ID |
Date |
Author |
Type |
Category |
Subject |
13740
|
Mon Apr 9 16:30:21 2018 |
Kira | Update | PEM | MEDM setup | I created an MEDM screen for the PID control. In addition, I added a new EPICS channel for the setpoint so that it could be adjusted using the MEDM screen.
Edit: forgot to mention the channel name is C1:PEM-SEIS_EX_TEMP_SETPOINT
Edit #2: the path for the MEDM is /opt/rtcds/caltech/c1/medm/c1pem/C1PEM_SEIS_EX_TCTRL.adl |
13741
|
Mon Apr 9 18:46:03 2018 |
gautam | Update | IOO | Further debugging |
- I analyzed the data from the free swinging MC test conducted over the weekend. Attachment #1 shows the spectra. Color scheme is same for all panels.
- I am suspicious of MC3: why does the LR coil see almost no Yaw motion?
- The "equilibrium" values of all the sensor signals (at the IN1 of the coil input filters) are within 20% of each other (for MC3, but also MC1 and MC2).
- The position resonance is also sensed more by the side coil than by the LR coil.
- To rule out satellite box shenanigans, I just switched the SRM and MC3 satellite boxes. But coherence between frequency noise as sensed by the arms remain.
- I decided to clean up my IMC nosie budget a bit more.
- Attachment #2 shows the NB as of today. I'll choose a better color palette for the next update.
- "Seismic" trace is estimated using the 40m gwinc file - the MC2 stack is probably different from the others and so it's contribution is probably more, but I think this will suffice for a first estimate.
- "RAM" trace is measured at the CM board input, with MC2 misaligned.
- The unaccounted noise is evident from above ~8 Hz.
- More noises will be added as they are measured.
- I am going to spend some time working on modeling the CM board noise and TF in LTspice. I tried getting a measurement of the transfer function fron IN1 to the FAST output of the CM board with the SR785 (motivation being to add the contribution of the input referred CM board noise to the NB plot), but I suspect I screwed up something w.r.t. the excitation amplitude, as I am getting a totally nonsensical shape, which also seems to depend on my input excitation amplitude. I don't think the output is saturated (viewed during measurement on a scope), but perhaps there are some subtle effects going on.
|
13743
|
Mon Apr 9 23:49:50 2018 |
rana | Update | PSL | PSL chans | I think we can scrap the 126MOPA channels since they're associated with the Lightwave NPRO and MOPA. We should add the channels that we need for monitoring the Innolight NPRO from the d-sub connector on its controller. |
13744
|
Tue Apr 10 14:28:44 2018 |
gautam | Update | IOO | Further debugging | I am working on IMC electronics. IMC is misaligned until further notice. |
13745
|
Tue Apr 10 15:42:08 2018 |
Kira | Update | PEM | MEDM setup | An update to the screen. I changed the min/max values for some of the parameters, as well as changing the script so that I could specify the integral gain in terms of 1e-5. I've also added this screen to the PEM tab in the sitemap. |
13746
|
Wed Apr 11 01:34:31 2018 |
gautam | Update | IOO | Activities today | [kevin, gautam]
activities done today - details/plots/data/evidence tomorrow.
- Checked XARM loop shape. Updated NB code to fetch POX data from NDS and undo loop shape rather than using calibration filter bank.
- Checked POX loop calibration (m/ct). Number I was using was 8e-13. Tonight we measured 9e-13. Updated filter bank.
- Tried to get Y arm green ALS going.
- Improved GTRY from ~0.05 to 0.3.
- Tried to improve mode matching onto BBPD on PSL table to see a green beat.
- But we were unsuccessful.
- I think I got the near and far field alignment right, and the EY laser temp is set such that I can see an IR beat @~30MHz (so green beat should be at 60 MHz).
- But I couldn't see anything with scope or with HP spec analyzer.
- More tomorrow. Motivation to get green ALS working is to get some more confidence that the excess noise is indeed on the PSL light.
|
13747
|
Wed Apr 11 10:47:26 2018 |
Steve | Update | SUS | satellite amps labeled | Satellite amplifiers labeled with date. Old labels left on. |
13748
|
Thu Apr 12 10:15:33 2018 |
Kira | Update | PEM | MEDM setup | Another update. I've changed the on/off button so that it's visible which state it's in. I did that by changing the type of C1:PEM-SEIS-EX_TEMP_SLOWLOOP from ai to bi (I checked the FSS script and copied the entry for the slowloop). Previously, MEDM was giving me an error that it wasn't an ENUM value when I wanted to use a choice button to indicate the value of slowloop, and this solved the issue. I've also added a StripTool button. |
13749
|
Thu Apr 12 18:12:49 2018 |
gautam | Update | ALS | NPRO channels hijacked | Summary:
- Today, the measured IR ALS noise for the X arm was dramatically improved. The main change was that I improved the alignment of the PSL pickoff beam into its fiber coupler.
- The noise level was non-stationary, leading me to suspect power modulation of the RF beat amplitude.
- I am now measuring the stability of the power in the two polarizations coming from EX table to the PSL table, using the PSL diagnostic connector channels.
- The EX beam is S-polarized when it is coupled into the fiber. The PSL beam is P-polarized. However, it looks like I have coupled light along orthogonal axes into the fiber, such that when the EX light gets to the PSL table, most of it is in the P-polarization, as judged by my PER measurement setup (i.e. the alignment keys at the PSL table and at the EX table are orthogonal). So it still seems like there is something to be gained by trying to improve the PER a bit more.
Details:
Today, I decided to check the power coupled into the PSL fiber for the BeatMouth. Surprisingly, it was only 200uW, while I had ~3.15mW going into it in January. Presumably some alignment drifting happened. So I re-aligned the beam into the fiber using the steering mirror immediately before the fiber coupler. I managed to get ~2.9mW in without much effort, and I figured this is sufficient for a first pass, so I didn't try too much more. I then tried making an ALS beat spectrum measurement (arm locked to IMC length using POX, green following the arm using end PDH servo). Surprisingly, the noise performannce was almost as good as the reference! See Attachment #1, in which the red curve is an IR beat (while all others are green beats). The Y arm green beat performance isn't stellar, but one problem at a time. Moreover, the kind of coherence structure between the arm error signal and the ALS beat signal that I reported here was totally absent today.
Upon further investigation, I found that the noise level was actually breathing quite significantly on timescales of minutes. While I was able to successfully keep the TEM00 mode of the PSL beam resonant inside the arm cavity by using the ALS beat frequency as an error signal and MC2 as a frequency actuator, the DC stability was very poor and TRX was wandering around by 50%. So my new hypothesis is that the excess ALS noise is because of one or more of
- Beam jitter at coupling point into fiber.
- Polarization drift of the IR beams.
While I did some work in trying to align the PSL IR pickoff into the fiber along the fast (P-pol) axis, I haven't done anything for the X end pickoff beam. So perhaps the fluctuations in the EX IR power is causing beatnote amplitude fluctuations. In the delay line + phase tracker frequency discriminator, I think RF beatnote amplitude fluctuations can couple into phase noise linearly. For such an apparently important noise source, I can't remeber ever including it in any of the ALS noise budgets.
Before Ph237 today, I decided to use my polarization monitoring setup and check the "RIN" of power in the two polarizations coming out of the fiber on the PSL table. For this purpose, I decided to hijack the Acromag channels used for the PSL diagnostics connector Attachment #2 shows that there is fluctuations at the level of ~10% in the p-polarization. This is the "desired" polarization in that I aligned the PSL beam into the fiber to maximize the power in this polarization. So assuming the power fluctuations in the PSL beam are negligible, this translates to sqrt(10) ~3% fluctuation in the RF beat amplitude. This is at best a conservative estimate, as in reality, there is probably more AM because of the non PM fibers inside the beatmouth.
All of this still doesn't explain the coherence between the measured ALS noise and the arm error signal at 100s of Hz (which presumably can only happen via frequency noise in the PSL).
Another "mystery" - yesterday, while I was working on recovering the Y arm green beat signal on the PSL table, I eventually got a beat signal that was ~20mVpp into 50ohms, which is approximately the same as what I measured when the Y arm ALS performance was "nominal", more than a year ago. But while viewing the Y arm beats (green and IR) simultaneously on an o'scope, I wasn't able to keep both signals synchronised while triggering on one (even though the IR beat frequency was half the green beat frequency). This means there is a huge amount of relative phase noise between the green and IR beats. What (if anything) does this mean? The differential noise between these two beats should be (i) phase noise at the fiber coupler/ inside the fiber itself, and (ii) scatter noise in the green light transmitted through the cavity. Is it "expected" that the relative phase noise between these two signals is so large that we can't view both of them on a common trigger signal on an o'scope? Also - the green mode-matching into the Y arm is abysmal.
Anyways - I'm going to try and tweak the PER and mode-matching into the X end fiber a little and monitor the polarization stability (nothing too invasive for now, eventually, I want to install the new fiber couplers I acquired but for now I'll only change alignment into and rotation of the fiber coupler on the EX table). It would also be interesting to compare my "optimized" PSL drift to the unoptimized EX power drift. So the PSL diagnostic channels will not show any actual PSL diagnostic information until I plug it back in. But I suspect that the EPICS record names and physical channel wiring are wrong anyways - I hooked up my two photodiode signals into what I would believe is the "Diode 1 Power" and "Laser crystal temperature" monitors (as per the schematic), but the signals actually show up for me in "Diode 2 Power" (p-pol) and "Didoe 1 Temperature" (s-pol).
Annoyingly, there is no wiring diagram - on my todo list i guess...
@Steve - could you please take a photo of the EX table and update the wiki? I think the photo we have is a bit dated, the fiber coupler and transmon PDs aren't in it... |
13750
|
Fri Apr 13 00:20:46 2018 |
rana | Update | PEM | MEDM setup | changed the setpoint of the EX Seismomter T ctrl servo from 35 to 39 C to see if this helps the stability by decreasing the cooldown time constant. |
13751
|
Fri Apr 13 11:02:41 2018 |
gautam | Update | ALS | EX fiber polarization drift | Attachment #1 shows the drift of the polarization content of the light from EX entering the BeatMouth. Seems rather large (~10%). I'm going to tweak the X end fiber coupling setup a bit to see if this can be improved. This performance is also a good benchmark to compare the PSL IR light polarization drift. I am going to ask Steve to order Thorlabs K6XS, which has a locking screw for the rotational DoF. With this feature, and by installing some HWPs at the input coupling point, we can ensure that we are coupling light into one of the special axes in a much more deterministic way. |
13752
|
Fri Apr 13 16:59:12 2018 |
gautam | Update | ALS | EX green mode-matching | THIS CALCULATION IS WRONG FOR THE OVERCOUPLED CAV.
Summary:
Mode-matching efficiency of EX green light into the arm cavity is ~70*%, as measured using the visibility.
Details:
I wanted to get an estimate for the mode-matching of the EX green beam into the arm cavity. I did the following:
- Locked arm cavities to IR. Ran dither alignment servos to maximize the transmission of IR on both arms. The X arm dither alignment servo needs some touching up, I can achieve higher TRX by hand than by running the dither.
- Aligned green PZT mirrors so as to maximize GTRX. Achieved level as 0.47.
- Went to EX table and tweaked the two available mode-matching lens positions on their translational stages. Saw a quadratic maximum of GTRX about some equilibrium position (where the lenses are now).
- Measured average value of the green PDH reflection DC level whiel green TEM00 mode was locked.
.
- Misaligned ITMX macroscopically. Measured the average value of the green PDH reflection DC level again.
.
- Closed EX Green shutter. Measured the average value of the green PDH reflection DC level.
.
- Modulation depth of the EX PDH was determined to be 90mrad. Based on this, power in sideband is negligible compared to power in the carrier, so I didn't bother correcting for sideband power in reflection.
- Mode-matching efficiency calculated as
.
Comments:
This amount of mode-matching is rather disappointing - using a la mode, the calculated mode-matching efficiency is nearly 100%, but 70% is a far cry from this. The fact that I can't improve this number by either tweaking the steering or by moving the MM lenses around suggests that the estimate of the target arm mode is probably incorrect (the non-gaussianity of the input beam itself is not quantified yet, but I don't believe this input beam can account for 30% mismatch). For the Y-arm, the green REFL DC level is actually higher when locked than when ITMY is misaligned. WTF?? Only explanation I can think of is that the PD is saturated when green is unlocked - but why does the ADC saturate at ~3000cts and not 32000?
This data is almost certainly bogus as the AA box at 1X9 is powered by +/-5VDC and not +/-15VDC. I didn't check but I believe the situation is the same at the Y-end.
3000 cts is ~1V into the ADC. I am going to change the supply voltage to this box (which also reads in ETMX OSEMS) to +/-15V so that we can use the full range of the ADC.
gautam Apr 26 630pm: I re-did the measurement by directly monitoring the REFLDC on a scope, and the situation is not much better. I calculate a MM of 70% into the arm. This is sensitive to the lens positions - while I was working on the EX fiber coupling, I had bumped the lens mounted on a translational stage on the EX table lightly, and I had to move that lens around today in order to recover the GTRX level of 0.5 that I am used to seeing (with arm aligned to maximize IR transmission). So there is definitely room for optimization here.
|
13753
|
Fri Apr 13 17:56:26 2018 |
gautam | Update | ALS | Fibers switched out | I swapped the EX fiber for the PSL fiber in the polarization monitoring setup. There is a lot more power in this fiber, and one of the PDs was saturated. I should really have put a PBS to cut the power, but I opted for putting an absorptive ND1.0 filter on the PD instead for this test. I want to monitor the stability in this beam and compare it to the EX beam's polarization wandering. |
13754
|
Sat Apr 14 14:42:09 2018 |
gautam | Update | ALS | Fibers switched out | It looks like the drift in polarization content in the PSL pickoff is actually much higher than that in the EX pickoff. Note that to prevent the P-pol diode from saturating, I put an ND filter in front of the PD, so the Y axis actually has to be multiplied by 10 to compare power in S and P polarizations. If this drift is because of the input (linear) polarization being poorly matched to one of the fiber's special axes, then we can improve the situation relatively easily. But if the polarization drift is happening as a result of time-varying stress (due to temp. fluctuations, acoustics etc) on the (PM) fiber from the PSL fiber coupler to the BeatMouth, then I think this is a much more challenging problem to solve.
I'll attempt to quantify the contribution (in Hz/rtHz) of beat amplitude RIN to phase tracker output noise, which will tell us how much of a problem this really is and in which frequency bands. In particular, I'm interested in seeing if the excess noise around 100 Hz is because of beat amplitude fluctuations. But on the evidence thus far, I've seen the beat amplitude drift by ~15 dB (over long timescales) on the control room network analyzer, and this drift seems to be dominated by PSL light amplitude fluctuations. |
13755
|
Mon Apr 16 22:09:53 2018 |
Kevin | Update | General | power outage - BLRM recovery | I've been looking into recovering the seismic BLRMs for the BS Trillium seismometer. It looks like the problem is probably in the anti-aliasing board. There's some heavy stuff sitting on top of it in the rack, so I'll take a look at it later when someone can give me a hand getting it out.
In detail, after verifying that there are signals coming directly out of the seismometer, I tried to inject a signal into the AA board and see it appear in one of the seismometer channels.
- I looked specifically at C1:PEM-SEIS_BS_Z_IN1 (Ch9), C1:PEM-SEIS_BS_X_IN1 (Ch7), and C1:PEM-ACC_MC2_Y_IN1 (Ch27). All of these channels have between 2000--3000 cts.
- I tried injecting a 200 mVpp signal at 1.7862 Hz into each of these channels, but the the output did not change.
- All channels have 0 cts when the power to the AA board is off.
- I then tried to inject the same signal into the AA board and see it at the output. The setup is shown in the first attachment. The second BNC coming out of the function generator is going to one of the AA board inputs; the 32 pin cable is coming directly from the output. All channels give 4.6 V when when the board is powered on regardless of wheter any signal is being injected.
- To verify that the AA board is likely the culprit, I also injected the same signals directly into the ADC. The setup is shown in the second attachment. The 32 pin cable is going directly to the ADC. When injecting the same signals into the appropriate channels the above channels show between 200--300 cts, and 0 cts when no signal is injected.
|
13756
|
Tue Apr 17 09:57:09 2018 |
Steve | Update | General | seismometer interfaces |
Quote: |
I've been looking into recovering the seismic BLRMs for the BS Trillium seismometer. It looks like the problem is probably in the anti-aliasing board. There's some heavy stuff sitting on top of it in the rack, so I'll take a look at it later when someone can give me a hand getting it out.
In detail, after verifying that there are signals coming directly out of the seismometer, I tried to inject a signal into the AA board and see it appear in one of the seismometer channels.
- I looked specifically at C1:PEM-SEIS_BS_Z_IN1 (Ch9), C1:PEM-SEIS_BS_X_IN1 (Ch7), and C1:PEM-ACC_MC2_Y_IN1 (Ch27). All of these channels have between 2000--3000 cts.
- I tried injecting a 200 mVpp signal at 1.7862 Hz into each of these channels, but the the output did not change.
- All channels have 0 cts when the power to the AA board is off.
- I then tried to inject the same signal into the AA board and see it at the output. The setup is shown in the first attachment. The second BNC coming out of the function generator is going to one of the AA board inputs; the 32 pin cable is coming directly from the output. All channels give 4.6 V when when the board is powered on regardless of wheter any signal is being injected.
- To verify that the AA board is likely the culprit, I also injected the same signals directly into the ADC. The setup is shown in the second attachment. The 32 pin cable is going directly to the ADC. When injecting the same signals into the appropriate channels the above channels show between 200--300 cts, and 0 cts when no signal is injected.
|
|
13757
|
Tue Apr 17 14:08:29 2018 |
gautam | Update | ALS | Fibers switched out | A follow-up on the discussion from today's lunch meeting - Rana pointed out that rotation of the fiber in the mount by ~5degrees cannot account for such large power fluctuations. Here is a 3 day trend from my polarization monitoring setup. Assuming the output fiber coupler rotates in its mount by 5 degrees, and assuming the input light is aligned to one of the fiber's special axes, then we expect <1% fluctuation in the power. But the attached trend shows much more drastic variations, more like 25% in the p-polarization (which is what I assume we use for the beat, since the majority of light is in this polarization, both for PSL and EX). I want to say that the periodicity in the power fluctuations is ~12hours, and so this fluctuation is somehow being modulated by the lab temperature, but unfortunately, we don't have the PSL enclosure temperature logged in order to compare coherence.
Steve: your plots look like temperature driven
The "beat length" of the fiber is quoted as <=2.7mm. This means that a linearly polarized beam that is not oriented along one of the special axes of the fiber will be rotated through 180 degrees over 2.7mm of propagation through the fiber. I can't find a number for the coefficient of thermal expansion of the fiber, but if temperature driven fluctuations are changing the length of the fiber by 300um, it would account for ~12% power fluctuation between the two polarizations in the monitoring setup, which is in the ballpark we are seeing... |
13758
|
Wed Apr 18 10:44:45 2018 |
gautam | Update | CDS | slow machine bootfest | All slow machines (except c1auxex) were dead today, so I had to key them all. While I was at it, I also decided to update MC autolocker screen. Kira pointed out that I needed to change the EPCIS input type (in the RTCDS model) to a "binary input", as opposed to an "analog input", which I did. Model recompilation and restart went smooth. I had to go into the epics record manually to change the two choices to "ENABLE" and "DISABLE" as opposed to the default "ON" and "OFF". Anyways, long story short, MC autolocker controls are a bit more intuitive now I think. |
13759
|
Wed Apr 18 12:18:39 2018 |
Kira | Update | PEM | final setup sketch | I've updated the sketches and added in front panels for the seismometer block and the 1U panel (attachments 3 and 4). There was an issue when it came to the panel on the block because the hole is only big enough for the cable that already exists there and there is no space to add in the D-9 connector. Not quite sure how to resolve this issue. Attachment 7 is the current panel on the seismometer block. Attachments 5 and 6 are the updated temperature circuit and the heater circuit.
The boxes will be located in the short racks at EX and EY to minimize cable length. |
13760
|
Wed Apr 18 16:59:35 2018 |
rana | Update | PEM | final setup sketch: EX Seis | Can you please add dimensions to the drawing, so we can see if things fit and what the cable lenghts need to be?
For the panel on the granite slab, we should use a thinner piece of metal and mount it with an offset so that the D-sub cable can be fished through the hole in the slab. The hole is wide enough for 2 cables, but not 2 connectors.
Attached is a 8-day minute trend of the heater control signals, as well as the in-loop temperature sensor (which underestimates the true fluctuations; we really need an out-of-loop sensor attached to the can or seismometer).
You can see that since the last tuning (on the 13th), its been stable at the set point of 39 C with 8.5 - 10 W of heating power. Need to add the PID loop settings (all the sliders on the MEDM screen) to the frames so that we can help in diagnosing. Also, fix the spelling of "Celcisususs". |
13762
|
Wed Apr 18 19:02:15 2018 |
gautam | Update | IOO | MC spot centering scripts | I'm working on fixing these (and the associated MEDM scripts) up so that we can get some reliable readback on how well centered the spots are on the MC mirrors. Seems like a bunch of MEDM display paths were broken, and it looks like the optimal demod phases (to put most of the output in I quadrature) are not what the current iteration of the scripts set them to be. It may well be that the gains that convert demodulated counts to mm of spot offset are also not correct anymore. I ran the script ~4times in ~1 hour time span, and got wildly different answers for the spot centering each time, so I wouldn't trust any of those numbers atm...
As you can see in Attachment #1, I stepped the demod phase of one of the servos from -180 to 180 degrees in 5degree increments. The previously used value of 57degrees is actually close to the worst possible point (if you want the signal in the I quadrature, which is what the scripts assume).
I used Attachment #2 to change up the demod phases to maximize the I signal. I chose the demod phase such that it preserved the sign of the demodulated signal (relative to the old demod phases). I also made some StripTool templates for these, and they are in the MC directory. Doing the spot centering measurement with the updated demod phases yields the following output from the script:
spot positions in mm (MC1,2,3 pit MC1,2,3 yaw):
[0.72506586251144134, 7.1956908534034403, 0.54754354165324848, -0.94113388241389784, -3.5325883025464959, -2.4934027726657142]
Seems totally unbelievable still that we are so far off center on MC1 yaw. Perhaps the gains and calibration to convert from counts to mm of spot offset need to be rechecked. |
13763
|
Wed Apr 18 20:33:19 2018 |
Kevin | Update | General | seismometer interfaces | Steve, the pictures you posted are not the AA board I was referring to. The attached pictures show the board which is sitting beneath the GPS time server. |
13765
|
Thu Apr 19 00:03:51 2018 |
gautam | Update | IOO | More IMC NBing | Summary:
As shown in the Attachments, it seems like IMC DAC and coil driver noise is the dominant noise source above 30Hz. If we assume the region around the bounce peak is real motion of the stack (to be confirmed with accelerometer data soon), this NB is starting to add up. Much checking to be done, and I'd also like to get a cleaner measurement of coil driver and DAC noise for all 3 optics, as there seems to be a factor of ~5 disagreement between the MC3 coil driver noise measurement and my previous foray into this subject. The measurement needs to be refined a little, but I think the conclusion holds.
Details:
- I had a measurement of the MC3 coil driver noise from ~2weeks ago when I was last working on this that I had not yet added to the NB.
- Today I added it. To convert from measured voltage noise to frequency noise, I assumed the usual 0.016N/A per coil number, which is probably a large source of systematic error.
- I define the "nominal" IMC operating condition as MC1 and MC3 having the analog de-whitening filters switched on, but MC2 switched off.
- So length noise should be dominated by coil driver noise on MC1 and MC3, and DAC noise on MC2.
- The measurement I had was made with the input to the coil driver board terminated in 50ohms. Measurement was made in-situ. The measurement has a whole bunch of 60Hz harmonics (despite the Prologix box being powered by a linear power adapter, but perhaps there are other ground loops which are coupling into the measurement). So I'd like to get a cleaner measurement tmrw.
- To confirm, Koji suggested some On/Off test by driving some broadband noise in the coils. I figured toggling the analog de-whitening, such that the DAC noise or coil driver electronics dominate is an equally good test.
- Attachment #2 shows the effect in arm error and control signal spectra. Note that I engaged analog de-whitening on all 3 optics for the red curves in this plot. But even leaving MC2 de-whitening off, I could see the read curve was below the black reference trace, which was taken with de-whitening off on all 3 optics.
Remarks:
Since I sunk some time into it already, the motivation behind this work is just to try and make the IMC noise budget add up. It is not directly related to lowering the IR ALS noise, but if it is true that we are dominated by coil driver noise, we may want to consider modifying the MC coil driver electronics along with the ITM and ETMs. |
13767
|
Thu Apr 19 09:57:03 2018 |
gautam | Update | Wiki | AP and ETMX tables uploaded to wiki | The most up to date pictures of the AP table and ETMX table that Steve took have been uploaded to the relevant page on the wiki. It seems like the wiki doesn't display previews of jpg images - by using png, I was able to get the thumbnail of the attachment to show up. It would be nice to add beam paths to these two images. The older versions of these photos were moved to the archive section on the same page. |
13768
|
Thu Apr 19 11:29:11 2018 |
rana | Update | PEM | PID tune | Yesterday, I changed the P gain of the PID loop from zero to +0.1. Seems good so far; will monitor for a couple days to see if we're in the right ballpark. Main issue in the stability may now be that the quantization noise is too big for the temperature sensor. If so, we should consider subtracting off the DC value (with a V ref) and then amplifying before ADC. |
13769
|
Thu Apr 19 12:23:30 2018 |
Kira | Update | PEM | final setup sketch update | I've added in the dimensions to my sketch.
It seems like placing the two connectors right next to each other would allow both cables to just barely go through the hole in the block.
Quote: |
Can you please add dimensions to the drawing, so we can see if things fit and what the cable lenghts need to be?
For the panel on the granite slab, we should use a thinner piece of metal and mount it with an offset so that the D-sub cable can be fished through the hole in the slab. The hole is wide enough for 2 cables, but not 2 connectors.
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13770
|
Thu Apr 19 17:15:35 2018 |
gautam | Update | IOO | More IMC NBing | Summary:
Today, I repeated the coil driver noise measurement. Now, the coil driver noise curve in the noise budget plot (Attachment #1) is the actual measurement of all 12 coils (made with G=100 SR560). I am also attaching the raw voltage noise measurement (input terminated in 50ohms, Attachment #2). Note that POX11 spectrum has now been re-measured with analog de-whitening engaged on all 3 optics such that the DAC noise contribution should be negligible compared to coil driver noise in this configuration. The rows in Attachment #2 correspond to 800 Hz span (top) and full span (bottom) on the FFT analyzer.
Details:
The main difference between this measurement, and the one I did middle of last year (which agreed with the expectation from LISO modeling quite well) is that this measurement was done in-situ inside the eurocrate box while last year, I did everything on the electronics benches. So I claim that the whole mess of harmonics seen in the raw measurements are because of some electronics pickup near 1X6. But even disregarding the peaky features, the floor of ~30nV/rtHz is ~6x than what one would expect from LISO modeling (~5nV/rtHz). I confirmed by looking that the series resistance for all 3 MC optics is 430ohms. I also did the measurement with the nominal bias voltages applied to the four channels (these come in via the slow ADCs). But these paths are low-passed by an 8th order low pass with corner @ 1Hz, so at 100 Hz, even 1uV/rtHz should be totally insignificant. I suppose I could measure (with EPICS sine waves) this low-pass filtering, but it's hard to imagine this being the problem. At the very least, I think we should get rid of the x3 gain on the MC2 coil driver de-whitening board (and also on MC1 and MC3 if they also have the x3 factor). |
13771
|
Thu Apr 19 18:23:51 2018 |
Kira | Update | PEM | final setup sketch update | since we're just going from the short rack (not the tall rack) to the seismometer, can't we use a cable shorter than 45' ?
Quote: |
I've added in the dimensions to my sketch.
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the panel should be completely replaced like I described. We don't want to try to squeeze it in artificially and torque the wires. It just needs to be separated from the slab by a few more cm. |
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Fri Apr 20 00:26:34 2018 |
gautam | Update | ALS | Fibers switched out | Summary:
I think the dominant cause for the fact that we were seeing huge swing in the power coupled into the fiber was that the beam being sent in was in fact not linearly polarized, but elliptically polarized. I've rectified this with the help of a PBS. Fiber has been plugged into my polarization monitoring setup. Let's monitor for some long stretch and see if the situation has improved.
Details:
- The new fiber mount I ordered, K6XS, arrived today. I like it - it has little keys with which all DoFs can be locked. Moreover, it is compatible with the fixed collimators which IMO is the easiest way to achieve good mode-matching into the fiber. It is basically a plug-and-play replacement for the mounts we were using. Anyways, we can evaluate the performance over the coming days.
- I installed it on the PSL table (started work ~10pm, HEPA turned up to maximum, PSL shutter closed).
- But even with the new rotational DoF locking feature, I saw that slight disturbances in the fiber caused wild fluctuations in my polarization monitoring setup PD outputs. This was a useful tool through the night of checking the polarization content in the two special axes - Aidan had suggested using a heat gun but shaking the fiber a bit works well too I think.
- The PM980 fiber has an alignment key that is aligned with the slow axis of the fiber - so it is a useful alignment reference. But even by perturbing the roational alignment about the vertical by +/-15 degrees, I saw no improvement in this behavior. So I began to question my assumption that the input beam itself had clean polarization content.
- Since my pickoff beam has gone through a QWP and two PBSs, I had assumed that the beam was linearly polarized.
- But by putting a PBS just upstream of the input fiber coupler, I could see a beam at the S-port with an IR card (while I expected the beam to be P-polarized).
- OK - so I decided to clean up the input polarization by leaving this PBS installed. With this modification to the setup, I found that me shaking the fiber around on the PSL table didn't affect the output polarization content nearly as dramatically as before!!

- The state I am leaving it in tonight is such that there is ~100x the power in the P-polarization output monitor as the S-polarization (PER ~ 20dB). I didn't try and optimize this too much more for now, I want to observe some long term trend to see if the wild power fluctuations have been mitigated.
- The output coupler is mounted on the inferior K6X mount, and so there is the possibility that some drift will be attributable to rotation of the output coupler in it's mount. Thermally driven length changes / time varying stresses in the fiber may also lead to some residual power fluctuations. But I don't expect this to be anywhere near the ~25% I reported in the previous elog.
- The rejected beam from the PBS was measured to be ~300 uW. I haven't dumped this properly, to be done tomorrow.
- HEPA turned back down to 30%, PSL enclosure closed up, PSL shutter re-opened ~0030am.
- Note that the EX and EY fiber coupled beams are also likely subject to the same problem. We have to double check. I think it's better to have a PBS in front of the input fiber coupler as this also gives us control over the amount of light coupled into the fiber.
Power budget:
Power in |
Measured power (Ophir, filter OFF) |
@Input coupler, before PBS |
4.4 mW |
P-pol content @ input coupler |
4.06 mW |
S-pol (rejected) from PBS |
275 uW |
@Output coupler |
2.6 mW (MM ~65%) |
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Fri Apr 20 15:07:45 2018 |
Kira | Update | PEM | final setup sketch update | If we lay the cable along the floor then it should be around 6' to the current setup and about 20' to the actual seismometer.
Edit: 16 gauge wire should be good.
Quote: |
since we're just going from the short rack (not the tall rack) to the seismometer, can't we use a cable shorter than 45' ?
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Fri Apr 20 16:22:32 2018 |
gautam | Update | General | Nodus hard-rebooted | Aidan called saying nodus was down at ~345pm. I was able to access it at ~330pm. I couldn't ssh in from my machine or the control room ones. So I went to 1X7 and plugged in a monitor to nodus. It was totally unresponsive. Since the machine wasn't responding to ping either, I decided to hard-reboot it. Machine seemed to come back up smoothly. I had trouble getting the elog started - it wasn't clear to me that the web ports were closed by default, so even though the startELOGD.sh script was running fine, the 8080 port wasn't open to the outside world. Anyways, once I figured this out, I was able to start the elog. DokuWiki also seems to be up and running now... |
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Fri Apr 20 16:25:08 2018 |
Steve | Update | Wiki | ETMX table layout uploaded to wiki | ETMX table layout uploaded with beam paths to the wiki.  |
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Fri Apr 20 23:36:28 2018 |
Kevin | Update | PEM | Seismometer BLRMs | Steve secured the GPS time server in the rack above the AA board and removed the wooden block that it was resting on. The new rack is shown in attachment 1.
I then opened the AA board to see why the channels aren't working. Even though the board was powered and outputting 4.6 V, none of the chips were getting power. I must have shorted something while trying to diagnose this and the board is no longer powered either.
The schematic is given in D990147. The D68L8EX filter is bypassed on all the channels, as can be seen in attachment 3, so the board isn't really doing anything. Rana suggested that we could just bypass the whole circuit by wiring the IN channels directly to the OUT channels going to the ADC. I'll try that next for a single channel. |
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Sat Apr 21 20:19:05 2018 |
gautam | Update | General | Megatron hard-rebooted | I found megatron in a similar state to that which nodus was in yesterday. Clued by the fact that MCautolocker wasn't executing the mc scripts (as was evident from looking at the wall StripTool trace), I tried ssh-ing into megatron, but was unable to (despite it being responsive to ping requests). So I went into the VEA and plugged in a monitor to megatron - saw nothing on it. With no soft reboot options available, I power cycled the machine via the front panel button. It came back up smoothly. I manually restarted the autolocker, FSSslow and EX thermal control processes (the former two with initctl, while the latter runs in a tmux session). Everything seems alright for now. Not sure how long megatron has been dead for. |
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Sat Apr 21 20:25:12 2018 |
gautam | Update | ALS | PSL fiber pickoff status | Seems like there is still a bit of variation in the power in the two polarizations, though it is much smaller now, at the ~5% level (see Attachment #1). Since the pattern is repeating itself over the day timescale, I think this effect is not because of rotation of the output coupler in the mount, but is in fact a temperature driven waveplate effect because of imperfect alignment at the input coupler (which itself is locked down). I'm going to rotate the input coupler by 5 degrees (old = 110 degrees, new=115degrees) to see if the situation improves...
gautam Apr 24 2pm: Steve suggested confirming the correlation by hooking up the PSL table temperature sensor. This used to be logged but since the c1psl ADC card failure, has not been recorded. Assuming the sensor and preamp still work fine, we can use the PSL diagnostic Acromag (whose channels I have hijacked to monitor polarization stability already) to at least temporarily monitor the temperature inside the PSL enclosure. I am in need of a DB25 breakout board for this purpose which I am missing right now, as soon as I obtain one, I'll hook this up... |
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Mon Apr 23 20:06:35 2018 |
rana | Update | PEM | PID tune | This shows a step response of the EX seis temp control with K_I = -1 and K_P = -0.1. The time constants for both heatup and cooldown are ~2 hours.
I'm not so sure if the PID code itself makes sense though:
# The basic finite-difference PID approximation
e[0] = (p-s)
print("Error signal = {}" .format(e[0]))
# These are the main equations of the PID Process
u[0] = u[1]
u[0] = u[0] + Kp * (e[0] - e[1])
u[0] = u[0] + Ki * (e[0])
u[0] = u[0] + Kd * (e[0] - 2*e[1] + e[2])
Seems like the Proportional term uses the difference (or derivative) of the error signal. This makes it more likely to pick up some high frequency noise; maybe we should low pass this signal somewhat, or at least implement a running average.
Since we still don't have an out of loop sensor or a PSL room temperature monitor or a particle counter in the frames, I've disabled the PID loop to see how much the can temperature varies with no feedback. Please leave it this way for a few days. |
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Tue Apr 24 09:10:20 2018 |
Kira | Update | PEM | final setup sketch | I've attached the final sketch for the panel on the granite block. |
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Tue Apr 24 10:10:43 2018 |
gautam | Update | Computer Scripts / Programs | Particle swarm hyper parameter optimization | I'm copying and pasting Nikhil's email here as he was unable to login to the elog (but should now be able to in order to reply to any comments, and add more details about this test, motivation, methodology etc).
I did some post-processing after running the grid search. The following steps were carried out:
1) Selected those sets whose cost fun were less than a specific threshold (here 10000)
2) Next task was to see if the parameters of these good solutions had some pattern
3) I used a dimensionality reduction technique called t-SNE to project the 6 dimensional parameter space to 2 dim (for better visualization )
4) Made a scatter plot of these (see fig )
5) Used K-Means to find the clusters in this data
6) MarkerSize & Color reflect the cost fun. Bigger the marker size means better the solution.
7) Visual inspection implied cluster 5 had the best ranking points & more than any other cluster
8) These points had the following Parameter set: Workers {20,40}, SwarmSize {500}, MaxIter {500}, Self Adjustment {1}, Social Adjustment {1}, Tolerance {1e-3,1e-8}
See fig: for the box plot
9) It looks like is a particular set of values rather than individual values that gives the best results.
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Tue Apr 24 15:59:23 2018 |
Steve | Update | Wiki | AP table layout 20180328 |
Quote: |
ETMX table layout uploaded with beam paths to the wiki. 
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The pdf file is uploaded into the wiki. |
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Tue Apr 24 21:19:08 2018 |
Kevin | Update | PEM | Seismometer BLRMs | In the ongoing attempt to recover the seismometer BLRMS, I removed the AA board from the rack and modified the BS seismometer Z channel. The BS_Z BLRMs seem to be recovered after this modification.
I removed the three resistors from the output of the circuit and wired the input and from the seismometer directly to the input to the ADC. The modified schematic is shown in attachment 1. Attachments 2 and 3 show the top and bottom of the modified board. The board is doing nothing now other than serving as a connector for this channel.
I put the board back in the rack and injected a 2 Vpp signal into the BS_Z channel and saw +/- 1600 cts in C1PEM-SEIS_BS_Z. I then plugged the seismometer back into the board and took the spectrum shown in attachment 4. This shows the working Z channel giving a reasonable seismic spectrum. Note that X and Y are not modified yet.
If there are no objections, I will modify all the other channels on the board in the same way tomorrow. |
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Wed Apr 25 17:44:39 2018 |
Arnold | Update | PEM | PEM Anti-Alias wiring | 
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Thu Apr 26 09:35:49 2018 |
Kevin | Update | PEM | PEM Anti-Alias wiring | I wired all 32 channels going to the AA board directly to the ADC as described in the previous log. However, instead of using the old AA board and bypassing the whole circuit, I just used a breakout board as is shown in the first attachment. I put the board back in the rack and reconnected all of the cables.
The seismic BLRMs appear to be working again. A PSD of the BS seismometers is shown in attachment 2. Tomorrow I'll look at how much the ADC alone is suppressing the common mode 60 Hz noise on each of the channels.
Steve: 5 of ADC DAC In Line Test Boards [ D060124 ] ordered. They should be here within 10 days. |
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Thu Apr 26 19:46:26 2018 |
rana | Update | PEM | PID Quixote | Increased the Integral gain (from -1 to -4) on the EX temperature controller. This didn't work a few weeks ago, but now with the added P gain, it seems stable. Daily temperature swings are now ~3x smaller.
Notes for Kira on what we need to do tomorrow (Friday):
add the MEDM screen EPICS values to the DAQ so that we can plot those trends DONE
- add the out-of-loop sensor to the EX can
reboot the AUX-EX so we can pick up the new channels and the fixed spelling of the old channels DONE
- Re-install EX seismometer and hook up seismometer channels to PEM DAQ so we can start testing its performance.
For those who are flabbergasted by the way I calibrated the TEMP_MON channel from volts to deg C, here's how:
XMgrace->Data->Transformations->Geometric Transforms...
use the 'scale' and 'translate' fields to change the slope and offset for calibration in the obvious ways
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Thu Apr 26 20:22:21 2018 |
Kevin | Update | PEM | ADC common mode rejection with new seismometer connections | Yesterday I wired the outputs from the seismometers directly to the ADC input bypassing the old AA board circuit as is described in this elog. The old circuit converted the single-ended output from the seismometers to a differential signal. Today I looked at whether 60 Hz noise is worse going directly into the ADC due to the loss of the common mode rejection previously provided by the conversion to differential signals.
I split the output from the BS Z seismometer to the new board and to an SR785. On the SR785 I measured the difference between the inner and outer conductors of the seismometer output, i.e. A-B with A the center conductor and B the outer conductor, with grounded input. At the same time I took a DTT spectrum of C1:PEM-SEIS_BS_Z_IN1. Both spectra were taken with 1 Hz bandwidth and 25 averages. The setup is shown in attachment 1.
The spectra are shown in attachment 2. The DTT spectrum was converted from counts to volts by multiplying by 2 * 10 V/32768 cts where the extra factor of 2 is from converting from single-ended to differential input. If there was common 60 Hz noise that the ADC was picking up we would expect to see less noise at 60 Hz in the SR785 spectrum measured directly at the output from the seismometer since that was a differential measurement. Since both spectra have the same 60 Hz noise, this noise is differential. |
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Thu Apr 26 23:00:42 2018 |
rana | Update | PEM | new Seis temp chans | After fixing the spelling of the EX temperature readback, I also added all of the MEDM sliders to the C0EDCU.ini file (making sure to add an even number of channels). Restarted FB (after installing telnet on rossa):
telnet fb 8083
> shutdown
preferred method of posting DataViewer images: print as a SVG image (since its vectorized). Then from the command line do:
inkscape steven.svg --export-pdf=vass.pdf |
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Fri Apr 27 16:55:31 2018 |
gautam | Update | General | EY area access blocked | Steve was calibrating the load cells at the EY table with the crane - we didn't get through the full procedure today, so the area near the EY table is kind of obstructed. The 100kg donut is resting on the floor on the North side of the EY table and is still connected to the crane. There are stopper plates underneath the donut, and it is still connected to the crane. Steve has placed cones around the area too. The crane has been turned off. |
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Fri Apr 27 18:42:02 2018 |
rana | Update | PEM | new Seis temp chans | for whatever reason, I am unable to get minute or second trends from nodus for any channels (IMC, PEM, etc) since the reboot. has there been some more recent FB failure or is this still a bug since last years FB catastrophe? |
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Sun Apr 29 22:53:06 2018 |
gautam | Update | General | DARM actuation estimate | Motivation:
We'd like to know how much actuation is required on the ETMs to lock the DARM degree of freedom. The "disturbance" we are trying to cancel is the seismic driven length fluctuation of the arm cavity. In order to try and estimate what the actuation required will be, we can use data from POX/POY locks. I'd collected some data on Friday which I looked at today. Here are the results.
Method:
- I collected the error and control signals for both arm cavities while they were locked to the PSL.
- Knowing the POX/POY sensing response and the actuator transfer functions, we can back out the free running displacements of the two arm cavities.
- I used numbers from the cal filters which may not be accurate (although POX sensing response which was recently measured).
- But the spectra computed using this method seem reasonable, and the X and Y arm asds line up around 1 Hz (albeit on a log scale).
- In this context,
is really a proxy for and similarly for L_Y so I think the algebra works out correctly.
- I didn't include any of the violin mode/AA/AI filters in this calculation.
- Having calculated the arm cavity displacements, I computed "DARM" as L_y- L_x and then plotted its asd.
- For good measure, I also added the quadrature sum of 4 optics' displacement noise as per the 40m GWINC model - there seems to be a pretty large discrepancy, not sure why.
If this approach looks legit, I will compute the control signal that is required to stabilize this level of disturbance using the DARM control loop, and see what is the maximum permissible series resistance we can use in order to realize this stabilization. We can then compare various scenarios like different whitening schemes, with/without Barry puck etc, and look at coil driver noise levels for each of them. |
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Mon Apr 30 15:36:18 2018 |
Kira | Update | PEM | final setup sketch | I've attached a sketch of how the panel will be mounted. We should make a small rectangular box that would raise the panel from the block by 1 cm or so to allow the cables to fit into the hole in the block without getting bent. It also has to be airtight so maybe having a thin layer of rubber between the mount and block would be good. |
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Mon Apr 30 23:13:12 2018 |
Kevin | Update | Computer Scripts / Programs | DataViewer leapseconds | I was trying to plot trends (min, 10 min, and hour) in DataViewer and got the following error message
Connecting.... done
mjd = 58235
leapsecs_read()
Opening leapsecs.dat
Open of leapsecs.dat failed
leapsecs_read() returning 0
frameMemRead - gpstimest = 1208844718
thoough the plots showed up fine after. Do we need to fix something with the leapsecs.dat file? |
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