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ID Date Author Type Categoryup Subject
  5487   Tue Sep 20 18:03:45 2011 PaulUpdateSUSITMY and SRM oplev calibrations - measured and estimated

The measured calibration factors for the oplevs are as follows:

 
SRM pitch: 666urad per count on channel C1-SUS-SRM-OLPIT-INMON
SRM yaw: 557urad per count on channel C1-SUS-SRM-OLYAW-INMON
 
ITMY pitch: 470urad per count on channel C1-SUS-ITMY-OLPIT-INMON
ITMY yaw: 491urad per count on channel C1-SUS-ITMY-OLYAW-INMON
 
Since I'm going to calibrate all the other oplevs with the rougher technique of estimating the angle from the OSEM signals directly, I thought I would check the result of such an estimation for the oplevs I have calibrated already. My method was as follows:
 
dA = change in angle
dx = change in OSEM flag position
dV = change in OSEM PD voltage
dC = change in OSEM counts
D = optic diameter
L = distance between OSEMs = D/sqrt(2)-0.002m = 0.052m
dV/dx = OSEMs volts per meter flag position change = 1700 V/m
dC/dV = OSEM counts per volt = 2^16/40 = 65536/40 counts/V
 
counts per radian = dC/dA = dV/dx  x   dC/dV   x  1/L = 1700*65536/40/0.052 = 5.3564x10^7 counts/rad
 
radians per count = dA/dC = 1.867x10^-8, or 0.019 urad/count
 
This is around a factor of 1000 smaller than what I measured earlier, reported in entry 5468. I guess this might be an issue with the whitening filter on the OSEMs, but my initial feeling was that this was only a factor of a few. If anyone can see a big obvious mistake in my above calculations please let me know!
 
 
  5488   Tue Sep 20 19:00:49 2011 PaulUpdateSUSITMY and SRM oplev calibrations - measured and estimated

 

Kiwamu noticed that the 1/L in the counts per radian should have just been L, which accounts for most of the discrepancy. We checked the input filters on the OSEMs, and they have 10dB of gain at DC. Accounting for this, estimates on the order of 20urad/count, which is much more reasonable!

  5493   Wed Sep 21 00:34:29 2011 ranaUpdateSUSSUS diag stuff... just so I remember what I'm doing

ETMX was ringing up when it was mis-aligned for Y arm locking. I restored the input matrix to something more diagonal and its now damping again. Needs more work before we can use the calculated matrix.

  5494   Wed Sep 21 00:37:01 2011 ranaUpdateSUSITMY and SRM oplev calibrations - measured and estimated

I found that some of the Optical Lever Servos were ON today and injecting nonsense into the interferometer optics. I have set all of the gains = 0 to save us more headaches.

Please leave them OFF until we review the servo and noise characterization results in the elog.

  5496   Wed Sep 21 09:10:15 2011 PaulUpdateSUSITMY and SRM oplev calibrations - measured and estimated

Quote:

I found that some of the Optical Lever Servos were ON today and injecting nonsense into the interferometer optics. I have set all of the gains = 0 to save us more headaches.

Please leave them OFF until we review the servo and noise characterization results in the elog.

 I had previously set the gains to zero, see the first line of my entry on Monday 5468. I should have the servo and noise characterisation done today for these oplevs today, so we can review it soon.

  5499   Wed Sep 21 14:44:25 2011 PaulUpdateSUSITMY and SRM open loop transfer functions

 

 Here are the open loop transfer functions for ITMY and SRM. The various settings for the OLTFs were as follows:

Oplev filter used for all OLTFs: 300^2:0

Gains for oplev servos (for each OLTF only the 1 servo for the measured TF was on. They are all set back to 0 now):

SRM yaw gain = 1

SRM pitch gain = -1

ITMY yaw gain = -1

ITMY pitch gain = 1

measurement band = 0.2Hz to 200Hz

points = 33

swept sine magnitude envelope: amp = 2 for f > 60Hz, amp = 0.1 for f < 60Hz

Measurement points were from e.g. C1-SUS-ITMY-OLPIT-IN2 to C1-SUS-ITMY-OLPIT-IN1 to give a TF of -(loop gain).

Next step is to divide this through by the sensor reponse (i.e. the calibration factor measured earlier) and the filter response to get just the actuator response. 

 

  5500   Wed Sep 21 16:22:14 2011 ranaUpdateSUSSummary screen

The SUS SUMMARY screen is now fully activated. You should keep it open at all times as a diagnostic of the suspensions.

No matter how cool you think you are, you are probably doing something bad when trying to lock, measure any loop gains, set matrices, etc. Use the screen.

 

This is the link to the automatic snapshot of the SUS SUMMARY screen. You can use it to check the Suspensions status with your jPhone.

Auto SUS SUMMARY Snapshot

When the values go yellow its near the bad level. When its red, it means the optic is misaligned or not damped or has the wrong gain, etc.

So don't ignore it Steve! If you think the thresholds are set too low then change them to the appropriate level with the scripts is SUS/

  5501   Wed Sep 21 16:31:28 2011 PaulUpdateSUSITMY and SRM actuator response functions

 I divided the open loop transfer functions by the filter response and the sensor responses (previously measured calibration factors) to leave just the actuator responses. I've attached the actuator responses plotted in radians/count and phase over frequency.

Next step: fit the actuator response with poles and zeros.

EDIT: I divided by the wrong filter function earlier - the plots there now are divided by the correct filter function

  5507   Wed Sep 21 23:05:16 2011 PaulUpdateSUSITMY and SRM actuator response functions - fitting results

 I used an fminsearch function to fit the SRM and ITMY actuator response magnitudes. The testfunction was just that for a single second order pole, but it gave what I consider to be good fits for the following reasons:

*for 3 of the 4 fits the residuals were less than 0.5% of the summed input data points. The worst one (ITMY pitch) was about 2.7%, which I think is due to the resonance happening to be right in the middle of two data points.

*the tolerance of 1 part in 10^9 was reached quickly from not very finely tuned starting points.

The test function was: G=abs(Gp./(1+1i.*f./fp./Qp-(f./fp).^2)), where G(f) is the actuator response magnitude, Gp is the pole gain, fp is the pole frequency, and Qp is the pole Q factor.

In the end I just fitted the response magnitude. I was initially fitting the complex response function, but ran into problems which I think were cased by overall phase offsets between the data and test function. Can I canvass for opinion if fitting the magnitude is OK, or should I try again fitting the phase too?

Anyway, here are the results of the fits, and I've attached plots of each too (each one in linear and log y axis because each on its own might be misleading for fits):

EDIT - I added more points to the otherwise sparse looking fitted curves

 

ITMY PITCH actuator response fit

-- Fit completed after 190 iterations--

 Started with: Gain = 3e-06,

 Q factor = 5,

 Pole frequency = 1,

 Fit results:  Gain = 1.32047e-06,

 Q factor = 4.34542,

 Pole frequency = 0.676676

 Residual (normalised against the sum of input datapoints) = 0.0268321

 

ITMY YAW actuator response fit

-- Fit completed after 156 iterations--

 Started with: Gain = 3e-06,

 Q factor = 5,

 Pole frequency = 1,

 Fit results:  Gain = 1.14456e-06,

 Q factor = 8.49875,

 Pole frequency = 0.730028

 Residual (normalised against the sum of input datapoints) = 0.00468077

 

SRM PITCH actuator response fit

 -- Fit completed after 192 iterations--

 Started with: Gain = 3e-06,

 Q factor = 5,

 Pole frequency = 1,

 Fit results:  Gain = 7.94675e-06,

 Q factor = 7.16458,

 Pole frequency = 0.57313

 Residual (normalised against the sum of input datapoints) = 0.00301265

 

SRM YAW actuator response fit

 -- Fit completed after 156 iterations--

 Started with: Gain = 3e-06,

 Q factor = 5,

 Pole frequency = 1,

 Fit results:  Gain = 3.34179e-06,

 Q factor = 9.57601,

 Pole frequency = 0.855322

 Residual (normalised against the sum of input datapoints) = 0.000840468

  5508   Wed Sep 21 23:25:51 2011 kiwamuUpdateSUSRe:ITMY and SRM actuator response functions - fitting results

Did you take the 180 deg shift into your account ?

Since your measurement was done when the loop was closed, there must be an additional 180 deg phase shift (in other words, minus sign).

Quote from #5507

In the end I just fitted the response magnitude. I was initially fitting the complex response function, but ran into problems which I think were cased by overall phase offsets between the data and test function. Can I canvass for opinion if fitting the magnitude is OK, or should I try again fitting the phase too?

  5509   Wed Sep 21 23:44:45 2011 PaulUpdateSUSRe:ITMY and SRM actuator response functions - fitting results

Quote:

Did you take the 180 deg shift into your account ?

Since your measurement was done when the loop was closed, there must be an additional 180 deg phase shift (in other words, minus sign).

Quote from #5507

In the end I just fitted the response magnitude. I was initially fitting the complex response function, but ran into problems which I think were cased by overall phase offsets between the data and test function. Can I canvass for opinion if fitting the magnitude is OK, or should I try again fitting the phase too?

 I thought I had, but apparently not, and I'd made another error or two in the complex version of my fitting routine. I've fixed them now, thanks! I'll put up the new fitting results tomorrow morning.

  5510   Thu Sep 22 00:00:10 2011 PaulUpdateSUSITMY and SRM actuator response functions - complex fitting results

Here are the results of the complex fitting. The residuals are bigger this time, but still probably small enough to be ok(?), with the possible exception of ITMY PITCH (due again I think to the data points straddling the resonance).

ITMY YAW actuator response complex fit

-- Fit completed after 282 iterations--

 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 1.14673e-06,
 Q factor = 12.9471,
 Pole frequency = 0.766531
 Residual (normalised against the sum of input datapoints) = 0.0688174
 
ITMY PITCH actuator response complex fit
-- Fit completed after 191 iterations--
 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 1.25105e-06,
 Q factor = 3.88981,
 Pole frequency = 0.706744
 Residual (normalised against the sum of input datapoints) = 0.144165
 
SRM YAW actuator response complex fit
-- Fit completed after 246 iterations--
 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 3.34137e-06,
 Q factor = 9.6875,
 Pole frequency = 0.854913
 Residual (normalised against the sum of input datapoints) = 0.0153646
 
SRM PITCH actuator response complex fit
-- Fit completed after 266 iterations--
 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 7.97529e-06,
 Q factor = 7.63888,
 Pole frequency = 0.568227
 Residual (normalised against the sum of input datapoints) = 0.0319653
  5514   Thu Sep 22 10:43:50 2011 PaulUpdateSUSPower spectrum with different filter gains

 I thought it might be informative before trying to optimise the filter design to see how the current one performs with different gain settings. I've plotted the power spectra for ITMY yaw with filter gains of 0, 1, 2, 3 and 4.

All of the higher gains seem to perform better than the 0 gain, so can I deduce from this that so far the oplev control loop isn't adding excess noise at these frequencies?

  5517   Thu Sep 22 13:45:17 2011 PaulUpdateSUSETMX actuator response fits

Fitting results: 

 Pitch

-- Fit completed after 305 iterations--
 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 1.85497e-06,
 Q factor = 23.7233,
 Pole frequency = 0.956686
 Residual (normalised against the sum of input datapoints) = 0.0202483
 
Yaw
-- Fit completed after 334 iterations--
 Started with: Gain = 3e-05,
 Q factor = 5,
 Pole frequency = 0.6776,
 Fit results:  Gain = 2.518e-06,
 Q factor = 7.21618,
 Pole frequency = 0.853559
 Residual (normalised against the sum of input datapoints) = 0.0570132
  5521   Thu Sep 22 17:48:20 2011 kiwamuUpdateSUSbad oplev on ETMY

It turned out the oplev controls on ETMY were just bad.

It looks like the whitening filters have been OFF and because of that the resultant open-loop was not crossing the unity gain.

I will check the whitening filters.

 

(open-loop transfer function)

The blue dots are the measured data points and the green curve is the fit.

Apparently the open-loop doesn't go above the unity gain, so the oplev had been doing nothing.

If we try to increase the overall gain it will oscillate because of the phase delay of more than 180 deg around 3 Hz.

The red curve is the expected one with the whitening filters (WFs) properly engaged.

Note that WF are supposed to have two zeros at 1 Hz and two poles at 10 Hz.

 OLETMY.png

Quote from #5518
(to do)
 + optimization of the ETMY oplevs and OSEM damping.

  5523   Thu Sep 22 20:12:54 2011 kiwamuUpdateSUSETMY oplev whitening engaged

The whitening filters for the ETMY oplevs are back.

The whitening board had been in the rack but the ADC was connected directly to the oplev interface board without going through the whitening board.

In fact the interface board and the whitening board had been already connected. So the ADC was making a shortcut.

I disconnected the ADC from the interface board and plugged it to the output of the whitening board.

Here is an example of the new open-loop transfer function with the whitening filters.

OLETMY_WF.png

 Note :

before the measurement I increased the control gain by an arbitrary number to obtain gain of more than 1 around 1 Hz.

Quote from #5521

I will check the whitening filters.

  5532   Fri Sep 23 17:57:34 2011 PaulUpdateSUSOplev filter optimization for 2 poles and 2 zeros

I have made a function to optimise the overall gain, pole frequencies and zero frequencies for the oplev filter. The script will optimize any user defined number of poles and zeros in order to minimise the RMS motion below a certain cut off frequency (in this case 20Hz). The overall gain is adjusted so that each trial filter shape always has a UGF of 10 Hz.

I have a attached a plot showing the power spectrum and RMS curves for the optimization result for 2 zeros and 2 poles, optimized to give a minimal RMS below 20Hz.

I have also attached a plot showing the loop gain and the filter transfer function.

The noise spectrum shows that the optimised filter gives a better noise performance below 10Hz, but a servo oscillation at the UGF of 10 Hz means it injects a lot of motion around this frequency. Should I consider some more aggressive way to force the script to keep a decent phase margin?

The fminsearch results show that the 'optimized' solution is two resonant peaks:

 

 -- Optimisation completed after 571 iterations--

 Started with: 

 Pole 1 frequency = 1 Hz 

 Pole 2 frequency = 2 Hz 

 Zero 1 frequency = 0.1 Hz 

 Zero 2 frequency = 5 Hz 

Overall gain = 1 

 Finished with: 

 Pole 1 frequency = 0.0497181 Hz 

 Pole 2 frequency = 2.01809 Hz 

 Zero 1 frequency = 0.0497181 Hz 

 Zero 2 frequency = 2.01809 Hz 

Overall gain = 71970.1 

 Initial RMS below 10 Hz = 5.90134e-06

 Remaining RMS below 10 Hz = 8.42898e-07

 

 

 

  5534   Sat Sep 24 01:21:11 2011 kiwamuUpdateSUSdamping test

As a suspension test I am leaving all of the suspensions restored and damped with OSEMS but without oplevs

  5536   Sat Sep 24 01:51:02 2011 ranaUpdateSUSOplev filter optimization for 2 poles and 2 zeros

Quote:

I have made a function to optimise the overall gain, pole frequencies and zero frequencies for the oplev filter. The script will optimize any user defined number of poles and zeros in order to minimise the RMS motion below a certain cut off frequency (in this case 20Hz). The overall gain is adjusted so that each trial filter shape always has a UGF of 10 Hz.

I think this is a nice start. Its clear that we don't want to use this feedback law, but the technique can be tweaked to do what we want by just tweaking our cost function.

Let's move the scripts into the SUS/ scripts area and then start putting in weights that do what we want:

1) Limit the gain peaking at the upper UGF to 6 dB.

2) Minimum phase margin of 45 deg.

3) Minimum gain margin of 10 dB.

4) Lower UGF = 0.1 Hz / Upper UGF = 10 Hz.

5) Assume a A2L coupling of 0.003 m/rad and constrain the injected noise at the test mass to be less than the seismic + thermal level.

6) Looser noise contraint above 50 Hz for the non TM loops.

  5537   Sat Sep 24 02:09:43 2011 kiwamuUpdateSUSRe:Oplev filter optimization for 2 poles and 2 zeros

Good work for the oplev noise simulations. Here are some comments/questions:

 (A) The noise looks suppressed but the open-loop transfer function doesn't look so good, because it doesn't have sufficient phase margins at the UGFs (0.01 and 10 Hz).

      I guess it is better to have a phase margin detector in your code so that the code automatically rejects a bad phase margin case.

      Actually since the number of data points are finite, the rms detector in the simulation can not always find a sharp loop oscillation.

 (B) The resultant poles and zeros seem canceling each other but the filter still has a structure. Is something wrong ?

Quote from #5332

 Pole 1 frequency = 0.0497181 Hz 

 Pole 2 frequency = 2.01809 Hz 

 Zero 1 frequency = 0.0497181 Hz 

 Zero 2 frequency = 2.01809 Hz

  5540   Sat Sep 24 17:45:56 2011 PaulUpdateSUSRe:Oplev filter optimization for 2 poles and 2 zeros

Quote:

 (B) The resultant poles and zeros seem canceling each other but the filter still has a structure. Is something wrong ?

Quote from #5332

 Pole 1 frequency = 0.0497181 Hz 

 Pole 2 frequency = 2.01809 Hz 

 Zero 1 frequency = 0.0497181 Hz 

 Zero 2 frequency = 2.01809 Hz

 Ah yes, well noticed. I think I have tracked this down to just a bug in printing of fitting results: It was just printing the pole results for the zeros too. The results for the same fit now read:

 

 Finished with: 

 Pole 1 frequency = 0.0497181 Hz 

 Pole 2 frequency = 2.01809 Hz 

 Zero 1 frequency = 0.0972455 Hz 

 Zero 2 frequency = 6.50126 Hz 

Overall gain = 71970.1

EDIT: sorry, I forgot that when you write a reply, the author is still by default the person you are replying to unless you change it!

 

  5544   Mon Sep 26 14:21:07 2011 kiwamuUpdateSUSITMX ULSEN shows jumps

Quote from #5534

As a suspension test I am leaving all of the suspensions restored and damped with OSEMS but without oplevs

According to the spectra, all of the suspensions had been damped with the OSEMs. The peaks around 1Hz are reasonably suppressed.

However the spectra from ITMX showed a noise floor at very high level. This is because of strange jumps in the signal of the UL shadow sensor.

I will check some analog circuits for the UL sensor.

 


(ITMX shadow sensors)

Here is the spectra of the ITMX shadow sensors taken during the damping test (#5534)- -

 ITMXspectra.png 

The UL sensor shows a unacceptable amount of noise.

 

Additionally I checked the time series of the ITMX shadow sensors and found ONLY the UL sensor frequently showed strange jumps in data.

Here is an example of the time series showing a jump ONLY in the UL sensor.

ITMX-sensors.png

It is possible that the jumps are coming from some circuits, since the rest of the sensors (including the oplevs) don't detect the same jump.

  5546   Mon Sep 26 15:54:46 2011 kiwamuUpdateSUSITMX ULSEN shows jumps

Currently the damping of the ITMX suspension is intentionally disabled for the noise investigation.

Quote from #5544

 

However the spectra from ITMX showed a noise floor at very high level. This is because of strange jumps in the signal of the UL shadow sensor.

I will check some analog circuits for the UL sensor.

 

  5547   Mon Sep 26 16:42:08 2011 kiwamuUpdateSUSITMX ULSEN : fixed

The issue on the ITMX UL sensor has been fixed. It was because of a loose connection in the sensor signal path.

After the fix, the sensor responses completely changed and the suspension became unable to be damped with the new matrix.

At the moment the ITMX suspension is damped by the default input matrix.

we should do the free swinging test once again.

 


(details)

 The loose connection was found on the rear side of the 1X5 rack.

There is an adapter card on the rear side, where the driver and sensor signals are combined into a single cable.

I pushed the sensor cable (bottom right in the picture) and the noise disappeared.

connection.png

Note that I changed the labels on the adapter cards from the old X/Y convention to the new one.

After fixing the loose cable the ITMX suspension became unable to be damped.

So I put the input matrix back to the default and it immediately started damping happily. It means our new matrix is not valid any more.

 

 Here is the latest noise spectra of the ITMX sensors damped with the default input matrix.

As usual all of them are limited by the ADC noise above 20 Hz. (ADC noise is plotted in purple curve)

ITMXsensors.png

 

During the work I also pushed not only ITMX ones but also the cable for the rest of the optics in the adapter cards.

Then PRM became unable to be damped, so it implies the PRM suspension also used to be the same situation.

The input matrix of PRM has been also back to the default.

 

Quote from #5546

Currently the damping of the ITMX suspension is intentionally disabled for the noise investigation.

 

  5554   Tue Sep 27 08:51:29 2011 PaulUpdateSUSOplev filter optimization for 2 poles and 2 zeros

Quote:

Quote:

I have made a function to optimise the overall gain, pole frequencies and zero frequencies for the oplev filter. The script will optimize any user defined number of poles and zeros in order to minimise the RMS motion below a certain cut off frequency (in this case 20Hz). The overall gain is adjusted so that each trial filter shape always has a UGF of 10 Hz.

I think this is a nice start. Its clear that we don't want to use this feedback law, but the technique can be tweaked to do what we want by just tweaking our cost function.

Let's move the scripts into the SUS/ scripts area and then start putting in weights that do what we want:

1) Limit the gain peaking at the upper UGF to 6 dB.

2) Minimum phase margin of 45 deg.

3) Minimum gain margin of 10 dB.

4) Lower UGF = 0.1 Hz / Upper UGF = 10 Hz.

5) Assume a A2L coupling of 0.003 m/rad and constrain the injected noise at the test mass to be less than the seismic + thermal level.

6) Looser noise contraint above 50 Hz for the non TM loops.

 I moved two matlab scripts into the folder /cvs/cds/rtcds/caltech/c1/scripts/SUS/Oplev_filter_optimization

These are the function 'filter_optimiser_zeros_and_poles.m', and the example script to run the function 'run_filter_optimiser.m'. Type 'help filter_optimiser_zeros_and_poles.m' to get details about the function.

I haven't implemented the new weights yet. I've pasted them into the the file header to remind me/us of the work to be done on the function.

  5559   Tue Sep 27 20:02:19 2011 KojiUpdateSUSWatchdog rearmed

I came to the control room and found the PMC and IMC were unlocked. ==> Relocked
I found the watch dogs of the vertex suspensions are tripped.

I checked the data for the past 6 hours and found they are independent events.
The unlock of the MCs occured 4 hours ago and the watchdogs tripped 2 hours ago.

The suspension damping was restored at around 7:50PM PDT.

  5560   Wed Sep 28 00:06:21 2011 JenneUpdateSUSWatchdog rearmed

Quote:

I came to the control room and found the PMC and IMC were unlocked. ==> Relocked
I found the watch dogs of the vertex suspensions are tripped.

I checked the data for the past 6 hours and found they are independent events.
The unlock of the MCs occured 4 hours ago and the watchdogs tripped 2 hours ago.

The suspension damping was restored at around 7:50PM PDT.

 Oops, I should have noticed all of those things.  Several hours of computer-battle exhausted me.  Thanks Koji.

  5562   Wed Sep 28 07:36:41 2011 steveUpdateSUSITMY damping restored

ITMY suspention damping restored

  5563   Wed Sep 28 07:46:42 2011 steveUpdateSUSDsub connections at the back of 1X5 are fixed

 

 I'm turning  the sus damping  off for Dsub connection fix at  the back of 1X5 rack

The plan is to install 4-40 jack screws to lock connector positions.

All dewittening(or called coil driver) and wittening D sub connectors are locked with two 4-40 socket head screws

  5587   Fri Sep 30 17:01:29 2011 steveUpdateSUSETMX oplev intensity effect on noise

Kiwamu and Steve,

This is one of the better oplev set up we have. Single bounce from TM, no mirror on stack. One lens and one  mirror on ISCT. Old Uniphase 1103P laser on heafty 3" od mounts.

Somewhat  big ~5-6 mm spot on qpd in  1,300 counts.

The intensity noise effect can be seen at 1 Hz and 3-20 Hz

Oplev servo was OFF

  5594   Sun Oct 2 02:21:27 2011 kiwamuUpdateSUSfree swinging test once more

The following optics were kicked:
MC1 MC2 MC3 ETMX ETMY ITMX ITMY PRM SRM BS
Sun Oct  2 02:13:40 PDT 2011
1001582036

They will automatically get back after 5 hours.

  5597   Sun Oct 2 18:33:36 2011 kiwamuUpdateSUSinversion of the input matrix on ETMX, ITMX and PRM

The input matrices of ETMX, ITMX and PRM have been newly inverted.

Those were the ones having some troubles (see #5444, #5547).

After a coarse adjustment of the damping Q factors, they look damping happily.

 

    optic                    spectra    inverted matrix   BADNESS
ETMX ETMX.png       pit     yaw     pos     side    butt
UL    0.848   0.108   1.578   0.431   1.025 
UR    0.182  -1.892   1.841  -0.128  -1.172 
LR   -1.818  -1.948   0.422  -0.122   0.939 
LL   -1.152   0.052   0.159   0.438  -0.864 
SD    1.756  -3.794  -0.787   1.000  -0.132 
  5.37028
ITMX ITMX.png     pit     yaw     pos     side    butt
UL    0.510   0.584   1.228   0.458   0.203 
UR    0.783  -1.350   0.348  -0.050   0.555 
LR   -1.217   0.065   0.772   0.264   0.312 
LL   -1.490   2.000   1.652   0.772  -2.930 
SD   -0.635   0.853  -1.799   1.000  -1.597  
 7.5125
PRM PRM.png       pit     yaw     pos     side    butt
UL    0.695   1.422   1.774  -0.333   0.954 
UR    1.291  -0.578   0.674  -0.068  -0.939 
LR   -0.709  -1.022   0.226   0.014   0.867 
LL   -1.305   0.978   1.326  -0.251  -1.240 
SD    0.392  -0.437  -0.500   1.000   0.420
 5.09674

 

(some notes)

 Before running the peakFit scripts, I woke up the nds2 sever process on Mafalda because it hasn't been recovered from the power outage.

To start the nds2 process I followed the instruction by Jamie (#5094).

Then I started requesting the data of the last night's free swinging test (#5594)

However the NDS2_GetData command failed everytime when data with long duration were requested.

It maybe because some of the data are missing in sometimes, but I haven't seriously checked the data stored in fb.

So for the reason, I had to use a short duration of 1200 sec (default is 3600 sec). That's why spectra look noisier than usual.

  5600   Mon Oct 3 13:04:12 2011 JenneUpdateSUSAUXEX, AUXEY rebooted

Quote:

  + I found that burtrestore for the ETMX DC coil forces were not functional.

  => currently ETMX's "restore" and "mislalign" buttons on the C1IFO_ALIGN screen are not working.

  => According to the error messages, something seemed wrong on c1auxex, which is a slow machine controlling the DC force.

 [Suresh, Jenne]

Suresh pointed out the oddity that all of the EX, EY slow channels were showing white boxes on the medm screens on all of the workstations except Rosalba.  I don't know why Rosalba seemed to be working, but whatever.  I'm not 100% sure that Rosalba was even working properly....I shutdown ETMX and ETMY's watchdogs before we went to boot computers, but when I came back to the control room the 2 optics were rung up anyway.  Turning back on the watchdogs, the optics immediately began to damp happily.

Since Kiwamu had trouble with the slow channels for EX, we decided to key some crates. 

We keyed the c1auxey, and c1auxex crates, waited a few seconds, and then things looked okay in medm-land.  I looked at the "View Backup" for ETMX, and there were no values for the DC sliders, so since the arms are both flashing right now, I did a "save", and then confirmed that I can misalign and restore the optic.  However, since I didn't fully align/lock the cavity, the saved value for right now shouldn't be fully trusted.  We might have to manually align the cavity using the BS.

  5601   Mon Oct 3 14:05:41 2011 JenneUpdateSUSFailing to set SUS summary screen values

I assume it's because the burt restore didn't work for the SUS summary screen, but all of the values for the ifo suspensions (not the MCs...they're okay) are red. 

I am trying to run Rana's setSensors.py script, but am failing.  Any inspiration would be appreciated:

rosalba:SUS_SUMMARY>./setSensors.py 1001708529 500 .1 .25
['./setSensors.py', '1001708529', '500', '.1', '.25']
/cvs/cds/caltech/apps/linux64/python/lib64/python2.4/site-packages/nds/__init__.py:28: RuntimeWarning: No protocol specified, attempting protocol nds_v2
  super(daq, self).__init__(host, port)
Connecting NDS2 .... authenticate done
Traceback (most recent call last):
  File "./setSensors.py", line 81, in ?
    mean = acquire(x)
  File "./setSensors.py", line 73, in acquire
    daq.request_channel(chans[x])
Boost.Python.ArgumentError: Python argument types in
    daq.request_channel(daq, str)
did not match C++ signature:
    request_channel(_daq_t {lvalue}, daq_channel_t*)

I'm not exactly sure what the problem is.  Line 73, looks like it should have 2 arguments in the daq.request_channel, but even if I put in the "daq" variable (which is set a few lines above), I get the exact same error.  So...something else is wrong.  Ideas from someone who "speaks" python??

  5604   Mon Oct 3 17:27:23 2011 JenneUpdateSUSFailing to set SUS summary screen values

Quote:

I am trying to run Rana's setSensors.py script, but am failing.  Any inspiration would be appreciated:

rosalba:SUS_SUMMARY>./setSensors.py 1001708529 500 .1 .25
['./setSensors.py', '1001708529', '500', '.1', '.25']
/cvs/cds/caltech/apps/linux64/python/lib64/python2.4/site-packages/nds/__init__.py:28: RuntimeWarning: No protocol specified, attempting protocol nds_v2
  super(daq, self).__init__(host, port)
Connecting NDS2 .... authenticate done
Traceback (most recent call last):
  File "./setSensors.py", line 81, in ?
    mean = acquire(x)
  File "./setSensors.py", line 73, in acquire
    daq.request_channel(chans[x])
Boost.Python.ArgumentError: Python argument types in
    daq.request_channel(daq, str)
did not match C++ signature:
    request_channel(_daq_t {lvalue}, daq_channel_t*)

I'm not exactly sure what the problem is.  Line 73, looks like it should have 2 arguments in the daq.request_channel, but even if I put in the "daq" variable (which is set a few lines above), I get the exact same error.  So...something else is wrong.  Ideas from someone who "speaks" python??

 My guess is that this has something to do with the NDS client version you're using.  Try running the script on a machine where pynds and nds-client are known to be compatible, like pianosa.

  5618   Tue Oct 4 19:31:17 2011 kiwamuUpdateSUSPRM and BS oplev laser died

The He-Ne laser which has been used for the PRM and BS oplevs were found to be dead.

According to the trend data shown below, it became dead during the dolphin issue.

(During the dolphin issue the output from the oplev QPDs are digitally zero)

oplevs.png

  5620   Wed Oct 5 11:33:25 2011 steveUpdateSUSPRM and BS oplev laser replaced

 

JDSU 1103P died after 4 years of service. It was replaced with new identical head of 2.9 mW output. The power supply was also changed.

The return spots of 0.04 mW  2.5 mm diameter on qpds are BS  3,700 counts and PRM 4,250 counts.

 

  5622   Wed Oct 5 17:08:49 2011 steveUpdateSUSBS oplev spectra

Kiwamu and Steve,

The He/Ne oplev shows no coherece so relative intensity noise is not limiting factor for the oplev servo

  5630   Fri Oct 7 14:04:48 2011 steveUpdateSUSHe/Ne intensity noise effect on oplevs

The SRM bounce peak 18.33 Hz. Suresh helped me to retune filter through Foton, but we failed to remove it.

ITMX_OPLEV_PERROR shows high coherence with oplev laser. This is our lousiest set up. I will work on it next week.

Generally speaking we can say that JDSU-Uniphase 1103P and 1125P laser intensity noise do not limit oplev servo performance.

However, the overall well being of filters, gain settings, beam sizes on qpds are poor.

 

  5633   Fri Oct 7 22:31:53 2011 kiwamuUpdateSUSnoisy ULSEN on ETMY

Yesterday Koji was claiming that the rms monitor of ULSEN on ETMY didn't well go down.

Indeed something bad is happening on ULSEN of ETMY.

I guess it could be a loose connection.

ETMY_OSEMs.png

(The unit of Y axis in the plot is not true. Don't believe it !)

  5636   Fri Oct 7 23:23:05 2011 kiwamuUpdateSUSSRM oplev was oscillating

The SRM oplevs were found to be oscillating because of a small phase margin.

I reduced the gains to the half of them. The peak which Steve found today maybe due to this oscillation.

Quote from #5630

The SRM bounce peak 18.33 Hz. Suresh helped me to retune filter through Foton, but we failed to remove it. 

  5645   Mon Oct 10 16:32:18 2011 steveUpdateSUSUL sensor of ETMY is recovered

 I lost UL osem voltage this morning when I was checking the actual connection at rack ETMY

This after noon I disconnected  the 64 pins IDE connector from satelite amp at the rack, and the two 25 pins Dsubs at this juction board.

UL OSEM recovered after reconnecting these three connectors.

Atm3, bad connection.........noisy UL

 

  5655   Wed Oct 12 08:43:30 2011 steveUpdateSUSITMX oplev improved a bit

 Atm2 is before optical path adjustment. The idea was to remove possible clipping in vacuum.

Coherense significantly reduced below 4 Hz

Today I will replace the He/Ne laser 1125P with 1103P

 

  5660   Thu Oct 13 14:23:09 2011 steveUpdateSUSITMX oplev with 3 mm beam on qpd

 I replaced the JDSU-Uniphase 1125P by 1103P He/Ne laser. This new laser had 2.8 mW output yesterday. It degraded to 0.5 mW by this morning.

The beam size on the QPD is ~3 mm  This should give us  better sensitivity. These are not the perfect lenses at all, but we have them here.

On the other hand, there are still some coherence below 1 Hz, so the laser intensity noise or clipping dominating  this  part of the spectrum.

 

  5666   Fri Oct 14 16:20:11 2011 ZachUpdateSUSC1:SUS-ETMX_SPDMon fixed

I offered to help Kiwamu with some of the 40m work. The first task was to figure out why the ETMX side OSEM monitor was so low, since we know that the depth is about right. It was showing ~0.13 V to the others' ~0.7 V.

TL,WR: There was a wire disconnected from the breakout panel on the side of the rack

I started by pulling the board out and checking to make sure that it was working properly. I injected a sine wave to the SIDE IN and found that it showed up in the signal coming out of the back (into the crate) just fine (see below). One strange thing I noticed while testing the board is that both inputs for each used channel of the MAX333 switches on the board are shorted to their respective outputs. That is, the switches seem to be open to BOTH 0 and 1 logic states. This seems counterintuitive, but perhaps there's something about how these work that I don't know.

board_works.png

 

Then I went about tracing the signal from the back of the crate to the breakout panel on the side of the rack. I opened it up, verified that the ribbon cable was transmitting correctly, and as I went to plug it back in I noticed that one of the wires---the correct one---had come completely undone.

rut_roh_raggie.png

The screw clamp appeared to be a bit finicky, as I had to loosen and tighten it a few times before it finally seemed to grab hold of the wire. It probably just wasn't tight in the first place and the wire was pulled out. Anyway, things are working now:

Screen_shot_2011-10-14_at_4.09.45_PM.png

  5667   Fri Oct 14 18:38:41 2011 kiwamuUpdateSUSC1:SUS-ETMX_SPDMon fixed

Quote from #5666

 Anyway, things are working now:

 Good job ! Thank you so much

  5675   Mon Oct 17 07:57:24 2011 steveUpdateSUSETMX sus damping restored
  5680   Mon Oct 17 17:07:30 2011 steveUpdateSUSETMX oplev returning beam od 3 mm

 ETMX oplev had 6 mm diameter beam on the qpd.  I relayed the beam path with 2 lenses  to get back  3 mm beam on the qpd

BRC 037  -100 Bi _concave lens and PCX 25  200 VIS do the job. Unfortunately the concave lens has the AR 1064.

 

 

  5690   Wed Oct 19 04:23:58 2011 kiwamuUpdateSUSSRM free swinging test

The following optics were kicked:
SRM
Wed Oct 19 04:22:53 PDT 2011
1003058589
 

  5691   Wed Oct 19 05:15:44 2011 kiwamuUpdateSUStaking care of SRM

I made some efforts to fix the situation of SRM but it is still bad.

The POS motion wasn't well damped. Something is wrong either (maybe both) sensing part or actuation part.

I am going to check the sensing matrix with the new free swinging spectra (#5690)

 

(Symptom)

 When I was trying to lock SRMI I found that the fringes observed at the AS camera didn't show spatial higher order modes, which is good.

So I thought the SRM suspension became quiet, but it actually wasn't. Because the RMS monitor of the SRM OSEMs already went to about 30 counts.

At the same time the opelev error signals were well suppressed. It means some DOFs which were insensitive to the oplev were ringing up, namely POS and SIDE.

According to the LSC error signal and the ASDC signal, I believe that the POS was going wild (although I didn't check the OSEM spectra).
 

(Some efforts)

 + Readjusted the f2a filters (see the attachment).

 + Tried to eliminate a coupling between the POS and SIDE drives by tweaking the output matrix.

    => In order to eliminate the coupling from the POS drive to SIDE sensor, I had to put a comparable factor into an element.

     So it might be possible that the POS sensor was showing the SIDE signal and vice versa.

      In order to check it I left SRM free swinging (#5690).

Quote from #5684

The main reason why I couldn't lock DRMI was that the suspensions were touchy and especially the SRM suspension wasn't good.

ELOG V3.1.3-