ID |
Date |
Author |
Type |
Category |
Subject |
6164
|
Wed Jan 4 00:43:06 2012 |
kiwamu | Update | IOO | MC became flaky |
I don't know what exactly is going on, but MC became flaky and it's been frequently unlocked.
I have turned off the MC WFS servo to check if the WFSs are doing something bad. But it still tends to be unlocked without the WFS servo.
Right now it doesn't stay locked for more than 10 min. |
6166
|
Wed Jan 4 03:03:24 2012 |
kiwamu | Update | LSC | locking activity tonight and beyond |
Last night and tonight, I was doing a kind of rehabilitation -- locking PRMI and DRMI with the new trigger system.
Although MC wasn't so awesome (#6164), I confirmed that the DRMI can stay locked with the conventional RFPD combination (#4760).
Additionally I have modified the IFO configure scripts, such that they also automatically restore the thresholds values for triggering.
The scripts are available in the C1IFO_CONFIGURE screen as usual.
Locking plan
Here is a plan in my mind and these are basically the details of the gantt chart (#6143):
- (1 day task) Measurement of the recycling gains of the RF sidebands with the PRMI and DRMI configuration, using POP22/110 RFPD.
- I need to have confidence that I am really locking the DRMI with SRC resonating to 55 MHz.
- Also those values will enable us to estimate losses and mode matching again (maybe ?).
- (3-4 days task) Measurement of the sensing matrix using the multiple-LOCKIN system.
- Write a script to automatically measure the sensing matrix. This must be easy.
- The results will enable us to diagonalize the input matrix and therefore it eventually gives more solid lock of the DRMI
- Also it will give us the optical gains of 3f signals. So this is actually a step toward the 3f signal check.
- (3-4 days task) Noise budgeting on the 3f signals
- This is a very important part of the DRMI characterization because the results will tell us whether we can hold the DRMI lock with a sufficient SNR or not.
- If it turns out that they don't have good SNRs, we then have to come up with some ideas to improve the SNRs.
- (Extra fun task depending on schedule) 3f DRMI lock + Y arm ALS
- If the beat-box electronics are not available by the time when the work above are completed, I will do this fun task.
- Probably it is better to start preparing the common mode servo electronics because it will be needed anyway.
|
6167
|
Wed Jan 4 05:02:58 2012 |
kiwamu | Update | LSC | Sidebands measurement at POP |
Just a quick report:
I did the first attempt to measure the recycling gains of the sidebands in the DRMI configuration (sidebands resonant condition)
by looking at the output of the POP22/110 RFPD.
Because this time what I measured is some absolute values of the sidebands power,
it doesn't tell us anything quantitatively until we calibrate it or compare it with similar data.
So I need to measure the same things in some different configurations (e.g. PRMI, SRMI, etc.)
in order to extract some useful information from the measurement.
The attached picture is the display of a power spectrum analyzer looking at the output of the POP22/110 broadband RFPD
while the DRMI (in the sideband resonant condition) was kept locked.
You can see that 111 MHz (twice of 55 MHz) is prominent. Also there are several peaks at 11, 22, 44 and 66 MHz.
|
6170
|
Wed Jan 4 16:22:30 2012 |
kiwamu | Update | LSC | power normalization in LSC : modification done |
The dynamic power normalization system has been modified such that the normalization happen after the LSC input matrix.
The attached screen shot below tells you how the signals flow.
The red circled region in the picture is the place where the power normalization are performed.
The dynamic normalization will be activated once you put some numbers into the elements in the matrix.
Otherwise the error signals are always normalized by 1.
Quote from #6158 |
It turned out that the power normalization need a modification.
I will work on it tomorrow and it will take approximately 2 hours to finish the modification.
|
|
6175
|
Fri Jan 6 01:00:56 2012 |
kiwamu | Update | CDS | c1scx out of sync |
Both the c1scx and its IOP realtime processes became out of sync.
Initially I found that the c1scx didn't show any ADC signals, though the sync sign was green.
Then I software-rebooted the c1iscex machine and then it became out of sync.
For tonight this is fine because I am concentrating on the central part anyway. |
6181
|
Mon Jan 9 13:19:09 2012 |
kiwamu | Update | SUS | ETMX damping restored |
No we can't do that because the c1scx model is not working properly.
If you look into the real time controller screen you will find what I mean.
Quote from #6180
|
ETMX sus damping restored
|
|
6182
|
Mon Jan 9 23:52:15 2012 |
kiwamu | Update | CDS | SUS channels not accessible from dataviewer |
[John / Kiwamu]
We found that some of the suspensions channels (for example C1:SUS-BS_POS_IN1 and etc) were not accessible from dataviewer for some reasons.
So far it seems none of the channels associated with c1sus are accessible from dataviewer. |
6183
|
Tue Jan 10 00:09:33 2012 |
kiwamu | Update | LSC | spike hunting in REFL33 |
[John / Kiwamu]
We tried to figure out what is causing spikes in the REFL33 signal, which is used to lock PRCL.
No useful information was obtained tonight and it is still under investigation.
(Background)
One thing preventing us from doing smooth measurements of the noise budget and the sensing matrix is some sharp spikes in the LSC error signals.
For example when we lock PRMI with REFL33 and AS55 fedback to PRCL and MICH respectively, both the REFL33 and AS55 signals show some spikes in time series.
Those spikes then bring the noise spectra higher than how they should be.
So for the reason, taking the noise budget doesn't give us much information about the interferometer rather than there are spikes.
Also the sensing matrix measurement has been suffered from those spikes, which excite the impulse responses of the low pass filters in the LOCKIN detection systems a lot.
(What we did)
We looked into the actual analog signals to see if there are indeed spikes or not before they are acquired to the ADCs.
But we didn't find any corresponding spikes in the signals that are after the mixers.
It maybe because the signals we looked into didn't have high enough SNR because they were coming out from the monitor lemo outputs on the demod boards.
Then we thought the spikes are from the whitening circuits, due to some kind of saturation.
We decreased the gain of the whitening filters by a factor of 10, but it didn't help and the spikes were still there. |
6187
|
Thu Jan 12 03:05:02 2012 |
kiwamu | Update | LSC | OSA installed in AS |
[John / Valera / Kiwamu]
We installed a new weapon, an optical spectrum analyzer in the AS port.
Like we used to do in the old days, two BNC cables were newly laid down and they bring the output of the OSA to the control room to monitor the spectrum with an oscilloscope.
(Some notes)
The photo diode of the OSA was replaced by a Thorlab PDA100A to amplify the signals.
The carrier peak is at about 6.9 V and the f1 and f2 sidebands peaks are at about 40 mV when the beam is in straight shot (everything is misaligned except ITMY and BS).
According to a rough calculation, those numbers correspond to a modulation depth of about 0.16 or so.
The depth agree with what Mirko measured before (#5519)
|
6202
|
Tue Jan 17 01:02:07 2012 |
kiwamu | Update | LSC | glitch hunting in REFL RFPDs : strange |
A very strange thing is going on.
The REFL11 and REFL55 demod signals show high frequency noise depending on how big signals go to the POS actuator of PRM.
This noise shows up even when the beam is single-bounced back from PRM ( the rest of the suspensions are misaligned) and it's very repeatable.
Any idea ?? Am I crazy ?? Is PRM making some fringes with some other optics ??
(background)
The most annoying thing in the central part locking is glitches showing up in the LSC error signals ( #6183).
The symptom is that when the motion in PRCL at 3 Hz becomes louder, somehow we get glitches in both the MICH and PRCL error signals.
In the frequency domain, those glitches are mostly contribute to a frequency band of about 30 - 100 Hz.
Last Thursday Koji and I locked the half PRM (PRMI with either ITMX or ITMY misaligned) to see if we still have the glitches in this simpler configuration.
Indeed there were the same kind of glitches --a loud 3 Hz motion triggers the glitches.
It was shown particularly in the REFL11 signal but not so much in the REFL33 while AS55 didn't show any glitches.
(Still glitches even in the single bounce beam)
We were suspecting some kind of coupling from a beam jitter, so that the 3 Hz motion somehow brings the beam spot to a bad place somewhere in the REFL paths.
I misaligned all the suspensions except for PRM such that the beam directly bounces back from PRM and go to the REFL port.
Indeed there still were glitches in the REFL11 and REFL55 demod signals. It showed up once per 30 sec or so and pushes up the noise floor around 30 - 100 Hz.
There might be a little bit of glitches also in the REFL33, but the ADC noise floor and the expected glitch noise level were comparable and hence it was difficult to see the glitches in REFL33.
(Glitch is related to the PRM POS actuation)
In the single-bounce configuration I started shaking the PIT and YAW motions of PRM at 3 Hz using the realtime LOCKIN oscillator to see if I can reproduce the glitches.
However no significant glitches were found in this test.
Then I started shaking the POS instead of the angular DOFs, and found that it causes the glitches.
At this point it didn't look like a glitch any more, it became more like a stationary noise.
The attached screen shot is the noise spectrum of the REFL11_I.
The red curve is the one taken when I injected the 3 Hz excitation in POS by the LOCKIN oscillator.
The excitation is at 3 Hz with an amplitude of 1000 counts.
As a comparison I plotted the same spectrum when no excitation was injected and it is plotted in pink.

It seems there is a cut off frequency at 100 Hz.
This frequency depends on the amplitude of the excitation -- increasing the amplitude brings the cut off frequency higher.
This noise spectrum didn't change with and without the oplevs and local damping.
(Possible scenario)
A possible reason that I can think of right now is : PRM is interfering with some other optics for some reason.
But if it's true, why I didn't see any fringes in the AS demod signals in the half PRM configuration ?
Quote from #6183 |
We tried to figure out what is causing spikes in the REFL33 signal, which is used to lock PRCL.
No useful information was obtained tonight and it is still under investigation.
|
|
6203
|
Tue Jan 17 02:27:49 2012 |
kiwamu | Update | LSC | fringe tests : all the suspensions are innocent |
I did a quick test to check a hypothesis that PRM is interfering with some other optics in the single bounce configuration.
I shook all the suspensions (except the MC mirrors) at 3 Hz in POS, PIT and YAW with an amplitude of 1000 counts.
No effects were found in the REFL demod signals.
So it is NOT a fringe effect caused by the other suspended mirrors.
Quote from #6202 |
The REFL11 and REFL55 demod signals show high frequency noise depending on how big signals go to the POS actuator of PRM.
Is PRM making some fringes with some other optics ??
|
|
6204
|
Tue Jan 17 02:44:59 2012 |
kiwamu | Update | CDS | awg not working |
AWG is not working. This needs to be fixed.
I could set the channel and the parameters in the AWGGUI screen, but it never inject signals to the realtime system. |
6205
|
Tue Jan 17 03:10:27 2012 |
kiwamu | Configuration | IOO | rotated lambda/2 plate |
I have slightly rotated the lambda/2 plate, which is used for attenuating the REFL beam's power on the AS table
because the plate had been at an unusual angle for investigation of the glitches since last Thursday.
It means the laser power going to the coating thermal noise setup has also changed. Just keep it in mind.
Quote from #6198 |
So today we set up the Jenny RC temperature setup to lock the LWE NPRO to the RC and then set up the beat note with the IFO REFL beam on the AS table. By using the 2 laser beat, we are avoiding the VCO phase noise issue which used to limit the PSL frequency noise at ~0.01 Hz/rHz. To do this we have reworked some of the optics on the PSL and AS tables, but I think its been done without disturbing the beams for the regular locking. Beat note has been found, but the NPRO has still not been locked to the RC - next we setup the lockin amp, dither the PZT, and then use the New Focus lock box to lock it to the RC.
|
|
6206
|
Tue Jan 17 13:47:40 2012 |
kiwamu | Update | LSC | dirty steering mirror in the REFL path |
Last night I found that there were many dust particles on the second steering mirror in the REFL path on the AS table.
Looking at it through an IR viewer, I saw the REFL beam hitting one of the biggest dust particles on that mirror.
This dust particle maybe causing the glitches or maybe not.
Anyway because it's always better to have clean mirrors, I will wipe the steering mirror in this evening and check the presence of the glitches again.
Quote from #6202 |
The REFL11 and REFL55 demod signals show high frequency noise depending on how big signals go to the POS actuator of PRM.
Is PRM making some fringes with some other optics ??
|
|
6207
|
Tue Jan 17 16:09:20 2012 |
kiwamu | Update | CDS | awg not working on the c1sus machine |
Actually awg works fine without any problems when the excitation channels belong to the c1lsc machine.
It seems that the awg doesn't inject signals on the channels of the c1sus machine, for example C1:SUS-BS_LSC_EXC and so on.
Quote from #6204 |
AWG is not working. This needs to be fixed.
|
|
6209
|
Wed Jan 18 12:36:26 2012 |
kiwamu | Update | LSC | wiped a steering mirror on the REFL path |
I wiped both surfaces of the REFL second steering mirror.
However no improvements. The glitches still remain.
(Pic.1 before wiping, Pic.2 after wiping)
 
Quote from #6206 |
Last night I found that there were many dust particles on the second steering mirror in the REFL path on the AS table.
|
|
6211
|
Wed Jan 18 14:28:36 2012 |
kiwamu | Update | LSC | estimation of optical length between PRM and scattering object |
Assuming that PRM is interfering with some other optics, I have estimated the optical distance between PRM and an object that interferes with PRM.
The optical distance is estimated to be 9.5 +/- 0.5 m.
If we believe this number the object is most likely outside of the vacuum chambers.
(The measurement)
In order to estimate the optical length between PRM and a scattering body, I swept the frequency of the main laser by actuating on the MC length.
With the sweep, the laser frequency go across some fringes and basically it allows us to estimate the FSR of a very low finesse cavity formed by PRM and the scattering body.
Therefore we get the the optical distance based on the resultant FSR.
The measurement goes as follows:
- Preparation : calibration of the MC2 actuator as a frequency actuator (for more details, see the next section)
- Set the interferometer to the single-bounce configuration such that the beam directly is reflected back from PRM
- Take spectra of REFL11_I without driving any optics. This spectra tells us how quiet the noise normally is.
- Drive MC2_POS at 10 Hz with an amplitude of 10000 counts so that we can see the high frequency up conversion noise
- The frequency was chosen such that the excitation is out of the local damping bands
- The amplitude was chosen to be as big as possible until the MC unlocked
- With this drive, the laser frequency should change by 20 MHz peak-peak at 10 Hz.
- Record the noisy spectrum when the MC2_POS was driven.
- Drive PRM instead of MC2 at 10 Hz.
- Adjust the amplitude of the excitation such that the cut-off frequency of the up conversion noise matches with that of the MC2 driven case.
- The amplitude was found to be 1700 - 2000 counts, this uncertainty is currently limiting the precision of the optical distance estimation.
- With this amount of the drive, PRM moves by 0.8 um peak-peak at 10Hz.
- Estimate the optical length based on the amount of the drives for PRM and MC2.
- Estimate the FSR using the following relation df/FSR = dx/ (lambda/2). => FSR = 17 MHz
- Since FSR = c/ (2L), L = c/(2 FSR) = 9.5 m or so

(Calibration of the MC2 actuator)
To do the measurement described above, the MC2 actuator must be calibrated in terms of a frequency actuator.
I did the same old technique ( #4721): lock a cavity, adjust the UGF as low as possible, and shake an actuator of interest.
This time I used the half-PRM (PRM + ITMY) for this measurement.
The actuator responses are calibrated from that of displacement to frequency by using df/f = dx/L and assumed that L = 6.760 ( #4585).
Also the PRM actuator was measured such that we can use this as a reference since we already know the response in displacement ( #5637).
The attached plot below is the actual responses that I measured yesterday. The y-axis is calibrated to Hz/counts.

Quote from #6202 |
Is PRM making some fringes with some other optics ??
|
|
6212
|
Wed Jan 18 16:31:10 2012 |
kiwamu | Update | LSC | estimation of optical length between PRM and scattering object |
I searched for a scattering body in the REFL path.
According to the result the REFL path on the AS table is innocent.
The idea of the search method is given as follows:
- Put a 1/10 ND attenuator at the origin of the REFL path on the AS table.
- Of course this reduces the signal level by the same factor of 10 in the REFL11_I demod signal.
- If the scattering body is in the REFL path the up conversion noise will be smaller by a factor of 100 because the scattered light go across the attenuator twice.
The attached plot below is the spectra of REFL11 with the 1/10 attenuator at the origin of the REFL path when the beam is single-bounced from PRM.
In the measurement PRM_POS was driven at 10 Hz with an amplitude of 1700 all the time. This is exactly the same situation as that explained in the previous elog entry ( #6211).
You can see that the up conversion noise level also decreased by the same factor of 10, which suggests there are no scattering object in the REFL path.
Note that the data with the attenuator in place is intentionally scaled by multiplying a factor of 10 for comparison.
Quote from #6211 |
Assuming that PRM is interfering with some other optics, I have estimated the optical distance between PRM and an object that interferes with PRM.
The optical distance is estimated to be 9.5 +/- 0.5 m.
If we believe this number the object is most likely outside of the vacuum chambers.
|
|
6213
|
Thu Jan 19 23:34:52 2012 |
kiwamu | Update | IOO | PMC realignment and HEPA |
I realigned the incident beam to PMC at 23:30. The transmitted light went up from 0.78 to 0.83.
Also I decreased the HEPA level down to 20 % for the night time locking. |
6214
|
Fri Jan 20 15:59:02 2012 |
kiwamu | Update | Green Locking | Y arm ALS noige budget |
One of my goals in this week is : measurement of the current best ALS noise budget.
Last night I took a new noise spectra of the Y arm ALS, which is shown in the attached figure below.
The displacement of the arm cavity observed from the IR PDH is at 66 pm in rms. In the measurement the arm length was stabilized with the ALS technique.

|
6215
|
Fri Jan 20 16:24:50 2012 |
kiwamu | Update | Green Locking | Y arm ALS : time series |
Here is a new time series plot showing how stably ALS can control the arm length.
In the middle of the plot the cavity length was held at the resonance point for ~ 2 min. and then it passed through the resonance point to show the full shape of the PDH signal.
Apparently the PDH signal is now quieter than before (#6133)

Quote from #6214 |
One of my goals in this week is : measurement of the current best ALS noise budget.
|
|
6218
|
Mon Jan 23 23:12:00 2012 |
kiwamu | Update | IOO | PMC realignment |
I have realigned the beam pointing to PMC. The transmitted light increased from 0.74 to 0.83.
The misalignment was mainly in pitch. |
6220
|
Tue Jan 24 18:11:13 2012 |
kiwamu | Update | Green Locking | Y arm ALS noise budget |
I did some more stuff for the Y arm ALS and updated the noise budget:
After the works, the rms displacement improved a little bit, so it is now at 24 pm in rms.
Though, it turned out that the MFD's ADC is now limiting the noise in a frequency band of 200 mHz - 5 Hz.
So tonight I will increase the gain of the whitening filter to push down the ADC noise more.

(What I did)
+ added the DAC noise and comparator noise based on measurements.
+ redesigned the servo filter shape to suppress the seismic noise below 10 Hz.
The attached plot below shows the newly designed open loop transfer function together with the old one for a comparison.
UGF is at 120 Hz and the phase margin is about 27 deg.

- FM7 = resonant gain (17)
- FM6 = resonant gain (3)
- FM5 = zero(1) * pole(500)
- FM4 = pole(1) * zero(40.) * 40.
- FM3 = pole(1) * zero(40.) * 40.
- FM2 = pole(0.001)*zero(1)*1000.
|
6221
|
Wed Jan 25 02:59:46 2012 |
kiwamu | Update | Green Locking | Y arm ALS noise budget |
Surprisingly increasing the gain of the whitening filter didn't improve the noise curve.
It suggests that the ADC noise is not the limiting factor below 10 Hz.
Quote from #6220 |
Though, it turned out that the MFD's ADC is now limiting the noise in a frequency band of 200 mHz - 5 Hz.
So tonight I will increase the gain of the whitening filter to push down the ADC noise more.
|
|
6224
|
Thu Jan 26 05:40:10 2012 |
kiwamu | Update | LSC | glitch in the analog demodulated signals |
Indeed the glitches show up in the analog demodulated signals. So it is not an issue of the digital processing.
With an oscilloscope I looked at the I/Q monitor outputs of the LSC demodulators, including REFL11, REFL33, REFL55, POY11, AS55 while keep locking the carrier-resonant PRMI.
I saw some glitches in REFL11, REFL55 and AS55. But I didn't see any obvious glitches in REFL33 and PO11 because the SNR of those signals weren't good enough.
(some example glitches)
The attached plot below is an example shot of the actual signals when the carrier resonant PRMI was locked.
The first upper row is the spectrogram of REFL11_I, REFL55_I, REFL33_I and AS55_Q in linear-linear scale.
The second row shows the actual time series of those data in unit of counts.
The bottom row is for some DC signals, including REFLDC, ASDC and POYDC.

You can see that there are so many glitches in the actual time series of the demod signals (actually I picked up the worst time chunk).
It seems that most of the glitches in REFL11, REFL33 and AS55 coincide.
The typical time scale of the glitches was about 20 msec or so.
Note that the PRMI was locked by REFL33 and AS55 as usual. |
6225
|
Thu Jan 26 06:09:52 2012 |
kiwamu | Update | Green Locking | noisy AS55 |
During the Y arm ALS I found that the noise of the AS55 demod signal was worse than that of POY11 in terms of the Y arm displacement.
There is a bump from 500 mHz to 100 Hz in the AS55 signal while POY11 didn't show such a structure in the spectrum.
The plot below is the noise spectra of the Y arm ALS. The arm length was stabilized by using the green beat-note fedback to ETMY.
In this measurement, POY11 and AS55 were served as out-of-loop sensors, and they were supposed to show the same noise spectra.
In the plot It is obvious that the AS55 curve is louder than the POY curve.

|
6229
|
Thu Jan 26 19:28:02 2012 |
kiwamu | Update | IOO | PMC low transmission |
After I recovered the lock of PMC, I found that the PMC transmission was quite low. It was about 0.26 in the EPICS display.
I zeroed the PSL temperature feedback value which had been -2.3 and then the PMC transmission went back to a normal value of 0.83.
I believe it was because the PSL was running with two different oscillation modes due to the big temperature offset. |
6230
|
Fri Jan 27 05:21:43 2012 |
kiwamu | Update | Green Locking | fine alignment of the Y end green setup |
I did a fine alignment on the Y end green setup. The green light became able to be locked again.
Quote from #6227 |
The alignment is finished after the realization that the 3rd steering mirror had to be adjusted too.
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|
6231
|
Fri Jan 27 06:07:47 2012 |
kiwamu | Update | LSC | glitch hunting |
I went through various IFO configurations to see if there are glitches or not.
Here is a summary table of the glitch investigation tonight. Some of the cells in the table are still not yet checked and they are just left blank.
IFO configuration |
Yarm
|
Xarm
|
MICH
|
Half PRMI
|
low finesse PRMI
|
PRMI (carrier)
|
PRMI (sideband)
|
DRMI
|
AS55 |
NO |
NO |
NO |
|
up conversion noise |
glitch |
glitch |
glitch |
REFL11 |
NO |
NO |
NO |
|
up conversion noise
|
glitch |
glitch |
glitch |
REFL33 |
NO |
NO |
NO |
|
- |
glitch |
glitch |
glitch |
REFL55 |
NO |
NO |
NO |
|
up conversion noise
|
glitch |
glitch |
glitch |
REFL165 |
NO |
NO |
NO |
|
- |
glitch |
glitch |
glitch |
POX11 |
- |
NO |
NO |
|
|
glitch |
glitch |
glitch |
POY11 |
NO |
- |
NO |
|
|
glitch |
glitch |
glitch |
POP55 |
- |
- |
|
|
|
|
|
|
|
|
|
|
|
|
|
|
|
Low finesse PRMI
The low finesse PRMI configuration is a power-recycled MIchelson with an intentional offset in MICH to let some of the cavity power go through MICH to the dark port.
To lock this configuration I used ASDC plus an offset for MICH and REFL33 for PRCL.
The MICH offset was chosen so that the ASDC power becomes the half of the maximum.
In this configuration NO glitches ( a high speed signal with an amplitude of more than 4 or 5 sigma) were found when it was locked.
Is it because I didn't use AS55 ?? or because the finesse is low ??
Also, as we have already known, the up conversion noise (#6212) showed up -- the level of the high frequency noise are sensitive to the 3 Hz motion. |
6235
|
Fri Jan 27 17:16:05 2012 |
kiwamu | Update | LSC | hypothetical glitch scenario |
Here is a hypothetical scenario which could make the glitches in the LSC error signals. It can be considered as a 4 step phenomenon.
(1) up conversion noise due to a large motion at 3 Hz
=> (2) rms level exceeds the line width (a.k.a. linear range) in some LSC sensors
=> (3) unlocks some of the DOFs in a moment
=> (4) glitches due to the short unlock.
- - plan - -
In order to check this hypothesis the low finesse PRMI must serve as a good test configuration.
What I will do is to gradually decrease the offset in MICH such that the finesse of PRMI becomes higher.
And at each different finesse I will check the spectra, glitch rate, and etc.
Quote from #6231 |
Low finesse PRMI
In this configuration NO glitches ( a high speed signal with an amplitude of more than 4 or 5 sigma) were found when it was locked.
Is it because I didn't use AS55 ?? or because the finesse is low ??
Also, as we have already known, the up conversion noise (#6212) showed up -- the level of the high frequency noise are sensitive to the 3 Hz motion.
|
|
6238
|
Mon Jan 30 23:10:02 2012 |
kiwamu | Update | SUS | drift mon script needs to be fixed |
[Rana / Kiwamu]
We tried to set some parameters for the suspension drift monitor but the old matlab script, which automatically sets the values, didn't run because it uses the old mDV protocol.
The attached link below is a description about the script.
https://wiki-40m.ligo.caltech.edu/Computers_and_Scripts/All_Scripts#Drift
It needs to be fixed or upgraded by pynds. |
6240
|
Tue Jan 31 14:58:30 2012 |
kiwamu | Update | IOO | laser shuts down |
[Steve/ Kiwamu]
We found that the laser had completely shut off for ~ 4 hours even with all the PSL doors closed.
We are guessing it is related to the interlock system and Steve is working on it to fix it.
Quote from #6239 |
The 2W Innilight shutdown shut when I opened side door for safety scan. This was not a repeatable by opening -closing side doors later on. Turned laser on, locked PMC and MC locked instantly. The MC was not locked this moring and it seemed that the MC2 spot was still some high order mode
like yesterday. MC lock was lost when the janitor bumped something around the MC.
|
|
6266
|
Fri Feb 10 02:35:29 2012 |
kiwamu | Update | IOO | crazy ground motion |
I gave up tonight's locking activity because the MC can't stay locked.
It seems that somehow the seismic noise became louder from about 1:00 AM. 
I walked around the outside of the 40-m building to see what's going on, but no one was jumping or partying.
I am leaving the MC autolocker disabled so that the laser won't be driven crazy and the WFS won't kick the MC suspensions.
The attachment is a 3-hour trend of the seismometer outputs and the MC trans.

|
6274
|
Fri Feb 10 23:19:09 2012 |
kiwamu | Update | IOO | cross talk causing fake seimometer signals |
[ Koji / Kiwamu ]
The frequent unlock of the MC are most likely unrelated to ground motion.
Although the reason why MC became unstable is still unclear.
There are two facts which suggest that the ground motion and the MC unlock are unrelated :
(1) It turned out that the seismometer signals (C1:PEM-SEIS-STS_AAA ) have a big cross talk with the MC locking signals.
For example, when we intentionally unlocked the MC, the seismometer simultaneously showed a step-shaped signals, which looked quite similar to what we have observed.
I guess there could be some kind of electrical cross talk happening between some MC locking signals and the seismometer channels.
So we should not trust the signals from the STS seismometers. This needs a further investigation.
(2) We looked at the OSEM and oplev signals of some other suspended optics, and didn't find any corresponding fluctuations.
The suspensions we checked are ETMX, ETMY, ITMX and MC1.
None of them showed an obvious sign of the active ground motions in the past 24 hours or so.
Quote from #6266 |
It seems that somehow the seismic noise became louder from about 1:00 AM. 
|
|
6281
|
Wed Feb 15 05:29:22 2012 |
kiwamu | Update | LSC | sensing matrix of PRMI |
I have measured the sensing matrix of PRMI.
It seems that the MICH signal in the 3f ports (REFL33 and REFL165) were quite tiny, and because of that it is very tough to use them for the actual MICH control.
The data is coming soon. |
6283
|
Wed Feb 15 17:15:33 2012 |
kiwamu | Update | LSC | sensing matrix of PRMI |
I think I have told a lie in the last meeting -- the measured sensing matrix doesn't look similar to what Optickle predicts.
Smells like something is very wrong.
Measured sensing matrix
The measured matrix are shown in the diagram below.
The lengths of arrows corresponds to the signal strength in unit of V/m. The radial axis in in log scale.
The angle of arrows corresponds to their best demodulation phases.
Some obvious things:
- REFL11 : The separation angle between MICH and PRCL is narrow and it is far from the ideal 90 degree. This doesn't agree with the simulation.
- REFL33: The MICH and PRCL signals are almost degenerated in their demodulation phase.
- REFL55 : It shows non-90 degree separation. This doesn't agree with the simulation.
- REFL165 : The separation is close to 90 degree, but the signals are small. And I am not sure if the MICH signal is real or just noise.
- AS55 : Somehow it shows a nice 90 degree separation, but this result doesn't agree with the simulation.
Expected sensing matrix from a simulation
For a comparison here is a result from an Optickle simulation.
This time the radial unit is W/m instead of V/m, but they are qualitatively the same unit.
The radial axis is in log, so when it says 2, it means 10^2 [W/m].
Simulation setup:
loss per optic = 50 ppm
Measurement
- Locked PRMI with the carrier anti-resonating in PRCL.
- Adjusted the control gains for both the MICH and PRCL control to have UGFs at ~ 100 Hz.
- Put a 30 dB notch filter in each control servo at 283.1 Hz where an excitation signal will be.
- Excited PRCL and MICH at different time via the realtime lockng in the LSC front end. The amplitude is 1000 counts and the frequency is at 238.1 Hz.
- For the MICH excitation, I have coherently and differentially excited ITMs
- Used DTT to take a transfer function (transfer coefficients at 283.1 Hz) from the lockin oscillator to each LSC demodulated signal.
- Including AS55I/Q, REFL11I/Q, REFL33I/Q, REFL55I/Q and REFL165I/Q.
- Calibrated the obtained transfer functions from unit of counts/counts to V/m using the actuator response (#5637)
Quote from #6281 |
I have measured the sensing matrix of PRMI.
It seems that the MICH signal in the 3f ports (REFL33 and REFL165) were quite tiny, and because of that it is very tough to use them for the actual MICH control.
The data is coming soon.
|
|
6284
|
Thu Feb 16 03:47:16 2012 |
kiwamu | Update | LSC | glitch table |
I updated the table which I posted some time ago (#6231). The latest table is shown below.
It seems that the glitches show up only when multiple DOFs are locked.
Interesting thing is that when the low finesse PRMI is locked with a big MICH offset (corresponding to a very low finesse) it doesn't show the glitches.
Qualitatively speaking, the glitch rate becomes higher as the finesse increases.
I will try SRMI tomorrow as this is the last one which I haven't checked the presence of the glitches.
|
Yarm
(POY11 -->
ETMY)
|
Xarm
(POX11 --> ETMX)
|
MICH
(AS55-->BS)
or
(AS55 --> ITMs)
|
Half PRMI
(REFL11 --> PRM)
or
(REFL33 --> PRM)
|
low finesse PRMI
(ASDC --> ITMs)
(REFL33 --> PRM)
|
PRMI (carrier)
(AS55 --> ITMs)
(REFL33 --> PRM)
|
PRMI (sideband)
(AS55 --> ITMs)
(REFL33 --> PRM)
|
DRMI
|
AS55 |
NO |
NO |
NO |
NO |
glitch (depends on finesse)
|
glitch |
glitch |
glitch |
REFL11 |
NO |
NO |
NO |
NO |
glitch (depends on finesse)
|
glitch |
glitch |
glitch |
REFL33 |
NO |
NO |
NO |
NO |
- |
glitch |
glitch |
glitch |
REFL55 |
NO |
NO |
NO |
NO |
glitch(depends on finesse) |
glitch |
glitch |
glitch |
REFL165 |
NO |
NO |
NO |
- |
- |
- |
- |
- |
POX11 |
- |
NO |
NO |
NO |
- |
glitch |
glitch |
glitch |
POY11 |
NO |
- |
NO |
NO |
- |
glitch |
glitch |
glitch |
POP55 |
- |
- |
- |
- |
- |
- |
- |
- |
|
|
|
|
|
|
|
|
|
|
6285
|
Thu Feb 16 04:02:16 2012 |
kiwamu | Update | LSC | insane REFL165 DC output |
I found that the DC monitor of the REFL165 was showing 9 V regardless of how much laser power goes to the diode.
I am worried about whether the RF output is also broken.
It needs to be checked and I will leave this to Suresh as one of his morning tasks.
|
6286
|
Thu Feb 16 04:29:30 2012 |
kiwamu | Update | LSC | upconversion noise from BS motion |
Sometimes ago I reported that there have been a kind of upconversion noise when PRM was excited (#6211).
This time I found another one, which showed up when BS was excited.
Assuming this is related to some kind of scattering process and also assuming this is from the same scattering body as that for the PRM driven case,
we may be able to localize and perhaps identify the scattering body.
(Measurement Condition)
All the suspended optics are intentionally misaligned except for ITMY so that the laser directly goes through to the dark port without any interference.
Then BS_POS is excited at 3 Hz with amplitude of 1000 counts by an oscillator in the realtime lockin system.
I also excited PITCH and YAW of BS and found that driving the angular motions didn't produce any upconversion noise.
I didn't excite ITMY to do the same test because I was too lazy.
(Noise spectrum)
The plot below shows the upconversion noise observed at AS55 and REFL11.
The reference curves were obtained when no excitation were applied on BS_POS.
It is obvious that the AS55 signal shows a typical upconversion behavior.
|
6291
|
Thu Feb 16 23:12:55 2012 |
kiwamu | Update | IOO | MC unlocking frequently |
The MC became crazy again.
It seems that there were corresponding steps in the OSEM signals. Look at the one-day trend posted below.

|
6292
|
Fri Feb 17 01:02:22 2012 |
kiwamu | Update | IOO | MC is back to normal |
[Koji / Kiwamu]
The MC is now back to normal. The beam pointing to the interferometer is good.
There were two different issues :
- A mechanical mount was in the MC WFS path.
- There were some loose connections in the SUS rack
Slid have we the position of the mechanical mount. Nicely the WFS beam go through now.
And also I pushed all the connectors associated with the MC SUS OSEMs in the SUS rack.
After pushing the connectors, the MC1 OSEM readouts dramatically changed, which actually more confused us.
As shown in the 3 hours trend below, the OSEM readouts have changed a lot (shown in the middle of the plot with arrows). Some bumps after the steps correspond to our alignment efforts.

Quote from #6291 |
The MC became crazy again.
|
|
6293
|
Fri Feb 17 04:45:48 2012 |
kiwamu | Update | LSC | sensing matrix of PRMI |
I locked the PRMI with the AS55I and Q combination.
It seems the glitche rate decreased,
but I am not 100 % sure because the rest of the demod signals (i.e. REFL11 and etc) were showing relatively big signals (noise ?), which may cover the glitches.
Also the optical gain of PRCL at AS55I doesn't agree with my expectation based on the obtained sensing matrix (#6283).
It looks too low and lower than the measured sensing matrix by a factor of 50 or so.
I will continue working on this configuration tomorrow and then move on to the SRMI locking as a part of the glitch hunting activity.
Quote from #6287 |
So why don't you use AS55I and Q for the control of PRMI???
|
|
6295
|
Sat Feb 18 16:58:59 2012 |
kiwamu | Update | IOO | MC suspension realigned |
[ Den / Kiwamu]
We have realigned the MC suspensions so that the WFS servos are smoothly engaged.
Now it seems working fine. The beam pointing to the interferometer also looks okay.
The WFSs control kept failing to engage the servos because of large misalignments in the MC suspensions.
When the TEM00 was locked, the transmitted light was only about 1200 counts and the reflected light was about 2.8 counts.
We tweaked MC1, MC2 and MC3.
Quote from #6294 |
When I came to the 40m this afternoon, the MC was unlocked. Here is the trend of MC_F for last 2 hours
|
|
6298
|
Tue Feb 21 04:30:02 2012 |
kiwamu | Update | LSC | Y arm + PRMI |
I tried the "Yarm + PRMI" configuration to see what happens.
The Y arm was locked at a resonance and held with the ALS technique.
On the other hand, the X arm was freely swinging.
I briefly tried severl demod signals to calm down the central part, but didn't succeed.
Now I feel I really want to have the X arm locked with the ALS technique too.
Give me the beat-box !
The attached screen shot shows the transmitted light of both arms as a function of time.
TRY is always above 1, since it was kept at a resonance.
Sometimes TRY went to 50 or so.

|
6300
|
Tue Feb 21 16:10:29 2012 |
kiwamu | Update | IOO | degradation in input PZT1 |
PZT1, the one with Koji's custom mid-HV driver (#5447), is getting degraded.
The movable range in the pitch direction became narrower than what it used to be (maybe a factor of 3 estimated by looking at the beam spots).
I think we should raise the priority level of the active TTs for the next vent.
I have been having a feeling that the PZT1 response is getting smaller since the end of the last year, but now I am confident
because I could see the difference between the movable ranges of Yaw and Pitch, and they used to have approximately the same amount of the movable ranges.
Right now this is not a serious issue as the beam pointing determined by the MC alignment is so good that the Pitch range doesn't rail.
I won't be surprised if it becomes completely immovable in 3 month. |
6301
|
Tue Feb 21 18:39:11 2012 |
kiwamu | Update | Green Locking | New BBPDs installed |
Two new BBPDs have been installed on the PSL table.
The first one was installed by Koji a few days ago, and I stalled the second one today.
They will serve as beat-note detectors for the green locking.
Next step : I have to lay down a long SMA cable which goes from the BBPD to the IOO rack. |
6303
|
Wed Feb 22 01:53:57 2012 |
kiwamu | Update | LSC | update on glitch table |
I tried SRMI. The glitch rate wasn't as high as that of PRMI but it happened once per 10 sec or so.
|
Yarm
(POY11 -->
ETMY)
|
Xarm
(POX11 --> ETMX)
|
MICH
(AS55-->BS)
or
(AS55 --> ITMs)
|
Half PRMI
(REFL11 --> PRM)
or
(REFL33 --> PRM)
|
low finesse PRMI
(ASDC --> ITMs)
(REFL33 --> PRM)
|
PRMI (carrier)
(AS55 --> ITMs)
(REFL33 --> PRM)
|
PRMI (sideband)
(AS55 --> ITMs)
(REFL33 --> PRM)
|
SRMI(NEW)
(AS55-->ITMs)
(REFL11I --> SRM)
|
DRMI
|
AS55 |
NO |
NO |
NO |
NO |
glitch (depends on finesse)
|
glitch |
glitch |
glitch |
glitch |
REFL11 |
NO |
NO |
NO |
NO |
glitch (depends on finesse)
|
glitch |
glitch |
glitch |
glitch |
REFL33 |
NO |
NO |
NO |
NO |
- |
glitch |
glitch |
glitch |
glitch |
REFL55 |
NO |
NO |
NO |
NO |
glitch(depends on finesse) |
glitch |
glitch |
glitch |
glitch |
REFL165 |
NO |
NO |
NO |
- |
- |
- |
- |
- |
- |
POX11 |
- |
NO |
NO |
NO |
- |
glitch |
glitch |
- |
glitch |
POY11 |
NO |
- |
NO |
NO |
- |
glitch |
glitch |
- |
glitch |
POP55 |
- |
- |
- |
- |
- |
- |
- |
|
- |
|
|
|
|
|
|
|
|
|
|
Quote from #6284 |
I updated the table which I posted some time ago (#6231). The latest table is shown below.
It seems that the glitches show up only when multiple DOFs are locked.
|
|
6304
|
Wed Feb 22 13:28:22 2012 |
kiwamu | Update | LSC | Y arm + central part locking |
Last night I tried the "Y arm + central part" locking again. Three different configuration were investigated :
- Y arm + DRMI
- Y arm + PRMI
- Y arm + MICH
In all the configurations I displaced the Y arm by 20 nm from the resonance.
As for the DRMI and PRMI configurations I wasn't able to acquire the locks.
As for the MICH configuration, the MICH could be locked with AS55. But after bringing the Y arm to the resonance point the lock of MICH was destroyed. |
6306
|
Wed Feb 22 19:45:33 2012 |
kiwamu | Update | LSC | how much length offset do we need ? |
I did a quick calculation to see if the offset of the arm length which I tried last night was reasonable or not.
The conclusion is that the 20 nm offset that i tried could be a bit too close to a resonance of the 55 MHz sidebands.
A reasonable offset can be more like 10 nm or so where the phases of all the laser fields don't get extra phases of more than ~ 5 deg.
The attached plot shows where the resonances are for each sideband as a function of the displacement from the carrier's resonance.

The red solid line represent the carrier, the other solid lines are for the upper sidebands and the dashed lines are for the lower sidebands.
The top plot shows the cavity power and the bottom plot shows how much phase shift the fields get by being reflected by the arm cavity.
Apparently the closest resonances to the the main carrier one are that of the 55 MHz sidebands, and they are at +/- 22 nm.
So if we displace the arm length by 22 nm, either of the 55 MHz sidebands will enter in the arm cavity and screw up the sensing matrix for the 55 MHz family.
Quote from #6304 |
In all the configurations I displaced the Y arm by 20 nm from the resonance.
|
|
6310
|
Fri Feb 24 03:58:13 2012 |
kiwamu | Update | LSC | Y arm + PRMI part II |
I tried the Yarm + PRMI configuration again.
The PRMI part was locked, but it didn't stay locked during the Y arm was brought to the resonance point.
I will post the time series data later.
(locking of the PRMI part)
Tonight I was able lock the PRMI when the arm was off from the resonance by 10 nm (#6306).
This time I used REFL11Q to lock the MICH instead of the usual AS55Q because the MICH didn't stay locked with AS55Q for some reason.
The PRCL was held by REFL33I as usual.
Also I disabled the power normalization for the error signals because it could do something bad during the Y arm is borough to the resonance.
In order to reduce the number of the glitches, PRM was slightly misaligned because I knew that the lower finesse gives fewer glitches. |