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  10971   Wed Feb 4 04:51:14 2015 diegoUpdateLSCCARM Transition to REFL11 using CM_SLOW Path

[Diego, Jenne, Eric]

Tonight we kept on following our current strategy for locking the PRFPMI:

  • the first few tries were pretty unsuccessful: the PRMI lock wasn't much stable, and we never managed to reduce CARM offset to zero before losing lock;
  • then we did some usual manteinance: we fixed the X arm green beatnote, fixed the phase tracker and given much attention to ASS alignment, since the X arm wasn't doing great;
  • the last few locks were consintently better: we managed to get to CARM offset zero "easily", but the arm power was not very high (~8);
  • then we tried to transition CARM to REFL11, both with the usual configuration and using CM_SLOW, using REFL11 as input for the Common Mode Board;
    • with the usual configuration, we lost lock right after the transition, because of MICH hitting the rail;
    • we did a very smooth CARM transition directly to REFL11 on the CM_SLOW path; we managed to take a spectrum with the SR785, but we couldn't take any more measurements before losing lock because of some weird glitch, as we can see from the lockloss plot;
  • another thing that helped tonight was changing the ELP of the MICH filter bank: it went from 4th order to 6th order, and from 40 dB suppression to 60 dB suppression;

both of the last two locks, the most stable ones (one transition to usual REFL11 and one transition to "CM_SLOW" REFL11) were acquired actuating on MC2;

 


EDITs by JCD:  At least one of the times that we lost PRMI lock (although kept CARM and DARM lock on ALS), was due to MICH hitting the rail, even after we increased the limiter to 15,000 counts.


 Here is the transfer function between CARM ALS (CARM_IN1) and REFL11 coming through the CM board (CARM_B), just before we transitioned over.  Coherence was taken simultaneously as usual, I just printed it to another sheet.

CARM_3Feb2015_CarmBwasCMslow_CarmAwasLiveALS.pdf

CARM_3Feb2015_CarmBwasCMslow_CarmAwasLiveALS_Coh.pdf


Here is the lockloss plot for the very last lockloss.  This is the time that we were sitting on REFL11 coming through the CM_SLOW path.  A DTT transfer function measurement was in progress (you can see the sine wave in the CARM input and output data), but I think we actually lost lock due to whatever this glitch was near the right side of the plots.  This isn't something that I've seen in our lockloss plots before.  I'm not sure if it's coming from REFL11, or the CM board, or something else.  We know that the CM board gives glitches when we are changing gain settings, but that was not happening at this time.


Q: Here's the SR785 TF of CARM locked through CM board, but still only digital control; nothing exciting. Excitation amplitude was only 1mV, which explains the noisy profile. 

  10979   Thu Feb 5 04:35:14 2015 diegoUpdateLSCCARM Transition to REFL11 using CM_SLOW Path

[Diego, Eric]

Tonight was a sad night... We continued to pursue our strategy, but with very poor results:

  • before doing anything, we made sure we had a good initial configuration: we renormalized the arm powers, retuned the X arm green beatnote, did extensive ASS alignment;
  • since the beginning of the night we faced a very uncooperative PRMI, which caused a huge number of locklosses, often just by itself, without even managing to reduce the MICH offset before reducing the CARM one;
  • we had to reduce the PRCL gain to -0.002 in order to acquire PRMI lock, but keeping it such or restoring it to -0.004 once lock was acquired either didn't improve the PRMI stability at all;
  • we also tweaked a bit the PRCL and MICH UGF servos (namely, their frequencies to ~80 Hz and ~40 Hz respectively) and that seemed to help earlier during the night, but not much longer;
  • we only managed to transition CARM to REFL11 via CM SLOW twice;
    • the first time we lost lock almost immediately, probably because of a non-optimal offset between CARM A and B;
    • the second time we managed to stay there a little longer, but then some spike in the PRCL loop and/or the MICH loop hitting the rails threw us out of lock (see the lockloss plot);
    • both times we transitioned at arm power ~18;
  • during the night we used an increased analog ASDC whitening gain, as from Eric's elog here http://nodus.ligo.caltech.edu:8080/40m/10972 ; even with this fix, though, MICH is still often hitting the rails and causing the lock losses;
  • the conclusion for tonight is that we need to figure what is going on with the PRMI...

 

  10982   Fri Feb 6 03:21:17 2015 diegoUpdateLSCCARM Transition to REFL11 using CM_SLOW Path

[Diego, Jenne]

We kept struggling with the PRMI, although it was a little better than yesterday:

  • we retuned the X Green beatnote;
  • we managed to reach lower CARM offsets than yesterday night, but we still can't keep lock long enough to perform a smooth transition to CM SLOW/REFL11;
  • we tweaked MICH a bit:
    • the ELP in FM8 now is always on, because it seems to help;
    • we tried using a new FM1 1,1:0,0 instead of FM2 1:0 because we felt we needed a little more gain at low frequencies, but unfortunately this didn't change much MICH's behaviour;
    • now, after catching PRMI lock, the MICH limiter is raised to 30k (in the script), as a possible solution for the railing problem; the down/relock scripts take care of resetting it to 10k while not locked/locking;

So, still no exciting news, but PRMI lock seems to be improving a little.

  10990   Mon Feb 9 17:23:17 2015 diegoUpdateComputer Scripts / ProgramsNew laptops

I forgot to elog about these ones, my bad... The new/updated laptops are giada, viviana and paola; paola is already in the lab, while giada and viviana are in the control room waiting for a new home. The Pool of Names Wiki page has already been updated to reflect the changes.

  10991   Mon Feb 9 17:47:17 2015 diegoUpdateLSCCM servo & AO path status

I wrote the script with the recipe we used, using the Yarm and AS55 on the IN2 of the CM board; however, the steps where the offset should be reduced are not completely deterministic, as we saw that the initial offset (and, therefore, the following ones) could change because of different states we were in. In the script I tried to "servo" the offset using C1:LSC-POY11_I_MON as the reference, but in the comments I wrote the actual values we used during our best test; the main points of the recipe are:

  • misalign the Xarm and the recycling mirrors;
  • setting up CARM_B for POY11 locking and enabling it;
  • setting up CARM_A for CM_SLOW;
  • setting up the CM_SLOW filter bank, with only FM1 and FM4 enabled;
  • setting up the CARM filter bank: FM1 FM2 FM6 triggered, only FM3 and FM5 on; usual CARM gain = 0.006;
  • setting up CARM actuating on MC2;
  • turn off the violin filter FM6 for MC2;
  • setting up the default configuration for the Common Mode Servo and the Mode Cleaner Servo; along with all the initial parameters, here is where the initial offset is set;
  • turn on the CARM output and, then, enable LSC mode;
  • wait until usual POY11 lock is acquired and, a bit later, transition from CARM_B to CARM_A;
  • then, the actual CM_SLOW recipe:
    • CM_AO_GAIN = 6 dB;
    • SUS-MC2_LSC FM6 on (the 300:80 filter);
    • CM_REFL2_GAIN = 18 dB;
    • servo CM_REFL_OFFSET;
    • CM_AO_GAIN = 9 dB;
    • CM_REFL2_GAIN = 21 dB;
    • servo CM_REFL_OFFSET;
    • CM_REFL2_GAIN = 24 dB;
    • servo CM_REFL_OFFSET;
    • CM_REFL2_GAIN = 27 dB;
    • servo CM_REFL_OFFSET;
    • CM_REFL2_GAIN = 31 dB;
    • servo CM_REFL_OFFSET;
    • CM_AO_GAIN = 6 dB;
    • SUS-MC2_LSC FM7 on (the :300 compensating filter);

I tried the procedure and it seems fine, as it did during the tries Q and I made; however, since it touches many things in many places, one should be careful about which state the IFO is into, before trying it.

The script is in scripts/CM/CM_Servo_OneArm_CARM_ON.py and in the SVN.

 

  17796   Fri Aug 18 16:07:38 2023 devenUpdatePEMSeismometer heater and temp sensors

I've turned off the power supply. I've attached a picture of the rack with the switch that I flipped circled

  9715   Tue Mar 11 15:14:34 2014 denSummaryLSCComposite Error Signal for ARms (1)

Quote:

The composite error signal


 

 Very nice error signal. Still, I think we need to take into account the frequency shape of the transfer function TR -> CARM. 

  9967   Sat May 17 14:48:06 2014 denUpdatePEMyend sei isolation kit is set

Yend seismometer isolation kit (elog 8461) hosts Guralp seismometer. I made a cable for inside connection, assembled the kit and relocated the instrument from its previous position at the yend inside the kit.

Seismometer is connected to the readout box and running.

IMG_1405.JPG    IMG_1406.JPG

  9968   Sun May 18 14:36:04 2014 denUpdateLSCoffsets in 3f and drmi stable lock on 1f

Eric, Den

We noticed that PRMI RIN is high when the cavity is locked on RELF33 I&Q signals. We compared the level of power fluctuations when PRMI was locked using REFL11, REFL55 and REFL 33. Attached plot "prmi_rin" shows the spectra.

Then we excited PRM and measured length to RIN coupling when PRMI was locked on REFL33 I&Q. DC offset of PRCL is only 3%. But MICH offset seems to be ~nm. When we gave offset of -15 cnts to the servo, power fluctuations improved by a factor of few.

Then we looked at DRMI. It seems that SRC macroscopic length is off but we still could lock it stably. To account for macroscopic length detuning we had to rotate REFL55 phase from 25 degrees to 50 degrees. Power at AS port increased by factor of ~2 compared to PRMI configuration. SPOP18 is decreased only by 30%. Attached plot "drmi_power" shows POP18, POP90, POPDC and ASDC in PRMI and DRMI configurations.

Plot "src_ol" shows srcl OL transfer function. UGF is 70 Hz. We have also centered SRM OL and copied the servo filters from PRM, gains are set to keep UGF at ~0.1 Hz and 7 Hz

This is a more detailed procedure:

1. Phase: REFL11: 19 degree, REFL55: 50 degrees (25 degrees for PRMI configuration)

2. Input matrix:

PRCL   0.15 0 0 REFL11I
MICH = 0 0.15 0 REFL55Q
SRCL   -0.09 0 1 REFL55I

3. Servo parameters:

PRCL: gain = -0.02, FM4,5 + trigger FM2,3,6,9

MICH: gain = 0.8, FM4,5 + trigger FM2

SRCL: gain = 0.25, FM4,5 + trigger FM2,3

4. Triggering:

signal is SPOP22 , levels 40:25

  9971   Mon May 19 22:44:21 2014 denUpdatePEMxend sei isolation kit is set

Quote:

Yend seismometer isolation kit (elog 8461) hosts Guralp seismometer. I made a cable for inside connection, assembled the kit and relocated the instrument from its previous position at the yend inside the kit.

Seismometer is connected to the readout box and running.

    

 Xend internal cabling and external connector is ready. We are waiting for seismometer from Gyro lab. We still need to fix the pot with clamps after we put the instrument in.

We also need a long cable from Xend to the guralp readout box.

  10032   Thu Jun 12 12:30:50 2014 denFrogsGeneralWorld Cup Soccer 2014

Quote:

 

 world-cup-2014-mascots.jpg

  11177   Fri Mar 27 04:36:46 2015 denUpdateLSCals->pdh transition, prcl on 1f, alignment

Tonight I have modified transition steps from als to pdh signals. I have added 1:20 filters to CARM_A and DARM_A filter banks to make them unconditionally stable. These filters made locking more robust -- duty cycle is was ~70% tonight. I have also modified slow/ao crossover to avoid ringing up of lines above 1kHz.

Once AO is engaged with high bandwidth, REFL55 signal looks good and I transition PRCL from 165I to 55I. Optical gain compared to PRMI reduced from 55I/165I = -330 down to 55I/165I = 30 in full lock.

I worked on alignment of ETMs. Looking on the cameras I could improve arm power up to 160 and ifo visibility was 80%. POP22 fluctuated by ~50% and every few minutes we loose lock because POP22 almost touches zero.

  11181   Sat Mar 28 03:21:49 2015 denUpdateLSCtowards angular ff

Tonight I measured seismic noise coupling to beam spot on PR2. There is coherence of 0.9 from X to PIT and Y to YAW around the stack resonances. TF was fited using vectfit and put into static matrix of oaf in the elements T240X -> PRM PIT, T240Y -> PRM YAW. I think we should actuate on the error point of the PRM OL but I decided not to go for a model change tonight. Data from seismometers and POP QPD was obtained during the UTC time 04:06:00 - 04:50:00 when PRMI was locked on sideband

Interferometer was locking rather robustly and every lock lasted on the everage of 3 minutes. During these lock periods I incresed bandwidth of optical lever servos of BS and test masses from 4Hz up to 10Hz and then closed transmission QPD loops. It seems from the camera that lock losses correspond to strong motion of the beam on pop camera. Scripts that change OPLEV bandwidth are in /users/den "increase_ol_bandwidth.sh" "decrease_ol_bandwidth.sh". Script "engage_qpd_servos" turns off ETM oplevs and turns on ETM -> trans QPD servos. These scripts can be copied to locking directrly if are useful.

Please, note that transition from 3f to 1f should still be tuned. Only PRCL was stably controlled using 1f so far

  11109   Fri Mar 6 13:48:17 2015 dark kiwamuSummaryIOOtriple resonance circuit

I was asked by Koji to point out where a schematic of the triple resonant circuit is.
It seems that I had posted a schematic of what currently is installed (see elog 4562 from almost 4 yrs ago!).

(Some transfomer story)
Then I immediately noticed that it did not show two components which were wideband RF transformers. In order to get an effective turns ratio of 1:9.8 (as indicated in the schematic) from a CoilCrfat's transformer kit in the electronics table, I had put two more transformers in series to a PWB1040L which is shown in the schematic. If I am not mistaken, this PWB1040L must be followed by a PWB1015L and PWB-16-AL in the order from the input side to the EOM side. This gives an impedance ratio of 96 or an effective turns ratio of sqrt(96) = 9.8.

(An upgrade plan document)

Also, if one wants to review and/or upgrade the circuit, this document may be helpful:
https://wiki-40m.ligo.caltech.edu/Electronics/Multi_Resonant_EOM?action=AttachFile&do=get&target=design_EOM.pdf
This is a document that I wrote some time ago describing how I wanted to make the circuit better. Apparently I did not get a chance to do it.

  2709   Wed Mar 24 12:40:25 2010 daisukeConfigurationGeneralPeriscope for green laser delivery from the BSC to PSL table

The periscope design for beam elevation of the green beams is posted. The design for the 90 deg steering version is also coming.

(2010-03-29: update drawings by daisuke)

90deg version: http://nodus.ligo.caltech.edu:8080/40m/2725

40m_periscope.png

  2725   Mon Mar 29 01:45:26 2010 daisukeConfigurationGeneralPeriscope version B for green laser ...

Here the design of the periscope for the 90 deg steering version is posted.

straight version http://nodus.ligo.caltech.edu:8080/40m/2709

  48   Thu Nov 1 16:51:33 2007 d40AoGGeneralD40
If you vant see D40 againn, you leave one plate goulash by N2 tank in morning.

Vit the good paprikash this time!!!
  14435   Tue Feb 5 10:22:03 2019 chubUpdate oil added to RP-1 & 3

I added lubricating oil to roughing pumps RP1 and RP3 yesterday and this morning.  Also, I found a nearly full 5 gallon jug of grade 19 oil in the lab.  This should set us up for quite a while.  If you need to add oil the the roughing pumps, use the oil in the quart bottle in the flammables cabinet.  It is labeled as Leybold HE-175 Vacuum Pump Oil.  This bottle is small enough to fill the pumps in close quarters.

  3308   Wed Jul 28 12:53:32 2010 channaUpdateComputersnds data listener

For the sake of writing it down: /cvs/cds/caltech/apps/linux64/rockNDS

  3310   Wed Jul 28 14:34:29 2010 channaUpdateComputersinstallation on allegra

I have done the following on allegra and rosalba:

[root@allegra caltech]# yum install glade2

On rosalba the matplotlib was out of date with respect to allegra.  I have no idea how the version 0.98 on allegra got there, but I left it.  However I updated rosalba to the epel version

  1 yum remove python-numpy
  2 yum install python-matplotlib numpy scipy --enablerepo=epel --disablerepo=rpmforge

 

This is all to support the LIGO data listener which now has a shortcut on rosalba and allegra's desktop.  It seems to work for (live mode) right now.
 

 

  1102   Thu Oct 30 20:39:47 2008 carynConfigurationPEMtemperature sensor
We attached the temperature sensor box to the MC1/MC3 chamber with a C-clamp. We connected the temp sensor to a 2nd box with a short BNC. Bob set up a power cable coming from the X-end towards the MC1/MC3 chamber(Thanks, Bob!) We soldered the end of Bob's power cable to a plug and attached it to the 2nd box (The power supply enters through the 2nd box). A ~20ft BNC cable connects the output signal of the 2nd box to the tall thing by the PSL where all the signals go labeled 1Y2. Once we had everything connected, we put in the fuses for the power supply. So, now the temperature sensor is receiving power. We checked that the power supply was working (we measured +15.08V and -14.95V, and we wanted 15V and -15V so it's OK for now). Tomorrow we will modify C1IOOF.INI file and reboot the frame builder.

About sensor-
There is an LM34 (looks like a transistor) glued w/ epoxy and thermal paste to the inside of a Pomona box ~1"x"1.5"x2". The lid to the box is covered with a 1-2mm thick piece of copper and a little thermal paste is sandwiched between the Pomona lid and the copper piece. A C-clamp attaches the copper piece to the chamber. A BNC is connected to one side of the box (the side with less copper)

About power supply box-
There is a power regulator and an op-amp inside a Pomona box ~2.5"x4"x2". The power regulator is attached to the center of lid of the pomona box with a screw and washer. There's a power plug on the front of the box
Left:+15V:red wire
Center:GND:white wire
Right:-15V:black wire
There are 2 BNC connections on the sides of the box. The left BNC connection is for the output signal and the right BNC connection is for the temperature sensor (if the power plug is coming out of the box towards you).

Sensor location-
Chamber which contains MC1/MC3. On the door facing towards the Y-end. On the bottom-left side. Behind the door. Attached with a C-clamp.

Power supply box location-
Chamber which contains MC1/MC3. On some metal leg thing near the floor facing towards the Y-end. Attached with a zip-tie

Power supply-
Coming from the X-end from a tall thing with all the fuses labeled 1X1
Fuse 160:+15V:red wire
Fuse 171:GND:white wire
Fuse 172:-15V:black wire

Signal-
Going towards the PSL to the tall thing labeled 1Y1 on the rack labeled SN208
ICS-110B
J12 (which we believe corresponds to 50-51 and channel number 13650)
Temperature sensor is connected to J12 with a ~20ft BNC attached to a BNC2LEMO connector we found lying around
  1176   Thu Dec 4 17:42:23 2008 carynUpdateIOOdrum modes observable without excitation
So, the mode cleaner was evidently aligned better and now the drum modes are observable using DTT.
The Lock-In was set to 27.8kHz and the drum mode frequencies were previously observed to be 28.039kHz(MC2), 28.222kHz(MC3) and 28.221kHz(MC1). So, we might expect peaks at ~239Hz,421Hz,422Hz.
Peaks have been observed around the expected frequencies in channel IOO-MC-DRUM1.
Note that it is possible to resolve the separate MC1 and MC3 peaks which are so close together.
(sorry these are pdf's and not png's)
  1185   Mon Dec 8 00:10:42 2008 carynSummaryGeneralcalibrating the jenne laser
I apologize in advance for the long list of numbers in the attachment. I can't seem to make them hide for some reason.

So, since Jenne's laser will probably be used for the Stoch mon calibration, Alberto and I took some measurements to calibrate Jenne's laser.
We focused the beam onto the New Focus RF 1GHz photodetector that we stole from rana's lab (powered with NewFocus power 0901). Measured the DC output of the photodetector with scope. Aligned the beam so DC went up (also tried modulating laser at 33MHz and aligning so 33MHz peak went up). Hooked up the 4395a Spectrum/Network Analyzer to the laser and to the AC out of the photodetector (after calibrating Network analyzer with the cables) so that the frequency response of the laser*photodetector could be measured.
(Note: for a while, we were using a splitter, but for the measurements here, I got rid of the splitter and just sent the RFout through the cables to channel A for the calibration, sent RFout to the laser and photodetector to channel A for the measurement)

Measured the frequency response. At first, we got this weird thing with a dip around 290MHz (see jcal_dip_2_norm.png below).
After much fiddling, it appeared that the dip was from the laser itself. And if you pull up just right on the corner of this little metal flap on the laser (see picture), then the dip in the frequency response seems to go away and the frequency response is pretty flat(see jcal_flat_3_norm below). If you press down on the flap, the dip returns. This at least happened a couple of times.
Note that despite dividing the magnitude by the DC, the frequency responses don't all line up. I'm not sure why. In some cases the DC was drifting a bit(I presume the laser was coming out of alignment or decided to align itself better) and maybe with avgfactor=16, and measuring mean DC on the scope, it made the DC meas not match up the the frequ resp meas...
I've attached the data for the measurements made (I'm so sorry for all the #'s. I can't figure out how to hide them)
name/lasercurrent/DC/analyzer SourcePower/analyzer avgfactor
jcal7_1/I=31.7mA/DC=-4.41/SourcePower=0dBm/avgfactor=16
jcal7_2/I=31.7mA/DC=-1.56/SourcePower=0dBm/avgfactor=none
jcal8_1/I=31.7mA/DC=-4.58/SourcePower=0dBm/avgfactor=16
jcal8_2/I=31.7mA/DC=-2.02/SourcePower=0dBm/avgfactor=16
jcal8_3/I=31.7mA/DC=-3.37/SourcePower=0dBm/avgfactor=16
Note also that the data from the 4395a seems to have column1-frequency, column2-real part, column3-imaginary part...I think. So, to calculate the magnitude, I just took (column2)^2+(column3)^2.


To get sort of an upper-bound on the DC, I measured how DCmax varied with laser current, where DCmax is the DC for the best alignment I could get. After setting the current, the laser was modulated at 33MHz and the beam was aligned such that the 33MHz peak in the photodetector output was as tall as I could manage. Then DC was measured. See IvsDCmax.png. Note the DC is negative. I don't know why.

Also, the TV's don't look normal, the alarm's going off and I don't think the mode cleaner's locked.
  1246   Thu Jan 22 14:38:41 2009 carynDAQPSLMC temperature sensor

Quote:

Quote:
I added a channel for the temperature sensor on the MC1/MC3 chamber: C1:PSL-MC_TEMP_SEN.
To do that I had to reboot the frame builder. The slow servo of the FSS had to get restarted, the reference cavity locked and so the PMC and MZ.


Where is this channel?


That's not the name of the channel anymore. The channel name is PEM-MC1_TEMPS. It's written in a later entry.
  1290   Wed Feb 11 00:50:24 2009 carynUpdateGeneralants?

So, near 2 of the trashcans in the control room and underneath a desk there are hundrends of ants. Is this normal?

  1331   Sun Feb 22 23:43:07 2009 carynSummaryGeneraltemperature sensor

Comparing  PSL-FSS-RMTEMP and PEM-MC1-TEMPS

So, to compare temp channels, I made a plot of PSL-FSS_RMTEMP and PEM-MC1_TEMPS(the test temp sensor channel after converting from cts to degC). This plot begins about 2 months ago t_initial=911805130. The temperature channels look kinda similar but MC1-TEMPS (the temp sensor clamped to MC1,3 chamber) is consistently higher in temperature than FSS_RMTEMP. See compare_temperature_channels.png.

MC1-TEMPS isn't exactly consistent with FSS-RMTEMP. I attached a few plots where I've zoomed in on a few hours or a few days. See compare_temperature_channels_zoom1.pdf & compare_temperature_channels_zoom2.pdf

Change the room temperature, see what happens to the chamber temperature

A while ago, somebody was fiddling around with the room temperature.  See compare_temperature_channels_zoom4.pdf.  This is a plot of PEM-MC1_TEMPS and PSL-FSS_RMTEMP at t0=911805130. You can see the chamber heating up and cooling down in happy-capacitory-fashion. Although, the PSL-FSS_RMTEMP and the PEM-MC1_TEMPS don't really line up so well. Maybe, the air in the location of the MC1,3 chamber is just warmer than the air in the PSL or maybe there's an offset in my calibration equation.

Calibration equation for PEM-MC1-TEMPS

For the calibration (cts to degC) I used the following equation based on the data-sheet for the LM34 and some measurements of the circuit:

TEMPERATURE[degC]=5/9*(((-CTS/16384/451.9/1.04094)-(.0499*10^-3))/(20*10^-6)-35);

How does the chamber temperature compare with the air temperature?

It looks like the chamber may be warmer than the air around it sometimes.

I wanted to check the temperature of the air and compare it with the temperature the sensor had been measuring. So, at t=918855087 gps, I took the temp sensor off of the mc1-mc3 chamber and let it hang freely, close to the chamber but not touching anything. See compare_temperature_chamber_air.png. MC1_TEMPS increases in temperature when I am handling the temp-sensor and then cools down to below the chamber temperature, close to FSS_RMTEMP, indicating the air temperature was less than the chamber temperature.

 When, I reattached temp sensor to the chamber at t=919011131 gps, the the temperature of the chamber was again higher than the temperature of the air. See compare_temperature_air2chamber.pdf.

Also, as one might expect, when the temp-sensor is clamped to the chamber, the temperature varies less, & when it's detached from the chamber, the temperature varies more. See compare_temperature_air_1day.pdf & compare_temperature_chamber_1day.pdf.

New temp-sensor power supply vs old temp-sensor power supply

The new temp-sensor is less noisy and seems to work OK. It's not completely consistent with PSL-FSS_RMTEMP, but neither was the old temp-sensor. And even the air just outside the chamber isn't the same temperature as the chamber. So, the channels shouldn't line up perfectly anyways.

I unplugged the 'old' temp-sensor power supply for a few hours and plugged in the 'new' one, which doesn't have a box but has some capacitors and and 2 more voltage regulators. The MC1_TEMPS channel became less noisy. See noisetime.png & noisefreq.pdf. For that time, the minute trend shows that with the old temp-sensor power supply the temp sensor varies +/-30cts and with the new power supply, it is more like +/-5cts (and Volt/16,384cts * 1degF/10mV -->  apprx +/-0.03degF). So, it's less noisy. 

I kept the new temp-sensor power supply plugged in for about 8 hours, checking if new temp sensor power supply worked ok. Compared it with PSL-FSS_RMTEMP after applying an approximate calibration equation. See ver2_mc1_rmtemp_8hr_appxcal.png.

Just for kicks

Measuring time constant of temp sensor when detached from chamber. At 918858981, I heated up the temp sensor on of the mc1-mc3 chamber with my hand. Took hand off sensor at  918859253 and let it cool down to the room temperature. See temperature_sensor_tau.pdf. 

  1540   Sat May 2 16:34:31 2009 carynDAQPEMGuralp channels plugged back in

I plugged the Guralp cables back into the PEM ADCU

       Guralp NS1b ---> #11

       Guralp Vert1b --->#10

       Guralp EW1b --->#12

  1546   Tue May 5 09:22:46 2009 carynUpdatePEMzeros

For several of the channels on the PEM ADCU, zeros are occuring at the same time. Does anyone know why that might happen or how to fix it?

  1571   Sun May 10 13:34:32 2009 carynUpdatePEMUnplugged Guralp channels

I unplugged Guralp EW1b and Guralp Vert1b and plugged in temp sensors temporarily. Guralp NS1b is still plugged in.

  1599   Mon May 18 10:06:56 2009 carynUpdatePEMTemp sensor

Quote:
To see if Caryn's data dropouts were happening, I looked at a trend of all of our temperature channels. Looks OK now.

Although you can't see it because I zoomed in, there's a ~24 hour relaxation happening before Caryn's sensors equilibrate.
I guess that's the insulating action of the cooler? We need a picture of the cooler in the elog for posterity.[/quote


Dropouts can't been seen with a minute trend, only a second trend. No big deal, but they are still occurring. See plot below.

The 24hr relaxation period is due to the cooler and some metal blocks that were cooled in the freezer and then put in the cooler to see if the relationship between the temp sensors changed with temperature. The relationship is not linear, which probably means there is some non-linearity in each temperature sensor's relationship to temperature. So, when calibrating them with Bob's temp sensor, more than 2 data points need to be collected.

Picture of cooler for posterity is attached
  1624   Mon May 25 21:31:47 2009 carynUpdatePEMplugged in Guralp channels

Guralp Vert1b and Guralp EW1b are plugged back in to PEM ADCU #10 and #12 respectively. Guralp NS1b remains plugged in. So,  PEM-SEIS_MC1_X,Y,Z should now corrsp to seismometer as before.

  1647   Wed Jun 3 11:28:01 2009 carynUpdatePEMUnplugged Guralp channels
  1648   Wed Jun 3 12:31:13 2009 carynUpdatePEMplugged in guralp channels
  13934   Fri Jun 8 14:40:55 2018 c1lscUpdateCDSi am dead
  12385   Tue Aug 9 13:53:57 2016 babbottUpdateSEIlong Guralp EX cable repaired on the D-sub side

I checked out the cable that I took from you, and all of the connections looked right.  The only thing I did notice was that some of the soldered wires on the 37-pin connector had gotten hot enough to melt their insulation, and potentially short together.  I cut off that connector, and left it on your desk to check out.  I put on a new connector, and checked the pinout.  If the Guralps still doesn't work, we'll have to check out other possibilities.

  12628   Sun Nov 20 23:53:38 2016 awadeUpdatePSLFSS Slow control -> Python, WFS re-engaged

I made a very slighly updated version of Yinzi's script that pulls the channel names and actuator hardstop limits from an external .ini config file. The idea was to avoid having as many versions of the script as there are implimentations of it. Seems like slighly better practice, but maybe I'm wrong. The config files are also easier to read. Its posted on the elog (PSL:1758) with lastest on the 40mSVN .../trunk/CTNLab/current/computing/scripts . 

If you're working off her first implimentation 'RCAV_thermalPID.py' then there is an indent issue after the if statement on line 88: only line 89 should be indended. If you deactivate the debug flag then the script fails to read in PID factors and dies.

Quote:

[yinzi, craig, gautam]

Yinzi had translated the Perl PID script used to implement the discrete-time PID control, and had implemented it with Andrew at the PSL lab. Today afternoon we made some minor edits to make this suitable for the FSS Slow loop (essentially just putting the right channel names into her Python script). I then made an init file to run this script on megatron, and it looks to be working fine over the last half hour of observation or so. I am going to leave things in this state over the weekend to see how it performs.


We have been running with just the MC2 Transmission QPD for angular control of the IMC for a couple of months now because the WFS loops seemed to drag the alignment away from the optimum. We did the following to try and re-engage the WFS feedback:

  • Close the PSL shutter, turned off all the lights in the lab and ran the WFS DC offsets script
  • Locked the IMC, optimized alignment by hand (WFS feedback turned off)
  • Unlocked the IMC, went to the AS table and centered the spots on the WFS
  • Ran WFS RF offsets script
  • Re-engaged WFS servo

 

 

  13456   Tue Nov 28 17:27:57 2017 awadeBureaucracyCalibration-RepairSR560 return, still not charging

I brought a bunch of SR560s over for repair from Bridge labs. This unit, picture attached (SN 49698), appears to still not be retaining charge. I’ve brought it back. 

  13500   Wed Jan 3 16:25:32 2018 awadeUpdateOptimal ControlOplev loop tuning

Another cool feature is client side pre-commit hooks. They can be used to run checks on the local version at the time of commit and refuses to push until the pass/fail exits 0.

Can be the same as the Gitlab CI or just basic code quality checks.  I use them to prevent jupyter notebooks being commited with uncleared cells. It needs to be set up on the user's computer manually and is not automatically cloned with the directory: a script can be included in the repo to do this and run manually on first time clone.

Quote:

When putting code into git.ligo.org, one way to have automated testing is to use the Gitlab CI. This is an automated 'checker', much like the 'Travis' system used in GitHub. Essentially, you give it a make files which it runs somewhere and your GIT repo web page gets a little 'failed/passing' badge telling you if its working. You can also browse the logs to see in detail what happened. This avoids the 'but it works on my computer!' thing that we usually hear.

 

  14174   Tue Aug 21 17:32:51 2018 awadeBureaucracyEquipment loanOne P-810.10 Piezo Actuators element removed

I've taken a PI Piezo Actuator (P-810.10) from the 40m collection. I forgot to note it on the equipment checklist by the door, will do so when I next drop by.

  14555   Fri Apr 19 12:06:31 2019 awadeBureaucracyElectronicsBorrowed Busby Box May 19th 2019

I've borrowed the Busby Box for a day or so.  Location: QIL lab at Bridge West.

Edit  Sat Apr 20 21:16:46 2019 (awade): returned.

  14565   Wed Apr 24 11:22:59 2019 awadeBureaucracyEquipment loanBorrowed Zurich HF2LI Lock in Amplifer to QIL

Borrowed Zurich HF2LI Lock in Amplifer to QIL lab Wed Apr 24 11:25:11 2019.

  13711   Tue Mar 27 19:32:03 2018 arijitUpdateIOOPSL noise eater was off

Kevin, Gautam and Arijit

We made a measurement of the MC_REFL photodiode transfer function using the network analyzer. We did it for two different power input (0dB and -10dB) to the test measurement point of the MC_REFL photodiode. This was important to ensure the measurements of the transfer function of the MC_REFL photodiode was in the linear regime. The measurements are shown in attachment 1. We corrected for phase noise for the length of cable (50cm) used for the measurement. With reference to ELOG 10406, in comparison to the transimpedance measurement performed by Riju and Koji, there is a much stronger peak around 290MHz as observed by our measurement.


We also did a noise measurement for the MC_REFL photodiode. We did it for three scenarios: 1. Without any light falling on the photodiode 2. With light falling on the photodiode, the MC misaligned and the NPRO noise eater was OFF 3. With light falling on the photodiode, the MC misaligned and the NPRO noise eater was ON. We observed that the noise eater does reduce the noise being observed from 80kHz to 20MHz. This is shown in attachment 2.


We did the noise modelling of the MC_REFL photodiode using LISO and tried matching the expected noise from the model with the noise measurements we made earlier. The modeled noise is in good agreement with the measured noise with 10Ohms in the output resistance. The schematic for the MC_REFL photodiode however reveals a 50Ohm resistance being used. The measured noise shows excess noise ~ 290MHz. This is not predicted from the simplied LISO model of the photodiode we took.


Discussion with Koji and Gautam revealed that we do not have the exact circuit diagram for the MC_REFL photodiode. Hence the simplified model that was assumed earlier is not able to predict the excess noise at high frequencies. One thing to note however, is that the excess noise is measured with the same amplitude even with no light falling on the MC_REFL photodiode. This means that there is a positive feedback and oscillation in the op-amp (MAX4107) at high frequencies. One way to refine the LISO model would be to physically examine the photodiode circuit.

We also recorded the POX and POY RF monitor photodiode outputs when the interferometer arms are independently stabilized to the laser. Given the noise outputs from the RF photodiodes were similar, we have only plotted the POY RF monitor output for the sake of clarity and convenience.

Quote:

While Kevin and Arijit were doing their MC_REFL PD noise measurements (which they will elog about separately shortly), I noticed a feature around 600kHz that reminded me of the NPRO noise eater feature. This is supposed to suppress the relaxation oscillation induced peak in the RIN of the PSL. Surprisingly, the noise eater switch on the NPRO front panel was set to "OFF". Is this the normal operating state? I thought we want the noise eater to be "ON"? Have to measure the RIN on the PSL table itself with one of the many available pick off PDs. In any case, as Attachment #1 showed, turning the noise eater back on did not improve the excess IMC frequency noise.

 

  13716   Wed Mar 28 21:47:37 2018 arijitUpdateIOOMCREFL_PD Optical response measurement

Kevin, Gautam and Arijit

We did a optical measurement of the MCREFL_PD transimpedance using the Jenny Laser set-up. We used 0.56mW @1064nm on the NewFocus 1611 Photodiode as reference and 0.475mW @1064nm on the MCREFL_PD. Transfer function was measured using the AG4395 network analyzer. We also fit the data using the refined LISO model. From the optical measurement, we can see that we do not have a prominent peak at about 300MHz like the one we had from the electrical transimpedence measurement. We also put in the electrical transimpedence measurement as reference. RMS contribution of 300MHz peak to follow.

 

As per Rana`s advice I have updated the entry with information on the LISO fit quality and parameters used. I have put all the relevant files concerning the above measurement as well as the LISO fit and output files as a zip file "LISO_fit" . I also added a note describing what each file represents. I have also updated the plot with fit parameters and errors as in elog 10406.

  13719   Thu Mar 29 17:57:36 2018 arijitUpdateIOOMCREFL_PD Optical response measurement

Kevin, Gautam and Arijit

Today we performed the in-loop noise measurements of the MCREFL-PD using the SR785 to ascertain the effect of the Noise Eater on the laser. We took the measurements at the demodulated output channel from the MCREFL-PD. We performed a series of 6 measurements with the Noise Eater ''ON'' and ''OFF''. The first data set is an outlier probably, due to some transient effects. The remaining data sets were recorded in succession with a time interval of 5 minutes each between the Noise Eater in the ''ON'' and ''OFF'' state. We used the calibration factor of 13kHz/Vrms from elog 13696 to convert the V_rms to Hz-scale.

The conclusion is that the NOISE EATER does not have any noticeable effect on the noise measurements.

ALS beat spectrum and also the arm control signal look as they did before. coherence between arm control signals (in POX/POY lock) is high between 10-100Hz, so looks like there is still excess frequency noise in the MC transmitted light. Looking at POX as an OOL sensor with the arm under ALS control shows ~10x the noise at 100 Hz compared to the "nominal" level, consistent with what Koji and I observed ~3weeks ago.

We tried swapping out Marconis. Problem persists. So Marconi is not to blame. I wanted to rule this out as in Jan, Steve and I had installed a 10MHz reference to the rear of the Marconi.

  8892   Mon Jul 22 17:17:30 2013 annalisaUpdateendtable upgradeEnd table picture
  74   Wed Nov 7 00:51:33 2007 andrey, rob, tobinConfigurationIOOMC ringdowns
We completed several ringdown measurements this afternoon; Andrey is currently processing the data.
  10424   Fri Aug 22 15:11:55 2014 andres, nicolasSummaryIOOMC WFS activity

1. Before doing anything, we centered the IOO QPDs.
2. With the WFS enabled, we offloaded the control signals onto the bias sliders. Then we saved the slider values. The MC LSC diode had a DC value of ~0.5
3. Turned down power with half wave plate before PMC.  Power injected to vacuum ~ 100mW.
4. We did a beam scan of MC REFL, it looks smaller than what Andres predicted based on the MC eigenmode by 10-20%.
5. We made many changes on the table, pictures to be added by Andres.
6. We didn't have the 80% reflector we wanted to increase the WFS power, so it's still a 98%.
6. Beams were aligned on MC REFL PL, camera, beam dumps, WFSs.
7. Clean up
8. PSL power increased to 1.2W, MC locked right away.
9 We didn't change the IOO WFS output matrix, but we changed some signs and gains to make everything stable. MC autolocker brings it back from cold just fine.
10. All time bombs that we've left will be E.Q.'s to clean up. Sorry.\
11. Yay

  17674   Fri Jul 7 21:54:44 2023 andreiUpdatePEMFoam setup

[andrei, advait]

We wrapped the puck in foam. We also performed a calibration on the AD590 sensors @ 25.3 Celsius and then proceeded with an additional 6-point calibration using a digital thermometer (DT310LAB).

This is the current setup There is also a lid similar in size with the bottom lid, and the entire foam is currently held together with a heavy wire role that was put on top of the lid.

We couldn't replace the red tape with the yellow-transparent tape because the yellow tape is not strong enough and an air gap forms between the resistor and the puck. As a result, we will avoid getting above ~45 Celsius in to prevent the red tape from becoming too hot. We are now proceeding with a step response measurement and will follow up on that soon.

  17687   Sat Jul 15 13:27:39 2023 andreiUpdatePEMFoam setup

Update: we have a working "I" controller for the puck. Here is the data:

In achieving this, we had to make a few changes;

 1. In the heater circuit, the resistor is now connected to its own power supply set for 10V. This enables us to have around 50% duty cycle at equilibrium for T_ref=45C:

*This is the heater profile for the above "I" controller run
 2.  We changed the frequency of the Pulse Width Modulation (PWM) of the RaspberryPi that is used to switch the MOSFET. It is now 100Hz compared to the previous 1kHz. I observed using the oscilloscope that the PWM was delivering ~870Hz when set for 1kHz and that it also struggled to deliver accurate duty cycles, especially for low duty cycles (below 5%). The duty cycles should always be kept between 5%-95% for accurate modulation.
 3. In case we want to change the power supply voltage, the controller code can be easily adjusted by just changing the maximum voltage constant.

Quote:

[andrei, advait]

We wrapped the puck in foam. We also performed a calibration on the AD590 sensors @ 25.3 Celsius and then proceeded with an additional 6-point calibration using a digital thermometer (DT310LAB).

This is the current setup There is also a lid similar in size with the bottom lid, and the entire foam is currently held together with a heavy wire role that was put on top of the lid.

We couldn't replace the red tape with the yellow-transparent tape because the yellow tape is not strong enough and an air gap forms between the resistor and the puck. As a result, we will avoid getting above ~45 Celsius in to prevent the red tape from becoming too hot. We are now proceeding with a step response measurement and will follow up on that soon.

 

  17695   Tue Jul 18 16:01:01 2023 andreiUpdatePEMFoam setup

We decided to verify the PWM accuracy by adjusting the oscilloscope to fit a hundred cycles of the signal and measuring the mean voltage - the variation is linear as expected, although it does diverge at the extremeties as noted earlier.

Additionally, I compared the experimental data in the previous plots with a simulation using the model that we constructed, and after accounting for time delays in heating the system, we see a very good agreement between the two - 

 

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