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ID Date Authorup Type Category Subject
  14485   Mon Mar 18 18:10:14 2019 KojiSummaryGeneralTask items and priority

[Gautam/Chub/Koji] ~ Mini discussion

Maintenance / Upgrade Items

(Priority high to low)

  • TT/IO suspension upgrade (solidworks work) -> order components -> TT characterization
  • Acromag upgrade c1susaux
    • Produce spread sheetfor DB files. Learn new format of the DB file with Acromag. Develop a python code for the DB file generation (Jon->Koji)
  • Satellite Box upgrade
    • Rack mount? Front panel DB connectors. New circuits (PD-LED)
       
  • Acromag iscaux1/2 & isc whitening upgrade
     
  • new RC mirror characterization -> installation
  14492   Thu Mar 21 18:09:36 2019 KojiUpdateCDSdb file preparation for acromag c1susaux

I have updated the google doc spreadsheet to indicate the required action for the new dbfile generation.

There are three types of actions:

1. COPY - Just duplicate the old EPICS db entry. This is for soft channels, calc channels.
2. DELETE - Delete the entry for some physical channels that will not be implemented on Acromag (oplev, dewhitening mon, AI monitor, etc)
3. REPLACE - For the physical channels, we want to replace the port names.

The blue part of the spreadsheet indicates the action for each channel. If it is a physical channel, the assigned module and the channel are indicated there. What we still want to do is to use the these information for generating the port name which looks like "@asynMask(C1VAC_XT1221A_ADC 1 -16)MODBUS_DATA".

The links to the spreadsheets can be found on 40m wiki: https://wiki-40m.ligo.caltech.edu/CDS/SlowControls/c1susaux

  14499   Thu Mar 28 23:29:00 2019 KojiUpdateSUSSuspension PD whitening and I/F boards modified for susaux replacement

Now the sus PD whitening bards are ready to move the back plane connectoresto the lower row and to plug the acromag interface board to the upper low.


Sus PD whitening boards on 1X5 rack (D000210-A1) had slow and fast channels mix in a single DIN96 connector. As we are going to use the rear-side backplane connector for Acromag access, we wanted to migrate the fast channel somewhere. For this purpose, the boards were modified to duplicate the fast signals to the lower DIN96 connector.

The modification was done on the back layer of the board (Attachment 1).
The 28A~32A and 28C~32C of P1 are connected to the corresponding pins of P2 (Attachment 2). The connections were thouroughly checked by a multimeter.

After the modification the boards were returned to the same place of the crate. The cables, which had been identified and noted before disconnection, were returned to the connectors.

The functionarity of the 40 (8sus*5ch) whitening switches were confimred using DTT one by one by looking at the transfer functions between SUS LSC EXC to the PD input filter IN1. All the switches showed the proper whitening in the measurments.

The PD slow mon (like C1:SUS-XXX_xxPDMon) channels were also checked and they returned to the values before the modification, except for the BS UL PD. As the fast version of the signal returned to the previous value, the monitor circuit was suspicious. Therefore the opamp of the monitor channels (LT1125) were replaced and the value came back to the previous value (attachment 3).

 

  14513   Wed Apr 3 12:32:33 2019 KojiUpdateALSNote about new fiber couplers

Andrew seems to have an integrated solution of PBS+HWP in a singe mount. Or, I wonder if we should use HWP/QWP before the coupler. I am interested in a general solution for this problem in my OMC setup too.

  14535   Thu Apr 11 11:42:10 2019 KojiUpdatePSLPSL fan is noisy

This thread: ELOG 10295

My interpretation of these ELOGs is that we did not have the replacement, and then I brought unknown fan from WB. At the same time, Steve ordered replacement fans which we found in the blue tower yesterday.
The next action is to replace the internal fan, I believe.

  14553   Fri Apr 19 09:42:18 2019 KojiBureaucracyGeneralItem borrowing (40m->OMC)

Apr 16, 2019
Borrowed two laser goggles from the 40m. (Returned Apr 29, 2019)
Apr 19, 2019
Borrowed from the 40m:
- Universal camera mount
- 50mm CCD lens
- zoom CCD lens (Returned Apr 29, 2019)
- Olympus SP-570UZ (Returned Apr 29, 2019)
- Special Olympus USB Cable (Returned Apr 29, 2019)

 

  14612   Wed May 15 19:36:29 2019 KojiUpdateSUSETMY instepction

A pair of tweezer is OK as long as there is no magnets around. You need to (somewhat) constrain the mirror with the EQ stops so that you can pull the fiber without dragging the mirror.

  14659   Thu Jun 6 22:11:53 2019 KojiUpdateIOOIMC diagnostics

As per Gautam's request, I looked at the IMC situation.

Locking path

  • Acquisition: IMC IN1 Gain +4 (nominal), Boost 0, VCO Gain (-32), FSS Common +6 (nominal), FSS FAST +20
    This is too low gain. So oscillate VCO Gain between -32 and ~0 until TEM00 lock is acquired
  • Once lock is acquired, bring the VCO gain to +11 (new nominal), and increase the FSS FAST to +23 (new nominal). Change the IMC BOOST to 3 (nominal)

Diagnosis

  • The PMC servo gain was checked. The control signal monitor for the PMC actuation was hooked up to SR785. The nominal gain was +18dB. Increasing the gain to 20dB made the servo oscillating. So the nominal gain of +18dB seems still reasonable.
  • The status of NOISE EATER was checked. Both the PMC REFL and TRANS were looked at by AG4395A. The power spectrum of them did not change much around the kHz~MHz region. It made the PSD slightly (x2~3) improved below 1kHz. I also did not recognize the relaxation oscillation peak. So I could not figure out where to see. NOISE EATSER was on and is still on.
  • IFO Modulation Freq: I took this chance to look at the IMC absolute length using the peak at 3.6MHz. The TP1A output of the IMC servo board was hooked up to AG4395A.
    The new FSR of the IMC (and thus the modulation frequency for the IFO) is 11.066275MHz (instead of the previous 11.066209MHz).
    This corresponds to 0.16mm difference in the roundtrip length.
  • (*Still working) IMC SERVO configuration:
    • FAST 25 (nominal) sometimes invoke the oscilattion. 24 has gain peaking ~30kHz. There is a big line peak at 35kHz so wanted to avoid the servo bump (PZT-EOM cross over). So decided to use 23dB. (This is not optimal for the CM servo as we need as much as bandwidth for CM servo.)
    • IMC VCO GAIN (bad name. this is actually overall output gain for IMC) was increased from the nominal 7 to 11. Increasing this above 11 makes the servo oscillating at ~200kHz.
  • (*Still working) Measured power spectrum of the error signal. Too many line peaks.
  • (*Still working) Single trigger observation: Oscilloscope monitoring started from 35kHz going up and ~20kHz oscillation +/-6V of the IMC servo output was observed. Could not capture good data for this. Try the other day.

I'll complete the entry later.

  14672   Thu Jun 13 22:21:44 2019 KojiConfigurationCDSPaola wireless connected to martian

SURFs had trouble connecting paola to martian via wireless.
Of course, it requires a fixed IP but it had not it yet. So I went to chiara and gave 192.168.113.110 as "paolawl". Note that the wired connection has .111 and it is "paola".

Followed the instruction on http://nodus.ligo.caltech.edu:8080/40m/14121

  14673   Thu Jun 13 22:46:41 2019 KojiUpdateIOOLeft IMC at the intermediate gains

SURFS want some locking of IMC for camera adjustment.

So I left the IMC with intermediate gains so that it keeps locking and unlocking.

VCO (overall) iMC gain of -32, FSS common gain 3, and the FAST gain 20. I believe MC2tickle is ON too.

  14685   Fri Jun 21 19:22:40 2019 KojiConfigurationBHDReviving the single OMC BHD design?

I think a Faraday rotator rotates the polarizations in a same way for both forward and backward beam, and it's not like in this figure.
And the transmission through multiple faradays will also be a big issue.

  14686   Fri Jun 21 19:36:26 2019 KojiUpdateIOOIMC diagnostics

The IMC REFL error signal was measured to compare it with the other spectra (if we have).

The blue curve is the in-loop IMC error and the red is the dark noise. So they are not an apple-to-apple comparison. But the red noise is going to be suppressed by the loop, and still the red is below blue. This means that the blue curve is the measured noise rather than the readout noise.

We suspect that the current issue is the PC drive saturation (as usual). Does this indicate that the laser freq noise is actually increased?

----

Another suspect was that the degradation of the LO level. We used to have the issue of slowly dying ERA-5 (ERA-5SM indeed). The RF levels on the demod board were measured using an active probe.

The LO input: 0dBm, ERA-5 input: -2.7dBm and -2.1dBm for I and Q. I found that the outputs of the ERA-5SM were +10.5dBm and +10.6dBm.
This lead me to replace the chips but the situation was not changed. Then I realized that the LO levels should have been measured with the load replaced from the mixers to a 50Ohm load. Somehow these mixers lower the apparent LO levels. So I decided to say this is OK.

  14689   Sun Jun 23 14:43:14 2019 KojiUpdateIOOIMC is locking normally again

Note that I have removed an SR785, an oscilloscope, some SRS instruments from the PSL and PMC last night.

But they (and RF Network Analyzer) were not there when the problem started.

We should record the IMC error (at test point monitor) too? If the IMC locks on Monday too, I'll do it.

  14712   Sun Jun 30 23:52:09 2019 KojiUpdateIOOPMC and IMC locked again, some MEDM maintenance

> For channels corresponding to continuous values (such as say exposure time or the like) changes to abs(1+current_value)

Why abs? Is the current_value is like -5.4321 (for example for the alignment slider), this returns +4.4321 and the suspension will suffer from huge motion (well it will be returned to the original value soon though). 

  14725   Thu Jul 4 10:54:21 2019 KojiSummarySUSSuspension damping recovered, ITMX stuck

So Cal Earthquake. All suspension watchdogs tripped.

Tried to recover the OSEM damping. 

=> The watchdogs for all suspensions except for ITMX were restored. ITMX seems to be stuck. No further action by me for now.

  14727   Fri Jul 5 20:57:04 2019 KojiUpdateSUSAnother M7.1 EQ

[Kruthi, Koji]

Koji came to the lab to align the IMC/IFO, but found the mirrors are dancing around. Kruthi told me that there was M7.1 EQ at Ridgecrest. Looks like there are aftershocks of this EQ going on. So we need to wait for an hour to start the alignment work.

ITMX and ETMX are stuck.

  14728   Fri Jul 5 21:53:10 2019 KojiUpdateSUSAnother M7.1 EQ

- ITM unstuck now
- IMC briefly locked at TEM00

A series of aftershocks came. I could unstick ITMX by turning on the damping during one of the aftershocks.
Between the aftershocks, MC1~3 were aligned to the previous dof values. This allowed the IMC flashing. Once I got the lock of a low order TEM mode, it was easy to recover the alignment to have a weak TEM00.
Now at least temporarily the full alignment of the IMC was recovered.

  14729   Fri Jul 5 22:21:13 2019 KojiUpdateSUSAnother M7.1 EQ

In fact, ETMX was not stuck until the M7.1 EQ today. After that it got stuck, but during the after shocks, all the OSEMs occasionally showed full swing of the light levels. So I believe the magnets are OK.

  14743   Wed Jul 10 14:55:32 2019 KojiUpdateGeneralProjector lightbulb blown out

In fact the projector is still working. The lamp timer showed ~8200hrs. I just reset the timer, but not sure it was the cause of the shutdown. I also set the fan mode to be "High Altitude" to help cooling.

  14744   Wed Jul 10 14:57:01 2019 KojiSummaryCDSChannel recipe for iscaux upgrade

The list of the iscaux channels and pin assignments were posted to google drive.
The spreadsheet can be viewable by the link sent to the 40m ML. It was shared with foteee@gmail for full access.

Summary

  • We need
    4 ADC modules
    5 DAC modules
    5 Binary I/O modules
  • Be aware that there are bundled multiple digital I/O channels such as "mbboDirect" and "mbbi".
  • The full db record of the new channels need to be inferred from the existing channels.

Necessary electronics modification

1. D990694 whitening filter modification (4 modules)

This module shares the fast and slow channels on the top DIN96pin (P1) connector. Also, the whitening selector (done by an analog signal per channel) is assigned over 17pin of the P1 connector, resulting in the necessity of the second DSUB cable. By migrating the fast channels, we can swap the cable from the P1 to P2.  Also, the whitening selectors are concentrated on the first Dsub. (See Attachment1 P1)

2. D040180 / D1500308 Common Mode Board

CM servo board itself doesn't need any modification. The CM board uses P1 and P2. So we need to manufacture a special connector for CM Board P2. (cf The adapter board for P1 T1800260). See also D1700058.

3. D990543A1 LSC Photodiode Interface

PD I/F board has the DC mon channels spread over the 16pin limit. P1 21A can be connected to 6A so that we can accommdate it in the first Dsub.
Also the board uses AD797s. This is not necessary. We can replace them to OP27s. I actually don't know what is happening to those bias control, temp mon, enable, and status. These features should be disables at the I/F and the PDs. (See Attachment2 P1)

  14756   Fri Jul 12 18:54:47 2019 KojiUpdateGeneralItem loan: optical chopper from Cryo Lab

Optical chopper borrowed from CryoLab to 40m

https://nodus.ligo.caltech.edu:8081/Cryo_Lab/2458

  14764   Tue Jul 16 15:17:57 2019 KojiHowToCDSFinal bit bug of the BIO CDS module

Yutaro talked about the BIO bug in KAGRA elog. http://klog.icrr.u-tokyo.ac.jp/osl/?r=9536

I think I made the similar change for the 40m model somewhere (don't remember), but be aware of the presense of this bug.

  14767   Wed Jul 17 17:56:18 2019 KojiConfigurationComputersGave resolv.conf to giada

Kruthi noticed that she could not login to rossa from giada.

I checked /etc/resolv.conf and it was

nameserver 127.0.0.1

so obviously it is useless to refer localhost (i.e. giada) as a nameserver.

I copied our usual resolv.conf to giada as following:

nameserver 192.168.113.104
nameserver 131.215.125.1
nameserver 8.8.8.8

search martian

Giada's ssh known_host had unupdated entry for rossa, so I had to clean it up, but after that we can connect to rossa from giada just by "ssh rossa".

Case closed.

  14770   Thu Jul 18 00:51:52 2019 KojiSummaryCDSiscaux electronics modifications

Along with the plan in ELOG 14744, the ISC PD interface and the whitening filter board have been modificed. The ISC PD I/Fs were restored to the crate and the cables were connected. The whitening filteres are still on the electronics bench for some more tests before being returned to the crate.

The updated schematics were uploaded as https://dcc.ligo.org/D1900318 and https://dcc.ligo.org/D1900319

- Modification of the ISC PD interface: Jumpers between DIN96 P1 and P2. Replace all AD797s with OP27. In fact only I/F #1 (the left most)  had total 12 AD797 but the other units already had OP27s.

- Modification of the whitening filter: Jumpers between DIN96 P1 and P2.

  14775   Thu Jul 18 22:34:40 2019 KojiSummaryCDSiscaux electronics modifications

The whitening filter modules have been restored to the crates. The SMA cables have been restored and fastened by a spanner. The ribbon cable to the antialiasing board was also connected. The backplane cables have not been moved from the upper DIN96 connector to the lower one.

Everything is expected to be good, but just keep eyes on the LSC signals as the boards were not quantitatvely tested yet. If you find something suspicious, report on the elog.

  14821   Wed Jul 31 17:57:35 2019 KojiUpdateBHDOMC cavity geometry

4 deg is not an optimized number optimized for criteria, but to keep the cavity short width to 0.1m. But the justification of 4deg is found in Section 3 and 4 of T1000276 on Page 4.

Quote:

Question for Koji: how is the aLIGO OMC angle of incidence of ~4 degrees chosen? Presumably we want it to be as small as possible to minimize astigmatism, and also, we want the geometric layout on the OMC breadboard to be easy to work with, but was there a quantitative metric? Koji points out that the backscatter is also expected to get worse with smaller angles of incidence.

  14843   Mon Aug 12 21:25:19 2019 KojiUpdateCDSMore bench test of c1iscaux

1.

> Looking through the manual, I found a recommendation (pg10) that the "IN-" terminal of the Acromag ADC units be tied to the "RTN" pins on the same units. I don't know if this preserves the differential receiving capability of the Acromag ADCs

I suppose, we loose the differential capability of an input if the -IN is connected to whatever defined potential. We should check if the channels are still working as a true differential or not.

 

2. If the multi bit operation is too complicated to solve, we can use EPICS Calc channels to breakout a value to bits and send the individual bits as same as the other individual binary channels.

 

  14851   Tue Aug 20 19:05:24 2019 KojiUpdateCDSMC1 (and MC3) troubleshoot

Started the troubleshoot from the MC1 issue. Gautam showed me how to use the fake PD/LED pair to diagnose the satellite box without involving the suspension mechanics.

This revealed that the MC1 has frequent light level glitches which are common for five sensors. This feature does not exist in the test with the MC3 satellite box. I will open and check the MC1 satellite box to find the cause of this common glitches tomorrow. MC1 is currently shutdown and undamped.

BTW, at the MC3 test, i found that J2 of the satellite box (male Dsub) has all the pins too low (or too short?). I brought the box outside and found that the housing of this connector was half broken down. The connector was reassembled and the metal parts of the housing was bent again so that the housing can hold the connector body tightly.

The MC3 satellite box was restored and connected to the cables. As I touched this box, it is still under probation.

  14852   Thu Aug 22 12:54:06 2019 KojiUpdateCDSMC1 glitch removed (for now) and IMC locking recovered

I have checked the MC1 satellite box and made a bunch of changes. For now, the glitches coming from the satellite box is gone. I quickly tested the MC1 damping and the IMC locking. The IMC was locked as usual. I still have some cleaning up but will work on them today and tomorrow.


Attachment 1: Result

The noise level of the satellite box was tested with the suspension simulator (i.e., five pair of the LED and PD in a plastic box).

Each plot shows the ASD of the sensor outputs 1) before the modification, 2) after the change, and 3) with the satellite box disconnected (i.e., the noise from the PD whitening filter in the SUS rack).

Before the modification, these five signals showed significant (~0.9) correlation each other, indicating that the noise source is common. After the modification, the spectra are lowered down to the noise level of the whitening filters, and there is no correlation observed anymore. EXCEPT FOR the LR sensor: It seems that the LR has additional noise issue somewhere in the downstream. This is a separate issue.


Attachment 2: Photo of the satellite box before the modification

The thermal environment in the box is terrible. They are too hot to touch. You can see that the flat ribbon cable was burned. The amps, buffers, and regulators generate much heat.

Attachment 3: Where the board was modified

- (upper left corner) Every time I touched C51, the diode output went to zero. So C51 was replaced with WIMA 10uF (50V) cap.

- (lower left area) I found a clear indication of the glitch coming from the PD bias path (U3C). So I first replaced another 10uF (C50) with WIMA 10uF (50V). This did not change the glitch. So I replaced U3 (LT1125). This U3 had unused opamp which had railed to the supply voltage. Pins 14 and 15 of U3 were shorted to ground.

- (lower right corner) Similarly to U3, U6 also had two opamps which are railed due to no termination. U6 was replaced, and Pins 11, 12, 14, and 15 were shorted to ground.

- (middle right) During the course of the search, I suspected that the LR glitch comes from U5. So U5 was replaced to the new chip, but this had no effect.


Attachment 4: Thermal degradation of the internal ribbon cable

Because of the heat, the internal ribbon cable lost the flexibility. The cable is cracked and brittle. It now exposes  some wires. This needs to be replaced. I'll work on this later this week.

Attachment 5: Thermal degradation of the board

Because of the excessive heat for those 20years, the bond between the board and the patten were degraded. In conjunction with extremely thin wire pattern, desoldering of the components (particularly LT1125s) was very difficult. I'd want to throw away this board right now if it were possible...

Attachment 6: Shorting the unused opamps

This shows how the pieces of wires were soldered to ground vias to short the unused opamps.


Attachment 7: Comparison of the noise level with the sus simulator and the actual MC1 motion

After the satellite box fix, the sensor outputs were measured with the suspension connected. This shows that the suspension is moving much more than the noise level around 1Hz. However, at the microseismic frequency there is also most no mergin. Considering the use of the adaptive feedforward, we need to lower the noise of the satellite box as well as the noise of the whitening filters.

=> Use better chips (no LT1125, no current buffers), use low noise resistors, better thermal environment.


  14853   Thu Aug 22 20:56:51 2019 KojiUpdateCDSMC1 glitch removed (for now) and IMC locking recovered

The internal ribbon cable for the MC1 satellite box was replaced with the one in the spare box. The MC1 box was closed and reinstalled as before. The IMC is locking well.

Now the burnt cable was disassembled and reassembles with a new cable. It is now in the spare box.

The case closed (literally)

  14862   Fri Sep 6 15:12:49 2019 KojiHowToCDSWFS discussion, restarting CDS

Assuming you are at pianosa, /etc/resolv.conf is like

# Generated by NetworkManager
nameserver 192.168.113.104
nameserver 8.8.8.8

But this should be like

nameserver 192.168.113.104
nameserver 131.215.125.1
nameserver 8.8.8.8

search martian

as indicated in https://nodus.ligo.caltech.edu:8081/40m/14767

I did this change for now. But this might get overridden by Network Manager.

  14865   Fri Sep 6 21:22:06 2019 KojiHowToCDSHow to save c1ioo

Q1 Can we run the machine with the reduced # of cores?

Q2 We might be able to order them quickly. What's the spec and configuration of the DIMMs (like DDR2-667MHz ECC 4GBx4, and even more specs (like Samsung 2GB DDR2 RAM PC2-6400 240-Pin DIMM M378T5663EH3) so that we are to identify the exact spec).

Q3 Can we scavenge the old OMC RT machine or even megatron to extract the memories?

  14870   Tue Sep 10 17:26:49 2019 KojiUpdateCDSD1900068 SR785 accessory box

I picked up a unit of D1900068 SR785 accessory box from Dean's office at Downs. 

  14877   Fri Sep 13 13:03:35 2019 KojiSummaryCDSDIN 96pin to DSUB37 adapter (single) ready for use

The PCB board of the adapter for DIN 96pin to DSUB37 conversion (single DSUB version) was delivered yesterday and I quickly soldered the connectors.

They are ready for use and stored in a JLCPCB cardboard box on a pile of acromag stuff. (Note that the lacel is written on the box with Sharpie)

  14884   Mon Sep 16 19:29:24 2019 KojiUpdateCamerasMC2 trans camera (?) rotated

The left one is analog and 90deg rotated.

See also: This issue tracker

  14892   Tue Sep 17 23:43:34 2019 KojiSummaryCDSAcromag logic checker

For the investigation of the latch logic issue for the CARM CM board, I have made the LED logic checkers with DB breakout boards. They require the pull up voltage supply of +15V because the acromag digital out is a open corrector (well... open "source") output.

The logic from Pin1 to Pin16 of DB37 can be monitored. The DB15 connector is only for monitoring the latch enable logic.

What Gautam and I found with the logic outputs was that the latch logic works fine but occasionally we found that the top 2 bits and the bottom 4bit were processed independently.

  14893   Tue Sep 17 23:46:21 2019 KojiUpdateCDSLatch Enable Logic

[Koji Gautam]

We continued to check the latch logic. Today we found that latch.py didn't catch the change of LSB but did for MSB. We determined that this happens when the slider value is chaged between the polling for LSB and MSB.
SInce these two should always be related to a single gain value, latch.py was modified so.

Now we don't observe any logic error for ~100 gain transisitions (see attached).

  14906   Wed Sep 25 20:10:13 2019 KojiUpdateCDSc1iscaux testing

== Test Status ==
[none]
Whitening gain switching test
[none] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[none] CM Board
[none] ALS I/F board


- LO Det Mon channel check

The StripTool template for the test was made:
/cvs/cds/caltech/target/c1iscaux/testScripts/testDetectMons.str
Then, the RF output of the main Marconi was toggled a few times. -> Confirmed the channels are respopnding. (Attachment 1)

- IPPOS channel check

(0th order check) The StripTool template for the test was made:
/cvs/cds/caltech/target/c1iscaux/testScripts/testIPPOS.str
Then, the IPPOS QPD was shined with a phone LED. Initially I saw no response of the QPD. It turned out that the IPPOS IF module had no input cable connected. After the connection, all the 4 segments are responding to the phone LED and also the IFO beam.

(more careful check)
I decided to do more careful check of IPPOS. As there was a f~30mm lens on the oplev table, beam was focused such that only one element reacted to the incident beam. The beam power (a few mW) was too strong for a single QPD element, which saturates at ~6, an ND filter of OD0.6 was used to reduce the incident power.

Here are the results:
SEG1 (UPPER LEFT seen from the beam) | C1:ASC-IP_POS_QPD_Seg1_Mon 3.651+/-0.003 (N=10) | Incident Power 2.35+/-0.01 mW, QPD X_Calc (+) Y_Calc (+)

Segment Arrangement
(Seen from the beam)
Epics Channel CH output

Incident Power
(mW)

Polarity for the
X/Y_Calc channels
SEG1 UPPER LEFT C1:ASC-IP_POS_QPD_Seg1_Mon 3.651+/-0.003
(N=10)
2.35+/-0.01 X(+) / Y(+)
SEG2 LOWER LEFT C1:ASC-IP_POS_QPD_Seg2_Mon 3.607+/-0.002
(N=12)
2.35+/-0.01 X(+) / Y(-)
SEG3 LOWER RIGHT C1:ASC-IP_POS_QPD_Seg3_Mon 3.658+/-0.002
(N=11)
2.37+/-0.01 X(-) / Y(-)
SEG4 UPPER RIGHT C1:ASC-IP_POS_QPD_Seg4_Mon 3.529+/-0.004
(N=11)
2.30+/-0.01 X(-) / Y(+)

After the measurement, the lens and the filter were removed and the beam was adjusted to the center of the QPD.

  14907   Thu Sep 26 17:56:28 2019 KojiUpdateCDSsome rebooting

Yesterday (Sep 25) evening: I had to reboot c1psl, c1iool0, and c1aux to recover nominal IMC locking

Today megatron had no response and I had to reboot it with the reset button. MCautolocker and FSSSlow were recovered and the IMC is locking as usual.

  14908   Thu Sep 26 20:09:40 2019 KojiUpdateCDSc1iscaux testing

== Test Status ==

[done] Whitening gain switching test => Some issues found (POP110Q, Whitening3_8 not switching, ASDC overall behavior, REFL33Q needs recheck)
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[none] CM Board
[none] ALS I/F board

And, the Y-arm lock was recovered! After some alignment work, the Y-arm was locked. The whitening gain for POY11 was +18dB. The servo gain was 0.015 (nominal).
Once the transmission reached 0.8, I could use ASS to align the cavity and the TTs.
The transmission reached just 1.00 at the end. Was the transmission recently normalized? (See attachment 5)


- Whitening Filter Gain Switching Test

Each whitening filters were tested individually. +50mV DC signal was connected to the 8 inputs using an SMA octopus cable.
The existing script ( /cvs/cds/caltech/target/c1iscaux/testScripts/testWhtGain.py ) did not work because cds.getdata failed to fetch all of the data requested. By giving some sleep before start downloading the data, the problem was avoided. Still some truncated data are seen in the result, but StripTools screenshots compliments the missing part.

Whitening Filters #2~4 were a little tricky because the code needed modification so that the spare channels can be tested.
The modified script is stored as /cvs/cds/caltech/target/c1iscaux/testScripts/testWhtGain_190926.py 

Whitening #1: No issue found.

Whitening #2: No issue found. Some of the step plots showed truncation of the data at the end. But this is an artifact of cds.getdat. The striptool show nothing irregular.

Whitening #3: POP110Q and the spare channel (CH8) did not show the reaction. REFL33Q showed some systematic gain deviation. It could just be the offset problem, but needs to be rechecked.

Whitening #4: The DC channels were found to be OK  except for ASDC. ASDC shows earlier saturation. The input was lowered to 5mVDC to avoid saturation in the second trial. The circuit needs to be checked. The spare channels look noisy, but this is because there is no way to turn off the whitening filters for them.


- AA Filter Test

Injected 11kHz 1Vpp sine wave to the whitening filters. The whiter gains were kept at 0dB. If the AA is disabled, the alias of the 11kHz signal appears in the time series.
-> Whitening #1, #3 and #4: the enable/disable worked correctly.
-> Whitening #2 AA
Bbypass no effect. this is an expected behavior.
 

  14921   Wed Oct 2 01:11:40 2019 KojiUpdateCDSc1iscaux testing

I worked on more troubleshooting of the whitening filters Tuesday afternoon

== Test Status ==

[done] Whitening gain switching test => Remaining issues ASDC overall behavior
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[none] CM Board
[none] ALS I/F board


Issue 1: POP110Q did not show any gain switching [Resolved]

A DB37 breakout board was connected to the acromag front panel. I found that Ch6 (POP110Q) did not show any differential DC output. I searched around the other pins and found that the corresponding signal showed up on PIn36  instead of Pin35. Opening the front panel revealed that the internal wiring was wrong (Attachment 1). The wire which should have gone to Pin 35 was connected to Pin 36. By correcting the wiring, POP110Q started to show identical behavior to POP110I. (Attachment 2)

Issue 2: LSC reboot [Resolved]

A rough activity around the acromag chassis crashed c1lsc realtime processes (as usual). I ran usual rebooting script /opt/rtcds/caltech/c1/scripts/cds/rebootC1LSC.sh. This successfully restored the status of the vertex RT processes.

Issue 3: REFL33 different behavior between I and Q [Resolved]

REFL33I and Q consistently showed a difference (Attachment 3). The whitening board was pulled out and powered with an extension card. The raw outputs were checked with a function generator and an oscilloscope connected. The outputs for 33I and Q were identical (Attachment 4). So I concluded that the observed difference was an artifact of the checking script.

Issue 4: Whitening 3_8 did not switch at all [Resolved]

To switch the gain stages, each channel of the whitening board takes a DAC output from acromag and convert it into 4bit digital signals. For CH8 of the WF#3, this signal did not reach the instrumentation amplifier AD620. After tracing the signal on the electronics bench, it was found that the CH8 gain input to the DIN96 connector is not conducive to the input of the AD620. As there were no exposed pads between the DIN96 connector and the AD620 input (pin2), a wire was additionally soldered (forgot to take a photo). This solved the gain switching issue as the test result indicates (Attachment 5). The noisiness came from the whitening filter which can not be turned off right now. For this reason, the test of the whitening part is pending too.

The StripTool plot during the overall WF#3 test is shown in Attachment 6.

Issue 5: ASDC behavior [Unresolved]

First of all, at this test, I found that WF#4 was not responding to the gain change at all. This issue was restored by power cycling the acromag chassis (as usual).

The whitening filter #4 was pulled, and the behavior of CH5,6,7,8 (CH8=ASDC) was compared. It was found that the analog outputs were identical and the problem lies further downstream.

Issue 6: Illeagal REFL11 LO cable [Unresolved]

This is a newly found issue. The cable between the LO distributor and the REFL11 demodulator is not the legit solder soaked RG402 coax, but flexible coax (Attachment 7). This cable needs to be replaced in the end. But for today, it was not so that we can have a consistent configuratin as before.

Issue 7: Signature of a damaged POPDC cable [Resolved]

The cable for POPDC cale indicated some damage at the WF#4 side. It was not a complete damage, and therefore the solder coating was added (Attachment 8).

  14932   Thu Oct 3 14:54:33 2019 KojiUpdateGeneralMake the Jenne-laser setup fiber-coupled

I'm afraid that the RF modualtion of the laser is nonlinear and the electrical and optical resoponse is dependent on the LD pumping current and RF input power. So I feel safe if we keep the reference PD. Of course, this is my feeling and it should be quantitatively tested.

  14936   Thu Oct 3 23:15:39 2019 KojiUpdateGeneralMake the Jenne-laser setup fiber-coupled

The 1GHz PD has a bit more flat response, but the laser and the driving network have more frequency dependence as you saw.

  14939   Fri Oct 4 01:57:09 2019 KojiUpdateCDSc1iscaux testing

The AA filter for ASDC was fixed.

== Test Status ==

[done] Whitening gain switching test
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[none] CM Board
[none] ALS I/F board


The AA filter for the 4th section of the LSC analog electronics bank (D000076) was pulled out for the test. On the workbench, questionable CH8 was checked. It tuned out that the filter amplifier module for the 8th-order elliptic filter at 7.5kHz was not properly working and exhibited unusual attenuation. This filter module (Frequency Devices Inc D68L8E-7.50kHz) was desoldered and replaced with a module from a spare board. Note that Gautam and I had tried to use this spare board instead of the current one, but it didn't give us any signal for an unknown reason. Since the desoldering required a lot of force and had a risk of damaging the PCB, a socket was made from an IC socket (see Attached 1). This change made CH8 functioning equally to the other channels do.


I took this opportunity to ckech the performance of the AA filters. For each channel, the input signal was injected from J3 using a pomona clip. The output was taken from pin 1, 5, 9, ... of J2. This is the + side of the differential output. The - side just has the equivalent performance but the signal polarity. The digital signals for the AA bypass switches were not connected. Fortunately, this was just fine as it made the anti-aliasing filters engaged.

Attachment 2 shows the transfer functions of all the channels. All the channels showed an identical response (at least visually). The transfer function for CH1 was fitted by LISO. The ZPK values are listed here:

pole 5.2860544577k 503.1473053928m
pole 5.9752193716k 1.0543411596
pole 8.9271953580k 3.5384364788
pole 8.2181747850k 3.4220607928
pole 182.1403534923k 1.1187869426 # This has almost no effect
zero 13.5305051680k 423.6130434049M
zero 15.5318357741k 747.6895990654k
zero 23.1746351749k 1.5412966100M


factor 989.1003181564m
delay 24.4846075283n

Attachment 3 shows the ASD of the output voltage noise measurement. Note the input was shorted for this measurement. The nominal output voltage was found to be 0.1 uV/rtHz and the 1/f noise corner freq was about 100Hz. Only CH3 showed a deviation from the typical values. It looks like this is neither an artifact nor transient noise. Fortunately, nothing is connected to this channel right now.

  14942   Sat Oct 5 00:03:21 2019 KojiUpdateCDSc1iscaux testing

[Gautam, Koji]

Input gain part of the CM servo board D1500308 was tested. A couple of problems were detected. One still remains.

== Test Status ==

[done] Whitening gain switching test
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[in progress] CM Board
[none] ALS I/F board


We started to test the CM Servo board from the input stages. Initially, DC offsets were provided to IN1 and IN2 to check the gain on the oscilloscope or a StripTool plot. However, the results were confusing, AC measurements with SR785 was carried out in the end. It turned out that both IN1 and IN2 had some issues. IN1 showed an increment of the gain by 2dB every two gain steps, having suggested that the 1dB gain stage had a problem. IN2 showed sudden drop of the signal at the gain +8~+15dB and +24~+31dB, having suggested that a particular 8dB stage had a problem. The board was exposed with the extender and started tracing the signals.

CH1: The digital signal to switch the 1dB stage reached Pin 1A of the DIN96 connector. However, the latch logic (U47 74ALS573) does not spit out the corresponding level for this bit. Note that the next bit was properly working. We concluded that this 74ALS573 had failed and need to be replaced. We have no spare of this wide SOIC-20 chip, but Downs seems to have some spares (see Todd's spare parts list). We will try to get the chip on Monday.

CH2: The stage only used between +8dB and +15dB and between +24dB and +31dB is the +8dB stage (U9 and U2A). I found that the amped output signal did not reach the FET switch U2A (MAX333A). Therefore it was concluded that the opamp U9 (AD829) has an issue. In fact, the amp itself was working, but the output pin was not properly soldered to the pad.  Resoldering this chip made the issue gone. Note that this particular channel has some OP27s soldered instead of AD829. Gautam mentioned that there was some action on the board a few years back to deal with the offset issue. Next time when the board is polled out, I'll take the photos of the board.


Using SR785, the swept sine measurements between 100 and 100kHz were taken for all the gain settings for each channel. Between -31dB and -11dB, the input signal amplitude of 300mV was used. Between -10dB and +10dB, it was reduced to 100mV. For the rest, the amplitude was 10mV. Note that the data for +11dB for CH1 and +2dB for CH2 are missing presumably due to a data transfer issue.

The results are shown in Attachments 1~4.

Attachments 1 and 3 show the gain at each slider value. The measured gain was represented by the average between 1kHz and 10kHz. The missing 1dB every two slide values are seen for CH1. The phase delay at 100kHz is show in the lower plot. There is some delay and delay variation seen but it is in fact less than 1deg at 10kHz (see later) so it's effectfor CM servo (IMC AO path) is minimum. The gain for CH2 tracks the slider value nicely. The phase delay is larger than that of CH1, as expected because of OP27.

Attachments 2 and 4 show the transfer functions. The slider value was subtracted from the measured gain magnitude to indicate the deviation between them. The missing 1dB is obviously visible for CH1 in addition to the overall gain offset of ~0.2dB. CH2 also shows the gain offset of 0.1dB~0.2dB. The phase delay comes into the play around 20kHz particularly at higher gains where the UGF of the AO path is.


gautam: Here is the elog thread for IN2 opAmps going AD829-->OP27. Also, I guess Attachment #1 and #3 x-axes should be "Gain [dB]" rather than "Frequency [Hz]".

  14947   Tue Oct 8 03:19:14 2019 KojiUpdateCDSFinal incarnation of latch.py

Now with the CM board tested with the signal injected, it turned out that the latch logic was flipped. As the default state locked the digital levels, the buttons other than the mbbo channels were inactive.

By giving 0 to C1:LSC-CM_LATCH_ENABLE, the modification of the digital state is enabled. And with the value of 1, the digital bits on the board is locked.

In order to reflect this, latch.py was modified and now the controls are all activated.

  14948   Tue Oct 8 03:32:42 2019 KojiUpdateCDSCM servo board testing

[Koji]

The logic chips 74ALS573 were replaced. And now the gain sliders are working properly.

== Test Status ==

[done] Whitening gain switching test
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[done] CM Board
[none] ALS I/F board


Last week we found that the logic chip for the REFL1 gain switching was not transmitting the input logic. I went to Downs and obtained the chips. After some inspection some other latch chips were suspicious. Therefore U46, U47, and U48 (#1, #3, and #4 from the top) were replaced. After the replacement, the gain measurements were repeated. This time the test for the AO gain was also performed. Now all three slideres show the gain as expected except for the consistent -0.2dB deficit.

Note that the transfer functions for the REFL gains were measured with the input at IN1 or IN2 and the output at TESTA1. The TFs for the AO gain was measured with the excitation at EXC B, the input at TESTB2 and the output at the SERVO output. The gain and phase variantions for the AO gain at low frequency is the effect of AC coupling existing between the excitation and the servo output.

[Update on Oct 14, 2019]

The measured transfer functions show the phase delay determined by the opamps involved. The phase delay well below the pole frequencies can be represented well by a simple time delay (a phase delay linear to the frequency). Attachment 7 shows the time delay estimated by LISO for each gain setting of each gain stage. REFL2 has particularly large phase delay because of the use of OP27s. The delay is even larger when the gain is high presunmably because of the limited GBW.

  14953   Tue Oct 8 17:59:29 2019 KojiUpdateCDSCM servo board testing (portal)

== Test Status ==

[done] Whitening gain switching test
[done] AA enable/disable switching
[0th order] LO Det Mon channel check
[none] PD I/F board check
[done] QPD I/F board check
[done] CM Board
[none] ALS I/F board


The photos of the latest board can be found as Attachments 3/4

With some input signals, the functionarities of the CM servo switches were tested.

  • Latch logic works. But latch alive signal is missing.
  • IN1 enable/disable, IN2 enable/disable are properly working
  • OUT2 toggle switch for REFL1/REFL2 mon is wokring
  • Boost / Super Boosts are working
  • EXC A enable/disable, EXC B enable/disable switches are working
  • Option 1 and Option 2 now isolate the input when either is enabled (as there is no option board)
  • 79Hz-1.6kHz pole zero pair works fine
  • OUT1 works fine
  • Disable/Enable switch for the fast path works
  • Polarity switch works
  • AO Gain property changes the gain
  • Limitter switch works (Attachments 4/5). The limitter clipps the output at 4~4.5V. The Limitter indicator also works.

After the tests the LSC cables were reconnected (Attachment 6)

  14955   Tue Oct 8 18:42:39 2019 KojiUpdateCDSCM servo board testing

The boost filters of the CM servo board were tested. Their ZPK models were made.


The transfer functions of the boost filters were measured with the SG output of a SR785 connected to IN1. The IN1 gain was set to be 0dB. The transfer function was taken between the IN1 input and the TEST1A output.
With no boost and normal boost, the input signal amplitude was fixed to 20mVpk. For the other boosts, however, I could expect large gain variation through a single sweep. Therefore automatic SG amplitude tracking was used. The target was to have the output to be 1V with maximum amplitude of 100mV.

Attachment 1 shows the measured transfer functions.

The pole and zero frequencies of the boosts were estimated using LISO. Here the TFs were normalized by the TF of 'no boost' to cancel the delay of the other stages including that of the monitor channel.

 

ZPK model of Normal Boost:

pole 44.0597566447
zero 4.3927650910k

factor 98.8275377818

 

ZPK model of Super Boost (State1):

pole 878.5368382789
zero 17.5107366335k
factor 20.0840668188

 

ZPK model of Super Boost (State2):

pole 714.8112014271
pole 1.0147609373k
zero 13.2470941080k
zero 22.2259701828k

factor 404.5411036031
 

ZPK model of Super Boost (State3):

pole 886.3650348470
pole 420.4089305781
pole 887.8490768202
zero 8.3635166134k
zero 15.7953592754k
zero 20.5144907279k

factor 8.2051379423k

 

  14964   Thu Oct 10 23:36:02 2019 KojiUpdateGeneralWednesday cleaning work

[Jon, Yehonathan, Gautam, Aaron, Shruti, Koji]

We get together on Wednesday afternoon for cleaning the lab. Particularly, we collected e-wastes: VME crates, VME modules, old slow control cables, and other old/broken electronics. They are piled up in the office area and the cage outside rioght now (Attachments 1/2). We asked Liz to come to pick them up (under the coordination with either Gautam or Koji). Eventually this will free up two office desks.

Also, we made the acromag components organized in plastic boxes. (Attachment 3)

ELOG V3.1.3-