnistructureVACcontroller failer

Ifo pressure was 5.5 mTorr this Monday morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Maglev got warm ~38C but it was still rotating at 560 Hz normal with closed V1

Pressure plots are not available because of computer problems.

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

Attachment 1: TP2controllerFails.png
TP2controllerFails.png
  13142   Tue Jul 25 08:48:57 2017 SteveUpdateVACRGA scan at d278

The RGA did not shut down at the turbo pump controller failing.

Quote:

Ifo pressure was 5.5 mTorr this morning. The PSL shutter was still open. TP2 controller failed. Interlock closed V1, V4 and VM1

Turbo pump 2 is the fore pump of the Maglev. The pressure here was 3.9 Torr so The Magelv got warm ~38C but it was still rotating at 560 Hz normal with closed V1

What I did:

Looked at pressures of Hornet and Super Bee  Instru Tech. Inc

Closed all annuloses and VA6,  disconnected V4 and VA6 and turned on external fan to cool Maglev

Opened V7 to pump the Maglev fore line with TP3

V1 opened manually when foreline pressure dropped to <2mTorr at P2 and the body temp of the Maglev cooled down to  25-27 C

VM1 opened at 1e-5 Torr

Valve configuration: vacuum normal with annuloses not pumped

Ifo pressure 8.5e-6 Torr -IT at 10am,  P2 foreline pressure 64 mTorr, TP3 controller 0.17A   22C  50Krpm

note: all valves open manually, interlock can only close them

 

Quote:

While walking down to the X end to reset c1iscex I heard what I would call a "rythmic squnching" sound coming from under the turbo pump.  I would have said the sound was coming from a roughing pump, but none of them are on (as far as I can tell).

Steve maybe look into this??

PS: please call me next time you see the vacuum is not Vacuum Normal

 

Attachment 1: RGA278d.png
RGA278d.png
  13143   Tue Jul 25 14:04:06 2017 SteveUpdateVACturbo controller installed and we are running at vac normal

Gautam and Steve,

Spare Varian turbo-V 70 controller, Model 969-9505, sn 21612 was swapped in. It is running the turbo fine @ 50Krpm but it does not allow it's V4 valve to be opened............

It turns out that TP2 @ 75Krpm will allow V4 to open and close. This must be a software issue.

So Vacuum Normal is operational if TP2 is running 75,000 rpm

We want to run at 50,000 rpm on the long term.

Note: the RS232 Dsub connector on the back of this controller is mounted 180 degrees opposite than TP3  and old failed TP2 controller

 

PS: controller is shipping out for repair 7-28-2017

 

Attachment 1: TP2@75Krpm.png
TP2@75Krpm.png
  13171   Tue Aug 8 17:04:26 2017 SteveUpdateVACunintended pump down

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

Attachment 1: pumping_down.png
pumping_down.png
  13172   Tue Aug 8 17:44:11 2017 SteveUpdateVACunintended pump down

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

Attachment 1: stopped_pumping.png
stopped_pumping.png
  13175   Wed Aug 9 11:59:51 2017 SteveUpdateVACunintended pump down at vacuum normal

pd80b has reached Vac Normal. IFO pressure 0.5 mTorr

We need our vauum channels back in dataviewer.

Quote:

Pumpdown stopped for over night  at ~  1 Torr

The roughing line disconnected.  Valves condition indicator  "moving " means that it is closed and it's cable disconnected so it can not move.

The RGA is off and VM1 is stuck.

Quote:

IFO pressure 2 Torr,    PSL  shutter closed.  I'm pumping down with 2 roughing pumps with ion pump gate valves open and annulosses at atm.

The vacuum envelope was vented to 17 Torr while I was replacing the USP battery stack. More about this later.....

Do not plan on using the interferrometer tonight.  I will complete the pumpdown tomorrow morning.

 

 

 

Attachment 1: pdc.png
pdc.png
Attachment 2: pd80b@vacnormal.png
pd80b@vacnormal.png
  13179   Wed Aug 9 16:34:46 2017 ranaUpdateVACVacuum Document recovered

Steve and I found the previous draft of the 40m Vacuum Document. Someone in 2015 had browsed into the Docs history and then saved the old 2013 version as the current one.

We restored the version from 2014 which has all of Steve's edits. I have put that version (which is now the working copy) into the DCC:  https://dcc.ligo.org/E1500239.

The latest version is in our Google Docs place as usual. Steve is going to have a draft ready for us to ready be Tuesday, so please take a look then and we can discuss what needs doing at next Wednesday's 40m meeting.

  13186   Thu Aug 10 15:45:34 2017 SteveUpdateVACaccidental vent to 17 Torr

Finally we got the cold cathode gauge working. IFO pressure 7e-6 Torr-it, vacuum normal valve configuration with all 4 ion pump gate valves closed at ~ 9e-6 Torr.  The cryo pump was also pumped yesterday to remove the accumulated outgassing build up.

The accidental vent was my mistake; made when I was replacing the battery pack of the UPS. The installed pack measured 51 V without any load. The "replace battery" warning light did not go out after the batteries were replaced. 

I then mistakenly and repeatedly pushed the "test" button to reset this, but I did not wait long enough for the batterries to get fully charged. The test put the full load on the new batteries and their charging condition got worse. I made the mistake when trying to put the load from the battery to online and pushed "O" so the power was cut and the computer rebooted to the all off condition. On top of this, I disconnected the wrong V1 cable to close V1.  As the computer rebooted it's interlock closed V1 at 17 Torr.

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

Attachment 1: Mag_UPS.jpg
Mag_UPS.jpg
Attachment 2: UPSbatteryPack.jpg
UPSbatteryPack.jpg
Attachment 3: closing_V1.jpg
closing_V1.jpg
  13233   Mon Aug 21 14:53:32 2017 gautamUpdateVACRGA reset

[gautam, steve]

In the aftermath of the accidental vent, it looks like the RGA was shutdown.

We followed the instructions in this elog to restart the RGA.

Seems to be working now, Steve says we just need to wait for it to warm up before we can collect a reliable scan.

Quote:

We have good RGA scan now. There was no scan for 3 months.

 

  13234   Mon Aug 21 16:35:48 2017 gautamUpdateVACUPS checkup

[steve, gautam]

At Rolf/Rich Abbott's request, we performed a check of the UPS today.

Steve believed that the UPS was functioning as it should, and the recent accidental vent was because the UPS batteries were insufficiently charged when the test was performed. Today, we decided to try testing the UPS.

We first closed V1, VM1 and VA6 using the MEDM screen. We prepared to pull power on all these valves by loosening the power connections (but not detaching them). [During this process, I lost the screw holding the power cord fixed to the gate valve V1 - we are looking for a replacement right now but it seems to be an odd size. It is cable tied for now.]

The battery charge indicator LEDs on the UPS indicated that the batteries were fully charged.

Next, we hit the "Test" button on the UPS - it has to be held down for ~3 seconds for the test to be actually initiated, seems to be a safety feature of the UPS. Once the test is underway, the LED indicators on the UPS will indicate that the loading is on the UPS batteries. The test itself lasts for ~5seconds, after which the UPS automatically reverts to the nominal configuration of supplying power from the main line (no additional user input is required).

In this test, one of the five battery charge indicator LEDs went off (5 ON LEDs indicate full charge).

So on the basis of this test, it would seem that the UPS is functioning as expected. It remains to be investigated if the various hardware/software interlocks in place will initiate the right sequence of valve closures when required.


Quote:
 

Never hit O on the Vacuum UPS !

Note: the " all off " configuration should be all valves closed ! This should be fixed now.

In case of  emergency  you can close V1 with disconnecting it's actuating power as shown on Atm3 if you have peumatic pressure 60 PSI 

 

  13245   Wed Aug 23 10:11:46 2017 SteveUpdateVACvacuum valve specifications

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

  13260   Mon Aug 28 10:28:07 2017 SteveUpdateVACRGA scan 20 day after 17 Torr

The RGA was turned on 7 days ago.  It's 46 C now.   The X-arm room tem ~20 C

IFO pressure 6.5e-6 Torr at IT-Hornet gauge. Valve configuration vacuum normal.

Attachment 1: 20d_after_17_torr.png
20d_after_17_torr.png
  13268   Tue Aug 29 15:35:19 2017 SteveUpdateVACvacuum pump specifications & manuals

RP1 and RP3 roughing pump manual of Leybold D30A oily rotory pump

Fore pump of TP2 & TP3 Varian SH-100 Dry Scroll

TP2 and TP3 small turbo drag pump  Varian 969-9361 

TP2 and TP3 turbo controller Varian 969-9505

TP1 magnetically suspended turbo pump  Osaka TG390MCAB, sn360 and controller TC010M  and note : this  pump  running on 208VAC single phaseIt is not on the UPS !  

                                                             Osaka Maglev Manual        and Osaka Controller Communication Wiring                                                                                                                                

VC1 cryo pump CTI-Cryogenics Cryo Torr 8 sn 8g23925  SAFETY note: compressor single phase 208VAC and the head driver 3 phase 208VAC Compressor and driver have each separate power cord!

Installed at 40m wiki  also

Quote:

The V1 gate valve specs installed at 40m wiki page. VAT model number 10846-UE44-0007 Our main volume pumping goes through this 8" id gate valve V1 to Maglev turbo  or Cryo pump to  VC1

The ion pumps have 6" id gate valves:VAT 10844-UE44-AAY1,  Pneumatic actuator with position indicator and double acting solenoid valve 115V 60Hz  Purchased 1999 Dec 22

UHV gate valves 2.5" id. VAT  10836-UE44    Pneumatic actuator with position indicator and double acting solenoid valve 115V 60 hz, IFO to RGA  VM1 &  RGA to Maglev  VM2

mini UHV gate valve 1.5" id.   VAT  01032-UE01      2016 cataloge page 14,   manual - no position indicator, VM4  next to manual adjustable fine leak valve to RGA

UHV angle valve 1.5" id, model VAT 28432-GE41, Viton plate seal, pneumatic actuator with position indicator & solenoid valve 115V & single acting closing spring  MEDM screen: VM3,VC2, V3,V4,V5,V6,VA6,V7 & annuloses Each chamber annulos has 2 valves.

UHV angle valve 1.5" id, model VAT 57132-GE05   go page 208,   Metal tip seal, manual actuating only with position indicator,   MEDM screen: roughing RV1 and venting VV1 hand wheel needed to close to torque spec

UHV angle valve  1.5" id. model VAT 28432-GE01           Viton plate seal, manual operation only at IT gauges Hornet & Super Bee and  ion pumps roughing  ports. These are not labeled.

                                                      

The Cryo pump interlock wiring was added too

Note: all moving valve plate seals are single.

 

  13321   Tue Sep 19 11:05:26 2017 SteveUpdateVACRGA scan at day 334

 

 

Attachment 1: RGAscan334d.png
RGAscan334d.png
  13403   Fri Oct 27 10:14:11 2017 SteveUpdateVACRGA scan at day 372

Valve configuration: Vacuum normal

Note: Tp2 running at 75Krpm 0.25A 26C has a  load high pitch sound today. It's fore line pressure 78 mTorr. Room temp 20C

 

Attachment 1: RGA_scan_d372.png
RGA_scan_d372.png
  13407   Mon Oct 30 10:09:41 2017 SteveUpdateVACTP2 failed

 IFO pressure 1.2e-5 Torr at 9:30am

Quote:

Valve configuration: Vacuum normal

Note: Tp2 running at 75Krpm 0.25A 26C has a  load high pitch sound today. It's fore line pressure 78 mTorr. Room temp 20C

 

Atm. 1,  This was the vacuum condition  this morning.

               IFO P1  9.7 mTorr, V1 openV4 was in closed position , ~37 C warm Maglev at normal 560Hz rotation speed with foreline pressure 3.9 Torr because V4 closed 2 days ago when TP2 failed .....see Atm.3

               The error messege at TP2  controller was: fault overtemp.

I did the following to restored IFO pumping: stopped pumping of the annulose with TP3 and valves were configured so TP3 can be the forepump of the Maglev.

closed VM1 to protect the RGA,  close PSL shutter .....see Gautam  entry

aux fan on to cool down Maglev-TP1, room temp 20 C,

aux drypump turned on and opend to TP3 foreline to gain pumping speed,

closed PAN to isolate annulos pumping,

opened V7 to pump Maglev forline with TP3 running at 50Krpm, It took 10 minutes to reach P2  1mTorr from 3.9 Torr

aux drypump closed off at P2  1 mTorr, TP3 foreline pressure 362 mTorr.......see Atm.2

As we are running now:

IFO pressure 7e-6 Torr at Hornet cold cathode gauge at 15:50  We have no IFO CC1 logging now.  Annuloses are in 3-5 mTorr range are not pumped.

TP3 as foreline pump of TP1 at 50 Krpm, 0.24 A, 24 C, it's drypump forline pressure 324 mTorr

V4 valve cable is disconnected.

I need help with wiring up the logging of the Hornet cold cathode gauge.

 

 

 

Attachment 1: tp2failed.png
tp2failed.png
Attachment 2: ifo_1.0E-5_Torrit.png
ifo_1.0E-5_Torrit.png
Attachment 3: tp2failed2dago.png
tp2failed2dago.png
Attachment 4: 4days.png
4days.png
  13409   Mon Nov 6 09:09:43 2017 SteveUpdateVACsetting up new TP2 turbo

Our new Agilent Technology TwisTorr 84FS AG rack controller ( English Manual pages 195-297 )  RS232/485, product number X3508-64001, sn IT1737C383

This controller, turbo and it's drypump needs to be set up into our existing vacuum system. The intake valve of this turbo (V4) has to have a hardwired interlock that closes V4 when rotation speed is less than 20% of preset RPM speed.

The unit has an analoge 10Vdc output that is proportional to rotation speed. This can be used with a comperator to direct the interlock or there may be set software option in the controller to close the valve if the turbo slows down more than 20%

The last Upgrade of the 40m Vacuum System  1/2/2000 discribes our  vauum system  LIGO-T000054-00-R 

Here the LabView / Metrabus controls were replaced by VME processor and  an Epic interface

We do not have schematics of the hardware wiring.

We need help with this.

 

  13423   Fri Nov 10 08:52:21 2017 SteveUpdateVACTP3 drypump replaced

PSL shutter closed at 6e-6 Torr-it    

   The foreline pressure of the drypump is 850 mTorr at 8,446 hrs of seal life

V1 will be closed for ~20 minutes for drypump replacement..........

9:30am dry pump replaced, PSL shutter opened at 7.7E-6 Torr-it

  Valve configuration: vacuum normal as  TP3 is the forepump of the Maglev  & annuloses are not pumped.

Quote:

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

 

  13454   Sun Nov 26 19:38:40 2017 SteveUpdateVACTP3 drypump replaced again

The TP3 foreline pressure was 4.8 Torr, 50K rpm 0.54A and 31C........Maglev rotation normal 560 Hz.......    IFO pressure 7.2e- 6 Torrit was not effected

V1 closed ......replaced drypump.........V1 opened

IFO 6.9e-6 Torrit at 19:55, TP3fl 18 mT,  50Krpm 0.15A 24C

VM1 is still closed

 

Attachment 1: after_replacement.png
after_replacement.png
  13459   Thu Nov 30 10:38:39 2017 SteveUpdateVACannuloses are not pumped

Annuloses are not pumped for 30 days, since TP2 failed.  IFO pressure 7e-6 Torr it,  Rga 2.6e-6 Torr

Valve configuration: Vacuum Normal as TP3 is the forepump of Maglev, annuloses are not puped at 1.1 Torr

TP3 50K rpm,  0.15A  24C, foreline pressure 16.1 mTorr

 

Quote:

The TP3 foreline pressure was 4.8 Torr, 50K rpm 0.54A and 31C........Maglev rotation normal 560 Hz.......    IFO pressure 7.2e- 6 Torrit was not effected

V1 closed ......replaced drypump.........V1 opened

IFO 6.9e-6 Torrit at 19:55, TP3fl 18 mT,  50Krpm 0.15A 24C

VM1 is still closed

 

 

Attachment 1: AnnulosesNotPumped.png
AnnulosesNotPumped.png
  13495   Tue Jan 2 15:43:35 2018 SteveUpdateVACpumpdown after power outage

 

Quote:

There was a power outage.

The IFO pressure is 12.8 mTorr-it and it is not pumped. V1 is still closed. TP1 is not running. The Rga is not powered.

The PSL output shutter is still closed. 2W Innolight turned on and manual beam block placed in its beampath.

3 AC units turned on at room temp 84F

IFO pumped down from 44 mTorr to 9.6e-6 Torr with Maglev  backed with only TP3

Aux drypump  was helping our std drypump during this 1 hour period. TP3 reached 32 C and slowed down 47K rpm

The peak foreline pressure at P2  was ~3 Torr

Hornet cold cathode gauge setting:   research mode, air,

                                                            2830 HV  1e-4A  at 9.6e-6 Torr,

                                                         [  3110 HV  8e-5A at 7.4e-6 Torr one day later ]

Annuloses are at 2 Torr, not pumped

Valve configuration:  vacuum normal, RGA is still off

PSL shutter is opened automatically. Manual block removed.

End IR lasers and doublers are turned on.

 

NOTE: Maglev " rotation X " on vacuum medm screen is not working! " C1:Vac-TP1_rot " channel was removed.  Use " NORMAL X " for rotation monitoring.

*We removed this (i.e. rotation) field from the MEDM screen to avoid confusion.

Attachment 1: pumpdown_from_44_mTorr.png
pumpdown_from_44_mTorr.png
  13588   Tue Jan 30 10:22:20 2018 SteveUpdateVACRGA scan at day 175

pd80b rga scan at 175 day.  IFO pressure 7.3e-6 Torr-it

Condition: vacuum normal, annuloses not pumped. Rga turned on yesterday.

The rga was not on since last poweroutage Jan 2, 2018 It is warming up and outgassing Atm2

Attachment 1: RGApd80-b-468-175d.png
RGApd80-b-468-175d.png
Attachment 2: RgaOn20hrs.png
RgaOn20hrs.png
  13615   Wed Feb 7 15:50:42 2018 SteveUpdateVACIFO pressure monitoring

Hornet cold cathode gauge analoge output  [ DSub9 pin 3 and 7 ] are wired to go ETMX Acromag. It was reading 4.9V at 7.8e-6 Torr [ 3,110 V  8.35e-5A ] at the end of a 24ft BNC cable. Now it has to be hook up to an Acromag channel.

This will replace the not functioning C1: Vac-CC1_pressure

gautam: the motivation behind hooking this gauge up to our DAQ system is that non-vacuum-system-experts have a quick diagnostic to make sure everything is in order. This gauge is physically placed adjacent to V1, and so if something goes wrong with our vacuum pumps, we would see the effect here immediately. we did note that occassionally, the reading fluctuated by ~1V on the DMM used to check the voltage output at the end of the BNC cable, so we still need to run some long-term stability analysis once this channel is hooked up to the Acromag.  For future reference, in order to make this gauge work, we need to check that

  1. Error flag has been cleared.
  2. HV is ON (state has to be manually toggled).
Quote:

 

Quote:

There was a power outage.

The IFO pressure is 12.8 mTorr-it and it is not pumped. V1 is still closed. TP1 is not running. The Rga is not powered.

The PSL output shutter is still closed. 2W Innolight turned on and manual beam block placed in its beampath.

3 AC units turned on at room temp 84F

IFO pumped down from 44 mTorr to 9.6e-6 Torr with Maglev  backed with only TP3

Aux drypump  was helping our std drypump during this 1 hour period. TP3 reached 32 C and slowed down 47K rpm

The peak foreline pressure at P2  was ~3 Torr

Hornet cold cathode gauge setting:   research mode, air,

                                                            2830 HV  1e-4A  at 9.6e-6 Torr,

                                                         [  3110 HV  8e-5A at 7.4e-6 Torr one day later ]

Annuloses are at 2 Torr, not pumped

Valve configuration:  vacuum normal, RGA is still off

PSL shutter is opened automatically. Manual block removed.

End IR lasers and doublers are turned on.

 

NOTE: Maglev " rotation X " on vacuum medm screen is not working! " C1:Vac-TP1_rot " channel was removed.  Use " NORMAL X " for rotation monitoring.

*We removed this (i.e. rotation) field from the MEDM screen to avoid confusion.

 

Attachment 1: CC_analog.png
CC_analog.png
  13637   Fri Feb 16 15:57:58 2018 SteveUpdateVACTP3 drypump replaced

The forline pressure of TP3 was 399 mTorr

It was replaced this morning at  TP3 controller 134,638hrs with the "failed TP2 station" drypump. The foreline pressure now at TP3 is 100 mTorr at 6 hrs of operation.[ at day 3  63 mT ]

IFO pressure at CC Hornet 7.9e - 6 Torr

Valve configuration: vacuum normal as TP3 is the forepump of the Maglev & the annuloses are not pumped

Quote:

PSL shutter closed at 6e-6 Torr-it    

   The foreline pressure of the drypump is 850 mTorr at 8,446 hrs of seal life

V1 will be closed for ~20 minutes for drypump replacement..........

9:30am dry pump replaced, PSL shutter opened at 7.7E-6 Torr-it

  Valve configuration: vacuum normal as  TP3 is the forepump of the Maglev  & annuloses are not pumped.

Quote:

TP3 drypump replaced at 655 mTorr, no load, tp3 0.3A 

This seal lasted only for 33 days at  123,840 hrs

The replacement is performing well: TP3 foreline pressure is 55 mTorr, no load, tp3 0.15A at 15 min  [ 13.1 mTorr at d5 ]

 

Valve configuration: Vacuum Normal, ITcc 8.5E-6 Torr

Quote:

Dry pump of TP3 replaced after 9.5 months of operation.[ 45 mTorr d3 ]

The annulosses are pumped.

Valve configuration: vac normal, IFO pressure 4.5E-5 Torr [1.6E-5 Torr d3 ] on new ITcc gauge, RGA is not installed yet.

Note how fast the pressure is dropping when the vent is short.

Quote:

IFO pressure 1.7E-4 Torr on new not logged cold cathode gauge. P1 <7E-4 Torr

Valve configuration: vac.normal with anunulossess closed off.

TP3 was turned off with a failing drypump. It will be replaced tomorrow.

All time stamps are blank on the MEDM screens.

 

 

 

  13647   Wed Feb 21 17:20:32 2018 johannesUpdateVACHornet gauge connected to DAQ.

I wired the six available BNC connectors on the front panel of the new XEND slow DAQ to physical Acromag channels. There were two unused ADC channels and eight DAC channels, of which I connected four. The following entries were added to /cvs/cds/caltech/target/c1auxex2/ETMXAUX2.db /caltech/target/c1auxex2/ETMXaux2.db

Connector Acromag Channel EPICS Name
In1 XT1221C #6 C1:Vac-CC1_HORNET_PRESSURE_VOLT
In2 XT1221C #7 C1:PEM-SEIS_XARM_TEMP_MON C1:PEM-SEIS_EX_TEMP_MON
Out1 XT1541B #4 C1:PEM-SEIS_XARM_TEMP_CTRL C1:PEM-SEIS_EX_TEMP_CTRL
Out2 XT1541B #5 Not Assigned
Out3 XT1541B #6 Not Assigned
Out4 XT1541B #7 Not Assigned

C1:Vac-CC1_HORNET_PRESSURE_VOLT is converted to the additional soft channel C1:Vac-CC1_HORNET_PRESSURE in units of torr using the conversion  10^{(\mathrm{Voltage}-10)} stated in the manual. A quick check showed that the resulting number and the displayed pressure on the vacuum gauge itself agree to ~1e-8 torr. Gautam added the new EPICS calc channel to the C0EDCU and restarted FB, now the data is being recorded.

Three of the output channels do not have a purpose yet, so their epics records were created but remain inactive for the time being.

Attachment 1: VacLog.png
VacLog.png
  13653   Fri Feb 23 07:47:54 2018 SteveUpdateVACCC1 Hornet

We have the IFO pressure logged again! Thanks Johannes and Gautam

This InstruTech cold cathode ionization vacuum gauge " Hornet " was installed 2016 Sep 14

Here is the CC1 gauge history of 10 years from 2015 Dec 1

The next thing to do is put this channel C1:Vac-CC1_HORNET_PRESSURE  on the 40m Vacuum System Monitor   [ COVAC_MONITOR.adl ] 

gautam 1pm: Vac MEDM screen monitor has been edited to change the readback channel for the CC1 pressure field - see Attachment #2. Seems to work okay.

Attachment 1: InstruTech_Hornet_CC1.png
InstruTech_Hornet_CC1.png
Attachment 2: CC1_readback_updated.png
CC1_readback_updated.png
  13664   Mon Mar 5 10:13:21 2018 gautamUpdateVACvacuum health

In Steve's absence, I've tried to keep an eye on the health of the vacuum system. From Attachment #1, the pressure of the main volume seems stable, no red flags there. I also don't here any anomalously loud sounds near the vacuum pumps. I've changed the N2 cylinders that keep V1 open twice, on Wednesday and Sunday of last week. So in summary, the vacuum system looks fine based on all the metrics I know of.

Attachment 1: VacuumStatus.png
VacuumStatus.png
  13685   Fri Mar 16 09:36:56 2018 SteveUpdateVACRGA scan at day 511,218d

Pumpdown 80 at 511 days and pd80b at 218 days

Valve configuration:  special vacuum normal, annuloses are not pumped at 3 Torr, IFO pressure 7.4e-6 Torr at vac envelope temp 22 +- 1C degrees

Quote:

pd80b rga scan at 175 day.  IFO pressure 7.3e-6 Torr-it

Condition: vacuum normal, annuloses not pumped. Rga turned on yesterday.

The rga was not on since last poweroutage Jan 2, 2018 It is warming up and outgassing Atm2

 

Attachment 1: RgaScan511d.png
RgaScan511d.png
Attachment 2: 08.png
08.png
  13702   Mon Mar 26 09:25:18 2018 SteveUpdateVACVM1 opened

CC1 old MKS cold cathode gauge randomly turns on- off. This makes software interlock close VM1 to protect RGA  So the closed off RGA region pressure goes up and the result is distorted RGA scan.

CC1 MKS gauge is disconnected and VM1 opened. This reminds me that we should connect our interlocks to CC1 Hornet Pressure gauge.

Quote:

Pumpdown 80 at 511 days and pd80b at 218 days

Valve configuration:  special vacuum normal, annuloses are not pumped at 3 Torr, IFO pressure 7.4e-6 Torr at vac envelope temp 22 +- 1C degrres

 

 

Attachment 1: CC4VM1.png
CC4VM1.png
  13709   Tue Mar 27 08:58:21 2018 SteveUpdateVACVM1 opened.......scan fine

 

Quote:

CC1 old MKS cold cathode gauge randomly turns on- off. This makes software interlock close VM1 to protect RGA  So the closed off RGA region pressure goes up and the result is distorted RGA scan.

CC1 MKS gauge is disconnected and VM1 opened. This reminds me that we should connect our interlocks to CC1 Hornet Pressure gauge.

Quote:

Pumpdown 80 at 511 days and pd80b at 218 days

Valve configuration:  special vacuum normal, annuloses are not pumped at 3 Torr, IFO pressure 7.4e-6 Torr at vac envelope temp 22 +- 1C degrres

 

 

 

Attachment 1: rga2018march27.png
rga2018march27.png
  13918   Wed Jun 6 10:02:52 2018 SteveUpdateVACRGA scan
Attachment 1: RGA302d.png
RGA302d.png
Attachment 2: annuloses_NOT_pumped.png
annuloses_NOT_pumped.png
Attachment 3: temp_vac.png
temp_vac.png
  13919   Wed Jun 6 10:44:52 2018 gautamUpdateVACAnnulus pressure channels added to frames

[steve, gautam]

We added the following channels to C0EDCU.ini and restarted the daqd processes. Channels seem to have been added successfully, we will check trend writing later today. Motivation is to have a long term record of annulus pressure (even though we are not currently pumping on the annulus).

C1:Vac-PASE_status

C1:Vac-PASV_status

C1:Vac-PABS_status

C1:Vac-PAEV_status

C1:Vac-PAEE_status

plot next day

Attachment 1: AnsPressureLogged.png
AnsPressureLogged.png
  14059   Thu Jul 12 16:18:22 2018 SteveUpdateVACVent preparations

We are getting ready to vent.

 

Attachment 1: before_Vent.png
before_Vent.png
Attachment 2: before_Vent_cond.png
before_Vent_cond.png
  14064   Fri Jul 13 10:54:55 2018 aaronUpdateVACVent 80

[aaron, steve]

Steve gave me a venting tutorial. I'll record this in probably a bit more detail than is strictly necessary, so I can keep track of some of the minor details for future reference.

Here is Steve's checklist:

  • Check that all jam nuts are tightened
  • all viewports are closed
  • op levs are off
  • take a picture of the MEDM screens
  • Check particle counts
  • Check that the cranes work & wiped
  • Check that HV is off

Gautam already did the pre-vent checks, and Steve took a screenshot of the IFO alignment, IMC alignment, master op lev screen, suspension condition, and shutter status to get a reference point. We later added the TT_CONTROL screen. Steve turned off all op levs.

We then went inside to do the mechanical checks

  • N2 cylinders in the 40m antechamber are all full enough (have ~700psi/day of nitrogen)
  • We manually record the particle count
    • this should be <10,000 on the 0.5um particles to be low enough to vent, otherwise we will contaminate the system
    • note: need to multiply the reading on the particle counter by 10 to get the true count
    • the temperature inside the PSL enclosure should be 23-24C +/- 3 degrees
    • We recorded the particle counts at ~830 and ~930, and the 0.5um count was up to ~3000
  • We put a beam stop in front of the laser at the PSL table
  • Checked that all HV supplies are either off or supplying something in air
    • we noticed four HV supplies on 1X1 that were on. Two were accounted for on the PSL table (FSS), and the other two were for C1IOO_ASC but ran along the upper cable rack. We got ahold of Gautam (sorry!) and he told us these go to the TT driver on OMC_SOUTH, where we verified the HV cables are disconnected. We took this to mean these HV supplies are not powering anything, and proceeded without turning these HV off.
    • There are HV supplies which were all either off or supplying something in-air at: 1Y4, 1Y2, OMC N rack, 1X9 (green steering HV)
  • Checked that the crane works--both move up and down
    • vertex crane switch is on the wall at the inner corner of the IFO
    • y arm crane switch is on the N wall at the Y end
    • turn off the cranes at the control strip after verifying they work
  • While walking around checking HV, we checked that the jam nuts and viewports are all closed
    • we replaced one viewport at the x arm that was open for a camera

After completing these checks, we grabbed a nitrogen cylinder and hooked it up to the VV1 filter. Steve gave me a rundown of how the vacuum system works. For my own memory, the oil pumps which provide the first level of roughing backstream below 500mtorr, so we typically turn on the turbo pumps (TP) below that level... just in case there is a calibrated leak to keep the pressure above 350mtorr at the oil pumps. TP2 has broken, so during this vent we'll install a manual valve so we can narrow the aperture that TP1 sees at V1 so we can hand off to the turbo at 500mtorr without overwhelming it. When the turbos have the pressure low enough, we open the mag lev pump. Close V1 if things screw up to protect the IFO. This 6" id manual gatevalve will allow us throttle the load on the small turbo while the maglev is taking over the pumping  The missmatch in pumping speed is 390/70 l/s [ maglev/varian D70 ]  We need to close down the conductive intake of the TP1 with manual gate valve so the 6x smaller turbo does not get overloaded...

We checked CC1, which read 7.2utorr.

Open the medm c0/ce/VacControl_BAK.adl to control the valves.

Steve tells me we are starting from vacuum normal state, but that some things are broken so it doesn't exactly match the state as described. In particular, VA6 is 'moving' because it has been disconnected and permanently closed to avoid pumping on the annulus. During this v ent, we will also keep pumping on the RGA since it is a short vent; steve logged the RGA yesterday.

We began the vent by following the vacuum normal to chamber open procedure.

  1. VM1 closed
  2. We didn't open VM3, because we want to keep the RGA on
  3. Closed V1
  4. Connect the N2 to the VV1 filter
    1. first puged the line with nitrogen
    2. We confirmed visually that V1 is closed
  5. We opened VM2 to pump on the RGA with the mag lev pump.
    1. This is a nonstandard step because we are keeping the RGA pumped down.
    2. The current on TP3 is ~0.19A, which is a normal, low load on the pump
  6. VV1 opened to begin the vent at ~10:30am
    1. use crescent wrench to open, torque wrench wheel to close
    2. Keep the pressure regulator below 10 psi for the vent. We started the vent with about 2psi, then increased to 8psi after confirming that the SUS sensors looked OK.
  7. We checked the pressure plot and ITMX/ETMX motion to make sure we weren't venting too quickly or kicking the optics
    1. Should look at eg C1:SUS-ITMX_SENSOR_LL, as well as C1:Vac-P1_pressure
  8. Once the pressure reaches 25torr, we switched over to dry air
    1. wipe off the outside dolly wheels with a wet rag, and exit through the x-arm door to get the air. Sweep off the area outside the door, and wipe off new air containers with the rag.
    2. Bring the cylinder inside, get the regulator ready/purged, and swap relatively quickly.
    3. We increased the vent speed to 10psi. 
    4. Steve says the vents typically take 4 of 300 cf cylinders from Airgas "Ultra Zero" AI  UZ300 that contains 0.1 PPM of THC

Everything looks good, so I'm monitoring the vent and swapping out cylinders.

At 12:08pm, the pressure was at 257 torr and I swapped out in a new cylinder.

Steve: Do not overpressurize the vacuum envelope! Stop around 720 Torr and let lab air do the rest. Our bellows are thin walled for seismic isolation.

Attachment 1: vent80wtiptilts.png
vent80wtiptilts.png
  14066   Fri Jul 13 16:26:52 2018 SteveUpdateVACVent 80 is completing...

Steve and Aaron,

6 hrs vent is reaching equlibrium to room air. It took 3 and a half instrument grade air cilynders [ AI UZ300 as labelled ] at 10 psi pressure. Average vent speed ~ 2 Torr/min

Valve configuration: IFO at atm and RGA is pumped through VM2 by TP1 maglev.

 

Attachment 1: @atm.png
@atm.png
Attachment 2: vent80_7h.png
vent80_7h.png
Attachment 3: ventregN2&Air_c.jpg
ventregN2&Air_c.jpg
  14073   Mon Jul 16 15:07:19 2018 KojiSummaryVACOven C vent

[Steve Koji]

- Attachment1: Removed the thermal cap. Checked the temperature of the oven. It was totally cold.

- Attachment2: Confirmed the RGA section was isolated. The pumps for the RGA was left running.

- Attachment3: Closed the main valve. The pumps for the main volume was left running.

- Attachment4: Started removing the rid. This did not change the gause readings as they were isolated from the venting main volume.

- Attachment5: Opened the rid. Took the components out on a UHV foil bag. The rid was replaced but loosely held by a few screws with the old gasket, just to protect the frange and the volume from rough dusts.

Attachment 1: P_20180716_141512.jpg
P_20180716_141512.jpg
Attachment 2: P_20180716_141601.jpg
P_20180716_141601.jpg
Attachment 3: P_20180716_141610.jpg
P_20180716_141610.jpg
Attachment 4: P_20180716_141827.jpg
P_20180716_141827.jpg
Attachment 5: P_20180716_143901.jpg
P_20180716_143901.jpg
  14074   Mon Jul 16 18:12:00 2018 KojiUpdateVACAdding a manual gate valve between TP1 and V1/VM2

[Steve Koji]

We are in the process of adding a manual gate valve between TP1 (Osaka Maglev) and the other gate valves (I suppose V1 and VM2).
The work is still on going and we will continue to work on this tomorrow. Because this section is isolated from the main volume, this work does not hold off the possible rough pumping tomorrow morning.

The motivation of this work is as follows:
- Since TP2 failed, the main vacuum volume has been pumped down by TP1 and TP3. However TP3 is not capable to handle the large pressure difference at the early stage of the turbo pumping. This cause TP3 to have excessive heating or even thermal shutdown.
- The remedy is to put a gate valve between TPs and the main vacuum to limit the amount of gas flowing into the TPs. This indeed slows down the pumping speed of turbo, but this is not the dominant part of the pumping time.

Actual work:
- Comfirmed TP1 is isolated.
- Unscrewed the flange of TP1.
- Remove TP1. This required to lift up TP1 with some shim as the nuts interferes with the TP1 body. (Attachment1, 2, 3)
- Now remove 10inch flange adapter. (Attachment4)
-
Attach 10"-8" adapter and 8" rotational sleeve. (Attachment5)

Attachment 1: P_20180716_155413.jpg
P_20180716_155413.jpg
Attachment 2: P_20180716_155645.jpg
P_20180716_155645.jpg
Attachment 3: P_20180716_155738.jpg
P_20180716_155738.jpg
Attachment 4: P_20180716_162307.jpg
P_20180716_162307.jpg
Attachment 5: P_20180716_172000.jpg
P_20180716_172000.jpg
  14079   Tue Jul 17 18:16:38 2018 SteveSummaryVACpumpdown 81 at 6 hrs

Precondition:  4 days at atm.   Atm5

HEPA tent used during the vent at ETMY  It reduced partical count 10 fold of 0.5 and 0.3 micron particals. Atm6

New items in vacuum:  Clean manual gate valve [Cetec made] from John Worden with 6" id....as it came from Hanford... [ Throttle able gate valve- TGV ] Atm3

                                 ( note: we have 3 more identical in the lab. The original intention was to use them for purging gates )

                                  Optiform Au plated reflector , Induceramics heating elements, similar as existing Cooner cables and related lenses, hardwear. see 14078

                                  OMC related item : none......... 14,110

 

The pumpdown is at 510 mTorr with RP1 & RP3 still pumping. Koji will shut it down the roughing later tonight. Tomorrow morning I will start the pumping by switching over to TP1 maglev.

Thanks for Koji and Gautam'  help of the installation of the manual gate valve. Atm4  This will allow us to control the load on our Varian foreline D70 turbo TP3

 

Attachment 1: pd81@6hrs.png
pd81@6hrs.png
Attachment 2: before_c.jpg
before_c.jpg
Attachment 3: tgv_c.jpg
tgv_c.jpg
Attachment 4: TGVinstalled.jpg
TGVinstalled.jpg
Attachment 5: 4_days_vent.png
4_days_vent.png
Attachment 6: tentHEPA.jpg
tentHEPA.jpg
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