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ID Date Author Type Category Subject
  3914   Sun Nov 14 02:59:31 2010 ranaConfigurationGeneralMEDM snapshots web page

Since Nodus is a Solaris machine it can barely handle doing the ImageMagick commands (such as convert and import). I removed the auto MEDM snapshot routine from it

awhile ago and I think the rate of ELOGD crashes has decreased, although its not definitive.

The snapshots have now been re-actived to run on MAFALDA, after I fixed the absolute pathnames in the scripts and installed (via yum) the packages that mafalda

needed to run this (Xvfb, openmotif, compat, etc.). The snapshots web page is now refreshing by itself and the statScreen/cronjob.sh is running on mafalda 5x per hour.

https://nodus.ligo.caltech.edu:30889/medm/screenshot.html

  3913   Sat Nov 13 16:57:21 2010 valeraConfigurationElectronicsPRM Side OSEM transimpedance change

Now that we have increased the range of the AA to +/- 10 V I have increased the PRM side OSEM transimpedance from 29 kV/A to 161 kV/A by changing the R64 in the satellite box. The first attached plot shows the ADC input spectrum before and after the change with analog whitening turned off. The PD voltage readback went up from 0.75 to 4.2 V. The second attached plot shows the sensor, ADC, and projected shot noise with analog whitening turned on and compensated digitally. The ADC calibration is 20 V/ 32768 cts. The PRM damping loops are currently disabled.

I checked for oscillation by looking at the monitor point at the whitening board. There was no obvious oscillation on a scope - the signal was 20 mV p-p on 1 us scale which was very similar to the LL channel.

Attachment 1: PRM-SD-ADC.pdf
PRM-SD-ADC.pdf
Attachment 2: PRM-SD-Current.pdf
PRM-SD-Current.pdf
  3912   Sat Nov 13 15:53:05 2010 yutaUpdateCDSdiagonalization of MC input matrix

Motivation:
  MC is aligned from the A2L measurement, but to do the beam centering more precisely, we need coils to be balanced.
  There are several ways to balance the coils, like using oplev or WFS QPD RF channels.
  But oplev takes time to setup, especially for MC3. Also, c1ioo WFS channels were newly setup and haven't been checked yet.
  So, I decided to use OSEM sensors.
  An OSEM sensor itself is sensitive to every DOF of an optic motion, but we can diagonalize them using 4 OSEM sensors and proper input matrix.

Method:

  1. Measure transfer functions between
     ULSEN and URSEN (H_UR(f))
     ULSEN and LRSEN (H_LR(f))
     ULSEN and LLSEN (H_LL(f))

  2. Make a matrix A.

    A =  [[ 1           1           1          ]
          [ H_UR(f_pos) H_UR(f_pit) H_UR(f_yaw)]
          [ H_LR(f_pos) H_LR(f_pit) H_LR(f_yaw)]
          [ H_LL(f_pos) H_LL(f_pit) H_LL(f_yaw)]]


    where f_dof are resonant frequencies.

  3. A is

    s = Ad


   where vectors s^T=[ULSEN URSEN LRSEN LLSEN] and d^T=[POS PIT YAW].
   So,

    d = Bs = (A^TA)^(-1)A^Ts

   where A^T is transpose of A.

   B is the input matrix that diagonalizes 3 DOFs.

What I did:

  1. Measured the TFs using diaggui and exported as ASCII.

  2. Made a script that reads that TF file, calculates and sets a new input matrix B.
    /cvs/cds/caltech/users/yuta/scripts/inputmatrixoptimizer.py
   You need to set resonant frequencies to use the script.

   New input matrices for MCs are;

C1:SUS-MC1_INMATRIX
[[ 1.17649712  0.94315611  0.85065054  1.02969624]
 [ 0.55939288  1.28066594 -0.85235358 -1.3075876 ]
 [ 1.23467139 -0.74521928 -1.29394051  0.72616882]]

C1:SUS-MC2_INMATRIX
[[ 1.12630748  1.01451545  0.9013457   0.95783137]
 [ 1.03043025  0.67826036 -1.37270598 -0.91860341]
 [ 0.83546271 -1.26311029 -0.6456881   1.2557389 ]]

C1:SUS-MC3_INMATRIX
[[ 1.18212117  1.26419447  0.77744155  0.77624281]
 [ 0.79344415  0.84959646 -1.10946339 -1.247496  ]
 [ 1.00225331 -0.84807863 -1.21772132  0.93194674]]


  I ignored SIDE this time.

Result:

  Spectra of each SUSDOF_IN1_DAQ before diagonalization (INMATRIX elements all 1 or -1) were
MCspectraNov09.png

  After diagonalization, spectra are
MCspectraNov13.png

  As you can see, each SUSDOF has only single peak (and SIDE peak) after the diagonalization.
  SUSSIDE still has 4 peaks because SIDE is not included this time.

  For MC2, POS to SUSPIT and POS to SUSYAW got worse. I have to look into them.

Effect of resonant frequency drift:

  As you can compare and see from the spectra above, resonant frequencies of MC1 are somehow drifted(~0.5%) from Nov 9 to Nov 13.
  If resonant frequency you expected was wrong, calculated input matrix will be also wrong.
  The effect of 0.5% drift and wrong input matrix can be seen from this spectra. DOFs are not clearly separated.
 MC1spetra_wrongmatrix.png

Plan:

 - learn how to use diaggui from command line and fully automate this process
 - balance the coils using these diagonalized SUSPOS, SUSPIT, SUSYAW

  3911   Fri Nov 12 20:40:51 2010 josephb, yuta, valeraConfigurationElectronicsAA voltage range

We changed the range of the two SUS AA boards in the corner from +/-2 V to +/-10 V by changing the supply voltage from +/-5 V to +/-15 V. The change was made by switching the AA power feed wires on  the cross connect. The max supply according to the spec of DRV134/INA134 is +/-18 V.

We checked the new range by applying the voltage to the input of AA and measuring the output going to the ADCs. The local damping MC1,2,3 appears to work.

  3910   Fri Nov 12 19:24:56 2010 KojiUpdateCDSTest of ADC noise

[Koji Yuta]

We found one of the ADC cables were left unconnected. This left the MC suspensions uncontrollable through the whole afternoon.
Please keep the status updated and don't forget to revert the configuration...

Quote:

Test:

Look at the effects of the ADC voltage range on the ADC noise floor.

ADC input was terminated with 50 ohms.  We then looked at the channel with DTT. This was at +/- 10 V range.  We used C1:SUS-PRM_SDSEN_IN1 as the test channel.

The map.c file (in /opt/rtcds/caltech/c1/core/advLigoRTS/src/fe/ ) then had two lines added at line 766.

//JCB temporary 2.5V test, remove me
  adcPtr[devNum]->BCR &= 0x84240;

This hard coded the 2.5 V range (we default to the 10 V range at the moment).

We then rebuilt the c1x02 model and reran the test.

Finally, we reverted the code change to map.c and rebuilt c1x02.

Results:
I've attached the DTT output of the two tests.

It appears the ADC is limited by 1.6 uV/rtHz.  Hence the increase in noise in counts by a factor of 4 when we drop to +/- 2.5 V from +/- 10 V.

 

  3909   Fri Nov 12 13:12:55 2010 kiwamuUpdatePSLincreased NPRO power

I maximized the laser power by rotating the HWP after the NPRO.

If someone works on the MC locking, one should decrease it again.

 

  3908   Fri Nov 12 12:06:11 2010 AidanConfigurationGreen LockingPID script working - now it needs to be tuned

 I've set up a PID script that senses the EX-PSL Green Beat note (from the frequency counter) and actuates on the temperature of the end laser to drive the beat note to a given setpoint.

  • I've added the necessary EPICS channels to c1iscaux and rebooted it so that the channels are live. They are listed in a new database file slow_grnx_pid.db
  • This database was added to the list of those loaded by startup.cmd.  
  • The PID script, GRNXSlowServo, is just a modified version of FSSSlowServo.
  • The version I've been running is currently in /cvs/cds/caltech/users/abrooks/.
  • There's also an MEDM screen in this directoy, C1LSC_EX_GRN_SLOW.adl, there that shows the PID settings.

Right now the script only passes the initial sanities checks, that is:

  1. It runs.
  2. You can enable/disable it without any errors and it starts actuating.

The settings all need to be tuned up - e.g. maximum_increment, hard_stops, time_step, PID constants.

Additionally, the units in the whole thing are pretty useless - some of the channels are in VOLTS, others in WATTS. I'd like to change all these to be in Hz. 


EPICS channels added:

  • grecord(ao,"C1:LSC-EX_GRN_SLOWKD")
  • grecord(ao,"C1:LSC-EX_GRN_SLOWKP")
  • grecord(ao,"C1:LSC-EX_GRN_SLOWKI")
  • grecord(ao,"C1:LSC-EX_GRN_PID_SETPT")
  • grecord(ao,"C1:LSC-EX_GRN_TIMEOUT")
  • grecord(stringin,"C1:LSC-EX_GRN_SLOWVERSION")
  • grecord(bi,"C1:LSC-EX_GRN_SLOWLOOP")
  • grecord(bi,"C1:LSC-EX_GRN_DEBUG")
  • grecord(bi,"C1:LSC-EX_GRN_SLOWBEAT")
 

 

Attachment 1: Screen_shot_2010-11-12_at_12.05.01_PM.png
Screen_shot_2010-11-12_at_12.05.01_PM.png
  3907   Fri Nov 12 11:36:06 2010 AidanConfigurationComputersFixed the PERL PATH errors from the scripts directory change

 I've been trying to get a PID loop running for the green locking and I've discovered that some of the directories in the path for the Perl Modules are now obselete. Specifically, since the scripts directory has been moved from /cvs/cds/caltech/scripts to /cvs/cds/rtcds/caltech/c1/scripts the following locations in the Perl @INC path list need to be changed:

  • /cvs/cds/caltech/scripts/general
  • /cvs/cds/caltech/scripts/general/perlmodules

I've added the above directories to the PERL5LIB path in /cvs/cds/caltech/cshrc.40m.

 

 

setenv PERL5LIB /cvs/cds/caltech/scripts/general:

/cvs/cds/caltech/scripts/general/perlmodules:

/cvs/cds/caltech/libs/solaris9/usr_local_lib/perl5/5.8.0/:

/cvs/cds/rtcds/caltech/c1/scripts/general:

/cvs/cds/rtcds/caltech/c1/scripts/general/perlmodules

 This seems to fix the problem .. at least, you no longer get an error if you try nodus:~>perl -e 'user EpicsTools'

 

  3906   Fri Nov 12 10:49:34 2010 josephb, valeraUpdateCDSTest of ADC noise

Test:

Look at the effects of the ADC voltage range on the ADC noise floor.

ADC input was terminated with 50 ohms.  We then looked at the channel with DTT. This was at +/- 10 V range.  We used C1:SUS-PRM_SDSEN_IN1 as the test channel.

The map.c file (in /opt/rtcds/caltech/c1/core/advLigoRTS/src/fe/ ) then had two lines added at line 766.

//JCB temporary 2.5V test, remove me
  adcPtr[devNum]->BCR &= 0x84240;

This hard coded the 2.5 V range (we default to the 10 V range at the moment).

We then rebuilt the c1x02 model and reran the test.

Finally, we reverted the code change to map.c and rebuilt c1x02.

Results:
I've attached the DTT output of the two tests.

It appears the ADC is limited by 1.6 uV/rtHz.  Hence the increase in noise in counts by a factor of 4 when we drop to +/- 2.5 V from +/- 10 V.

Attachment 1: ADC_noise.pdf
ADC_noise.pdf
  3905   Fri Nov 12 06:10:24 2010 yutaUpdateIOOMC aligned (without coil balancing)

Background:
  Last night, we found that one of DAC channels are poorly connected, so we fixed the connectors.
  Rana and Koji used their incredible eyeballs to roughly align MC.
  Next thing to do is to balance the coils, but it takes some time for the setup.
  So, we decided to do A2L anyway.

What I did:
  Using the last steering mirror at PSL table and IM1, changed the incident beam direction to align MC.

Result:
MCalignCALIB.png
 
  I was amazed by their eyeballs.
  I turned the nobs of SM@PSL and IM1 in small increments, so I never lost TEM00.

Is it enough?:
  The length of the whole faraday is about 20cm and aperture diameter is about 12mm. (I couldn't measure the aperture size of the core)
  The beam is about 9mm diameter at 6w.
  So, if the beam is vertically tilted at more than ~3/200rad, it(6w) cannot go through.
  3/200 rad is about 20% difference in position at MC1 and MC3.
  So, the result meets the requirement.

  Also, assuming that coils have 5% imbalance, the beam position I measured have ~3% error.
  So, to do more precise beam centering, we need to balance the coils.

  3904   Fri Nov 12 02:51:20 2010 KevinUpdateElectronicsPhotodiode Testing

[Jenne and Kevin]

I started testing the REFL55 photodiode. With a light bulb, I saw ~270 mV of DC voltage from the photodiode but still could not see any RF signal. I connected the RF out from the spectrum analyzer to the test input and verified that the circuit was working.

I then set up the AM laser and looked at the laser light with REFL11 and an 1811 photodiode. I was able to see an RF signal and verified that the resonant frequency is 55 MHz.

The current setup is not very reliable because the laser is not mounted rigidly. Next, I will work on making this mounting more reliable and will continue to work on finding an RF signal with a flashlight.

  3903   Fri Nov 12 00:42:11 2010 rana, kojiUpdateIOOMC alignment

We decided to ignore the computer script outputs for the beam positions and use instead the eyeball method to get the beam into the MC:

  1. Adjust PSL launch beam to get the beam centered on IM1.
  2. Eyeball the beam to hit the center of MC1. We can get this pretty good by using the brackets to get the vertical and using the centering of the input/refl beams to center it horizontally.
  3. Use MC3 suspension to hit the center of MC2. We did this by hitting each of the 3 EQ stop screw heads and triangulating the MC3 bias settings.
  4. Use MC2 bias to hit the center of MC1.
  5. Use MC1 to get good flashes.
  6. Use all 3 MC sus biases to maximize the transmitted light and minimize the REFL DC.

With this rough alignment in place, we leave it to Yuta to finish the coil balancing and the A2L. We will have an aligned MC in the morning and will start the BS chamber alignment.

  3902   Fri Nov 12 00:13:34 2010 SureshUpdateSUSETM assembly started

[Jenne, Suresh]

Selection of ETMs

Of the four ETMs (5,6,7 and 8) that are with us Koji gave us two (nos. 5 and 7) for use in the current assembly.  This decision is based on the Radius of Curvature (RoC) measurements from the manufacturer (Advanced Thin Films).   As per their measurements the four ETMs are divided into two pairs such that each pair has nearly equal RoC. In the current case, RoCs are listed below:

   

Radii of Curvature of ETMs
ETM # RoC from Coastline Optics (m) RoC from Advanced Thin Films (m)
5 57.6 60.26
6 57.4 54.58
7 57.1 59.48
8 57.9 54.8

 

The discrepancy between the measurements from these two companies leaves us in some doubt as to the actual radius of curvature.  However we based our current decision on the measurement of Advanced Thin Films. 

 

Assembly of ETMs

We drag wiped both the ETMs (5 and 7) and placed them in the Small Optic Gluing Fixture.  The optics are positioned with the High Reflectace side facing downwards and with the arrow-mark on the Wire Standoff side (big clamp).  We then used the microscope to position the Guide Rod and the Wire Standoff in the tangential direction on the ETMs (step 4 of the procedure specified in E010171-00-D)

We will continue with the rest of the assembly tomorrow.

 

  3901   Thu Nov 11 23:35:23 2010 KojiSummaryCDSfound poor contact of DAC cable, previous A2L results were wrong

[Koji / Yuta]

There were the guys who used the PENTEK 40pin connectors into the IDC 40pin connectors.
Those connectors are not compatible at all.

==> We replaced the connectors on the cables from DAC to IDC adapters to the dewhitening board for the vertex SUSs.

In addition, I found one of the Binary OUT IDC50pin connector has no clamp.

==> We put the IDC50pin clamp on it.

bad-boys.png

PENTEK connectors were inserted. The latches are not working!

IMG_3698.jpg

the vertical pitch is different between PENTEK and IDC!
IMG_3705.jpg

Wow! Where is the clamp???

IMG_3706.jpg

Quote:

The cause is apparent! The connectors on the cables are wrong!
Currently only 50% of the pin length goes into the connector!

Quote:

(Koji, Jenne, Yuta)

We found one of DAC cables had a poor contact.
That probably caused our too much "tilt" of the beam into MC.

  It was because one of the DAC cables(labeled CAB_1Y4_88) had a poor contact.
  If I push it really hard, it is ok. But maybe we'd better replace the cable.

What caused a poor connection?:
  I don't know.
  A month ago, we checked that they are connected, but things change.

 

 

  3900   Thu Nov 11 21:07:49 2010 josephbUpdateCDSPlugged c1iscex into DAQ network - still causes network slowdown

I connected the c1iscex computer to the dedicated DAQ network switch (located in 1X7).

This does not seem to have helped c1iscex stop spewing out "OMX: Failed to find peer index of board 00:00:00:00:00:00 (Peer Not Found in the Table)" at the rate of ~1 Gigabyte per minute.

c1iscex is currently off until a solution can be found.

  3899   Thu Nov 11 18:05:55 2010 valeraUpdatePSLPMC mode matching at full laser power

 The PMC mode matching was initially done at low power ~150 mW. It was expected and found that at full power ~2 W (injection current 2.1 A) the mode matching got much worse:

the visibility degraded from 80% to 50% (1 - refl locked/refl unlocked) . The thermal lensing could be in the laser, EOM, or FI.

The first attached plot shows the scan of the beam after the EOM at low and full laser power. At full power the waist position is 10 mm after the turning mirror after the EOM and the waist size is 310 um.

The second plot shows the ABCD calculation for the mode matching solution.

I removed the MM lens PLCX-25.4-77.3-C and placed the PLCX-25.4-180.3-UV about 20 mm after the first PMC periscope mirror (the second mirror after the EOM).

The PMC visibility improved to 94% and the power through the PMC, as measured by the PMC transmission PD, went up by a factor of 2.

Attachment 1: scan.pdf
scan.pdf
Attachment 2: pmc2-abcd.png
pmc2-abcd.png
  3898   Thu Nov 11 17:47:36 2010 kiwamuUpdateGreen Locking80MHz VCO : improve PLL hold-in range and put a boost

In order to enlarge the hold-in range I modified the control filter and increased the gain by factor of 25 in the PLL.

It successfully enlarged the range, however the lock was easily broken by a small frequency change.

So I put a low frequency boost (LFB) and it successfully engaged the PLL stiffer.

Now it can maintain the lock even when the frequency disturbance of about 1MHz/s is applied.

 


(enlargement of the hold-in range)

I modified the control filter by replacing some resistors in the circuit to increase the gain by factor of 25.

        - R18 390 [Ohm]  => 200 [Ohm]

    - R20 1000 [Ohm] => 5000 [Ohm]

    - R41 39 [Ohm] => 10 [Ohm]

 This replacement also changes the location of the pole and the zero

    - pole 1.5 [Hz] => 0.3 [Hz]

    - zero 40 [Hz] => 159 [Hz]

 Note that this replacement doesn't so much change the UGF which was about 20 kHz before.

It becomes able to track the input frequency range of +/- 5MHz if I slowly changes the frequency of the input signal. 

However the PLL is not so strong enough to track ~ 1 kHz / 0.1s frequency step.  

 

(make the PLL stiffer : a low frequency boost)

One of the solution to make the PLL stiffer is to put a boost filter in the loop.

I used another channel to more drive the VCO at low frequency. See the figure below.

 vco_pll.png

The 80MHz VCO box originally has two input channels, one of these inputs was usually disabled by MAX333A.

This time I activated both two input channels and put the input signal to each of them.

Before signals go to the box, one of the signal path is filtered by SR560. The filter has G=20000, pole=0.3Hz. So it gives a big low frequency boost.

VCO_lfb.png

Once the PLL was achieved without the boost, I increased the filter gain of SR560 to 20000 because locking with the boost is difficult as usual.

 

  3897   Thu Nov 11 15:27:43 2010 valera, steveConfiguration ISS AOM installed

 We installed the ISS AOM in the PSL. The AOM was placed right after the EOM. The beam diameter is ~600 um at the AOM. The AOM aperture is 3 mm.

We monitored the beam size by scanning the leakage beam through the turning mirror after the AOM. The beam diameter changed from 525 um to 515 um at a fixed point. We decided that the AOM thermal lensing is not large enough to require a  new scan of the mode going into the PMC and we can proceed with PMC mode matching using the scan that was taken without the AOM (to be posted).

  3896   Thu Nov 11 13:54:05 2010 kiwamuUpdateGreen Locking80MHz VCO : about PLL hold-in range

The hold-in range of the PLL must be greater than +/- 4MHz in order to bring the arm cavity to its resonance. 

(Hold-in range is the range of frequencies over which the PLL can track the input signal.)

However as I mentioned in the past elog (see this entry), the PLL showed a small hold-in range of about +/- 1MHz which is insufficient.

In this entry I explain what is the limitation factor for the hold-in range and how to enlarge the range.

 


(Requirement for hold-in range )

 We have to track the frequency of the green beat signal and finally bring it to a certain frequency by controlling the cavity length of the arm.

For this purpose we must be able to track the beat signal at least over the frequency range of 2*FSR ~ +/- 4MHz.

Then we will be able to have more than two resonances, in which both the end green and the PSL green are able to resonate  to the arm at the same time. 

And if we have just two resonances in the range, either one of two resonances gives a resonance for both IR and green. At this phase we just bring it to that frequency while tracking it.

 

  Theoretically this requirement can be cleared by using our VCO because the VCO can drive the frequency up to approximately +/- 5MHz (see this entry)

 The figure below is an example of resonant condition of green and IR. The VCO range should contain at least one resonance for IR.

(In the plot L=38.4m is assumed)

 

 range_green.png

 

(an issue) 

However the measured hold-in range was about +/- 1MHz or less. This is obviously not large enough.

According to a textbook[1], this fact is easily understandable.

The hold-in range is actually limited by gains of all the components such as a phase detector's, a control filter's and a VCO's gain.

Finally it is going to be expressed by,

                         [hold-in range] = G_pd * G_filter * G_vco

PLL.png

 

 At the PD (Phase Detector which is a mixer in our case) the signal does not exceed G_pd [V] because it appears as G_pd * sin(phi).

When the input signal is at the edge of the hold-in range, the PD gives its maximum voltage of G_pd to maintain the lock.

Consequently the voltage G_pd [V] goes through to G_filter [V/V] and G_vco [Hz/V].

This chain results the maximum pushable frequency, that is, hold-in range given above equation.

In our case, the estimated hold-in range was 

                      [hold-in range] ~ 0.4 [V] * 3 [V/V] * 1 [MHz/V]

                          = 1.2 [MHz]

This number reasonably explains what I saw.

In order to enlarge the hold-in range, increase the gain by more than factor of 5. That's it.

* reference [1]  "Phase-Locked Loops 6th edition" Rolan E. Best

  3895   Thu Nov 11 11:51:30 2010 KojiSummaryCDSfound poor contact of DAC cable, previous A2L results were wrong

The cause is apparent! The connectors on the cables are wrong!
Currently only 50% of the pin length goes into the connector!

Quote:

(Koji, Jenne, Yuta)

We found one of DAC cables had a poor contact.
That probably caused our too much "tilt" of the beam into MC.

  It was because one of the DAC cables(labeled CAB_1Y4_88) had a poor contact.
  If I push it really hard, it is ok. But maybe we'd better replace the cable.

What caused a poor connection?:
  I don't know.
  A month ago, we checked that they are connected, but things change.

 

  3894   Thu Nov 11 11:08:26 2010 steveBureaucracyPEMAP table found open

Please remember to cover the optical tables !

  3893   Thu Nov 11 07:26:03 2010 AlbertoUpdateElectronicsREFL11 Photodiode Not Working

Quote:

[Koji and Kevin]

I was trying to characterize the REFL11 photodiode by shining a flashlight on the photodiode and measuring the DC voltage with an oscilloscope and the RF voltage with a spectrum analyzer. At first, I had the photodiode voltage supplied incorrectly with 15V between the +15 and -15 terminals. After correcting this error, and checking that the power was supplied correctly to the board, no voltage could be seen when light was incident on the photodiode.

We looked at the REFL55 photodiode and could see ~200 mV of DC voltage when shining a light on it but could not see any signal at 55 MHz. If the value of 50 ohm DC transimpedance is correct, this should be enough to see an RF signal. Tomorrow, we will look into fixing the REFL11 photodiode.

I just wanted to remind you that the most up to date resource about the RF system upgrade, including photodiodes, is the SVN.

https://nodus.ligo.caltech.edu:30889/svn/trunk/alberto/40mUpgrade/RFsystem/

There you can find everything: measurements, schematics, matlab scripts to plot and fit, etc. Poke around it to find what you need.
For instance, the schematic of the modified REFL11 photodiode is at:

https://nodus.ligo.caltech.edu:30889/svn/trunk/alberto/40mUpgrade/RFsystem/RFPDs/REFL11/REFL11Schematics/40mUpgradeREFL11schematic.pdf

Because I was doing new things all the time, the wiki is not up to date. But the SVN has all I've got.

  3892   Thu Nov 11 05:56:04 2010 yutaSummaryIOOsetting up temporary oplev for coil balancing of MCs

(Suresh, Yuta)

Background:
  Previous A2L measurement is based on the assumption that actuator efficiencies are identical for all 4 coils.
  We thought that the unbelievable "tilt" may be caused by imbalance of the coils.

Method:
  1. Setup an optical lever.
  2. Dither the optic by one coil and demodulate oplev outputs(OL_PIT or OL_YAW) in that frequency.
  3. Compare the demodulated amplitude. Ideally, the amplitude is proportional to the coil actuation efficiency.

What we did:
[MC2]
  MC2 is the least important, but the easiest.
  1. Placed a red laser pointer at MC2 trans table. During the installation, I moved the mirror just before QPD.
  2. Made a python script that measures coil actuation efficiency using the above method. I set the driving frequency to 20Hz.
  It is /cvs/cds/caltech/users/yuta/scripts/actuatorefficiency.py.
  The measurement result is as follows. Errors are estimated from the repeated measurement. (Attachment #1)

MC2_ULCOIL 1
MC2_URCOIL 0.953 ± 0.005
MC2_LRCOIL 1.011 ± 0.001
MC2_LLCOIL 0.939 ± 0.006


[MC1]
  For MC1, we can use the main laser and WFS1 QPD as an oplev.
  But we only have slow channels for QPD DC outputs(C1:IOO_WFS1_SEG#_DC).
  So, we intentionally induce RF AM by EOM(see Kiwamu's elog #3888) and use demodulated RF outputs of the WFS1 QPD(C1:IOO_WFS1_I/Q#) to see the displacement.
  1. Replaced HR mirror in the MCREFL path at AP table to BS so that we can use WFS1.(see Koji's elog #3878)
    The one we had before was labeled 10% pick-off, but it was actually an 1% pick-off.
  2. Checked LO going into WFS1 demodulator board(D980233 at 1X2).
    power: 6.4dBm, freq: 29.485MHz
  3. Turned on the hi-voltage(+100V) power supply going into the demodulator boards.
  4. Noticed that no signal is coming into c1ioo fast channels.
    It was because they were not connected to fast ADC board. We have to make a cable and put it in.

[MC3]
  Is there any place to place an oplev?

Plan:
 - prepare c1ioo channels and connections
 - I think we'd better start A2L again than do oplev and coil balancing.

Attachment 1: MC2coils.png
MC2coils.png
  3891   Thu Nov 11 04:32:53 2010 yutaSummaryCDSfound poor contact of DAC cable, previous A2L results were wrong

(Koji, Jenne, Yuta)

We found one of DAC cables had a poor contact.
That probably caused our too much "tilt" of the beam into MC.

Story:
  From the previous A2L measurement and MC aligning, we found that the beam is somehow vertically "tilted" so much.
  We started to check the table leveling and the beam height and they looked reasonable.
  So, we proceeded to check coil balancings using optical levers.
  During the setup of optical levers, I noticed that VMon for MC1_ULCOIL was always showing -0.004 even if I put excitation to coils.
  It was because one of the DAC cables(labeled CAB_1Y4_88) had a poor contact.
  If I push it really hard, it is ok. But maybe we'd better replace the cable.

What caused a poor connection?:
  I don't know.
  A month ago, we checked that they are connected, but things change.

How to prevent it:
  I made a python script that automatically checks if 4 coils are connected or not using C1:IOO_LOCKIN oscillator.
  It is /cvs/cds/caltech/users/yuta/scripts/coilchecker.py.
  It turns off all 3 coils except for the one looking at, and see the difference between oscillation is on and off.
  The difference can be seen by demodulating SUSPOS signal by oscillating frequency.
  If I intentionally unplug CAB_1Y4_88, the result output for MC1 will be;

==RESULTS== (GPS:973512733)
MC1_ULCOIL      0.923853382664 [!]
MC1_URCOIL      38.9361304794
MC1_LRCOIL      55.4927575177
MC1_LLCOIL      45.3428533919


Plan:
 - Make sure the cable connection and do A2L and MC alignment again
 - Even if the cables are ok, it is better to do coil balancings. See the next elog.

  3890   Thu Nov 11 02:17:27 2010 KevinUpdateElectronicsREFL11 Photodiode Not Working

[Koji and Kevin]

I was trying to characterize the REFL11 photodiode by shining a flashlight on the photodiode and measuring the DC voltage with an oscilloscope and the RF voltage with a spectrum analyzer. At first, I had the photodiode voltage supplied incorrectly with 15V between the +15 and -15 terminals. After correcting this error, and checking that the power was supplied correctly to the board, no voltage could be seen when light was incident on the photodiode.

We looked at the REFL55 photodiode and could see ~200 mV of DC voltage when shining a light on it but could not see any signal at 55 MHz. If the value of 50 ohm DC transimpedance is correct, this should be enough to see an RF signal. Tomorrow, we will look into fixing the REFL11 photodiode.

  3889   Thu Nov 11 01:34:27 2010 JenneUpdateSUSNew-Old ETM towers assembled

[Suresh, Jenne]

We have put together the new-old ETM towers.  These are the ones which were hanging out on the flow bench down the arm for years and years, and have recently been re-baked.  Interestingly, these are predominantly steel, whereas the newer ones are mostly aluminum.  This caused momentary drama while we scrounged for the correct screws (we needed more silver-plated screws than anticipated, since we were screwing into steel and not aluminum), however the miscellaneous clean hardware collection came to the rescue.  We did however use up all of the 1/4-20 3/4" silver plated screws, so hopefully no one else needs more later...

We only found 5 (enough for one of the two towers) spring plungers which are used to hold the OSEMs in place.  Suresh is sending an email to Steve to ask him to buy some more, so we can get them cleaned in time for use.  This is important, but not super urgent, since we have ~ 2 weeks before the ETMs will be ready for installation. 

Koji has not yet had a chance to inspect the ETM data sheets and choose for us which pair of ETMs to use (ATF sent the 4 ETMs in matched pairs).  So we will not begin the "arts and crafts" until tomorrow-ish.

  3888   Wed Nov 10 22:29:42 2010 kiwamuUpdateIOOmisaligned the wideband EOM

For Yuta's business, I intentionally misaligned the wideband EOM slightly to Yaw direction.  Good luck.

It should show a big AM component at photo detectors.

I touched only the top right knob on the EOM mount and tweaked it by exactly  2 turns in counterclockwise direction.

  3887   Wed Nov 10 14:28:33 2010 KojiSummaryIOOlimitation of current MC aligning

1. Look at the Faraday.

2. Look at the wiki. There is the optical layout in PNG and PDF.

3. 5% (0.8mm) and 2.5%(0.4mm) sounds a big difference for the difficulty, but if you say so, it is not so different.

Actualy, if you can get to the 5% level, it is easy to get to the 1-2% level as I did last time.
The problem is we are at the 15-20% level and can not improve it.

  3886   Wed Nov 10 12:21:18 2010 yutaSummaryIOOlimitation of current MC aligning

1. We didn't measure the aperture size last night. We have to check that.

2. We have to measure the length of FI. Or find a document on this FI.

3. Yes, 5%/sqrt(4). But I didn't think the factor of 2 is important for this kind of estimation.

  3885   Wed Nov 10 11:46:19 2010 KojiSummaryIOOlimitation of current MC aligning

It didn't make sense in several points.

1. Is the Faraday aperture really 3mm? The beam has the gaussian radius of ~1.5mm. How can it be possible to go through the 3mm aperture?

2. Why the MC3-FT distance is the matter? We have the steering mirror after MC3. So we can hit the center of the Faraday.
But if we have VERTICAL TILT of the beam, we can not hit the center of the Faraday entrance and exit at the same time.
That would yield the requirement.

3. If each coil has 5% variance in the response, variance of the nodal point (measured in % of the coil imbalance) by those four coils will be somewhat better than 5%, isn't it?

  3884   Wed Nov 10 02:51:35 2010 yutaSummaryIOOlimitation of current MC aligning

(Suresh, Yuta)

Summary:
  We need MC to be locked and aligned well to align other in-vac optics.
  We continued to align the incident beam so that the beam passes the actuation nodes of MC1 and MC3.
  From the previous measurement, we found that beam height at IM1 has to be increased by ~3cm.
  Today, we increased it by ~1cm and achieved about 1/3 of the required correction.
  But we cannot proceed doing this because the beam is hitting IM1 at the edge already.

What is the goal of this alignment?:
  If the beam doesn't hit MC optics in the center, we see angle to length coupling, which is not good for the whole interferometer.
 
  Also, if the beam is tilted so much, transmitted beam though MC3 cannot go into FI at right after MC3.
  Say, FI has an aparture of 3mm and MC3-FT distance is 300mm. The beam tilt should be smaller than 3/300 rad. MC1-MC3 distance is 200mm, so the displacement at each mirror should be smaller than ~1mm.
  1mm is about 7% (see Koji's elog #2863) TO_COIL gain imbalance in A2L measurement.
 
  We are currently assuming that each coils are identical. If they have 5% variance, it is meaningless to try to reduce the beam displacement less than ~5%.

  So, we set the goal to 7%.

What we did:

  1. Leveled the MC table.

  2. Measured the table height using DISTO D3 laser gauge.
    PSL table 0.83m (+-0.01m)
    OMC table 0.82m
    MC table  0.81m

  3. Using the last steering mirror(SM@PSL) and IM1, tilted the beam vertically

Result:

MCalignNov9.png

  At t=0 (this morning), the beam tilt was ~40%/(MC1-MC3 distance). Now, it is ~30%/(MC1-MC3 distance).
  30%/(MC1-MC3 distance) is ~5/200 rad.

Plan:

 We have to somehow come up with the next story. Too much vertical tilt. What is wrong? Table leveling seems OK.
 - measure in-vac beam height
 - maybe OSEMs are badly aligned. we have to check that.

  3883   Tue Nov 9 05:40:12 2010 yutaSummaryIOOMC aligning going on

(Suresh, Yuta)

Background:
  Last week, we reduced the common mode displacement of the beam through MC1 to MC3. 
  Next work is to tilt the beam and center it.

What we did:
  1. Changed the offset going into 1201 Low Noise Amplifier(1201 is for adding +5V offset so that the feedback signal will be in the range of 0-10V)
  2. Using the last steering mirror(SM@PSL) and IM1, tilted the beam
  3. As the beam height changed alot(~0.5cm higher at IM1), MC1 reflection could not reach MCREFL PD. So, we tilted the mirror just after MC1, too.

Result:
MCalignNov9.png

Plan:

  - continue to tilt IM1 in small increments in order to reduce PIT/YAW to length coupling
      If large increments, it takes so much time re-aligning MC to get flashing!

By the way:

    The signal we kept saying "MCL" was not the error signal itself. It was a feed back signal(output of the mode cleaner servo board). The cable labeled "MC REFL" is the error signal. Compare MEDM screen C1IOO_MC_SERVO.adl and the mode cleaner servo board at 1X2. You will be enlightened.

Quote (from elog #3857):

4. Disconnected the cable labeled "MC OUT1" at 1X2 (which is MCL signal to ADC) and put MC2_ULCOIL output directly using long BNC cable.

 

  3882   Mon Nov 8 18:30:33 2010 SureshUpdateIOOMC Trans Mon QPD gain increased by 50x

Increased the transimpedance gain of the MC-Trans-Mon QPD ckt

The gain of this QPD was insufficient to see the light transmitted through the MC2.  The resulting voltage output was about  10 steps of the 16-bit ADC card.  As the input power, which is currently held at about 40mW may be increased to the vicinity of 2W (total output of the NPRO) we would have 500 ADC steps.  But the dynamic range of the ADC is 64k and  increasing the gain of this QPD ckt by a factor of 50 would enable us to utilise this dynamic range effectively.  However as we do not need a response faster than 10Hz from this ckt its response time has been limited by increasing the feedback capacitance value.

The ckt diagram for the QPD ckt is D980325-Rev-C1  .  The particular unit we are dealing with has the Serial No. 110.  The resistors R1, R2, R3, R4 are now 499 kOhm.  As per the guidelines in the ckt diagram, we increased the capacitance values C3,C4,C5,C6 to 2.2 nFThe current cut off frequency for the MC-Trans-Mon is 145 Hz (computed).

Initially, while reassembling the QPD unit, the IDC 16 connector to the ckt board was reversed by mistake and resulted in the OP497 chip over-heating.  Consequently one of the opamps on the chip was damaged and showed monotonously increasing ouput voltage.  Todd Etzel gave us a spare OP497 and I replaced the damaged chip with this new one. The chips are also available from  Newark Stock No. 19M8991 . The connector has been marked to indicate the correct orientation. The ckt was checked by temporarily connecting it in the place of the PRM Optical lever QPD.  It worked fine and has been put back in its place at the MC2 Transmission.  The QPD was wiped with a lens tissue+Methanol  to remove dust and finger prints from its surface.

It may need to be repositioned since the beam would have shifted under the MC realignment procedure.

 

 

 

  3881   Mon Nov 8 16:03:46 2010 kiwamuUpdateGreen Locking80MHz VCO : PLL open loop looks good

Quote:

I measured the open loop transfer function of the 80MHz VCO's PLL while locking it to Marconi.

 

Bad; there should be a passive ~1 MHz LP filter between the mixer and anything that comes after. The SR560 + mixer does not equal a demodulator.

  3880   Mon Nov 8 14:30:15 2010 josephb, yutaUpdateCDSAdded LIGONDSIP setting to cshrc.40m

We added the following line to the cshrc.40m file in the 64-bit linux and 32-bit linux sections:

setenv LIGONDSIP fb

This allows codes like tdsdmd to work properly on the linux machines (seemed to already work fine on the solaris op440m without this change).

  3879   Mon Nov 8 10:48:58 2010 kiwamuUpdateGreen Locking80MHz VCO : PLL open loop looks good

I measured the open loop transfer function of the 80MHz VCO's PLL while locking it to Marconi.

 This measurement is for a health check and a characterization of the PLL

The transfer function looks good, it agrees with the designed filter shape.

 


(measurement setup) 

vco_pll.png

 The frequency of Marconi is set to 79.5MHz which is the center frequency of the VCO.

The signal from Marconi is mixed down with the VCO signal at a mixer ZLW-3SH.

Then the demodulated signal goes to a 80MHz LPF to cut off high frequency components.

And it goes through a control filter which has 1Hz pole and 40Hz zero (see this entry).

The 80MHz LPF, the controls filter, the VCO and the RF amplifier are all built in the box.

 

 In order to measure the open loop transfer function I inserted SR560 before the 80MHz LPF.

Using T-splitters the input and the output of SR560 are connected to a spectrum analyzer SR785.

 

(results)

 VCO_PLL.png

 Exciting the system using a source channel of SR785, I measured the open loop transfer function.

The unity gain frequency was measured to about 20 kHz.

It agrees with the designed filter shape (though the gain factor is a little bit underestimated).

Apparently there is a phase delay at high frequency above 10kHz, but it is okay because the phase margin is quite acceptable up to 100kHz.

 

However I found that the control range was quite narrow.

The PLL was able to be kept in only +/- 1MHz range, this fact was confirmed by shifting the frequency of Marconi during it's locked.

I will post another elog entry about this issue.

 


 (notes)

 Marconi power = 6dBm

 VCO power after RF amp. = -0.6 dBm

 Marconi frequency = 79.5 MHz

 Phase detection coefficient = 0.4 V/rad (measured by using an oscillo scope)

 

  3878   Mon Nov 8 10:37:14 2010 KojiUpdateIOOThe 10% pick-off for MCREFL was replaced to a HR mirror

As MC2 Trans mon QPD is temporary removed for fixing, we needed a reference for the MC alignment.

I replaced the 10% pick-off in the MCREFL path to the HR mirror.
Now the MCREFL DC with MC unlock is ~2.2, while it is ~0.29 in lock.
i.e. The visibility is 87%.

This means that the MCWFS were disabled for the moment.

  3877   Sat Nov 6 16:13:14 2010 ranaSummaryCDS40m computer slow down solved

As part of the effort to debug what was happening with the slow computers, I disabled the auto MEDM snapshots process that Yoichi/Kakeru setup some long time ago:

https://nodus.ligo.caltech.edu:30889/medm/screenshot.html

We have to re-activate it now that the MEDM screen locations have been changed. To do this, we have to modify the crontab on nodus and also the scripts that the cron is calling. I would prefer to run this cron on some linux machine since nodus starts to crawl whenever we run ImageMagick stuff.

Also, we should remember to start moving the old target/ directories into the new area. All of the slow VME controls are still not in opt/rtcds/.

  3876   Sat Nov 6 07:26:54 2010 yutaSummaryIOOreduced common mode displacement of the beam through MC1 to MC3

(Koji, Suresh, Yuta)

Summary:

  We need MC to be locked and aligned well to align other in-vac optics.
  By using a new python script A2L.py(see elog #3863), we are measuring A2L coupling and centering the beam.
  Tonight's goal was to reduce common mode displacement of the beam through MC1 to MC3, and we succeeded.

Strategy of beam centering:

  We first ignore the beam position at MC2 and focus on MC1,MC3. If MC1,MC3 alignments are given, MC2 alignment is determined.

  For MC1 and MC3, we first reduce the common mode displacement using the last steering mirror at PSL table.
  The last steering mirror makes translation of the incident beam because it is far (~m) from the MC.
  So,
    1. Rotate the steering mirror nob a little
    2. Lock MC so that MC beam axis will be the same as the incident beam axis
    3. A2L measurement
    4. To 1-3 over until the beam crosses MC1 center to MC3 center axis
        The amount of vertical/horizontal displacements of the beam spot at MC1 and MC3 should be the same.
        From our convention, for vertical, MC1 and MC3 should have opposite sign. For horizontal, same sign. (see picture below)

Result:
A2LMCalign.png
 
  From the A2L measurement, now the beam spot is lower right at MC1 and upper right at MC3.
 

  The directions of the beam spot motion agree with the steering mirror tilts.
  Also, the amount of the motion seems reasonable.
    1 tooth rotation of the steering mirror nob makes ~1e-3 inch push which equals to ~0.5mrad rotation.
    The steering mirror to MC is like ~2m and 0.5mrad mirror tilt makes ~2mm displacement at the MC optics.
    2mm displacement is ~15% at the mirror (see Koji's elog #2863;note that coil-coil distance is 1/sqrt(2) of the mirror diameter).
    The measured vertical spot motion is ~15%/1tooth. Horizontal is sqrt(2) times bigger because of the angle of the MC1, MC3 and they are about that much, too.

Plan:
 - Use IM1 to make beam tilt and finally center the beam
 - Improve the script so that it features weighting in fitting
 - Write a script that balances actuation efficiency of the 4 coils.
     We are currently assuming that 4 coils are well balanced.
     In order to do the balancing, we need to balance OSEMs too.

  3875   Sat Nov 6 01:54:15 2010 FrankSummaryComputersvirus definition file update on laptop for dinocam

i took some pictures with the dinocam this afternoon. I used the laptop computer next to it using wireless lan connection to the caltech network to send the pictures to me.

The installed anti virus software was bitching about the old database and wanted to update that. As the installed virus definition database was from mid last year i agreed and started downloading the update. As the file was huge (~100MB) it wasn't finished when i left. computer is still running and probably waiting for instructions.

Will come back on the weekend to finalize the new virus definition file database installation.

  3874   Sat Nov 6 00:49:04 2010 KojiUpdateIOOIMC table work

[Suresh, Koji]

- Removed MCT optics in the IMC chamber

- Rotated MC1 and MC3 in clock-wise to debias the YAW bias offsets (-5V and -8V to -1.5V and -0.5V).

- Adjusted insertion of the MC1 OSEMs so as to have the outputs of about 1.0V.

- Locked to TEM00. Trying to get the beams at the center of the mirror using Yuta's A2L.

  3873   Fri Nov 5 23:05:43 2010 ranaConfigurationIOOioo.db file changed in c1iool0 to get back MC TRANS

 

We like to have the MC TRANS channels so that we can run all of our old scripts and trends on it. This is the usual BROWN

channel that's on the LockMC screen. Its also the thing that we use for thresholding to activate the MC Autolocker Daemon.

I modified the ioo.db file in the target/c1iool0/ directory so that the MC_TRANS_SUM, _P, and _Y channels are all now just

CALC records of the MC2 OL channels (where the calculation is MC_TRANS_SUM = MC2 OL_SUM + 0.001, etc.). I then

rebooted c1iool0 a few times to get the syntax right. It SEEMS to be working now. I'm sure that this won't effect anything.
I've committed the new file to the SVN repo. Once Suresh is done hacking the QPD circuit, we can set the threshold in the Autolocker.

  3872   Fri Nov 5 21:49:12 2010 ranaSummaryCDS40m computer slow down solved

Quote:

Problem:

The 40m computers were responding sluggishly yesterday, to the point of being unusable.

Cause:

The mx_stream code running on c1iscex (the X end suspension control computer) went crazy for some reason.  It was constantly writing to a log file in /cvs/cds/rtcds/caltech/c1/target/fb/192.168.113.80.log.  In the past 24 hours this file had grown to approximatel

The moral of the story is, PUT THINGS IN THE ELOG. This wild process is one of those things where people say 'this won't effect anything', but in fact it wastes several hours of time.

  3871   Fri Nov 5 19:33:18 2010 JenneUpdateElectronicsThe beginnings of the new phase of the RF work

Joon Ho and I took a look at the RF stuff that Alberto left, and we determined that we've got most everything that we need.  On Monday, Joon Ho will list off the stuff that we're missing, and we'll have Steve order it.

Joon Ho also replaced the temporary front panel to the RF generation box with Alberto's fancy new panel.  Pics are here (although you have to sign in as foteee to see them). 

Work on the frequency distribution box will continue on Monday.

  3870   Fri Nov 5 16:40:22 2010 josephb, alexUpdateCDSc1ioo now has working awgtpman

Problem:

We couldn't set testpoints on the c1ioo machine.

Cause:

Awgtpman was getting into some strange race condition.  Alex added an additional sleep statement and shifted boot order slightly in the rc.local file.  This apparently is only a problem on c1ioo, which is a Sun X4600.  It was using up 100% of a single CPU for the awgtpman process.

Status:

We now have c1ioo test points working.

Future:

Need to examine the startc1ioo script and see if needs a similar modification, as that was tried at several points but yielded a similar state of non-functioning test points. For the moment, reboot of c1ioo is probably the best choice after making modifications to the c1ioo or c1x03 models.

Current CDS status:

MC damp dataviewer diaggui AWG c1ioo c1sus c1iscex RFM Sim.Plant Frame builder  TDS
                     
  3869   Fri Nov 5 15:20:18 2010 josephb, alexSummaryCDS40m computer slow down solved

Problem:

The 40m computers were responding sluggishly yesterday, to the point of being unusable.

Cause:

The mx_stream code running on c1iscex (the X end suspension control computer) went crazy for some reason.  It was constantly writing to a log file in /cvs/cds/rtcds/caltech/c1/target/fb/192.168.113.80.log.  In the past 24 hours this file had grown to approximately 1 Tb in size. The computer had been turned back on yesterday after having reconnected its IO chassis, which had been moved around last week for testing purposes - specifically plugging the c1ioo IO chassis in to it to confirm it had timing problems.

Current Status:

The mx_stream code was killed on c1iscex and the 1 Tb file removed.

Computers are now more usable.

We still need to investigate exactly what caused the code to start writing to the log file non-stop.

Update Edit:

Alex believes this was due to a missing entry in the /diskless/root/etc/hosts file on the fb machine.  It didn't list the IP and hostname for the c1iscex machine.  I have now added it.  c1iscex had been added to the /etc/dhcp/dhcpd.conf file on fb, which is why it was able to boot at all in the first place.  With the addition of the automatic start up of mx_streams in the past week by Alex, the code started, but without the correct ip address in the hosts file, it was getting confused about where it was running and constantly writing errors.

Future:

When adding a new FE machine, add its IP address and its hostname to the /diskless/root/etc/hosts file on the fb machine.

  3868   Fri Nov 5 14:06:19 2010 yutaUpdateIOOtried to align MC by A2L measurement

(Suresh, Kiwamu, Yuta)

Summary:
  Lastnight, we locked the MC and tried angle to length(A2L) measurement using my new python script (see elog #3863).
  Although the amount of position script shows looks too big, the response seemed somewhat reasonable.
  Using the results of A2L measurement, we managed to reduce the displacement from the center of the MC optics, but we lost TEM00 mode after changing the incident beam direction and PMC lock got off .
  We restored the alignments and now it is 00, but the displacements got worse than the best we achieved last night.

  I think I have to rethink how to align MC. Even if I could somehow get exact position of the beam, how to align the beam to the center of the optics?

What we did:
  1. At first we tried to align by changing the direction of the incident beam. We found that A2L.py shows opposite direction(lower <-> upper). It was because of my misunderstanding and we agreed that the direction is opposite.

  2. Aligned MC optics without changing the direction of the incident beam. We could understand which directions decrease the displacements from the center, and managed to decrease them.

  3. There seemed to be a limit in aligning the MC optics without changing the incident beam direction. So, we started to change the incident beam direction again by steering mirrors at PSL table.

  4. During the change, PMC lock got off. We restored it, but we lost MC's 00 mode.

  5. We restored MC 00 mode, and measured the final A2L. The result was worse than we achieved by step #2.

Result:
  The final result from last night using my script was as follows;

  MC1 MC2 MC3
vertical 36% -19% 19%
horizontal 49% 6% -37%

  % is the length compared to the half of coil to coil length. Low / right are positive.
  We can see the beam position got better by looking at the monitor from MC2, and the A2L measurement result agrees with that.

  Here's some pictures from the measurement last night. Each plots are not taken at the same time.
A2LmeasurementFigures.png
   (It was painful using slow computers to make measurement. The StripTool graph shows straight lines when computers got frozen)

Plan:
 - Plan a strategy
 - The script needs self-estimation of the measurement. Now, the script fits the plot assuming every data has the same error.
 - When the beam is near the center, the signal gets smaller and the result will be unreliable. One thing I can do is to change TO_COIL gains radically so that the axis of rotation go far from the center.

  3867   Fri Nov 5 09:08:14 2010 steveUpdateSUSepoxy

Physical Electronics: Vac-Seal #288-6000 arriving Monday. Our last bag used last week had a p/n 1002003 with expiration date   .....2009 ? and it was stored in the

refrigerator all times. We are getting 68 small bags.

We should have precision gluing notes of epoxies/procedures used on our sus upgrade.

Attachment 1: 11081001.PDF
11081001.PDF
  3866   Thu Nov 4 19:26:51 2010 SureshUpdateLockingChanges to the Video MUX reversed

All the temporary changes to the video cables and the video MUX ( 3843 ) have been reversed and the system returned to its original state.

  3865   Thu Nov 4 19:00:57 2010 SureshUpdateLockingFibre coupling 1064nm light at the south-end table

The Fluke Visual Fault locator (Visifault) arrived and I used it to couple 1064nm light into the single mode fibre at the south-end-table.

Procedure used:

When the output end of the fiber is plugged into the Visifault the light emerges from at the south end (input side for 1064nm).  This light is collimated with the fiber coupler at that end and serves as a reference for the optical axis along which the 1064 light must be directed.  Once the two beams (red and 1064) are overlapped with the beam steering mirrors, the Visifault was disconnected from the fiber and the  fibre output ( 1064 at the PSL table) is maximized by walking the beam at the input end and adjusting the collimation at the input.

The output of the fiber has been collimated with a fiber coupler.

7.5mW are incident on the input end and 1.3mW have been measured at the output.    This output power is adequate for the observing the beats with PSL NPRO.

 

 

 

ELOG V3.1.3-