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ID Date Author Type Category Subject
13907   Thu May 31 23:12:17 2018 gautamUpdateLSCDRMI locking attempt

Summary:

I wanted to recover the DRMI locking. Among other things, Jon mentioned that his mode spectroscopy can be done in the DRMI config. But I was foiled last night by a rogue waveplate in the AS beampath, and today evening, I noticed the resurfacing of this problem. Clearly, this is indicative of some issue in the analog whitening electronics, as the DC light level on the AS55 PD is consistent with previous measurements. Moreover, last time, the problem "fixed itself" so I don't know what exactly the problem was in the first place. I'll try doing the same test in the linked elog tomorrow. As a quick test, I cycled through the whitening gains (0-45dB) to see if it was some stuck ADC register, but that didn't fix the problem.

The problem seems to be with REFL55 only - I am able to lock the PRMI with carrier resonant without any issues, and the error signal levels are consistent with what I remember them being while the PRMI is swinging around. AS55 lives on the same whitening board and doesn't seem to suffer from the same probelms.

Decided to do the check tonight, but as Attachment #1 shows, no real red flags from the whitening gain side.

Attachment 1: REFL55_whtCheck.pdf
13908   Fri Jun 1 01:22:50 2018 gautamUpdateLSCDRMI locking restored

As it happened last time, the problem apparently fixed itself - somehow the act of me disconnecting the cables and reconnecting them seems to solve the problem, need to think about this.

Anyway, DRMI was locked a few times tonight. I got in a good long stretch where I ran some sensing lines and collected some data, analysis tomorrow. I am going to center the vertex oplevs as an alignment reference for now. A major source of lockloss seems to be angular instability - see for example this video grab of POP:

Could be due to noise injection from the noisy PRM Oplev HeNe, or just TT mirror angular motion (I couldn't get the PRC angular FF going tonight).

Attachment 1: DRMI_20180531.png
13913   Mon Jun 4 11:00:37 2018 gautamUpdatePSLaux laser replacement
 Quote: I couldn't locate an appropriate heat sink for the driver, which is still in factory condiction, but since the PSL AOM also runs on 80MHz I used that one instead.

We have the appropriate heatsink - I'd like to minimize interference with the main beam wherever possible.

 Quote: For the PSL beat the AOM drive is not needed, and the power in the optical fiber should not exceed 100 mW, so the offset voltage to the AOM RF driver has to remain below 300 mV.

If damage to the fiber is a concern, I think it's better to use a PBS + waveplate to attenuate the power going into the fiber. When the AOM switching is hooked up to CDS, it's easy to imagine a wrong button being pressed or a wrong value being typed in.

It would probably also be good to have a pickoff monitor for the NPRO DC power so that we can confirm its health (in the short run, we can hijack a PSL Acromag channel for this purpose, as we now do for FSS_RMTEMP). I don't know that we need an EOM for the PLL, as in order to get that going, we probably need some fast electronics for the EOM path, like an FSS box.

STEVE: I ordered the right heatsink for the acousto after Koji pointed out that the vertical fins are 20% more efficient. Why? Because hot air rises. It will be here in 3-4 days.

13916   Tue Jun 5 02:06:59 2018 gautamUpdatePSLaux laser first (NULL) results

[johannes, gautam]

1. Johannes aligned the single bounce off the ITM into the AUX fiber on the AS table, and also the AUX beam into the fiber on the PSL table.
• Mode matching isn't spectaular anywhere in this chain.
• But we have 2.6mW of light going into the SRM with the AOM deflection into the 1st order beam (which is what we send into the IFO) maximum.
2. We set up some remote capabilities for the PLL and Marconi frequency (=PLL setpoint) control.
3. Motivation was to try and lock DRMI, and look for some resonance of the AUX beam in the SRC.
• We soon realized this was a way too lofty goal.
• So we decided to try the simpler system of PRMI locked on carrier.
• We were successfully able to sweep the Marconi setpoint in up to 20kHz steps (although we can only move the setpoint in one direction, not sure I know why now).
• Then we decided to look for resonances of the AUX beam in the arm cavity.
• Still no cigar
4. Plus points:
• PLL can be reliably locked remotely.
• Marconi freq. can be swept deterministically remotely.
5. Tomorrow:
• Fix polarization issues. There is some low freq drift (~5min period) of the power incident on the fiber on the PSL table which we don't understand.
• Verify MM into IFO and also into fiber at PSL table.
• Do mode spectroscopy.

I was wondering why the PMC modulation sidebands are showing up on the control room analyzer with ~6dB difference in amplitude. Then I realized that it is reasonable for the cabling to have 6dB higher loss at 80 MHz compared to 20 MHz.

13919   Wed Jun 6 10:44:52 2018 gautamUpdateVACAnnulus pressure channels added to frames

[steve, gautam]

We added the following channels to C0EDCU.ini and restarted the daqd processes. Channels seem to have been added successfully, we will check trend writing later today. Motivation is to have a long term record of annulus pressure (even though we are not currently pumping on the annulus).

C1:Vac-PASE_status

C1:Vac-PASV_status

C1:Vac-PABS_status

C1:Vac-PAEV_status

C1:Vac-PAEE_status

plot next day

Attachment 1: AnsPressureLogged.png
13920   Wed Jun 6 14:36:15 2018 gautamUpdateLSCTRX clipping

For some time now, I've been puzzled by the unreliability of the ASS_X dither alignment servo. Leaving the servo on, TRX often begins to decay to a lower value, and even after freezing the dither at the maximum TRX values, I can manually align the mirrors to increase TRX. We have suspected some kind of clipping in the TRX path that is responsible for this behaviour. Today I decided to investigate this a bit further. To have the arm locked and to inspect the beam, we have to change the locking trigger - TRX is what is normally used, but I misaligned the Y arm completely, and used AS110 as a trigger instead. There is some strangeness in the triggering topology, but this deserves a separate elog.

Once the arm was locked (and relocks using the AS110 trigger in the event of an unlock), I was able to trace the beampath on the EX table with an IR card. The TRX beam is rather large and weak, so it is hard to see, but as best as I can tell, the only real danger of clipping (or perhaps the beam is already clipped) is on the final steering mirror before the beam hits the (Thorlabs) PD. Steve/Pooja are working on getting a photo of this, and will upload it here shortly. Options to mitigate this:

1. Use the harmonic separator to steer the beam lower, and center it on the 1" steering mirror. However, this could possibly lead to clipping on some of the upstream lenses.
2. Raise the height of the 1" steering mirror by 0.25". However, this would require a custom 3/4" dia post height or some shims, which I am not sure is in line with our optomechanic mounting practises.
3. Use a 2" mirror instead of a 1" mirror.

The EX QPD has stopped working since the Acromag install. If it were working, we wouldn't have to rely on the alternate triggering with AS110 and instead just use the QPD as TRX, while we debug the Thorlabs PD path.

13921   Wed Jun 6 14:50:25 2018 gautamUpdateGeneralLSC triggering

I though that the "C1LSC_TRIG_MTRX" MEDM screen completely controls the triggring of LSC signals. But today while trying to trigger the X-arm locking servo on AS110 instead of TRX, I found some strange behaviour. Summary of important points:

1. Even though the servo was supposed to be triggered on AS110, the act of me blocking the beam on the EX table destroyed the lock. I verified the correlation between me blocking the beam and the lock being destroyed by repeating the blocking at least 10 times at different locations along the beam path (to make sure I wasn't accidentally clipping the Oplev beam for example).
2. Investigating further, I found that me turning off the TRX signal digitally also deterministically led to the X arm lock being lost. To be clear, the TRX DC element in the trigger matrix was 0.
3. Confirmed that TRX wasn't involved in any way in the locking servo (I was checking for normalization of the PDH error signal by the DC transmission value, but this is not done). To do this, I locked the arm, and then turned all elements corresponding to TRX in the PowNorm matrix to 0. Then I disabled the locking servo and re-enabled it, and the lock was readily re-acquired readily.

All very strange, not sure what's going on here. The simulink model diagram also didn't give me any clues. Need's further investigation.

Attachment 1: LSC_TRIG.png
13925   Thu Jun 7 12:20:53 2018 gautamUpdateCDSslow machine bootfest

FSS slow wasn't running so PSL PZT voltage was swinging around a lot. Reason was that was c1psl unresponsive. I keyed the crate, now it's okay. Now ITMX is stuck - Johannes just told be about an un-elogged c1susaux reboot. Seems that ITMX got stuck at ~4:30pm yesterday PT. After some shaking, the optic was loosened. Please follow the procedure in future and if you do a reboot, please elog it and verify that the optic didn't get stuck.

Attachment 1: ITMX_stuck.png
13927   Thu Jun 7 16:15:03 2018 gautamUpdateLSCTRX clipping

I opted for the quickest fix - I raised the height of the offending steering mirror using a 0.25" shim. In the long term, we can get a taller post machined. After raising the mirror height, I then checked the DC centering of the spot on the DC PD using a scope.

Looking at the performance of the X arm ASS, I no longer see the strange oscillatory behaviour I described in my previous post . Moreover, the TRX level was ~1 before be raising the steering mirror - but it is now ~1.2. So we were certainly losing some power.

13931   Fri Jun 8 00:36:54 2018 gautamUpdatePSLobserving the resonance signal corresponding to the injected frequency.

It isn't clear to me in the drawing where the Agilent is during this measurement. Over 40m of cabling, the loss of signal can be a few dB, and considering we don't have a whole lot of signal in the first place, it may be better to send the stronger RF signal (i.e. Marconi pickoff) over the long cable rather than the weak beat signal from the Transmission photodiode.

13933   Fri Jun 8 01:58:56 2018 gautamUpdateLSCDRMI locking attempt again

Given the various changes to the IFO config since last Thursday when I was last able to lock the DRMI, I wanted to try once again tonight. However, I had no success. By my judgement, the alignment is fine as judged by looking at mode flashes on the cameras. However, despite following the usual alignment procedures, I did not get a single lock in tonight.

Perhaps we can use a flip mount on the BS that combines the PSL and AUX beams on the AS table, so we have the option of recovering the usual IFO config when we so desire - while Jon needs the SRC locked for his measurement, it would be nice to not have to figure out the correct demod phases etc each time there is a change in the optical setup of the AUX beam.

13935   Fri Jun 8 20:15:08 2018 gautamUpdateCDSReboot script

Unfortunately, this has happened (and seems like it will happen) enough times that I set up a script for rebooting the machine in a controlled way, hopefully it will negate the need to repeatedly go into the VEA and hard-reboot the machines. Script lives at /opt/rtcds/caltech/c1/scripts/cds/rebootC1LSC.sh. SVN committed. It worked well for me today. All applicable CDS indicator lights are now green again. Be aware that c1oaf will probably need to be restarted manually in order to make the DC light green. Also, this script won't help you if you try to unload a model on c1lsc and the FE crashes. It relies on c1lsc being ssh-able. The basic logic is:

2. Shutdown all vertex optic watchdogs, PSL shutter.
3. ssh into c1sus and c1ioo, shutdown all models on these machines, soft reboot them.
4. ssh into c1lsc, soft reboot the machine. No attempt is made to unload the models.
5. Wait 2 minutes for all machines to come back online.
6. Restart models on all 3 vertex FEs (IOPs first, then rest).
7. Prompt user for confirmation to re-enable watchdog status and open PSL shutter.
Attachment 1: 31.png
13942   Mon Jun 11 18:49:06 2018 gautamUpdateCDSc1lsc dead again

Why is this happening so frequently now? Last few lines of error log:

[  575.099793] c1oaf: DAQ EPICS: Int = 199  Flt = 706 Filters = 9878 Total = 10783 Fast = 113
[  575.099793] c1oaf: DAQ EPICS: Number of Filter Module Xfers = 11 last = 98
[  575.099793] c1oaf: crc length epics = 43132
[  575.099793] c1oaf:  xfer sizes = 128 788 100988 100988
[240629.686307] c1daf: ADC TIMEOUT 0 43039 31 43103
[240629.686307] c1cal: ADC TIMEOUT 0 43039 31 43103
[240629.686307] c1ass: ADC TIMEOUT 0 43039 31 43103
[240629.686307] c1oaf: ADC TIMEOUT 0 43039 31 43103
[240629.686307] c1lsc: ADC TIMEOUT 0 43039 31 43103
[240630.684493] c1x04: timeout 0 1000000
[240631.684938] c1x04: timeout 1 1000000
[240631.684938] c1x04: exiting from fe_code()

I fixed it by running the reboot script.

Attachment 1: 36.png
13947   Mon Jun 11 23:22:53 2018 gautamUpdateCDSEX wiring confusion

[Koji, gautam]

Per this elog, we don't need any AIOut channels or Oplev channels. However, the latest wiring diagram I can find for the EX Acromag situation suggests that these channels are hooked up (physically). If this is true, there are 12 ADC channels that are occupied which we can use for other purposes. Question for Johannes: Is this true? If so, Kira has plenty of channels available for her Temperature control stuff..

As an aside, we found that the EPICS channel names for the TRX/TRY QPD gain stages are somewhat strangely named. Looking closely at the schematic (which has now been added to the 40m DCC tree, we can add out custom mods later), they do (somewhat) add up, but I think we should definitely rename them in a more systematic manner, and use an MEDM screen to indicate stuff like x4 or x20 or "Active" etc. BTW, the EX and EY QPDs have different settings. But at least the settings are changed synchronously for all four quadrants, unlike the WFS heads...

Unrelated: I had to key the c1iscaux and c1auxey crates.

13948   Tue Jun 12 03:22:25 2018 gautamUpdateLSCAUX laser shuttered

I worked a bit on recovering the DRMI locking again tonight. I decided to shutter the AUX laser on the PSL table at least until I figured out the correct locking settings. As has become customary now, there was a cable in the AS beampath (leading from the AS55 DC monitor to nothing, through the enclosure side panel, it is visible in Attachment #3 in this elog) which I only found after 30mins of futility - please try and remove all un-necessary cables and leave the AS beampath in a usable state after working on the AS table!  In the end, I got several short (~3mins) stretches in tonight, but never long enough to do the loop characterization I wanted to get in tonight, probably wrong gains in one or more of the loops. In the last 30 minutes, the IMC has been frequently losing lock, so I am quitting for now. The AUX laser remains shuttered.

13949   Tue Jun 12 14:47:37 2018 gautamBureaucracyGeneralUnlabelled components from EX moved to SP table and labelled

Steve mentioned two unlabelled optics were found at EX, relics from the Endtable upgrade.

• One was a 1" 45 deg p-pol optic (Y1-1025-C-45P), it looks a bit scratched.
• The other was a Beam Sampler (BSF10-C).

These are now labelled and forked down on the SP table.

13952   Wed Jun 13 01:02:40 2018 gautamUpdateLSCReliable and repeatable 1f DRMI locking

[koji, gautam]

With Koji's help, I got repeatable and reliable DRMI locking going again tonight - this is with the AS path optics for the spectroscopy measurement in place, although the AUX laser remained shuttered tonight. Results + spectra tomorrow, but here's what I did:

• Initial alignment procedure was as usual - use arms+ASS to align ITMs, and then PRMI carrier+ASS to align PRM and BS.
• Found the appropriate gains and demod phases.
• Measured loop TFs - PRCL is a big mystery. Used these to finalize loop gains.
• Ran some sensing lines.
• Whitened DRMI PDs for a calibrated "low-noise" spectrum (although the coils were not de-whitened).

As I have found before, it is significantly easier to get the locking going post 11pm - the wall Seis BLRMS don't look that much quieter at midnight compared to 10pm, but this might be a scaling issue. I'll do a quantitative assessment next time... Also, Foton takes between 25-45 secs to save an updated filter (timed twice today).

13953   Wed Jun 13 11:17:40 2018 gautamUpdateLSCPRCL loop shape anomaly

Attachment #1 shows the measured PRCL loop shape. The blue line is meant to be the "expected" loop shape. While the measured loop shape tracks the expectation down to ~100 Hz, I cannot explain the shape below it. I am also not sure what to make of the fact that there is high coherence down to 10 Hz fron IN2 to IN1, but no coherence between EXC/IN2. I confirmed that the low-frequency boost filters were ON during the measurement. I don't understand how a pendulum TF + the digital filters we used can account for the shape below 100Hz.

gautam 11pm: After discussing with Koji, I conclude that the low frequency loop shape is consistent with the excitation amplitude being insufficient below 100 Hz. Coherence is good between In1/In2 because they are the same signal effectively - what we need is coherence between In1 and EXC, which isn't plotted. It is still strange that Coherence between In2/EXC is ZERO....

 Quote: Measured loop TFs - PRCL is a big mystery. Used these to finalize loop gains.
Attachment 1: PRCL_12Jun2018_WeirdShape.pdf
13955   Wed Jun 13 12:21:09 2018 gautamUpdateALSPDFR laser checkout

I want to use the Fiber Coupled laser from the PDFR system to characterize the response of the fiber coupled PDs we use in the BeatMouth. The documentation is pretty good: for a first test, I did the following in this order:

• Removed the input fiber to the 1x16 splitter located in the rack near the OMC chamber.
• Connected aforementioned fiber to a collimator.
• Aligned the output of the collimator onto a razor beam dump.
• Turned on the laser controller - it came on with a TEC temperature of 22.5 C and I_diode 0 mA, and the "output shorted" LED was ON (red).
• Turned up the diode current to 80 mA, since the "threshold current" is stated as 75 mA in the manual. In fact, I could see a beam using an IR card at 30 mA already.
• At 80mA, I measured 3.5 mW of output power using the Ophir.

Seems like stuff is working as expected. I don't know what the correct setpoint for the TEC is, but once that is figured out, the 1x16 splitter should give me 250 uW from each output for 4mW input. This is well below any damage threshold of the Menlo PDs. Then the plan is to modulate the intensity of the diode laser using the Agilent, and measure the optoelectronic response of the PD in the usual way. I don't know if we have a Fiber coupled Reference Photodiode we can use in the way we use the NF1611 in the Jenne laser setup. If not, the main systematic measurement error will come from the power measurement using a Fiber Power Meter.

13957   Wed Jun 13 22:07:31 2018 gautamUpdateALSBeatMouth PDFR measurement

Summary:

Neither of the Menlo FPD310 fiber coupled PDs in the beat mouth have an optoelectronic response (V/W) as advertised. This possibly indicates a damaged RF amplification stage inside the PD.

Motivation:

I have never been able to make the numbers work out for the amount of DC light I put on these PDs, and how much RF beat power I get out. Today, I decided to measure the PD response directly.

Details:

In the end, I decided that slightly modifying the Jenner laser setup was the way to go, instead of futzing around with the PDFR laser. These PDs have a switchable gain setting - for this measurement, both were set to the lower gain such that the expected optoelectronic response is 409 V/W.

[Attachment #1] - Sketch of the experimental setup.

[Attachment #2] - Measured TF responses, the RF modulation was -20dBm for all curves. I varied the diode laser DC current a little to ensure I recovered identical transfer functions. Assumptions used in making these plots:

1. NF1611 and FPD310 have equal amounts of power incident on them.
2. The NF1611 transimpedance is 700V/A.

[Attachment #3] - Tarball of data + script used to make Attachment #2.

Conclusions:

• The FPD310 does not have a DC monitor port.
• So the dominant uncertainty in these plots is that I don't know how much power was incident on the PD under test.
• The NF1611 DC power level could be measured though, and seemed to scale with DC pump current linearly (I had only 3 datapoints though so this doesn't mean much).
• Neither PD has transimpedance gain as per the specs.
• The X PD shows levels ~x10 lower than expected.
• The Y PD shows levels ~x3 lower than expected.
• I will repeat the measurement tomorrow by eliminating some un-necessary patch fiber cables, and also calibrating out the cable delays.
• The setup shown in Attachment #1 was used because I didn't want to open up the BeatMouth.
• But I can pipe the port of the BS not going to the FPD310 directly to the collimator, and that should reduce the systematic uncertainty w.r.t. power distribution between FPD310 and NF1611.
Attachment 1: IMG_7056.JPG
Attachment 2: BeatMouthPDFR.pdf
Attachment 3: BeatMouth_PDFRdata.tgz
13959   Thu Jun 14 00:40:42 2018 gautamUpdateLSCPRCL loop shape anomaly

don't use IN_1/IN_2: recall pizza meeting from a few weeks back: use IN1/EXC + Al-Gebra

Quote:
 Quote: Measured loop TFs - PRCL is a big mystery. Used these to finalize loop gains.

13961   Thu Jun 14 10:41:00 2018 gautamUpdateCDSEX wiring confusion

Do we really have 2 free ADC channels at EX now? I was under the impression we had ZERO free, which is why we wanted to put a new ADC unit in. I think in the wiring diagram, the Vacuum gauge monitor channel, Seis Can Temp Sensor monitor, and Seis Can Heater channels are missing. It would also be good to have, in the wiring diagram, a mapping of which signals go to which I/O ports (Dsub, front panel BNC etc) on the 4U(?) box housing all the Acromags, this would be helpful in future debugging sessions.

Quote:

 TYPE Total Available now Available after ADC 24 2 14

13962   Thu Jun 14 13:29:51 2018 gautamUpdateGeneralPSL shutter closed, all optics misaligned

[jon, gautam]

Jon is doing some characterization of the AUX laser setup for which he wanted only the prompt retroreflection from the SRM on the AS table, so the PSL shutter is closed, and both ITMs and ETMs are misaligned. The prompt reflection from the SRM was getting clipped on something in vacuum - the ingoing beam looked pretty clean, but the reflection was totally clipped, as I think Johannes aligned the input beam with the SRM misaligned. So the input steering of the AUX laser beam into the vacuum, and also the steering onto AS110, were touched... Also, there were all manner of stray, undumped beams from the fiber on the AS table Jon will post photos.

Before we began this work, we found that c1susaux was dead so we rebooted it.

13963   Thu Jun 14 15:21:58 2018 gautamUpdateComputer Scripts / Programs/cvs/cds Backup in danger

I think this is because /cvs/cds is getting too big. lsblk reveals:

controls@chiara|~> lsblk NAME   MAJ:MIN RM   SIZE RO TYPE MOUNTPOINT sda      8:0    0 465.8G  0 disk  ├─sda1   8:1    0 446.9G  0 part / ├─sda2   8:2    0     1K  0 part  └─sda5   8:5    0  18.9G  0 part [SWAP] sdb      8:16   0   2.7T  0 disk  └─sdb1   8:17   0     2T  0 part /home/cds sr0     11:0    1  1024M  0 rom   sdc      8:32   0   1.8T  0 disk  └─sdc1   8:33   0   1.8T  0 part /media/40mBackup sdd      8:48   0   1.8T  0 disk  └─sdd1   8:49   0   1.8T  0 part 

I believe one of sdc or sdd is connected via SATA while the other is an external USB drive. Maybe we have to get bigger backup disks, but this may be a huge pain to setup as it will involve taking chiara down. Actually, now that I check the backup log, seems like backup is executing successfully - not sure if this is due to my unelogged mounting of sdc (using sudo mount /dev/sdc1 /media/40mBackup) last week, or if this is some LDAS backup. But in any case, seems undesirable that sdb1 is larger than sdc1 or sdd1.

2018-06-06 07:00:01,086 INFO       Updating backup image of /cvs/cds 2018-06-06 07:00:01,086 ERROR      External drive not mounted!!! 2018-06-07 07:00:01,147 INFO       Updating backup image of /cvs/cds 2018-06-07 07:00:01,147 ERROR      External drive not mounted!!! 2018-06-08 07:00:01,244 INFO       Updating backup image of /cvs/cds 2018-06-08 08:23:32,939 INFO       Backup rsync job ran successfully, transferred 316870 files. 2018-06-09 07:00:01,465 INFO       Updating backup image of /cvs/cds 2018-06-09 07:12:11,865 INFO       Backup rsync job ran successfully, transferred 1926 files. 2018-06-10 07:00:01,842 INFO       Updating backup image of /cvs/cds 2018-06-10 07:12:28,931 INFO       Backup rsync job ran successfully, transferred 1656 files. 2018-06-11 07:00:01,294 INFO       Updating backup image of /cvs/cds 2018-06-11 07:06:14,748 INFO       Backup rsync job ran successfully, transferred 1664 files. 2018-06-12 07:00:02,081 INFO       Updating backup image of /cvs/cds 2018-06-12 07:07:36,775 INFO       Backup rsync job ran successfully, transferred 1870 files. 2018-06-13 07:00:02,194 INFO       Updating backup image of /cvs/cds 2018-06-13 07:08:37,356 INFO       Backup rsync job ran successfully, transferred 1818 files. 2018-06-14 07:00:01,753 INFO       Updating backup image of /cvs/cds 2018-06-14 07:01:43,270 INFO       Backup rsync job ran successfully, transferred 1744 files.
 Quote: Local backup on chiara seems not working since Nov 19, 2017. /opt/rtcds/caltech/c1/scripts/backup/localbackup.log 2017-11-18 07:00:01,504 INFO       Updating backup image of /cvs/cds 2017-11-18 07:03:00,113 INFO       Backup rsync job ran successfully, transferred 1954 files. 2017-11-19 07:00:02,564 INFO       Updating backup image of /cvs/cds 2017-11-19 07:00:02,592 ERROR      External drive not mounted!!!

13966   Thu Jun 14 18:09:24 2018 gautamUpdateLSCReliable and repeatable 1f DRMI locking

I finally analyzed the sensing measurement I ran on Tuesday evening. Sensing responses for the DRMI DOFs seems consistent with what I measured in October 2017, although the relative phasing of the DoFs in the sensing PDs has changed significantly. For what it's worth, my Finesse simulation is here

Attachment 1: DRMI1f_June14.pdf
13967   Thu Jun 14 19:30:12 2018 gautamUpdateGeneralIFO alignment restored

All optics have been re-aligned. Jon/Johannes will elog about the work today.

13969   Fri Jun 15 00:53:21 2018 gautamUpdateLSCCalibrated MICH spectrum

Using the numbers from the sensing measurement, I calibrated the measured in-loop MICH spectrum from Tuesday night into free-running displacement noise. For convenience, I used the noise-budgeting utilities to make this plot, but I omitted all the technical noise curves as the coupling has probably changed and I did not measure these. The overall noise seems ~x3  higher everywhere from the best I had last year, but this is hardly surprising as I haven't optimized anything for low noise recently. To summarize:

• DRMI was locked using 1f error signals.
• MICH was controlled using AS55_Q.
• Main difference is that we have a little less (supposedly 10%) light on the AS55 PD now because of the AUX laser injection setup. But the AUX laser was shuttered.
• 1f LSC PDs (REFL11, REFL55 and AS55) had ADC whitening filters engaged in while this data was taken.
• ITM and BS coils were not de-whitened.

I will do a more thorough careful characterization and add in the technical noises in the coming days. The dominant uncertainty in the sensing matrix measurement, and hence this free-running noise spectrum, is that I haven't calibrated the actuators in a while.

 Quote: I finally analyzed the sensing measurement I ran on Tuesday evening. Sensing responses for the DRMI DOFs seems consistent with what I measured in October 2017, although the relative phasing of the DoFs in the sensing PDs has changed significantly. For what it's worth, my Finesse simulation is here.
Attachment 1: C1NB_disp_40m_MICH_NB_2018-06-14.pdf
13973   Fri Jun 15 14:22:05 2018 gautamUpdateALSBeatMouth PDFR measurement

I did the measurement with the BeatMouth open today. Main changes:

• Directly pipe the RF output of the Menlo PDs to the Agilent, bypassing the 20dB coupler inside the BeatMouth.
• Directly pipe the unused port of the Fiber Beamsplitter used to send light to the Menlo PD to an in-air collimator, which then sends the beam to the NF1611 reference detector.

So neglecting asymmetry in the branching ratio of the fiber beamsplitter, the asymmetry between the test PD optical path and the reference PD optical path is a single fiber mating sleeve in the former vs a collimator in the latter. In order to recover the expected number of 409 V/W for the Menlo PDs, we have to argue that the optical loss in the test PD path (fiber mating sleeve) are ~3x higher than in the NF1611 path (free space coupler). But at least the X and Y PDs show identical responses now. The error I made in the previously attached plot was that I was using the 20dB coupled output for the X PD measurement .

Revised conclusion: The measured optoelectronic response of the Menlo PDs at 10s of MHz, of ~130 V/W, is completely consistent with the numbers I reported in this elog. So rogue polarization is no longer the culprit for the discrepancy between expected and measured RF beatnote power, it was just that the expectation, based on Menlo PD specs, were not accurate.#2 of the linked elog seems to be the most likely, although "broken" should actually be "not matching spec".

While killing time b/w measurements, I looked on the ITMY optical table and found that the NF1611 I mentioned in this elog still exists. It is fiber coupled. Could be a better substitute as a Reference PD for this particular measurement.

 Quote: I will repeat the measurement tomorrow by eliminating some un-necessary patch fiber cables, and also calibrating out the cable delays. The setup shown in Attachment #1 was used because I didn't want to open up the BeatMouth. But I can pipe the port of the BS not going to the FPD310 directly to the collimator, and that should reduce the systematic uncertainty w.r.t. power distribution between FPD310 and NF1611.
Attachment 1: BeatMouthPDFR.pdf
Attachment 2: BeatMouth_PDFRdata.tgz
13974   Sat Jun 16 00:26:48 2018 gautamUpdateGeneralPRC modescan attempt

[Jon, Gautam, Johannes]

We did the following today:

1. Dither align arms such that ITMs were reliable arm references.
2. Configure the IFO such that ITMX single bounce was the only visible beam reaching the AS port from the symmetric side - ITMY, both ETMs, PRM and SRM were misaligned.
3. Do coarse alignment on the AS table using the usual near field / far field overlap technique, with "near" and "far" dictated by arm reach on the AS table. In this way, the ingoing AUX beam and the PSL single bounce from ITMX were collimated on the AS table.
4. Lock the AUX / PSL PLL. We expected a beatnote on AS110 at eithe (80-50)=30 MHz or (80+50)=130 MHz. 80 MHz is the AOM driver frequency, while 50 MHz is the PLL offset. (Marconi was actually set to 60 MHz, prolly Keerthana forgot to reset it after some remote experimentation).
5. Beat was found at 30 MHz.
6. Input steering of AUX beam into the IFO was tweaked to maximize the beat. Johannes claims he saw -35 dBm on AS110 last week. But Jon reported a best effort of ~-60 dBm today. Not sure how to square that circle.
7. Once we were confident that the input of the AUX and PSL beams were well aligned, we decided to do a scan. PRC was chosen as PRMI can be locked but I don't yet know the correct settings for SRMI locking, and DRMI seemed too ambitious for daytime.
• PRMI was locked on carrier.
• Jon can comment more here, but the measurement with AM sidebands does not rely on any beatnote on the AS110 PD, it is just looking for coupling of the AM sideband into the IFO from the AS port at resonant frequencies of the PRC.
• For a coarse sweep, we swept from 1-60 MHz, 801 points, and the IF bandwidth was set at 30 kHz on the AG4395.
• Transfer function being measured was the ratio of AM signal detected at AS110 PD, to RF drive applied to the AOM driver.
• We were expecting to see dips separated by the PRC FSR (~25 MHz, since the PRC RT length is ~12.5m), when the AM sideband becomes resonant in the PRC.
• But we saw nothing. Need to think about if this is an SNR problem, or if we are overlooking something more fundamental in the measurement setup.

This measurement seems like a fine candidate to trial the idea of looking for the FSRs (and in general, cavity resonances) of the PRC in the phase of the measured TFs, rather than the amplitude.

13981   Mon Jun 18 14:32:42 2018 gautamUpdatePSLOptics on AS table

Yesterday, I moved the following optics:

1. Lens in front of AS110 PD.
2. BS splitting light between AS110 and AS55.

After moving these components around a bit, I locked them down once I was happy that the beam was pretty well centered on both of them, and also on AS110 and AS55 (measured using O'scope with single bounce from one ITM, other optics misaligned).

The beam was close to clipping on the lens mentioned in #1, probably because this wasn't checked when the 90-10 BS was installed for the AUX laser. Furthermore, I believe we are losing more than 10% of the light due to this BS. The ASDC (which is derived from AS55 PD) level is down at ~110cts as the Michelson is fringing, while it used to be ~200 cts. I will update with a power measurement shortly. But I think we should move ahead with the plan to combine the beam into the IFO's AS mode as discussed at the meeting last week.

Unrelated to this work, but c1psl and c1iscaux were keyed.

ASDC has something weird going on with it - my main goal yesterday was to calibrate the actuators of ITMX, ITMY and BS using the Michelson. But with the Michelson locked on a dark fringe, the ASDC level changed by up to 50 counts seemingly randomly (bright fringe was ~1000 cts, I had upped the whitening gain to +21dB), even though the CCD remained clearly dark throughout. Not sure if the problem is in the readout electronics or in the PD itself.

13984   Mon Jun 18 19:47:02 2018 gautamUpdateGeneralMICH actuator calibration

Summary:

The actuator (pendulum) gains for the Beam Splitter and the two ITMs were measured to be:

BS: 9.54 +/- 0.05 nm/ct [100 ohm series resistor in coil driver board]

ITMX: 2.44 +/- 0.01 nm/ct [400 ohm series resistor in coil driver board]

ITMY: 2.44 +/- 0.02 nm/ct [400 ohm series resistor in coil driver board]

Counts here refers to DAC counts at the output of the coil filter banks (as opposed to counts at the LSC servo output). The dominant (systematic) uncertainty (which isn't quoted here) in this measurement is the determination of the peak-to-peak swing of the dark port sensor, AS55_Q. I estimate this error to be ~1ct/33cts = 3%. These values are surprisingly consistent with one another once we take into account the series resistance.

Details:

The last time this was done, we used ASDC to do the measurement. But I don't know what signal conditioning ASDC undergoes (in PD or in readout electronics). In any case, in my early trials yesterday, ASDC was behaving unpredictably. So I decided to do redo the measurement.

[Attachment #1]- Flowchart describing the calibration procedure.

[Attachment #2] - AS55_Q output while the Michelson was freeswinging. I had first aligned the ITMs using ASS. The peak-to-peak value of this corresponds to $\lambda/4$. So we know AS55_Q in terms of cts/m of MICH displacement.

[Attachment #3] - Magnitudes of transfer function from moving one of the MICH optics, to the now calibrated AS55_Q. Fits are to a shape $a/f^2$, with $a$ being the fitted parameter. Coherence during the measurement is also plotted.

• Note that the excitation is applied to the channels C1:SUS-<optic>_LSC_EXC, for <optic> in [BS, ITMX, ITMY]. But since my de-whitening board re-work to remove the analog x3 gain, there is a digital x3 gain in the coil driver filter banks. So while the calibration numbers given above are accurate, be aware that when using them for sensing matrix measurements etc, you have to multiply these by x3.
• Furthermore, moving the BS by $x$ results in a Michelson length change of $\sqrt{2}x$, and this has been factored into the above number.

Next Steps:

1. Now that I have a calibration I trust more, re-analyze my DRMI sensing matrix data. Actually the sensing response numbers aren't significantly different from what I have been assuming. It's just that in terms of counts applied at the LSC input of a suspension, there is a digital x3 gain that has to be explicitly factored in.
2. Calibrate POX and POY by locking the arms and driving the now calibrated ITMs by a known number of counts.
3. Calibrate the ETMs, and MC1/MC2/MC3 by looking at calibrated POX/POY.
4. Lock DRMI, and calibrate SRM and PRM.

Reference:

Attachment 1: AS55cal_process.pdf
Attachment 2: AS55cal.pdf
Attachment 3: MICH_act_calib.pdf
13985   Tue Jun 19 00:19:00 2018 gautamUpdateASCPOP status check

Motivation:

1. I want to use the QPD at POP, calibrate it into physical units, and quantify the amount of angular jitter in the PRC (which I claim is what limits DRMI stability atm).
2. I want to revive the PRC angular feedforward to try and mitigate this a bit. But is feedforward even the best approach? Can we use feedback using the POP QPD?

POP QPD checkout:

• The POP QPD sits on the ITMX optical table.
• It is interfaced to the CDS system via an OT301 and then a Pentek whitening stage (z:p = 15:150).
• The OT301 claims to have a switchable offset nulling capability - but despite my best efforts tonight, I couldn't use the knobs on the front to null the offset (even with the PRC locked on carrier and a strong POP beam on the QPD).
•
• So I moved the QPD with the PRC locked, to center the CDS readback of the spot position at (0,0).
• Next step is to calibrate the POP QPD readback into physical units.
• I'm thinking of using the EricG diode laser for this purpose.
• I can calibrate counts to mm of displacement on the QPD active area.
• After which I can use the estimated position to PR2 (from which POP is extracted) to convert this to angular motion.
• I guess I should check for coherence between the POP QPD signal and all angular sensors of PRM/BS/MC1/MC2/MC3 to try and confirm the hypothesis that the folding mirrors are dominating the angular noise of the cavity. Unfortunately we don't have readbacks of the angular positions of TT1 and TT2.
• I moved the POP camera a bit in YAW so that the POP spot is now better centered on the CCD monitor.
• I also wanted to check the centering on the other POP QPD (POP22/POP110/POPDC?) but I think the POPDC signal, used for triggering the PRCL LSC servo, is derived from that PD, so everytime I blocked it, the lock was lost. Need to think of another strategy.
• MC3 has been rather glitchy tonight.
• So I will wait for a quieter time when I can collect some data to train the WF for angular FF.
13988   Tue Jun 19 23:27:27 2018 gautamUpdateSUSETMX coil driver work in AM tomorrow

Per discussion today eve, barring objections, I will do the following tomorrow morning:

1. Remove ETMX coil driver board from 1X9
• Change series resistances on the fast path to 2x4k in parallel. One will be snipped off once we are happy we can still lock.
• Thick film-->thin film for important components.
2. Remove ETMX de-whitening board from 1X9
• Remove x3 analog gain.
• Thick film-->thin film for important components.
13992   Thu Jun 21 00:14:01 2018 gautamUpdateSUSETMX coil driver out

I finished the re-soldering work today, and have measured the coil driver noise pre-Mods and post-Mods. Analysis tomorrow. I am holding off on re-installing the board tonight as it is likely we will have to tune all the loops to make them work with the reduced range. So ETMX will remain de-commissioned until tomorrow.

13993   Thu Jun 21 03:13:37 2018 gautamUpdateSUSETMX coil driver noise

I decided to take a quick look at the data. Changes made to the ETMX coil driver board:

1. Fast path series resistances: 400 ohm ---> 2.25 kOhm (= 2x 4.5 kohm in parallel). Measured (with DMM) resistance in all 5 paths varied by less than 3 ohms (~0.2%).
2. All thick film resistors in signal (fast and bias) paths changed to thin film.
3. AD797 ---> Op27 for monitor output.
4. Above-mentioned mon output (30Hz HPF-ed) routed to FP LEMO mon via 100ohm for diagnostic purposes.
5. 4x Trim-pots in analog path removed.

I also took the chance to check the integrity of the LM6321 ICs. In the past, a large DC offset on the output pin of these has been indicative of a faulty IC. But I checked all the ICs with a DMM, and saw no anomalies.

Measurement condition was that (i) the Fast input was terminated to ground via 50ohm, (ii) the Bias input was shorted to ground. SR785 was used with G=100 Busby preamp (in which Steve installed new batteries today, for someone had left it on for who knows how long) for making the measurement. The voltage measurement was made at the D-Sub connector on the front panel which would be connected to the Sat. Box, with the coil driver not connected to anything downstream.

Summary of results:

[Attachment #1] - Noise measurement out to 800 Hz. The noise only seems to agree with the LISO model above 300 Hz. Not sure if the low-frequency excess is real or a measurement artefact. Tomorrow, I plan to make an LPF pomona box to filter out the HF pickup and see if the low-frequency characteristics change at all. Need to think about what this corner freq. needs to be. In any case, such a device is probably required to do measurements inside the VEA.

[Attachment #2] - Noise measurement for full SR785 span. The 19.5 kHz harmonics are visible. I have a theory about the origin of these, need to do a couple of more tests to confirm and will make a separate log.

[Attachment #3] - zip of LISO file used for modeling coil driver. I don't have the ASCII art in this, so need to double check to make sure I haven't connected some wrong nodes, but I think it's correct.

Measurements seem to be consistent with LISO model predictions.

*Note: Curves labelled "LISO model ..." are really quad sum of liso pred + busby box noise.

My main finding tonight is: With the increased series resistance (400 ohm ---> 2.25 kohm), LISO modeling tells me that even though the series resistance (Johnson noise) used to dominate the voltage noise at the output to the OSEM, the voltage noise of the LT1125 in the bias path now dominates. Since we are planning to re-design the entire bias path anyways, I am not too worried about this for the moment.

I will upload more details + photos + data + schematic + LISO model breakdown tomorrow to a DCC page

gautam noon 21 June 2018: I was looking at the wrong LISO breakdown curves. So the input stage Op27 voltage noise used to dominate. Now the Bias path LT1125 voltage noise dominates. None of the conclusions are affected... I've uploaded the corrected plots and LISO file here now.

Attachment 1: ETMXsticthced.pdf
Attachment 2: ETMXFullSpan.pdf
Attachment 3: ETMXCoilDriver.fil.zip
13998   Thu Jun 21 15:32:05 2018 gautamUpdateElectronicsEX AA filter range change

[steve, gautam]

I took this opportunity of EX downtime to change the supply voltage for the AA unit (4-pin LEMO front panel) in 1X9 from +/-5V to +/-15V. Inside the AA board are INA134 and DRV135 ICs, which are rated to work at +/-18V. In the previous state, the inputs would saturate if driven with a 2.5Vpp sine wave from a DS345 func. gen. After the change, I was able to drive the full range of the DS345 (10Vpp), and there was no saturation seen. This AA chassis is only used for the OSEM signals and also some ALS signals. Shadow sensor levels and spectra are consistent before and after the change. The main motivation was to not saturate the Green PDH Reflection signal in the digital readout. The steps we took were:

1. Confirm (by disconnecting the power cable at the back of the AA box) that the power supplied was indeed +/- 5 V.
2. Remove DIN fuse blocks from DIN rail for the relevant blocks.
3. Identify a +15 V, -15 V and GND spot to plug the wires in.
4. Effect the swap.
5. Re-insert fuses, checked supply voltage at connector end of the cable was now +/- 15 V as expected.
6. Re-connect power cable to AA box.
13999   Thu Jun 21 18:25:57 2018 gautamUpdateSUSETMX coil driver re-installed

Initial tests look promising. Local damping works and I even locked the X arm using POX, although I did it in a fake way by simply inserting a x5.625 (=2.25 kohm / 400 ohm) gain in the coil driver filter banks. I will now tune the individual loop gains to account for the reduced actuation range.

Now I have changed the loop gains for local damping loops, Oplev loops, and POX locking loop to account for the reduced actuation range. The dither alignment servo (X arm ASS) has not been re-commissioned yet...

14000   Thu Jun 21 22:13:12 2018 gautamUpdateCDSpianosa upgrade

pianosa has been upgraded to SL7. I've made a controls user account, added it to sudoers, did the network config, and mounted /cvs/cds using /etc/fstab. Other capabilities are being slowly added, but it may be a while before this workstation has all the kinks ironed out. For now, I'm going to follow the instructions on this wiki to try and get the usual LSC stuff working.

14003   Fri Jun 22 00:59:43 2018 gautamUpdateCDSpianosa functional, but NO DTT

MEDM, EPICS and dataviewer seem to work, but diaggui still doesn't work (it doesn't work on Rossa either, same problem as reported here, does a fix exist?). So looks like only donatella can run diaggui for now. I had to disable the systemd firewall per the instructions page in order to get EPICS to work. Also, there is no MATLAB installed on this machine yet. sshd has been enabled.

14007   Fri Jun 22 15:13:47 2018 gautamUpdateCDSDTT working

Seems like DTT also works now. The trick seems to be to run sudo /usr/bin/diaggui instead of just diaggui. So this is indicative of some conflict between the yum installed gds and the relic gds from our shared drive. I also have to manually change the NDS settings each time, probably there's a way to set all of this up in a more smooth way but I don't know what it is. awggui still doesn't get the correct channels, not sure where I can change the settings to fix that.

Attachment 1: Screenshot_from_2018-06-22_15-12-37.png
14009   Fri Jun 22 18:30:21 2018 gautamUpdateSUSITMY_UL sensor

I think if the magnet fell off, we would see high DC signal, and not 0 as we do now. I suspect satellite box or PD readout board/cabling. I am looking into this, tester box is connected to ITMY sat. box for now. I will restore the suspension later in the evening.

Suspension has now been restored. With combination of multimeter, octopus cable and tester box, the problem is consistent with being in the readout board in 1X5/1X6 or the cable routing the signals there from the sat. box.

• Tester box hooked up to sat box ---> UL coil still shows 0 in CDS.
• Tester box hooked up to sat box ---> Mon D-sub on sat box shows expected voltages on DMM. So tester box LEDs are being powered and seem to work.
• Sat box re-connected to test mass ---> Mon D-sub on sat box shows expected voltages on DMM. So OSEM LEDs are being powered and seem to work.
• Sat box remains connected to TM ---> Front panel LEMO monitor points on readout board shows 0 for UL channel, other channels are okay.
 Quote: We may lost the UL magnet or LED

14012   Sun Jun 24 20:02:07 2018 gautamUpdateSUSSome notes about coil driver noise

Summary:

For a series resistance of 4.5 kohm, we are suffering from the noise-gain amplified voltage noise of the Op27 (2*3.2nV/rtHz), and the Johnson noise of the two 1 kohm input and feedback resistances. As a result, the current noise is ~2.7 pA/rtHz, instead of the 1.9 pA/rtHz we expect from just the Johnson noise of the series resistance. For the present EX coil driver configuration of 2.25 kohm, the Op27 voltage noise is actually the dominant noise source. Since we are modeling small amounts (<1dB) of measurable squeezing, such factors are important I think.

Details:

[Attachment #1] --- Sketch of the fast signal path in the coil driver board, with resistors labelled as in the following LISO model plots. Note that as long as the resistance of the coil itself << the series resistance of the coil driver fast and slow paths, we can just add their individual current noise contributions, hence why I have chosen to model only this section of the overall network.

[Attachment #2] --- Noise breakdown per LISO model with top 5 noises for choice of Rseries = 2.25 kohm. The Johnson noise contributions of Rin and Rf exactly overlap, making the color of the resulting line a bit confusing, due to the unfortunate order of the matplotlib default color cycler. I don't want to make a custom plot, so I am leaving it like this.

[Attachment #3] --- Noise breakdown per LISO model with top 5 noises for choice of Rseries = 4.5 kohm. Same comments about color of trace representing Johnson noise of Rin and Rf.

Possible mitigation strategies:

1. Use an OpAmp with lower voltage noise. I will look up some candidates. LT1028/LT1128? LISO library warns of a 400 kHz noise peak though...
2. Use lower Rin and Rf. The values of these are set by the current driving capability of the immediately preceeding stage, which is the output OpAmp of the De-Whitening board, which I believe is a TLE2027. These can source/sink 50 mA according to the datasheet . So for +/-10V, we could go to 400 ohm Ri and Rf, source/sink a maximum of 25mA, and reduce the Johnson noise contribution by 40%.

I've chosen to ignore the noise contribution of the high current buffer IC that is inside the feedback loop. Actually, it may be interesting to compare the noise measurements (on the electronics bench) of the circuit as drawn in Attachment #1, without and with the high current buffer, to see if there is any difference.

This study also informs about what level of electronics noise is tolerable from the De-Whitening stage (aim for ~factor of 5 below the Rseries Johnson noise).

Finally, in doing this model, I understand that the observation the voltage noise of the coil driver apparently decreased after increasing the series resistance, as reported in my previous elog. This is due to the network formed by the fast and slow paths (during the measurement, the series resistance in the slow path makes a voltage divider to ground), and is consistent with LISO modeling. If we really want to measure the noise of the fast path alone, we will have to isolate it by removing the series resistance of the slow bias path.

Comment about LISO breakdown plots: for the OpAmp noises, the index "0" corresponds to the Voltage noise, "1" and "2" correspond to the current noise from the "+" and "-" inputs of the OpAmp respectively. In future plots, I'll re-parse these...

 Quote: I will upload more details + photos + data + schematic + LISO model breakdown tomorrow to a DCC page.

Attachment 1: CoilDriverSchematic.pdf
Attachment 2: D010001_2k_fastOnly_2.25k.pdf
Attachment 3: D010001_4k_fastOnly_4.5k.pdf
14019   Tue Jun 26 16:28:00 2018 gautamUpdateSUSCoil driver protoboard characterization

I wanted to investigate my coil driver noise measurement technique under more controlled circumstances, so I spent yesterday setting up various configurations on a breadboard in the control room. The overall topology was as sketched in Attachment #1 of the previous elog, except for #4 below. Summary of configurations tried (series resistance was 4.5k ohm in all cases):

1. Op 27 with 1kohm input and feedback resistors.
2. LT1128 with 1kohm input and feedback resistors.
3. LT1128 with 400 ohm input and feedback resistors.
4. LT1128 with 400 ohm input and feedback resistors, and also the current buffer IC LM6321 implemented.

Attachments:

Attachment #1: Picture of the breadboard setup.

Attachment #2: Noise measurements (input shorted to ground) with 1 Hz linewidth from DC to 4 kHz.

Attachment #3: Noise measurements for full SR785 span.

Attachment #4: Apparent coupling due to PSRR.

Attachment #5: Comparison of low frequency noise with and without the LM6321 part of the fast DAC path implemented.

All SR785 measurements were made with input range fixed at -42dBVpk, input AC coupled and "Floating", with a Hanning window.

Conclusions:

• I get much better agreement between LISO and measurement at a few hundred Hz and below with this proto setup. So it would seem like the excess noise I measure at ~200 Hz in the Eurocrate card version of the coil driver could be real and not simply a measurement artefact.
• I am puzzled about the 10 Hz comb in all these measurements:
• I have seen this a few times before - e.g. elog13655.
• It is not due to the infamous GPIB issue - the lines persist even though I disconnect both power adaptor and GPIB prologix box from the SR785.
• It does not seem to be correlated with the position of the analyzer w.r.t. the DC power supply (Tektronix PS280) used to power the circuit (I moved the SR785 around 1m away from the supply).
• It persists with either of the two LN preamp boxes available.
• It persists with either "Float" or "Ground" input setting on the SR785.
• All this pointed to some other form of coupling - perhaps conductive EMI.
• The only clue I have is the apparent difference between the level of the coupling for Op27 and LT1128 - it is significantly lower for the latter compared to the former.
• I ruled out position on the breadboard: simply interchanging the Op27 and LT1128 positions on the breadboard, I saw higher 10 Hz harmonics for the Op27 compared to the LT1128. In fact, the coupling was higher for the DIP Op27 compared to an SOIC one I attached to the breadboard via an SOIC to DIP adapter (both were Op27-Gs, with spec'ed PSRR of 120 dB typ).
• To test the hypothesis, I compared the noise for the Op27 config, on the one hand with regulated (via D1000217) DC supply, and on the other, directly powered by the Tektronix supply. The latter configuration shows much higher coupling.
• I did have 0.1uF decoupling capacitors (I guess I should've used ceramic and not tantala) near the OpAmp power pins, and in fact, removing them had no effect on the level of this coupling
• As a quick check, I measured the spectrum of the DC power used to run the breadboard - it is supplied via D1000217. I used an RC network to block out the DC, but the measurement doesn't suggest a level of noise in the supply that could explain these peaks.
• The regulators are LM2941 and LM2991. They specify something like 0.03% of the output voltage as AC RMS, though I am not sure over what range of frequencies this is integrated over.
• But perhaps the effect is more subtle, some kind of downconversion of higher frequency noise, but isn't the decoupling cap supposed to protect against this?
• The 19.5 kHz harmonics seem to originate from the CRT display of the SR785 (SVGA).
• The manual doesn't specify the refresh rate, but from a bit of googling, it seems like this is a plausible number.
• The coupling seems to be radiative. The box housing the Busby preamp provides ~60dB attentuation of this signal, and the amplitude of the peaks is directly correlated to where I position the Busby box relative to the CRT screen.
• This problem can be avoided by placing the DUT and preamp sufficiently far from the SR785.

Punchlines:

1. The actual coildriver used, D010001, doesn't have a regulated power supply, it just draws the +/- 15V directly from Sorensens. I don't think this is good for low noise.
2. The LM6321 part of the circuit doesn't add any excess noise to the circuit, consistent with it being inside the unity gain feedback loop. In any case, with 4.5 kohm series resistance with the coil driver, we would be driving <2.5 mA of current, so perhaps we don't even need this?
Attachment 1: IMG_7060.JPG
Attachment 2: ETMXstitchced.pdf
Attachment 3: ETMXfullSpan.pdf
Attachment 4: PSRR.pdf
14024   Wed Jun 27 18:12:04 2018 gautamUpdateElectronicsCoil driver dewhitening

Summary:

I've been thinking about what we need to do to the de-whitening boards for the ITMs and ETMs, in order to have low noise actuators. Noting down what I have so far, so that people can comment / point out things I've overlooked.

Attachment #1: Block diagram schematic of the de-whitened signal path on D000183 as it currently exists. I've omitted the unity gain buffer stage at the output, though this is important for noise considerations.

Some considerations, in rough order of priority:

1. Why do we need de-whitening?
• Because we want the Johnson noise of the series resistor (4.5 kohm) in the coil driver path to dominate the current noise to the coils at ~200 Hz where we want to measure the squeezing.
2. What should the shape of this de-whitening filter be?
• The DAC noise was measured to be ~1 uV/rtHz at 200 Hz.
• The Johnson noise spectral density of 4.5 kohm at 300 K is ~9 nV/rtHz
• So we need ~60dB of attenuation at 200 Hz relative to DC. Currently, they have ~80dB of attenuation at 200 Hz.
• However, we also need to consider the control signal multiplied by the inverse of this shape in the digital domain (required for overall flat shape). This should not saturate the DAC range.
• Furthermore, we'd like for the shape to be such that we don't have a large transient when transitioning between high range and low noise modes. We should use the DARM control signal estimate to inform this choice.
3. What about the electronics noise of the de-whitening filter itself?
• This shows up at the input of the coil driver stage, and gets transmitted to the coil with unity gain.
• So we should aim for < 3nV/rtHz at 200 Hz, such that we are dominated by the Johnson noise of the 4.5 kohm series resistance [the excess will be 5%].
• This can be realized by using the passive network which is the final stage in the de-whitening (there is a unity gain output buffer stage implemented with LT1128, which we also have to account for).

I will experiment with a few different shapes and investigate noise and de-whitened digital signal levels based on these considerations. At the very least, I guess we should remove the x3 gain on the ETM boards, they have already been bypassed for the ITMs.

Attachment 1: DeWhiteningSketch.pdf
14027   Wed Jun 27 21:18:00 2018 gautamUpdateCDSLab maintenance scripts from NODUS---->MEGATRON

I moved the N2 check script and the disk usage checking script from the (sudo) crontab of nodus to the controls user crontab on megatron .

14032   Thu Jun 28 16:48:27 2018 gautamUpdateSUSSOS cage towers

For the upcoming vent, we'd like to rotate the SOS towers to correct for the large YAW bias voltages used for DC alignment of the ITMs and ETMs. We could then use a larger series resistance in the DC bias path, and hence, reduce the actuation noise on the TMs.

Today, I used the calibrated Oplev error signals to estimate what angular correction is needed. I disabled the Oplev loops, and drove a ~0.1 Hz sine wave to the EPICS channel for the DC yaw bias. Then I looked at the peak-to-peak Oplev error signal, which should be in urad, and calibrated the slider counts to urad of yaw alignment, since I know the pk-to-pk counts of the sine wave I was driving. With this calibration, I know how much DC Yaw actuation (in mrad) is being supplied by the DC bias. I also know the directions the ETMs need to be rotated, I want to double check the ITMs because of the multiple steering mirrors in vacuum for the Oplev path. I will post a marked up diagram later.

Steve is going to come up with a strategy to realize this rotation - we would like to rotate the tower through an axis passing through the CoM of the suspended optic in the vertical direction. I want to test out whatever approach we come up with on the spare cage before touching the actual towers.

Here are the numbers. I've not posted any error analysis, but the way I'm thinking about it, we'd do some in air locking so that we have the cavity axis as a reference and we'd use some fine alignment adjust (with the DC bias voltages at 0) until we are happy with the DC alignment. Then hopefully things change by so little during the pumpdown that we only need small corrections with the bias voltages.

SoS tower DC bias correction
Optic

EPICS excitation

[V pk-pk]

ETMX 0.06 110 1.83 -5.5305 -10.14
ITMX 0.02 180 9 -1.4500 -13.05
ITMY 0.02 120 6 -0.3546 -2.13
ETMY 0.06 118 1.97 0.5532 1.09

Some remarks:

1. Why the apparent difference between ITMs and ETMs? I think it's because the bias path resistors are 400 ohms on the ETMs, but 100 ohms on the ITMs
2. If we want the series resistance for the bias path to be 10 kohm, we'd only have ~800 urad actuation (for +10V DC), so this would be an ambitious level of accuracy.
14038   Thu Jul 5 10:15:30 2018 gautamUpdateSUSPRM watchdog tripped

PRM watchdog was tripped around 7:15am PT today morning. I restored it.

Attachment 1: PRM_watchdogTrip.png
14055   Thu Jul 12 11:13:39 2018 gautamUpdateGeneralOMC revival

Aaron and I are going to do the checkout of the OMC electronics outside vacuum today. At some point, we will also want to run a c1omc model to integrate with rtcds. Barring objections, I will set up this model on one of the spare cores on the physical machine c1ioo tomorrow.

14061   Thu Jul 12 23:59:14 2018 gautamUpdateGeneralVent objectives and prep

Vent objectives:

1. Install radiative heater setup in EY chamber.
2. Re-direct 50% of AS beam to OMC
• First, we need to check if the OMC trans PDs work. Else, we have to consider using some in-air PDs for the transmon.
• Check that OMC length PZT works.
• Check that OMC steering PZTs work (Koji and I have used this in 2016 to check AS beam clipping so they should work).

We only anticipate opening up the IOO chamber and the EY chamber.

Vent preparation: see here.

14063   Fri Jul 13 02:52:11 2018 gautamUpdateGeneralVent objectives and prep

[KA, GV]

1. Arm scan setup moved from West side of PSL table to North side of AP table
• Marconi is now providing the LO for the loop. A ~5m 50ohm BNC cable needs to be laid out from the PLL area to the NW corner of the AP table where the Agilent is for the TF measurement scheme which allows phase discrimination.
• We took this opportunity to characterize/improve the setup a bit, and also clean up the 10s of cables around the PSL table. There were some Video cables (75ohm instead of 50ohm ) that were part of the scanning setup which we excised.
• Mode matching onto beat PD on PSL table was improved - beat signal Vpp increased by factor of 2. PLL gain was adjusted accordingly.
• AUX power @AP table ~37mW (before recombination BS), ~3.7mW onto SRM, ~200uW onto ITMY.
• We got a beatnote in transmission of ~120uV (rms?) after optimizing alignment into Y arm cavity with the AUX frequency on an arm FSR.
• From Sandrine's calculations, I expected ~20mV of beat signal. We leave it to Annalisa and Terra to square that circle. Probably the MM into the arm isn't stellar either, and we didn't check the polarization of the aux beam (that it is matched to the IFO's p-pol).
• The entire AUX injection chain needs careful characterization before
2. Vent prep
• Both arms were locked to IR, TRY maximized using ASS, TRX maximized by hand.
• GTRY and GTRX were also maximized.
• All test mass/PRM/SRM oplevs were centered with this "good" alignment.
• PSL power into the IMC was cut from 1.07 W (measured after G&H mirror) to 97 mW, by rotating the waveplate immediately after the PSL (original angle 180deg, new angle 216 degrees).
• PMC was locked. I did not need to change any of the gain settings.
• 2" R=10% BS in the IMC REFL path was replaced with a Y2, so there is no MCREFL till we turn the power back up.
• IMC was locked. I touched up my IMC low power autolocker, but this probably needs a bit more touching up tomorrow. MC has remained locked at low power for ~25mins, but as I typed this, I jinxed it and it lost the lock. anyway we have good alignment references.
• PSL shutter will remain closed.

@SV, we are ready to vent tomorrow. Aaron is supposed to show up ~830am to assist.

Attachment 1: preVentStatus.png
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