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ID Date Authorup Type Category Subject
  8079   Wed Feb 13 19:30:45 2013 KojiSummaryGeneralpossible explanations to oval REFL beam

>> "What has changed since:"

Recently the REFL path has been rearranged after I touched it just before Thanksgiving.
(This entry)

If the lenses on the optical table is way too much tilted, this astigmatism happens.
This is frequently observed as you can find it on the POP path right now.

Also the beam could be off-centered on the lens.

I am not sure the astigmatism is added on the in-air table, but just in case
you should check the table before you put much effort to the in-vacuum work.

  8089   Fri Feb 15 16:09:19 2013 KojiUpdateGeneralbeam traps ready to be installed

For the hexagonal one, insert one of the glass plate only half. Use a 1"x.5" piece if exists.

For the diamond one, you don't need the forth glass piece.

 

Attachment 1: HexBeamDump.pdf
HexBeamDump.pdf
Attachment 2: DiamondBeamDump2in.pdf
DiamondBeamDump2in.pdf
  8100   Mon Feb 18 21:43:05 2013 KojiUpdateAlignmentPOP path set up but AS55 is broken

I undertook the investigation of the AS55 PD. I found the PD is not broken.

I tested the PD on the PD test bench and it works just fine.

I attatched the characterization result as there has been no detailed investigation of this PD as far as I remember.

The transimpedance gain at 55MHz is 420Ohm, and the shotnoise intercept current is 4.3mA.

Attachment 1: AS55.pdf
AS55.pdf AS55.pdf AS55.pdf
  8104   Tue Feb 19 05:42:28 2013 KojiUpdateElectronicsPOP path set up but AS55 is broken

10010 Ohm for POP55 vs 50 Ohm for AS55 (cf. http://nodus.ligo.caltech.edu:8080/40m/4763)

I wonder if you used an LED flash light, which emits no IR.

  8106   Tue Feb 19 08:42:31 2013 KojiUpdateVACETMX door open

[Steve, Yuta, Koji]

The ETMX heavy door was removed.

  8134   Thu Feb 21 21:12:42 2013 KojiUpdateVACpumpdown at 230 Torr

[Rana, Yuta, Koji]

21:05 at the pressure of 10torr
V3 closed. RV1 manually closed. RPs were turned off. And the bellows between RV1 and the rughing pumps are disconnected.

  8144   Sat Feb 23 14:04:07 2013 KojiUpdateComputersapache retarted (Re: linux1 dead, then undead)

apache has been restarted.
How to: search "apache" on the 40m wiki

Quote:

I had to reboot nodus to get it recovered

 

  8156   Mon Feb 25 13:01:39 2013 KojiSummaryGeneralQuick, compact, and independent tasks

- IMC PDH demodulation phase adjustment

- Permanent setup for green transmission DC PDs  on the PSL table

  8166   Tue Feb 26 02:04:51 2013 KojiUpdateLockingPRMI locked

One of the biggest issues we had was that any Q signals (i.e. the quadrature where PRCL is absent.) of REFL11/33/55/(165) haven't been consistent each other.
i.e. We never had reliable lock of MICH with REFL_any_Q, regardless of the resonant condition. This is definitely one of the things to be tried in order to prepare for the full lock.

We don't trust any demodulation phases of any PDs any more as the previous PRC mode (or say, absence of the stable mode) was unreasonable to determine any of the demodulation phases.

I remember that the POP DC saturates at 27000. You may need to reduce the gain switch again.

The AS OSA and/or POP BBPD would be useful for the sideband PR gain estimation.

  8187   Wed Feb 27 18:01:46 2013 KojiUpdate Photodiode transimpedance

How much is the exact resonant frequency?

And what's the unit of the plot? The resonant "transimpedance" in the unit of Ohm can not be ~100.

  8198   Thu Feb 28 03:41:31 2013 KojiUpdateLSCPR gain ~ 25 from PRMI carrier lock

VERY GOOD!
This is how the carrier lock PRMI should look like.

- There is more room to improve the differential ITM alignment to make the dark port more dark, then you will gain more PRG

- The AS spot is definitely clipped.

  8239   Wed Mar 6 09:44:29 2013 KojiUpdateLSCPRMI locking for g-factor measurement

- What about normalizing POPDC to indicate the carrier recycling gain?

- When you align the PMC, confirm FSS SLOW DC is around zero. Some region of the slow thermal actuation makes the laser source emit at multiple frequencies. In the case, the cavity visibility get worse.

- Do you guys think we can determine if the TT is longitudinally quiet enough? Is there any comparison between the simple Michelson and the PRC motion in m/rtHz?

  8247   Wed Mar 6 22:11:19 2013 KojiUpdateElectronicsPOX whitening was fine all along

At the time you, den and I worked together, we could not lock the X-arm on TEM00 with the FM1s of the POX11 on.
We could lock the arm only on the higher order mode but he gain was low. Once we turned off the FM1s, we immediately
locked the cavity on TEM00.

Don't you have the direct measurement of the TF with FM1 on and off?

  8251   Thu Mar 7 16:55:28 2013 KojiUpdateLockingErudite discussion on PRMI locking

PRMI for the sidebands may have different situation. Investigate our wiki to find our the simulation result.

Also I'm not confident how much is the modulation depth at 55MHz is.

  8264   Sat Mar 9 19:29:27 2013 KojiUpdatePSLModulation depth

Last night I measured the modulation depth of the MC incident beam.


Method:

The beam is taken from one of the  PO beam at the wedge plate before the IMC.
After removing the knife edge to dump this beam, the beam is sent to the west side
of the PSL table and put into the OSA cavity.
[The beam dump was returned after the measurement.]

I had some confusion and after all I use the OSA labeled as AS OSA rather than the one on the PSL table.
[The AS OSA was returned to the AP table.]

The transmission was detected by PDA255 and filtered by ITHACO 1201 preamp with G=10, no HPF, 30kHz LPF.
It was confirmed that the peak amplitudes are not reduced by the LPF filter. The resulting time series
was recorded by an oscilloscope.

Three measurements have been taken. The 11MHz peaks are offset by the carrier peak. They appropriately
removed. The ratio of the sideband and carrier peaks is converted to the modulation depth using the following formula.

P_sb / P_ca = [J1(m)/J0(m)]^2


Measurement

The modulation depth for the 11MHz: 0.190 +/- 0.003

The modulation depth for the 55MHz: 0.2564 +/- 0.0003

The three scans showed very similar numbers. That's why the statistical error is such small.
I don't think the systematic error is not such good.

This number is much different form the previous meaurement by Mirko.

http://nodus.ligo.caltech.edu:8080/40m/5519 m=0.14 (11MHz) & 0.17 (55MHz)
but the measured voltages and the modulatio depths are inconsistent.

http://nodus.ligo.caltech.edu:8080/40m/5462 m=0.17 (11MHz) & 0.19 (55MHz)

Probably the modulation depths should be checked by the IMC again.
However, it is certain that the 55MHz modulation exists, and even larger than the 11MHz one.

The next is to confirm that the modulation frequency is matched with the IMC FSR.
It is to make sure that the modulation is transmitted to the main IFO without attenuation.

Attachment 1: mod_depth.pdf
mod_depth.pdf
  8265   Sun Mar 10 13:29:29 2013 KojiHowToIOOHow to calculate the accumulated round-trip Gouy phase

How to calculate the accumulated round-trip Gouy phase (and namely the transverse mode spacing) of a general cavity
only from the round-trip ABCD matrix

T1300189

  8301   Fri Mar 15 15:26:13 2013 KojiUpdateGreen LockingYarm ALS laser is funny / dying

I took a look at the laser. It is probably the LD TEC (DTEC) failure.
As the temperature of the LD (DTMP) gradually deviated from 25degCish,
the DTEC voltage also went up from 2Vish to 2.1, 2.2... 

When DTEC reaches 3V, it stopped lasing. This cools the diode a bit, and
it start lasing but repeat the above process.

I am not sure which of the head and controller has the issue.

The situation did not improve much by reducing the pumping current (ADJ: -15).

BTW, Turning on/off the noise eater did not change the situation.

I think the head/controller set should be sent out to JDSU and find how they will say.

  8306   Mon Mar 18 13:10:19 2013 KojiBureaucracyAuxiliary lockingYend table upgrade - go fetch NPRO from ATF

1) Annalisa is going to start  working on mode profiling and beat note search for the old MOPA NPRO.

2) In the meantime, Manasa is working on the end table items. This will be reviewed by KA in the afternoon.

The laser at ATF is moved to the 40m when the status of 1) and 2) is determined by KA to be reasonable.

We also make the beat note measurement for the ATF laser too.
 

  8323   Thu Mar 21 10:19:28 2013 KojiUpdateLockingFinding the beat note

Give us more info on the elog:
What PD are you using? How much power the beams on the recombining BS are? What kind of BS is it?
How are you looking for the beat note? (on the scope? or spectrum analyzer?)
What was the scanned temp range?

Three points to be checked:

- Polarization

- Alignment

- Temperature

  8332   Fri Mar 22 19:46:29 2013 KojiSummaryLSCDiode impedance test result

I've tested Perkin-Elmer InGaAs PDs at OMC Lab.

- The diode impedances were measured with the impedance measurement kit. Reverse bias of 5V was used.

- Diode characteristics were measured between 10MHz and 100MHz.

- 4-digit numbers are SN marked on the can

- Ls and Rs are the series inductance and resistance

- Cd is the junction capacitance.

- i.e. Series LCR circuit o--[Cd]--[Ls]--[Rs]--o

C30665GH, Ls ~ 1nH

0782 Perkin-Elmer, Rs=8.3Ohm, Cd=219.9pF
1139 Perkin-Elmer, Rs=9.9Ohm, Cd=214.3pF
0793 Perkin-Elmer, Rs=8.5Ohm, Cd=212.8pF

C30642G, Ls ~ 12nH

2484 EG&G, Rs=12.0Ohm, Cd=99.1pF
2487 EG&G, Rs=14.2Ohm, Cd=109.1pF
2475 EG&G glass crack, Rs=13.5Ohm, Cd=91.6pF
6367 ?, Rs=9.99Ohm, Cd=134.7pF
1559 Perkin-Elmer, Rs=8.37Ohm, Cd=94.5pF
1564 Perkin-Elmer, Rs=7.73Ohm, Cd=94.5pF
1565 Perkin-Elmer, Rs=8.22Ohm, Cd=95.6pF
1566 Perkin-Elmer, Rs=8.25Ohm, Cd=94.9pF
1568 Perkin-Elmer, Rs=7.83Ohm, Cd=94.9pF
1575 Perkin-Elmer, Rs=8.32Ohm, Cd=100.5pF

C30641GH, Perkin Elmer, Ls ~ 12nH

8983 Perkin-Elmer, Rs=8.19Ohm, Cd=25.8pF
8984 Perkin-Elmer, Rs=8.39Ohm, Cd=25.7pF
8985 Perkin-Elmer, Rs=8.60Ohm, Cd=25.2pF
8996 Perkin-Elmer, Rs=8.02Ohm, Cd=25.7pF
8997 Perkin-Elmer, Rs=8.35Ohm, Cd=25.8pF
8998 Perkin-Elmer, Rs=7.89Ohm, Cd=25.5pF
9000 Perkin-Elmer, Rs=8.17Ohm, Cd=25.7pF

 

Note:  Calculated Ls&Rs of straight wires
  1mm Au wire with dia. 10um -> 1nH, 0.3 Ohm
20mm BeCu wire with dia. 460um -> 18nH, 0.01 Ohm

  8349   Tue Mar 26 01:40:49 2013 KojiUpdateIOOTuning MC length/FSR

I'm still waiting for the follow-up analysis of the modulation freq tuning.

  8357   Tue Mar 26 17:27:17 2013 KojiUpdateIOOTuning MC length/FSR

Please add the discussions on the cavity absolute length (and its change, adjustment precision),
identification of the peaks, before/after comparison of the plot, the effect of the MC REFL PD response,
and comparison of the cavity linewidth vs deviation of the 55MHz SBs from the resonance.

  8388   Tue Apr 2 11:08:16 2013 KojiUpdateLSCPRMI lock

> The two REFL55 signals

Wow! It's a good news.
I think this is our first ever lock of PRMI with the REFL I/Q signals.

We kept having difficulty to obtain MICH from the REFL beam.

Next time could you make calibration of REFL55 MICH and AS55 MICH and compare the ratio with any simulation?

  8406   Wed Apr 3 18:27:03 2013 KojiUpdate QPD Voltage Regulators

Breadboards may not be suitable for a reliable work. Why don't you switch to any protoboard and real soldering?

  8413   Thu Apr 4 10:46:54 2013 KojiSummaryLSCREFL55 error signals

Beautiful double peaks. I don't see the triple zero-crossings. Is this because you adjusted the phase correctly (as predicted)?

Don't you want to have a positive number for POP22? Should we set the demod phase in the configuration script for the positive POP22, shouldn't we?

  8468   Mon Apr 22 11:26:25 2013 KojiConfigurationCDSsome RT processes restarted

When I came to the 40m, I found most of the FB signals are dead.

The suspensions were not dumped but not too much excited. Use watchdog switches to cut off the coil actuators.

Restarted mxstream from the CDS_FE_STATUS screen. The c1lsc processes got fine. But the FB indicators for c1sus, c1ioo, c1iscex/y are still red.

Sshed into c1sus/ioo, run rtcds restart all . This made them came back under control.

Same treatment for c2iscex and c1iscey. This made c1sus stall again. Also c1iscey did not come back.

At this point I decided to kill all of the rt processes on c1sus/c1ioo/c1iscex/c1iscey to avoid interference between them.
And started to restart from the end machines.

c1iscex did not come back by rtcds restart all.
Run lsmod on c1iscey and found c1x05 persisted stay on the kernel. rmmod did not remove the c1x05 module.
Run software reboot of c1iscey. => c1iscey came back online.

c1iscey did not come back by rtcds restart all.
Run software reboot of c1iscex. => c1iscex came back online.

c1ioo just came back by rtcds restart all.

c1sus did not come back by rtcds restart all.
Run software reboot of c1sus => c1sus came back online.

This series of restarting made the fb connections of some of the c1lsc processes screwed up.
Run the following restarting commands => all of the process are running with FB connection.
rtcds restart c1sup
rtcds restart c1ass
rtcds restart c1lsc

Enable damping loops by reverting the watchdog switches.

All of the FE status are green except for the c1rfm bit 2 (GE FANUC RFM CARD 0).

  8469   Mon Apr 22 11:46:09 2013 KojiSummaryIOOMC locked/aligned. MC WFS offloading by ezcaservo

Еру ьс шы тщц дщслув фтв фдшптувю

Фдыщ ш кфт еру ащддщцштп ыскшзе ещ щаадщфв еру ЬС ЦАЫ ыукмщю

I blame Den for russian keyboard installation on the control machines.

ezcaservo -r 'C1:SUS-MC2_ASCPIT_OUT16' -g '0.00001' -t 60 C1:SUS-MC2_PIT_COMM&
ezcaservo -r 'C1:SUS-MC2_ASCYAW_OUT16' -g '0.00001' -t 60 C1:SUS-MC2_YAW_COMM&
ezcaservo -r 'C1:SUS-MC1_ASCPIT_OUT16' -g '0.00001' -t 60 C1:SUS-MC1_PIT_COMM&
ezcaservo -r 'C1:SUS-MC1_ASCYAW_OUT16' -g '0.00001' -t 60 C1:SUS-MC1_YAW_COMM&
ezcaservo -r 'C1:SUS-MC3_ASCPIT_OUT16' -g '0.00001' -t 60 C1:SUS-MC3_PIT_COMM&
ezcaservo -r 'C1:SUS-MC3_ASCYAW_OUT16' -g '0.00001' -t 60 C1:SUS-MC3_YAW_COMM&

  8470   Mon Apr 22 12:03:58 2013 KojiUpdatePSLPMC aligned too

PMC aligned. C1:PSL-PMC-PMCTRANSPD improved from 0.72ish to 0.835ish.

  8482   Wed Apr 24 00:44:33 2013 KojiUpdateSUSPRMI locked, ITMX pitch OpLev ringing up

I tried to reproduce the locking situation described in this entry tonight.
The momentary lock was regularly seen but there was no stable lock.

I wonder why the actuators are always saturated. The feedback signals have the dominant component at ~400Hz.

It would also be nice if the servos have some immunity to gain fluctuation.

I didn't check how the situation of the AP table is. I'll look into some details tomorrow.

  8483   Wed Apr 24 14:20:49 2013 KojiUpdateCDSFE Web view not updated?

The FE web view seems not up-to-date, does it? ( maybe for a year)

https://nodus.ligo.caltech.edu:30889/FE/c1mcs_slwebview_files/index.html

  8487   Wed Apr 24 18:51:12 2013 KojiConfigurationoptical tablesPD frequency response

The fibers should be routed beneath the electrical cables.
They should be fixed on the table for strain relieving.
The slack of the fibers should be nicely rolled and put together at the splitter side.

These are expected to be done next time when the fiber team work around the table.

We also expect to have the table photo every time the work of the day is finished.

  8491   Thu Apr 25 10:19:10 2013 KojiSummaryLSCLocking activity on Apr 24th

Last night I worked on the several locking configurations:

General preparations / AS table inspection

- The AS beam looked clipped. I went to the AP table and confirmed this is a clipping in the chamber.
  This may be fixed by the invacuum PZTs.

Modulation frequency tuning

RFPD Mon of the MC demodulator was check with the RF analyzer. Minimized the 25.8MHz (=55.3-29.5MHz) peak by changing the marconi freq.
This changed the modulation freq from 11.066147MHz to 11.066134MHz. This corresponds to the change of the MC round-trip length from
27.090952m to 27.090984m (32um longer).

Michelson tests

- I wonder why I could not see good Michelson signal at REFL ports.

- I roughly aligned the Michelson. On the AP table, the RF analyzer was connected to the REFL11 RF output.
  By using "MAX HOLD" function of the analyzer, I determined that the maximum output of the 11.07MHz peak
  was -61.5dBm.

- I went to the demodboard rack. I injected -61dBm from DS345 into the RFEL11 demodboard. This produced
  clean sinusoidal wave with the amplitude of 4 count. The whitening gain was 0dB.

- The output from the PD cable was -64.0dBm. So there is ~2.5dB loss in the cable. Despite this noise, the demodulation
  system should be sufficiently low noise. i.e. the issue is optical

- The Michelson was locked with AS55Q. And the REFL11 error signals were checked.Fringe like feature was there.
  This suggested the scattering from the misaligned PRM. The PRM was further misaligned. Then some reasonable
  (yet still noisy) Michelson signal appeared. (Usual misaligned PRM is not at the right place)

  Q. How much scattering noise (spurious cavity between PRM and the input optics) do we have when the PRM is aligned?
  Q. Where should we put the glass beam dumps in the input optics?
  Q. Can we prepare "safe" misaligned place for the PRM with the beam dump?

- The Michelson was locked with REFL11Q. From the transfer function measurement, the gain difference between AS55Q (whitening gain 24dB)
  and REFL11Q was 32dB. The whitening gain was 0dB. In fact I could not lock the Michelson with the whitening gain 33dB (saturation???)
  The element in the Input matrix was 1, The gain of the servo was +100. BS was actuated.

Coupled cavity tests

- At least REFL11 is producing reasonable signals. So what about the other REFL ports? The Michelson signals in the other frequencies
  were invisible. So I decided to use three-mirror coupled cavity with the loss PRC.

- Aligned X arm, Misaligned ETMX, ITMY. Aligned PRM.

- Locked the PRM-ITMX cavity with REFL11 and REFL33.

- Aligned ETMX. If I use REFL11I for the PRC locking, I could not lock the coupled cavity. But I could with REFL33I.
  This is somewhat familiar to me as this is the usual feature of the 3f signal.

- The coupled cavity could be locked "forever". To realize this I needed to tweak the normalization factor from 1.0 to 1.6.
  Q. How does the coupled cavity change the response of the cavity? Can we compensate it by something?
  Q. Measure open loop transfer functions to check if there is any issue in the servo shapes.

- Transmission during the lock is 3.2 while the nominal TRX with PRM misaligned was 0.93.
  This corresponds to power recycling gain of 0.17.

 - X arm:

    - Source: POX11I, phase 79.5 deg, whitening gain 36dB
    - Input matrix: POX11I->1.0->XARM, Normalization TRX*1.60
    - XARM servo gain +0.8, actuation ETMX
    - XARM trigger 0.25 up, 0.05 down. XARM Filter trigger untouched.

- PRC: (sideband locking)
    - Source: REFL33I, phase -34.05 deg, whitening gain 30dB
    - Input matrix: REFL33I->1.0->PRCL, Normalization None
    - PRCL servo gain +4.0, actuation PRM
    - PRCL trigger None

- Same test for the Y arm. At the moment ETMY did not have the OPLEV.
  Same level of transmission (~3.3)

 - Y arm:

    - Source: POY11I, phase -61.00 deg, whitening gain 36dB
    - Input matrix: POY11I->1.0->YARM, Normalization TRX*2.1
    - YARM servo gain +0.25, actuation ETMX
    - YARM trigger 0.25 up, 0.05 down. YARM Filter trigger untouched.

- PRC: (sideband locking)
    - same as above

Sideband PRMI attempt

    - Now I got some kind of confidence on the REFL33 signal.
    - So I tried to get any stable setup for sb PRMI, then to find any reasonable MICH signals anywhere else than AS55Q.
    - With REFL33I(PRCL) & AS55Q(MICH), I got maximum ~10sec lock. It regularly locked. It was enough long to check
      the spectrum on DTT. But it was not enough long to find anything about the MICH signals at the REFL ports.

    - I tried REFL33Q for MICH. The lock was even shorter but could lock for 1~2 sec.

    Q. What is the cause of the lock loss? I did not see too much angluar fluctuation. The actuation was also quiet (below 10000).

- PRCL: (sideband locking)
    - Same as above except for
      - the PRCL servo gain +0.05, No limitter at the servo output.
      - Trigger POP22I (low pass filtered by LP10) 20 up, 3 down

- MICH:
    - AS55Q -24.125 24dB -> x1.0 -> MICH -0.7, No limitter -> ITMX/Y differential
    or
    - REFL33Q -34.05dB -> x2.0 -> MICH same as above
    - For both case, trigger POP22I (low pass filtered by LP10) 20 up, 3 down

 

At this point Jenne came back from dinner. Explained what I did and handed over the IFO.

  8493   Thu Apr 25 18:58:06 2013 KojiConfiguration PD frequency response

No.... what I told was to put the roll next to the splitter, not on the table.
The table area is more precious than the rack space.

Koji> The slack of the fibers should be nicely rolled and put together at the splitter side.

  8494   Thu Apr 25 20:48:48 2013 KojiUpdateASSDen fixed the Yarm ASS scripts

I contacted Den about malfunctioning of the Yarm ASS.

He found the scripts were modified during the attempt to make it available for Xarm (cf. a related elog entry)
So far, he could manage to make the current scripts being modified to run.
A striptool file is still missing but this is what we can handle locally.

I thank Den for the remote caring of the issue despite the limited network bandwidth.

  8500   Sat Apr 27 00:21:06 2013 KojiUpdateLSCLocking activity on Apr 26th

When I talked with Den via phone, he recommended to use the trigger and normalization with POP110I.
So I decided to try this approach. Also I investigated how the REFL33 signals are useful.

I could find the state where the PRMI(sb) locks regularly, although the lock is ~1min at most.

PRCL: REFL33I
whitening gain 30dB, -14.0deg (finely tuned in lock)
-> x1.0 -> Triggered by POP110I (20up, 1down)
-> Normalized by POP110I x0.04
-> Gain 0.2~0.12 FM3, 4, 5, 6 always on, no triggered FMs
-> PRM

MICH: REFL33Q
whitening gain 30dB, -14.0deg (finely tuned in lock)
-> x1.0 -> Triggered by POP110I (20up, 1down)
-> Normalized by POP110I x0.04
-> Gain -20 FM4, 5 always on, no triggered FM
-> ITMX (-1.0) and ITMY (+1.0)

I needed to tune the phase very precisely to reach this state. Also the alignment of the michelson and PRM
was very crtiical to acquire the lock.

Later in the same night I was plagued by PRM alignment drift. It seems that the PRM alignment is bistable or
slightly drifting in pitch. I had to align PRM continuously. When the PRMI is locked, the alignment fluctuation
was mainly in yaw. This was as people commented before.

Attachment 1: Screenshot.png
Screenshot.png
  8501   Sat Apr 27 00:29:40 2013 KojiUpdateLSCLSCoffset script fixed

Prior to the locking trials...

scripts/LSC/LSCoffset script had behaved peculiarly:

This script spawns LSC/offset3 in order to remove the dark offset from the channels.
How ever the offsets had been nulled every other PDs
(i.e. The offsets REFL11 I&Q were nulled.
The offsets REFL33 I&Q had been left untouched
The offset REFL55 I&Q had been nulled
and so on.)

I found that the script run many instances of "offset3" scripts in background.
It seemed that tdsavg did not like too many averaging channels at once.

So the "&"s in the LSCoffsets were removed and now the script runs much more slowly,
but works for all of the PDs listed.

I think I have never seen the offsets in REFL33 and REFL165 nulled down to this level before.

  8508   Mon Apr 29 22:13:41 2013 KojiUpdateLSCLocking with ASDC

Today the locking was not as easy as that was last Friday.
So I tried something new. Today Rana talked about the ASDC locking with POPDC normalization.
This technique was tried. (This is somewhat similar to DC readout.)

PRCL
Signal source: REFL33I / Normalization POP110I x 0.04 / Trigger POP110I 20up 3down, otherwise  untouched from Friday locking
Servo: input matrix 1.00 -> PRCL Servo FM3/4/5/6 Always ON G=+0.06
Actuator: output matrix 1.00 -> PRM

MICH
Signal source: ASDC Offset -109.5 (nominal of the day -49.5) / Normalization POPDC x 1.00 / Trigger POP110I 20up 3down
Servo: input matrix 1.00 -> MICH Servo FM5 Always On G=+10000
ActuaroL output matrix -1.00 -> ITMX / +1.00 -> ITMY

Observation

- POP110I was ~120 during the lock (cf 170 on Friday). So there is some small leakage from the dark port.

- Lock was easier when FM4 of the MICH loop was turned off.

- During the lock horizontal motion of the intracavity mode was visible as usual.

Screenshot.png

  8509   Mon Apr 29 23:02:48 2013 KojiConfigurationLSCQuestons

Q. How much Schnupp asymmetry we want in order to improve the signal ratio between PRCL/MICH in REFL ports?

Q. How much can we increase Schnupp asymmetry in the practical constraints?

Q. How PRCL/MICH ratio is different the REFL ports?
=> My modeling (many years ago) shows the ratio of {115, 51, 26, 23} for REFL{11, 33, 55, 165}.
These numbers should be confirmed by modern simulation of the 40m with updated parameters.
I should definitely use 55MHz but also prepare better 165MHz too.

Q. How the TT/PRM motions are affecting the lock stability? How can we quantify this effect? How can we mitigate this issue?

Q. Can we somehow change the sensing matrix by shifting the modulation frequency?

Q. Is normalization by POP22 or POP110 actually working well?
=> Time series measurement of error signals & servo inputs

  8517   Wed May 1 00:05:03 2013 KojiUpdateLSCMore stable lock of PRMI (REF33I and AS55Q)

[Jenne Koji]

- Today the spots were moving more than the usual. The OPLEV screens showed that the spots are too much off from the center.

- Each vertex OPLEVs were checked and OPLEV wonderland was discovered: Other than the usual misalignment of the spots,
it was found that PRM/ITMX/ITMY beams were clipped somewhere in the paths, BS/PRM oplevs had many loose components
including the input lenses (they are still clamped by a single dog clamp THIS SHOULD BE FIXED ASAP).

- On the ITMY table there were so many stray optics. They were removed and put on the wagon next to the ITMY table.
THIS SHOULD BE CLEARED ON THE WEDNESDAY CLEANING SESSION.

- During this OPLEV session, LSCoffset nulling was run.

- After the OPLEV session, the locking became really instantaneous. We wonder which of the OPLEV cleaning, LSC offset nulling,
and the usual seismic activity decay in the evening was effective to make it better.

- Initially the lock was attempted with REFL33I/Q and some ~10sec lock streches were obtained. During this lock,
  the optical gain of AS55Q was measured in relative to REFL33Q. In deed they were calibrated to be the same
  gain at the input matrix.

- After the MICH signal source was switched to AS55Q, the lock streches became more regular and the minutes long.
We precisely tuned the phase of AS55 and REFL55 in terms of the differential excitation of ITMX/Y using lockin (FREQ 250, AMP 1000).

- We noticed that the AS port spot with AS55Q MICH was darker than the REFL33Q MICH. This suggests the existence of residual offset
in REFL33Q. In deed we observed +30cnt offset in REFL33Q when the PRMI is locked with AS55Q MICH.

- Phases and relative gains of the signals were as follows:

PRCL: REFL33I 1.00 =REFL55I +0.4
MICH: AS55Q 29deg x1.00 = REFL33Q -14deg x1.00 = REFL55Q 118deg 0.03?

- We tried to lock PRMI with AS55Q. The acquisition was not as easy as that with REFL33I. This might be from the saturation of the
REFL55I signal. This configuration should tested with different whitening gain. Handing off using the input matrix went well once the
lock was obtained by REFL33I.

- Handing off from AS55Q to REFL55Q was not successful.

- At the end of the session, Jenne told me that the POP PD still has a large diameter beam. (and a steering mirror with a peculiar reflection angle.)
==> THIS SHOULD BE FIXED ASAP
because the normalization factor can be too much susceptible to the misalignment of the spot.

- The configuration of the filters:

PRCL FM3/4/5/6 G=+0.05 / NORM 0.04 POP110I
MICH FM4/5 G=-5.00 / NORM 0.01 POP110I (or none)

Screenshot.png

  8521   Thu May 2 00:34:57 2013 KojiUpdateLSClocking

- Routine alignment

Locked the arm cavties. Ran ASS. As this was not enough precise alignment for PRMI locking, Yarm alignment was re-adjusted by sliders.
Xarm was also aligned in the same way.

- OPLEV alignment

Once the arms were aligned, OPLEV spots were adjusted. For this adjustment, PRM had to be aligned and OPLEV servos needed to be turned off.

- LSC offset nulling

While Jenne was measuring the dark output of the POP PD, LSC offset nulling script was executed.

- Compensation of the POP spot size fix

As Jenne reported the POP path now has a lens and the denominator for the normalization got bigger.
To compensate this change, PRMI(sb) was locked by the same configuration as yesterday (i.e. AS55Q for MICH, REFL33I for PRCL). 
After some try and error, configuration for stable locking was found. 

PRCL
Signal source: REFL33I / Normalization POP110I x 1.00 / Trigger POP110I 80up 10down
Servo: input matrix 1.00 -> PRCL Servo FM3/4/5/6 Always ON G=+8.00
Actuator: output matrix 1.00 -> PRM

MICH
Signal source: AS55Q / Normalization POP110I x 0.01 / Trigger POP110I 80up 10down
Servo: input matrix 1.00 -> MICH Servo FM4/5 Always On G=-30
Actuator output matrix -1.00 -> ITMX / +1.00 -> ITMY

This suggests that POP110I signal is 5~6 times more than before the lens was installed. 

- SQRTing option for POP110I was implemented

The PRMI optical gain is derived from (Carrier)x(1st order Sideband) or (2nd order SB)x(1st order SB).
Here the carrier and the 2nd order sidebands are nonresonant.
Therefore the optical gain is proportional to the amplitude power recycling gain of the 1st order sidebands.
On the other hand, POP 2f signals are derived from the product of the 1st and -1st order sidebands.
This means that we should take a sqrt of the POP signals to compensate the recycling gain fluctuation.

Screenshot.png

- Locking with SQRT(POP110I)

PRCL
Signal source: REFL33I / Normalization SQRT(POP110I) x 10 / Trigger POP110I 10up 3down
Servo: input matrix 1.00 -> PRCL Servo FM3/4/5/6 Always ON G=+8.00
Actuator: output matrix 1.00 -> PRM

MICH
Signal source: AS55Q / Normalization SQRT(POP110I) x 0.1 / Trigger POP110I 10up 3down
Servo: input matrix 1.00 -> MICH Servo FM4/5 Always On G=-30
Actuator output matrix -1.00 -> ITMX / +1.00 -> ITMY

The lock seems not so different from the ones without SQRTing.

The spot was still moving in yaw direction. If I chose a correct alignment, I could minimize the modulation of the internal power
by misalignment. As you can see in the following plot.

Screenshot2.png

When the alignment was deviated from the optimum, the misalignment induced RIN was much worse although this was the longest lock I ever had with the PRMIsb. (more than 8 min)

Screenshot3.png

- Locking with other signal sources

REF55I/Q trial:

Demodulation phase was adjusted to make the difference of the peak heights for MICH maximized.
After the lock is acquired, I tried to swap the signal source at the input matrix. PRCL swapping was successful but
MICH swapping was not successfull.

It is much more hard to lock the interferometer with REFL55I compared with REFL33I.

REFL165I/Q trial:

As REFL165 PD never produced any useful signal, I tried to swap it with the BBPD used in the green setup.

- Borrowed the PD, power supply from the green setup.

- Put REFL165PD aside. Placed the BBPD in the path. The DC output was 0.8V. This corresponds to the input power of ~5mW.

- Checked the signal but it was very litte (several counts even at the maximum whitening gain).

- Decided to use the power reduction pick off to introduce much more light on the PD.
  This PO mirror is 90% reflector. Therefore I had to be careful no to fry the diode.
  Currently there are OD1.3 (x1/20) power attenuator to reduce the input power down to 6.5V (40mW).

- The resulting signal is very wiered suggesting the saturation of the PD at the RF stages.

- Probably I need to make a new PD circuit which has the high pass filter to reject other low frequency components.

  8525   Fri May 3 01:24:25 2013 KojiUpdateASSDen fixed the Yarm ASS scripts

Output matrices are added to ASS. Currently ASS is based on the mirror bases.
I prefer to have the actuator bases as the coils are more stable than the sensors.

At this point, the output matrices are identity. So Den's scripts are still working.

Striptool settings were also fixed.

  8535   Tue May 7 10:30:32 2013 KojiUpdateLockingPRM yaw responsible for RIN

Quote:

BS is contributing a little bit, but PRM is clearly contributing

No.

While the peak in the PRM OPLEV was more than 10 times higher than the spectrum level without the excitation,
we only saw small peaks in the RIN spectra. This suggests that the PRM angular motion did not contribute to the RIN spectra.

You should divide the POP110I and POPDC spectra by 400 and 450, which was the DC values of these channels, in order to convert them into RIN (1/rtHz)
The OPLEV spectra is calibrated to be urad/rtHz (is this true?) so you can obtain the conversion factor from OPLEV to RIN (1/urad)
by matching the peaks. This way you make a angular noise projection.

Quote:

I think that I need to install one of the T240's on the new granite slab, and see what kind of coherence we have between seismic and PRM yaw motion, and if FF can get rid of it.

Yes we should do that. BTW what should be pushed?

  8539   Tue May 7 17:30:28 2013 KojiUpdateRF SystemIdeal PRMI RF frequency

To change the MC length is not the point.

If we can improve the length sensing by the intentional shift of the modulation frequency from the MC FSR, that's worth to try, I thought.

But that is tough as the freq difference is 18kHz that is ~x4 of the line width of the MC.
Not only the 55MHz sidebands, but also the 11MHz sidebands will just be rejected.

Nevertheless: Is there any possibility that we can improve anything by shifting the modulation frequency by ~1kHz?

  8547   Tue May 7 23:03:12 2013 KojiConfigurationCDSCDS work

Summary:

c1rfm / c1lsc / c1ass / c1sus were modified. They were recomplied and installed. They are running fine
and confirmed PRMI locking (attempt), arm locking, and Yarm ass with the new codes.

Motivation:

1a. SQRTing switching for POP110 was wrong. 0 enabled sqrting, 1 disabled sqrting. I wanted to fix this.
1b. Sqrting for POP22 was not implemented.

2. Preparation for the shadow sensor control with POPDC.

3. ASS had only an input. I want to run two ASS for the X and Y arms.

SQRTing for POP110/22:

- Flipped the input of the bypass switch. Correspoding MEDM indicators are fixed on the power normalization screen.
- Copied the sqrting structure from POP110 to POP22. Correspoding MEDM buttom was made on the power normalization screen.

- The function of the sqrting buttons were confirmed.

Additional ASS output:

- The output path "NPRO" was removed. Corresponding RFM channels have also removed.
- The previous NPRO path was turned to the "ASS1" path. The previous "ASS" path was turned to "ASS2".
- Corresponding shared memory channel are created/renamed.
- c1ass was modified to receive the new ASS shared memory channels. ASS1 is assigned to the X arm. ASS2 is assigned to the Y arm
- The output matrix screen and the lockin screen were modified accordingly.
- Only script/ASS/Arm_ASS_Setup.py was affected. The corespoding lines (matrix assignment) was fixed.

- The function of Den's version of  ASS was confirmed.

LSC->PRM ASC path

- We want to connect POPDC to PRM ASC. POPDC is acquired on c1lsc.
- So, for now we use the LSC input matrix to assign POPDC to one of the servo bank.
- The last row of the LSC output matrix was assigned to the PCIE connection to c1sus.
- This PCIE connection was connected to the PRM ASC YAW input.

- The connection between LSC and SUS was confirmed.

- During this process I found that there are bunch of channels transferred from LSC to SUS via RFM.
  These channels are transferred via PCIE(dolphin) and then via RFM. But LSC and SUS are connected
  with dolphin. So this just adds additional sampling delay while there is no benefit. I think we should remove the RFM part.
  Note that we need to use RFM for the end mirrors but this also should use only the RFM connection.


Rebuilding the codes

- Prior to the tests of the new functionalities, the codes were rebuild/installed as usual.
- The suspension were shutdown with the watch dogs before the restart of the realtime codes.
- Once the realtime codes were restarted successfully, the watch dogs were reloaded.
- As we removed/added the channels, fb was restarted.
- c1rfm / c1lsc / c1ass / c1sus codes were checked-in to svn
 

  8552   Wed May 8 18:33:02 2013 KojiUpdateASSYARM ASS - faster and more precise convergence

Precise arm alignment is more demanded. as the PRMI locking requires good and reliable alignment of the ITMs.

I previously added the output matrix to ASS.

Now the input and output matrix as well as the gains and filters have been updated.

The current concept is

Fast loop: align the arms by the arm mirrors with regard to the given beam.

Slow loop: move the incident beam position and angle to make the spot at the center of the mirrors

This is actually opposite to Den's implementation.

In order to realize the faster alignment of the arm, I increased the corner frequency of the lockins for the arm signals from 0.5Hz to 1Hz.

With the new configuration the arm alignment converges in 10sec and the input pointing does in ~15sec.

The actuation to the input pointing TTs are done together with the feedforward actuation to the arms.
This way we can avoid too much coupling from the input pointing servos to the arm alignment servos.

The corresponding script /opt/rtcds/caltech/c1/scripts/ASS/YARM/DITHER_Arm_ON.py was also modified.

Attachment 1: YARM_ASS.png
YARM_ASS.png
Attachment 2: Screenshot.png
Screenshot.png
  8554   Wed May 8 22:36:42 2013 KojiUpdateASSXARM ASS (YARM ASS - faster and more precise convergence)

Same ASS setup for the X arm has been done.

Now Arm ASS can run simultaneously.

I reverted the number of the lockin banks from 6 to 8 for future implementation of A2L for the ITMX by coil balancing.
Since A2L for the ITMX is just barely visible for now, I am going to leave the coil balance untouched.

Attachment 1: XARM_ASS.png
XARM_ASS.png
  8562   Sat May 11 01:11:52 2013 KojiUpdateASCPRC mode stabilization with a shadow sensor at POP

Ah, AWESOME. Indefinite PRMI lock was finally achieved.

POP setup

- Looked at the POP setup. Checked the spot on POP110 PD. Found some misalignment of the beam.
  The beam spot was aligned to the PD with PRMI locked. The value of POP110I almost doubled by the alignment
  and recovered previous value of 400. Therefore previous normalization values of MICH 0.01 / PRCL 100 were restored.

- Placed PDA36A (Si 3.6mmx3.6mm) on the POP path that Jenne prepared. The gain knob was set to 40dB.
  Since the original spot had been too small, a lens with f=50mm was inserted in order to expand the beam.
  Connected the PD output to the SMA feedthrough on the ITMX table enclosure.
  I found the BNC cable labeled "PO DC" hanging. Connected this cable to the enclosure SMA.

- Went to the LSC rack. Found the corresponding PO DC cable. Stole the POPDC channel from POP110I Bias T to this PO DC cable.

- Razor blade setup: Machined a junk Al bracket in order to fix a razor blade on it. Attached the Al bracket to a sliding stage.

Locking

- Locked the PRMI with REFL33I&AS55Q. Cut the beam into half by the razor blade.

- Made a temporary PRM_ASC_YAW filter.
  Zero: 0Hz Pole: 2kHz
  Resonant Gain 3.2Hz Q:2 Height 30dB
  Butterworth 2nd-order 60Hz

  => Expected UGF 0.1Hz&10Hz

- CDS: By the work described in this entry, the POPDC signal was connected to the "MC" bank of the LSC.
            BTW, the 11th row of the LSC output matrix is connected to the PRM_ASC_YAW.

- The "MC" servo input (i.e. the POPDC signal) was normalized by POP110I (without SQRTing).

- Engaged the PRM ASC path. Gradually increased the gain of PRM_ASC_YAW. G=+100 seemed to be the best so far.
  It was visible that the spot on the POP CCD was stablized in yaw.

- The lock lasted for ~40min. Took several measurements, alignment adjustment, etc.

- Tweaking the PRM ASC unlocked the PRMI.

- Locked again. Switched from REFL33I/AS55Q (x1/x1) combination to REFL55I/REFL55Q (x1/x0.3) combination.
  This also kept the lock more than 20min.

Attachment 1: Screenshot.png
Screenshot.png
Attachment 2: 130510_PRMI.pdf
130510_PRMI.pdf
  8566   Mon May 13 23:05:26 2013 KojiConfigurationLSCPRMI locking

- Disabled MCL path in mcdown/mcupscript.

Nominal gain in mcdown/mcup was -50 and -100 respectively.

- Confirmed the stable lock was just because of the quiet seismic of the Friday night.

- Improvement of the PRM ASC servo
RG3.2 (3.2Hz Q=2 Height 30dB)
=>
RG3.2 (3.2Hz Q=10 Height 30dB) +  zero[f, 1, .5] pole[f, 2, 3] zero[f, 4.5, .5] pole[f, 3.5, 3]

Filter shape comparison is found in the second plot attached.

The resulting spectra (freerun vs controlled) is found in the first plot.

Nominal PRM ASC gain is +70

- Openloop TF measurement

OLTF PRCL 250Hz 30deg / MICH 200Hz 45deg

- REFL55/REFL33 phase adjustment (in lock)

REFL55 phase fine tune (95.25deg) (x1,x0.3)
REFL33 phase (-13.0deg) (x1, x2)

Attachment 1: 130513_PRC_ASC.pdf
130513_PRC_ASC.pdf
Attachment 2: 130513_PRC_ASC_servo.pdf
130513_PRC_ASC_servo.pdf
  8570   Tue May 14 02:19:13 2013 KojiUpdateGreen LockingXend Green tweaked

Note that I'm supposed to return one of the two green beat PDs and the power supply.
They are on the REFL path. I'll work on the restoration of the beat configuration.

  8574   Tue May 14 20:27:19 2013 KojiConfigurationLSCOpenloop gain for PRMI lock May 13

The OLTFs for PRCL and MICH for the last night's lock were modelled using Yuta's python script.

Attachment 1: LSCPRCLOLTF.png
LSCPRCLOLTF.png
Attachment 2: LSCMICHOLTF.png
LSCMICHOLTF.png
Attachment 3: 130513.zip
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