M4.5 EQ in LA 2020-09-19 06:38:46 (UTC) / -1d 23:38:46 (PDT) https://earthquake.usgs.gov/earthquakes/eventpage/ci38695658/executive
I only checked the watchdogs. All watchdogs were tripped. ITMX and ETMY seemed stuck (or have the OSEM magnet issue). They were left tripped. The watchdogs for the other SUSs were reloaded.
I came to the campus and Gautam notified that he just had received the alert from the vac watchdog.
I checked the vac status at c1vac. PTP3 went up to 10 torr-ish and this made the diff pressure for TP3 over 1torr. Then the watchdog kicked in.
To check the TP3 functionality, AUX RP was turned on and the manual valve (MV in the figure) was opened to pump the foreline of TP3. This easily made PTP3 <0.2 torr and TP3 happy (I didn't try to open V5 though).
So the conclusion is that RP for TP3 has failed. Presumably, the tip-seal needs to be replaced.
Right now TP3 was turned off and is ready for the tip-seal replacement. V5 was closed since the watchdog tripped.
I supplied a bottle of hand soap. Don't put water in the bottle to dilute it as it makes the soap vulnarable for cotamination.
There were two SUSs which didn't look normal.
- ITMX was easily released by the bias slider -> Shake the pitch slider and while all the OSEM values are moving, turn on the damping control (with x10 large watchdog threshold)
- ETMY has UR OSEM 0V output. This means that there is no light. And this didn't change at all with the slider move.
- Went to the Y table and tried to look at the coils. It seems that the UR magnet is detached from the optic and stuck in the OSEM.
We need a vent to fix the suspension, but until then what we can do is to redistribute the POS/PIT/YAW actuations to the three coils.
I came to the lab. The control room AC was off -> Now it is on.
Here is the setting of the AC meant for continuous running
Gautam reported that the PSL HEPA stopped running (ELOG 15592). So I came in today and started troubleshooting.
It looks like that the AC power reaches the motors. However, both motors do not run. It looks like the problem exists in the capacitors, the motors, or both.
Parts specs can be found in the next ELOG.
Attachment 1 is the connection diagram of the HEPA. The AC power is distributed by the breaker panel. The PSL HEPA is assigned to use M22 breaker (Attachment 2). I checked the breaker switch and it was (and is) ON. The power goes to the junction box above the enclosure (Attachment 3). A couple of wires goes to the HEPA switch (right above the enclosure light switch) and the output goes to the variac. The inside of the junction box looked like this (Attachment 4).
By the way, the wires were just twisted and screwed into a metal threaded (but isolated) caps (Attachment 5). Is this legit? Shouldn't we use stronger crimping? Anyway, there was nothing wrong with the caps w.r.t the connection for now.
I could easily trace the power up to the variac. The variac output was just fine (Attachment 6). The cord goes from the variac to the junction box (and then HEPAs) looked scorched. The connection from the plug to HEPAs was still OK, but this should be eventually replaced. Right now the cable was unplugged after the following tests for the safety reason.
The junction box for each HEPA unit was opened to check the voltage. The supply voltage came to the junction boxes and it was just fine. In Attachments 8 & 9, the voltages look low but this is because I just turned the variac only a little.
At the (main) junction box, the resistances of the HEPAs were checked with the Fluke. As the HEPA units are connected to the AC in parallel, the resistances were individually checked as follows.
The coils were not disconnected (... I wonder if the wiring of South HEPA was flipped? But this is not the main issue right now.)
By removing the pre-filters, the motors were inspected Attachments 10 & 11. At least the north HEPA motor was warm, indicating there was some current before. A capacitor was connected per motor. When the variac was tuned up a bit, one side of the capacitor could see the voltage. I could not judge which has the issue between the capacitor and the motor.
Dimensions / Specs
- HEPA unit dimentions
- HEPA unit manufacturer
Here is the timeline. This suggests TP2 backing RP failure.
1st line: TP2 foreline pressure went up. Accordingly TP2 P, current, voltage, and temp went up. TP2 rotation went down.
2nd line: TP2 temp triggered the interlock. TP2 foreline pressure was still high (10torr) so TP2 struggled and was running at 1 torr.
3rd line: Gautam's operation. TP2 was isolated and stopped.
Between the 1st line and 2nd line, TP2 pressue (=TP1 foreline pressure) went up to 1torr. This made TP1 current increased from 0.55A to 0.68A (not shown in the plot), but TP1 rotation was not affected.
Tue evening from 4pm~6pm, Koji made a social distant tour for Anchal. We were present around the PSL/AS/ETMX tables.
Is it better than Luxor? https://labcit.ligo.caltech.edu/~jharms/luxor.html
The two ITM spares and two ETM spares are together stored in the optic storage (B110) at Downs. c/o Liyuan and GariLynn
The AC cord from the PSL HEPA variac to the junction box was replaced.
Now the HEPA is running at 70%
Showed up at the 40m at 7pm
Closing the work
Leaving the 40m at 9:30pm
Memo: 40m wiring/Mask/Camera/Red Pitaya/Particle Counter
I'll bring a file binder "40m wiring diagram" to home at the next chance.
There is another one on the shelf in the control room.
(I thought I put it in my bag, but it looks like that I left it somewhere around the fax area)
Alaska M7.5 20:54UTC https://earthquake.usgs.gov/earthquakes/eventpage/us6000c9hg/executive
I looked at the suspensions. The watchdogs have not been tripped.
IMC was locked but continually shaken. (and occasional unlock)
I set up an action cam (DJI OSMO Pocket) and brought it back to the 40m. The kit is now placed in the control room cabinet together with the Canon DSLR.
I might have left the USBC chaging cable at home this time. Will bring it back next time.-> The cable was returned to the kit on Oct 23rd.
We wanted to track down the excess noise seen in MC_F and other places (see the previous report by Gautam)
Setup1: The IMC was locked and MC_F signal between 500 and 1500Hz was observed. The DTT template was saved as /users/Templates/MC/MCF_noise_201023.xml
- Suspected mech resonance/jitter coupled with clipping or any other imperfections. Poked the various optics and optomechanics on the table. Basically no change. If we tap the laser chassis and the optics close to the laser source, we occasionally unlocked the IMC
- When we touched (lifted) the Innolight controller box from the shelf, for the first time we saw a significant change in the shape of the noise spectrum. The peak around the 700Hz shited towards lower frequency by a few %. Other peaks have no obvious change in the shapes and the heights.
- While observing the MC_F signal on the laptop, we went to the back of the laser controller. Placing a hand close to the fan clearly changes the peak frequency lower. By temporarily disconnecting the fan from the power supply for a short moment, the 700Hz peak could be eliminated. We also tried to see the noise level with the slow thermal servo and diagnosis DB cable disconnected, but we didn't see any significant change of the noise level.
Setup 2: Using the ALS phase tracker, we can observe the relative freq noise of the PSL laser and the ETMY AUX laser without any servo involved. This way we can freely disconnect any cables from the lasers. The measurement template for DTT was saved as /users/Templates/ALS/Y_ALS_FINE_PHASE_OUT_102320.xml
- Noise spectrum before disconnecting the cable (REF0, RMS REF1)
- The Fast PZT input to the PSL was disconnected => This made all the peaks (including the 700Hz) disappeared (REF2, RMS REF3)
- The Fast PZT input was restored as before, then the chain was disconnected at the input of the HV PZT driver (Thorlabs) => Again, this made the peaks disappeared (REF4, RMS REF5)
- The chain was disconnected at the input of the TTFSS box => Again, this made the peaks disappeared (REF6, RMS REF7)
- Disconnected the demod input and the AO cables from the IMC servo board => This made the peaks came back (REF8)
- Disconnected all the input/peripheral cables from the IMC servo board except for the connection to the TTFSS box => Still the excess noise was observed (REF9)
- In addition to the above, the cable to the FSS box was disconnected but the ground was still touching the MC servo board => This made the peaks disappeared (REF10)
The conclusion is that the noise is injected from the main circuit of the IMC servo board.
Next time we will check if the backplane connection is doing something wrong. Also, we'll test if the presence of the RF signals does something bad to the IMC board via EMI and RFI.
We have reverted the connection and tested if we lock the IMC and Y arm. ==> We saw at least they were locked for a short period. The things are still stabilizing, but left them turned on so they keep trying to lock automatically for the night.
The particle counter on the 40m PSL was removed. The package was made together with the OMC lab particle counter (see the packing list below).
The kit was picked up by Radhika for a python code to read out the numbers.
=== Packing List ===
In fact, the problem was the grounding issue (presumably on the IOO racks).
A temporary differential receiver at the TTFSS side was built using an SR560 and a few ponoma cables. This removed the structures ~850Hz.
The MC Servo Output was disconnected from the TTFSS box and monitored with SR785. The 850Hz structure was kept visible no matter what cables, including all the acromag DB cables, were removed. This made me suspicious about the measurement setup. The SR785 was connected to an AC power strip under the SP table and this was too far from the IOO rack.
The SR785 was connected to the AC power strip on 1X2, and now the difference becomes clear. No matter if the acromag cables are connected or not, the connection (particularly ground connection) between the MC servo module and the TTFSS box causes the MC servo output contaminated. (Comparison between Blue and Orange of Attachment #1). During the measurement, the EPICS switch for the fast path was disengaged (=no signal) and the VCO gain (...so called. It's just the MC Servo Gain) was set to be 0dB.
To test if the differential receiving of the MC Servo Output at the PSL helps to reduce this noise, I've built a simple (hacky) differential receiver using an SR560. (Attachment #2)
This kept the noise level same as the disconnected case (Comparison between Green and Orange of Attachment #1, I don't think the difference between them is not significant), while the IMC is locked as before.
Note that we can see that the 36kHz line was significantly reduced. Did we remove this annoying noise?
After talking with Gautam, we decided to leave this configuration while the SE-Diff cable was replaced with a more robust one. (See Attachment #3)
The PSL laser frequency performance was evakluated in the following two ways as we did last week:
1) Use the beat frequency of the free running PSL and the Y-end laser (Attachment #4). The PSL shutter was closed and thus the IMC was not locked.
2) Use the IMC MCF while the IMC was locked. (Attachment #5)
For both cases, the improvement was confirmed.
I also tried to check the reported issue by Gautam on this elog. He used 1Hz BW, but I cheated with 16Hz BW and 10x12.8kHz span PSDs. (Attachment #6)
For the measurement, IN1 GAIN of the IMC Servo was set to be 0dB and the OUT2 was switched to monitor the IN1 noise, while IN1 was terminated by a 50Ohm.
As I mentioned above, the AC power of SR785 was taken from a 1X2 power strip. Is this the reason for the power line forest look less severe compared to the previous case???
Anyway, I tried to use the same differential receiving technique (but with gain of x100) to see if this helps. The differential receiver helped to reduce the structure above 50kHz. The floor noise level was observed to be higher. I didn't pursue this any further, but the forest of the power line looked like a part of the measurement noise. This is indicative that the grounding condition on 1X2 is really not great and we need to review the configuration of the acromag grounding.
I'm starting the model restarts from remote. Then later I'll show up in the lab to do more hard resets.
==> It seems that the RFM errors are gone. Here are the steps.
At this point, I'm leaving the lab. All the suspensions (incl SRM) are aligned. PSL/GRX/GRY shutters were left open.
I believe the mirror next to IM1 is for the green beams to be delivered to the PSL table. I think we still want to keep it. Otherwise, the plan looks fine.
> I didn't bother to align the green beams to the arm cavities or re-center the Oplevs - is this necessary? It is a step in the pre-close up checklist, so maybe we should do it... The green transmission does reach the PSL table...
I don't think so. The beam is reaching the PSL, so we have no motivation to change the green alignment. Regarding the oplev, the green refl should come back to the PDH PD and this gives us additional beam reference. As soon as we find the green resonance after the pumping, we can tweak the green axis so that the spots on the mirrors become reasonable (as well as the green trans CCD on the PSL table).
Main volume pressure as of 11:30AM 2020/11/10
Yes. The datasheet has a recommendation circuit with 10uF caps. Companies are careful to show reproducible, reliably functional circuit examples on datasheets. So, if the caps are there you should try to replicate the design.
Additional bypass capacitors? I use 0.1 uF, 700V DC ceramic capacitors as bypass capacitors close to the leads of the PA95, as is recommended in the datasheet. Can adding a 10uF capacitor in parallel provide better filtering? I'm not sure if one with compatible footprint and voltage rating is readily available, I'll look around.
Basically, they repeated our specs and showed the coating performances for HR/AR for 10deg P and PR/AR for 45deg P. There is no RoC measurement by the vendor.
Nevertheless, their RoC (paper) specs should be compared with our request.
Last week and this week I've been working on the characterization of the Q3000 QPDs. The QPDs were named 81, 82, 83, and 94.
My recommendation is to use #81 and #84 as they have similar dark current characteristics between the segments. But basically, all the QPDs look fine.
The actual junction capacitance and the RF dark noise should be characterized by the actual WFS head circuit.
The QPD packages were labeled and returned to Gautam to be implemented in the WFS heads.
gautam: S/N #84 was installed as the AS WFS QPD. The remaining 3 are stored in the clean cabinet at EX (where the rest of the RF photodiodes are).
I got a bit confused by your description.
The demod board claims that the nominal power at each LO port is 10dBm. So we want to give at least 16dBm to the (external?) 4way power splitter, but we only have 15dBm. As you said, the actual LO power reaching the FET mixier (PE4140) is the level of ~20dBm. But you said the requirement for the mixer is -7dBm. So are you proposing to reduce the LO level (slightly) than the LIGO recommendation because the minimum for PE4140 is -7dBm?
If that's the message, then I can say "yes". We supply 8~9dBm to the LO ports instead of 10dBm. I suppose the mixers don't care about this level of reduction.
Looking at my original post [40m ELOG 11817], the necessary modification is much larger than you have indicated in your post (as yours is the modification of my modification plan.)
If you do your modification you have to deal with the components rearrangement in the chassis. I think you can still accomplish it as you are going to remove an amplifier and gain the space from it.
The main RF line still has 5dBm Attn. How about to insert another 3dB power splitter there and create a spare 55MHz port for the future use?
Before doing any modification you should check how much the distributed powers are at the ports.
Also your modification will change the relative phase between 11MHz and 55MHz.
Can you characterize how much phase difference you have between them, maybe using the modulation of the main marconi? And you might want to adjust it to keep the previous value (or any new value) after the modification by adding a cable inside?
Let's use RG405 for better shielding. It is not too stiff. The bending (just once) does not break the cable.
Are you going to full replacement of the 55MHz system? Or just remove the 7dBm and then implement the proposed modification for the 55MHz line?
1. That's true. But we are already in that regime with the Var attn at 0dB, aren't we? We can reduce the input to the amp by 1-2dBm sacrificing the EOM out by that amount (we can compensate this for the demo out by removing the 1dB attn).
2. Not 100% sure but one possible explanation is that we wanted to keep the Marconi output large (or as large as possible) to keep the SNR between the signal and the noise of the driver in Marconi. The attenuator is less noisy compared to the driver noise.
3. My guess is that theoretically we were supposed to have 13dBm input and 20dBm output in design. However, the actual input was as such. We can restore it to the 13dBm input.
I checked the backplane connection for IMC WFS2 and found that the cables for IMC WFS2 and the IMC demod were swapped during my IMC noise hunting activities. I reverted it just now.
But we need to check if this damaged anything such as the WFS2 head, the WFS2 demod, etc, once the IMC locking is back.
I have the setup built for the AA/AI board testing around the PD testing area. Please let me leave it like that for a week or so.
12/4 TF Tested 5 PCBs
12/6 TF Tested 19 PCBs (12min/PCB) - found 1 failure (S2001479 CH1) -> Fixed 12/11
12/8 TF Tested 16 PCBs (12min/PCB)
PSD Tested 4 PCBs (11min/PCB)
12/11 TF Tested 10 PCBs + 1 fixed channel (All channels checked)
PSD Tested 10 PCBs (11min/PCB)
12/14 PSD Tested 4 PCBs (6.5min/PCB) fixed noise issue of 2 ch, TF issue of 1 ch
12/15 PSD Tested 32 PCBs (6.5min/PCB) fixed noise issue of 1ch
Temp dependence measurement
Our favorite (flexible) RF cable is Belden's 1671J (Jacketed solder-soaked coax cable). It is compatible RG405. I'm not sure if there is off-the-shelf SMA cables with 1671J.
I wanted to check the functionality of the IMC WFS. I just turned on the WFS servo loops as they were. For the past two hours, they didn't run away. The servo has been left turned on. I don't think there is no reason to keep it turned off.
How about resurrecting the PSL table green beat for the X arm to see if the non-fiber setup shows the same level of the freq noise (e.g. the PDH locking became super noisy due to misalignment etc).
If the sensing noise level of the end PDH degraded for some reason, it'd make the out of loop stability worse without making the end pdh error level degraded.
It's just speculation.
You can remove the components of the optical table enclosure (black ones) and use the optical table as your working area too.
I worked around the racks and the feedthru flanges this afternoon and evening. This inevitably crashed c1lsc real-time process.
Rebooting c1lsc caused multiple crashes (as usual) and I had to hard reboot c1lsc/c1sus/c1ioo
This made the "DC" indicator of the IOPs for these hosts **RED**.
This looked like the usual timing issue. It looked like "ntpdate" is not available in the new system. (When was it updated?)
The hardware clock (RTC) of these hosts are set to be PST while the functional end host showed UTC. So I copied the time of the UTC time from the end to the vertex machines.
For the time adjustment, the standard "date" command was used
> sudo date -s "2021-02-03 07:11:30"
This made the trick. Once IOP was restarted, the "DC" indicators returned to **Green**, restarting the other processes were straight forward and now the CDS indicators are all green.
controls@c1iscex:~ 0$ timedatectl
Local time: Wed 2021-02-03 07:35:12 UTC
Universal time: Wed 2021-02-03 07:35:12 UTC
RTC time: Wed 2021-02-03 07:35:26
Time zone: Etc/UTC (UTC, +0000)
NTP enabled: yes
NTP synchronized: no
RTC in local TZ: no
DST active: n/a
:~ 0$ timedatectl
Local time: Wed 2021-02-03 07:35:12 UTC
Universal time: Wed 2021-02-03 07:35:12 UTC
RTC time: Wed 2021-02-03 07:35:26
Time zone: Etc/UTC (UTC, +0000)
NTP enabled: yes
NTP synchronized: no
RTC in local TZ: no
DST active: n/a
NTP synchronization is not active. Is this OK?
With the recovered CDS, the IMC was immediately locked and the autolocker started to function after a few pokes (like manually running of the "mcup" script). However, I didn't see any light on the AS/REF cameras as well as the test mass faces. I'm sure the IMC alignment is OK. This means the TTs are not well aligned.
So, burtrestored c1assepics with 12:19 snapshot. This immediately brought the spots on the REFL/AS.
Then the arm were aligned, locked, and ASSed. I tried to lock the FP arms. The transmissions were at the level of 0.1~0.3. So some manual alignment of ITMY and BS were necessary. After having the TRs of ~0.8, I still could not lock the arms. The signs of the servo gains were flipped to -0.143 for X arm and -0.012 for Y arm, and the arms were locked. ASS worked well and the ASS offsets were offloaded to the SUSs.
Really!? I didn't reboot the machines between "sudo date" and "rtcds start c1x0*". I tried rtcds. If it didn't work, it used date. Then tried rtcds. (repeat) The time was not synched at all wrt the time zones and also the time. There were 1~3 sec offset besides the TZ problem.
Testing the satellite amp i.e. PD driver
- To test the noise of the PD transimpedance amps: Leave the PD input open (do not short the terminal goes to the PD)
- To test the current noise of the LED drivers: Short the output with an appropriate Rs to have the nominal current.
- To test the overall noise level together with the LED/PD pair: Connect the dummy OSEM module.
Testing the coil drivers
- Short the output with an appropriate Rs.
The curie temp of SmCo seems about x2 (in K) of the one for NdFeB. i.e. 600K vs 1000K. So I believe 177degC = 450K is not an issue. Just make sure the curie temp, referring the specific property for the magnets from this company. (You already know the company from the procurement doc). It'd be great if you upload the doc on the 40m wiki.
Note from today's meeting:
1. Can we adjust the thickness of the cylindrical hole for the mirror to move the COM in the plane of the wires. (We should be able to do that)
2. Please check how much we can displace the COM by the bottom dumbbell.
For your planning:
Yeah, it's really inconsistent. You had 35mA LED drive and the current noise of the noisy channel was 5e-7 A/rtHz at 1Hz. The RIN is 1.4e-5 /rtHz. The approx. received photocurrent is 30uA as we discussed today and this should make the noise around 4e-10 A/rtHz at 1Hz. However, the readout noise level is better than this level. (well below 1e-10 A/rtHz)
BTW, the IMC seemed continuously locked for 5 hours. Good sign.
Todd provided us a bunch of electronics. I went to Downs to pick them up this afternoon and checked the contents in the box. Basically, the boxes are pretty comprehensive to produce the following chassis
Some panels are missing (we cannibalized them for the WFS electronics). Otherwise, it seems that we will be able to assemble these chassis listed.
They have placed inside the lab as seen in the attached photo.
HAM-A COIL DRIVER (Req Qty 28+8)
- 8 Chassis
- 8 Front Panels
- 8 Rear Panels
- 8 HAM-A Driver PCBs
- 8 D1000217 DC Power board
- 8 D1000217 DC Power board
16bit AA (Req Qty 7)
- 7 CHASSIS
- 6 7 Front Panels (1 missing -> [Ed 2/22/2021] Asked Chub to order -> Received on 3/5/2021)
- 7 Rear Panels
- 28 AA/AI board S2001472-486, 499-511
- 7 D070100 ADC AA I/F
- 7 D1000217 DC Power board
18bit AI (Req Qty 4)
- 4 CHASSIS
- 4 Front Panels
- 4 Rear Panels
- 8 AA/AI board S2001463-67, 90-92
- 4 D1000551 18bit DAC AI I/F
- 4 D1000217 DC Power board
- bunch of excess components
16bit AI (Req Qty 5)
- 5 CHASSIS
- 4 5 Front Panels (D1101522) (1 missing -> [Ed 2/22/2021] Asked Chub to order -> Received on 3/5/2021)
- 3 5 Rear Panels (D0902784) (2 missing -> [Ed 2/22/2021] Asked Chub to order -> Received on 3/5/2021)
- 10 AA/AI board S2001468-71, 93-98
- 5 D1000217 DC Power board
- 5 D070101 DAC AI I/F
Internal Wiring Kit
Asked Chub to order:
- Qty 12 1U Hamilton Chassis
- Qty 5 x Front/Rear Panels/Internal PCBs for D1002593 BIO I/F (The parts and connectors to be ordered separately)
-> Front/Rear Panels received (3/5/2021)
-> PCBs (unpopulated) received (3/5/2021)
-> Components ordered by KA (3/7/2021)
We want to move the CoM with the adjustment range so that the residual deviation is adjusted by the bottom dumbbell. 0.0003" is well within the range and good enough.
Jordan's screenshot actually shows that the vertical distance (Y) is 0.0000". We want to have the vertical distance of CoM from the wire clamping point to be 0.9mm in the nominal SOS design (this might need to be adjusted to have a similar pitch resonant freq for the different inertia of moment). Let's say it is ~mm ish.
The full range of the bottom dumbbell adjustment gives us the CoM adjustment range of +/-0.002” = +/-50um. This corresponds to an alignment range of +/-50mrad. And we want to set it within +/-500urad.
So we need to adjust the dumbbell position with the precision of 1/100 of the full range (precision of 0.5um).
The groove does not extend to the top of the clamp. The groove shallower than the wire diameter cause the hysteresis of the alignment. Also, the material of the pieces should be stainless steel. Al clamp is softer than the wire and will cause the groove to be dug on the material, causing increased bending friction and hysteresis again.
Saying, all of our suspended masses with Al stand-offs are suffering this issue to some extent. That was the reason to buy the ruby standoffs.
We received currently available sets. We are supposed to receive more coil drivers and sat amps, etc. But they are not ready yet.
I can't obtain a consistent view between the existing drawings/photographs and your pin assignment. Please review the pin assignment again to check if yours is correct.
Looking from the back side and the wires are going down, the left bottom pin is "Coil Start" and the upper right adjacent pin is "Coil End". (See attachment)
So in your picture 1 should be the coil start and 4 should be the coil end, but they are not according to your table.
This is my current understanding of the in-vacuum wiring:
2. From the above facts, the in-vacuum cable is
Accuglass has the DSUB25 F-F cable off-the-shelf. However, this cable mirrors the pinout (see the datasheet on the pdf in the following link)
3. The options are
- ask Accuglass to make a twisted version so that the pinout is not mirrored.
- combine Accuglass female-male cable (https://www.accuglassproducts.com/connector-connector-extension-cable-25-way-femalemale) and a gender changer (https://www.accuglassproducts.com/gender-adapter-25d)
4. The length will be routed from the feedthrough to the table via the stacks like a snake to be soft. So, it will require some extra length.
5. Also, the Accuglass cables don't have a flap and holes to fix the connector to a cable post (tower). If we use a conventional 40m-style DSUB25 post (D010194), it will be compatible with their cables. But this will not let us use a DSUB25 male connector to mate. In the future, the suspension will be upgraded and we will need an updated cable post that somehow holds the connectors without fastening the screws...