While fixing up some medm screens and getting spectra of the simulated plant, I realized that the naming convention for the Matrices of Filter banks was backwards when compared to that of the normal matrices (and the rest of the world). The naming was incorrectly column, row.
This has several ramifications:
1) I had to change the suspensions screens for the TO_COIL output filters.
2) I had to change the filters for the suspension with regards to the TO_COIL output filters so they go in the correct filter banks.
3) Burt restores to times previous March 11th around noon, will put your TO_COIL output filters in a funny state that will need to be fixed.
4) The simplant RESPONSE filters had to be moved to the correct filter banks.
5) If you have some model I'm not aware of that uses the FiltMuxMatrix piece, it is going to correctly build now, but you're going to have to move filters you may have created with foton.
New Focus Servo Controller has just arrived. We have 25 days to evaluate this product.
It will have to be shipped back to the vendor on April 4, 2011 the latest in order to get full refund.
The FM1 filter module change for XXSEN was propagated to the ETMX suspension. This was a change from a 30,100:3 with a DC gain of 1 to a 3:30 which just compensates the hardware filter.
The good gains for the Sim damping were found to be: 100 for ETMX_SUSPOS, 0.1 ETMX_SUSPIT, and 0.1 ETMX_SUSYAW, ETMX_SUSSIDE is -70. Gains much higher tended to saturate the simulated coils (i.e. hitting 10V limit) and then had to have the histories cleared for the RESPONSE matrix.
These seem to work to damp the real ETMX as well.
I did some work on the ETMY real and Sim.
It seems like there is still a problem with the input whitening filters. I believe the Xycom logic is set such that the analog whitening of the OSEM signals is turned ON only when the FM1 is turned OFF. Joe has got to fix this (and elog it) so that we can damp the suspension correctly. For now, the damping of the ETMY and the SETMY require different servo gains and signs, probably because of this.
4. The blue Output Filters section has been changed to agree with the new filter of matrices row, column labeling. My fault for not testing it and realizing it was broken. The change was made in /opt/rtcds/caltech/c1/medm/master/C1SUS_DEFAULTNAME.adl and then ,/generate_master_screens.py was run, updating all the screens.
5. I have swapped the logic for the sensor filter banks (ULSEN, URSEN, etc). It now sends a "1" to the Binary Output board controlling the OSEM analog whitening when the FM1 filter is ON. This has been done for all the suspensions (BS, ITMX,ITMY, SRM, PRM, MC1, MC2,MC3, ITMX, ITMY).
I am also updating the first sensor filter banks for the BS, ITMX, ITMY, SRM, PRM,MC1,MC2,MC3, called "3:30", to match the Y and X ends.
8. I can't find any documentation on how to get a momentary button press to toggle states. I could stick a filter bank in and use the on/off feature of that part, but that feels like a silly hack. I've decided for the moment to split the TM offset button into 2, one for ON, one for OFF. I'll put in on the list of things to have added to the RCG code (either a method, or documentation if it already exists).
EDIT: TM offset still doesn't work. Will worry about it next week.
9. Fixed a connection in SPY/SPX models where the side senor path that was missing a constant to a modulo block.
Steve pointed out to me today he couldn't get trends for his PEM slow channels like C1:PEM-count_full.
I experimented a bit and found for long time requests (over 20 days), it would produce minute trends up to the current time, but only if they started far enough back. So the data was being written, but something was causing a problem for dataviewer/NDS to find it.
On further investigation it looks to be some incorrect time stamps at several points in the last few months are causing the problems. Basically when Alex and I made mistakes in the GPS time stamp settings for the frame builder (daqd) code, the wrong time got written for hours to the raw minute trend data files.
So Alex is going to be running a script to go through the roughly 180 gigabytes of affected trend data to write new files with the correct time stamps. Once it done, we'll move the files over. We'll probably lose a few hours worth of recent trend data, depending on how quickly the scripts run, but after which minute trends should work as they are supposed to.
Prior to the works on the Y end setup I propose to perform the temperature scan business like Koji and Suresh did before (see this entry).
This business will allow us to easily find a beatnote at 532nm after the installation on the Y end.
I guess the right persons for this work are Bryan and Suresh.
Bryan will have a safety guidance from Steve in this after noon. So after that they can start working on it.
/* - - - coarse plan - - - */
* remove Alberto's laser from the AS table
* setup Alberto's laser on the PSL table
* put some stuff such as lenses, mirrors and etc. (Use the IR beam picked off after the doubling crystal for the main laser source)
* mode matching
Which laser are we going to use, Alberto's laser or MOPA laser ?
We use Alberto's laser for the Y end Green Locking.
Which laser are we going to use, Alberto's laser or MOPA laser ?
The reason for using Alberto's laser is that some amount of work has already gone into characterising its phase noise. Ref elog entry 2788
I updated our lockin simulink pieces to use the newer, more streamlined lockin piece that is currently in CDS_PARTS (with new documentation block!). It means we are no longer passing clock signals through three levels of boxes.
In order to use the piece, you need to right click on it after copying from CDS_PARTS and go to Link Options->Disable Link. This forces the .mdl to save all the relevant information about the block rather than just a pointer to the library. I talked with Rolf and Alex today and we discussed setting up another model file, non-library format for putting generically useful user blocks into, rather than using the CDS_PARTS library .mdl.
The BS, ITMX, ITMY, PRM, SRM, ETMX, ETMY now have working lockins, with the input matrix to them having the 2nd input coming from LSC_IN, the 3rd from the oplev pitch, and the 4th from oplev yaw.
This necessitated a few name changes in the medm screens. I also changed the lockin clock on/off switch to a direct amplitude entry, which turns green when a non-zero value is entered.
Currently, the Mode cleaner optic suspension screens have white lockins on them. I started modifying a new set of screens just for them, and will modify the generate_master_screens. Unfortunately, this requires modifying two sets of suspension screens going forward - the main interferometer optics and the MC optics.
PMC TRANS/REFL on MEDM showed red values for long time.
TRANS (a.k.a C1:PSL-PSL_TRANSPD) was the issue of the EPICS db.
REFL (a.k.a. C1:PSL-PMC_RFPDDC) was not physically connected.
There was an unknown BNC connected to the PMC DC output instead of dedicated SMA cable.
So they were swapped.
Now I run the following commands to change the EPICS thresholds:
ezcawrite C1:PSL-PMC_PMCTRANSPD.LOLO 0.8
ezcawrite C1:PSL-PMC_PMCTRANSPD.LOW 0.85
ezcawrite C1:PSL-PMC_PMCTRANSPD.HIGH 0.95
ezcawrite C1:PSL-PMC_PMCTRANSPD.HIHI 1
ezcawrite C1:PSL-PMC_RFPDDC.HIHI 0.05
ezcawrite C1:PSL-PMC_RFPDDC.HIGH 0.03
ezcawrite C1:PSL-PMC_RFPDDC.LOW 0.0
ezcawrite C1:PSL-PMC_RFPDDC.LOLO 0.0
As these commands only give us the tempolary fix, /cvs/cds/caltech/target/c1psl/psl.db was accordingly modified for the permanent one.
field(DESC,"RFPDDC- RFPD DC output")
field(INP,"#C0 S32 @")
field(DESC,"PMCTRANSPD- pre-modecleaner transmitted light")
field(INP,"#C0 S10 @")
Bryan Barr is visiting us from Glasgow for a month. He received 40m specific safety training on Friday.
I added a new ADC channel for a DC signal from the X end green PD.
It is called C1:GCX-REFL_DC and connected to adc_0_1, which is the second channel of ADC_0.
By the way, when I tried connecting it to an ADC I found that most of the channels on the AA board on 1X9 were not working.
Since the outputs form the board are too small the circuits may have benn broken. See the picture below.
In addition to that I realized that the signal from the PDH box for the temperature actuation is limited by +/- 2V due to the range of this AA board.
In fact the signal is frequently saturated due to this small voltage range.
We have to enlarge the range of this AA board like Valera did before for the suspensions (see this entry).
A comparator has been installed before the MFDs (mixer-based frequency discriminator) to eliminate the effect from the amplitude fluctuation (i.e. intensity noise).
As a result we reached an rms displacement of 580 Hz or 80 pm.
As a result we reached an rms displacement of 580 Hz or 80 pm.
(differential noise measurement)
Here is the resultant plot of the usual differential noise measurement.
The measurement has been done when the both green and red lasers were locked to the X arm.
In the blue curve I used only MFD. In the black curve I used the combination of the comparator and the MFD.
Noise below 3 Hz become lower by a factor of about 4, resulting in a better rms integrated from 40 Hz.
Note that the blue and the black curve were taken while I kept the same lock.
A calibration was done by injecting a peak at 311 Hz with an amplitude of 200 cnt on the ETMX_SUS_POS path.
Yesterday Koji modified his comparator circuit such that we can take a signal after it goes thorough the comparator.
The function of this comparator is to convert a sinusoidal signal to a square wave signal so that the amplitude fluctuation doesn't affect the frequency detection in the MFD.
I installed it and put the beat-note signal to it. Then the output signal from the comparator box is connected to the MFDs.
The input power for the comparator circuit has been reduced to -5 dBm so that it doesn't exceeds the maximum power rate.
- Plan for tomorrow
* Video cable session (I need ETMY_TRNAS) (team)
* Characterization of the Y end laser (Bryan / Suresh)
* LPF for the X end laser temperature control (Larisa)
* Frequency Divider (Matt)
* X end mechanical shutter (Kiwamu)
Succeeded in handing off the servo from the green to the red.
This time we found that the fluctuation in the IR signals became lesser as the gain of the ALS servo increased.
Therefore I increased the UGF from 40 Hz to 180 Hz to have less noise in the IR PDH signal.
Here is a preliminary plot for today's noise spectra.
The blue curve is the ALS in-loop spectrum, that corresponds to the beat fluctuation.
The red curve is an out-of-loop spectrum taken by measuring the IR PDH signal.
Since the UGF is at about 180 Hz the rms is integrated from 200 Hz.
The residual displacement noise in the IR PDH signal is now 1.2 kHz in rms.
I am going to analyze this residual noise by comparing with the differential noise that I took yesterday (see the last entry ).
Solid door, numbered 4 at south west corner of PSL enclosure was replaced by laser protective window.
The carpenter shop's Mark is making 4 more identical ones for the east side.
The Lightwave NPRO126 of 700mW was moved from the AP-table into the PSL-enclosure temporarily.
It's emergency shutdown switch can be seen at the center bottom picture
Yesterday during the day, Alex ran a script to fix the time stamps in the trends files we had messed up back during the daqd change overs around Feb 17th and 23rd. See this elog for more information on the trend problem.
Due to how the script runs, basically taking all the data and making a new copy with the correct time stamps, the data collected while the script was running didn't get converted over. So when he did the final copy of the corrected data, it created a several hour gap in the data from yesterday during the day time.
The original files still exist on the fb machine in /frames/trend/minute_raw_22mar2011 directory.
[Steve, Suresh, Larisa]
The following cables were laid today: ETMYT, ETMY, IFOPO, MC1, OMCR, AS Spare, and MC2T.
Though the paper suggested 135' for the MC2T, we used a 110'. This is too short: need at least another 15' for the MC2T.
The RCR cable wasn't crossed off on the list, but a cable exists at the RCR cable which is black and is labeled (old label, 75 ohms)
There was no indication of which length was needed for MC1, so a 95' cable was used.
Kiwamu and I looked at all the electronics that are currently in place for the green locking on the X-arm and have made a set of block diagrams of the rack mounted units that we should build to replace the existing ... "works of art" that sprawl around out there at the moment.
1. "ETM Green Oscillator/PDH support box". Not a great name but this would provide the local oscillator signal for the end PDH (with a controllable phase rotator) as well as the drive oscillator for the end laser PZT. Since we need to hit a frequency of 216.075kHz with a precision that Kiwamu needs to determine, we'd need to be able to tune the oscillator ... it needs to be a VCO. It'd be nice to be able to measure the output frequency so I've suggested dividing it down by N times to put it into the DAQ - maybe N = 2^7 = 128x to give a measured frequency of around 1.7kHz. Additionally this unit will sum the PDH control signal into the oscillation. This box would support the Universal PDH box that is currently at the X-end.
2. "Vertex X-arm beatnote box" - this basically takes the RF and DC signals from the beatnote PD and amplifies them. It provides a monitor for the RF signal and then converts the RF signal into a square wave in the comparator.
3. "Mixer Frequency Discriminator" - just the standard MFD setup stored in a box. For temperature stability reasons, we want to be careful about where we store this box and what it is made of. That's also the reason that this stage is separated from the X-arm beatnote box with it's high-power amps.
4. RS232 and EPICS control of the doubling ovens
5. Intensity stabilization of the End Laser
P.S. I used Google Diagrams for the pictures.
I tidied up some of the stuff that was on the SP table. The ISS box that has been sitting on there for months is now underneath the X-arm on top of the spare Marconi which is stored there.
Last Friday, we discovered a bug in the RCG where the delay part was not actually delaying. We reported this to Alex who promptly put a fix in the same day. This allowed Matt's newly proposed frequency discriminator to work properly.
It also required a checkout of the latest RCG code (revision 2328), and rebuild of the various codes. We backed up all the kernel and executables first such as mbuf.ko and awgtpman.
We did the following:
1) Log into the fb machine.
2) Go to /opt/rtcds/caltech/c1/core/advLigoRTS/src/drv/mbuf and run make. Copy the newly built mbuf.ko file to /diskless/root/modules/18.104.22.168/kernel/drivers/mbuf/mbuf.ko on the fb machine.
3) Use "sudo cp" to copy the newly built mbuf.ko file to /diskless/root/modules/22.214.171.124/kernel/drivers/mbuf/
4) Go to /cvs/cds/rtcds/caltech/c1/core/advLigoRTS/src/gds and run make.
5) Copy the newly built awgtpman executable to /opt/rtcds/caltech/c1/target/gds/bin/
6) Go to /opt/rtcds/caltech/c1/core/advLigoRTS/src/mx_stream/ and run make.
7) Copy the newly built mx_stream executable to /opt/rtcds/caltech/c1/target/fb/
Koji was unable to build his c1lst model first thing this morning. Turns out there was a bug with RCG parser that was introduced on Friday when we did the RCG updates. We talked Alex who did a quick comment fix. The diff is as follows:
--- Parser3.pm (revision 2328)
+++ Parser3.pm (working copy)
@@ -1124,8 +1124,8 @@
print "Flattening the model\n";
print "Finished flattening the model\n";
- CDS::Tree::do_on_nodes($root, \&remove_tags, 0, $root);
- print "Removed Tags\n";
+ #CDS::Tree::do_on_nodes($root, \&remove_tags, 0, $root);
+ #print "Removed Tags\n";
CDS::Tree::do_on_nodes($root, \&remove_busses, 0, $root);
This was some code to remove TAGs from the .mdl file for some reason which I do not understand at this time. I will ask tommorrow in person so I can understand the full story.
Koji then rebuilt and started the c1lst process. This is his new test version of the LSC code. We descovered (again) that when you activate too many DAQ channels (simply uncommenting them, not even recording them with activate=1 in the .ini file) that the frame builder crashes. In addition, the c1lsc machine, which the code was running on, also hard crashed.
When a channel gets added to the .ini file (or uncommented) it is sent to the framebuilder, irregardless of whether its recorded or not by the frame builder. There is only about 2 megabytes per second bandwidth per computer. In this case we were trying to do something like 200 channels * 16384 Hz * 4 bytes = 13 megabytes per second.
The maximium number of 16384 channels is roughly 30, with little to no room for anything else. In addition, test points use the same allocated memory structure, so that if you use up all the capacity with channels, you won't be able to use testpoints to that computer (or thats what Alex has led me to believe).
The daqd process then core dumped and was causing all sorts of martian network slowdowns. At the same time, the c1lsc computer crashed hard, and all of the front end processes except for the IOP on c1sus crashed.
We rebooted c1lsc, and restarted the c1sus processes using the startc1SYS scripts. However, the c1susfe.ko apparently got stuck in a wierd state. We were completely unable to damp the optics and were in general ringing them up severely. We tried debugging, including several burt restores and single path checks.
Eventually we decided to reboot the c1sus machine after a bit of debugging. After doing a burt restore after the reboot, everything started to damp and work happily. My best guess is the kernel module crashed in a bad way and remained in memory when we simply did the restart scripts.
I measured some laser powers associated with the beat-note detection system on the PSL table.
The diagram below is a summary of the measurement. All the data were taken by the Newport power meter.
The reflection from the beat-note PD is indeed significant as we have seen.
In addition to it the BS has a funny R/T ratio maybe because we are using an unknown BS from the Drever cabinet. I will replace it by a right BS.
During my work for making a noise budget I noticed that we haven't carefully characterize the beat-note detection system.
The final goal of this work is to draw noise curves for all the possible noise sources in one plot.
To draw the shot noise as well as the PD dark noise in the plot, I started collecting the data associated with the beat-note detection system.
* Estimation and measurement of the shot noise
* measurement of the PD electrical noise (dark noise)
* modeling for the PD electrical noise
* measurement of the doubling efficiency
* measurement of an amplitude noise coupling in the frequency discriminators
In the last week Matt and I modified the MFD configuration because the mixer had been illegally used.
Since the output from the comparator is normally about 10 dBm, a 4-way power splitter reduced the power down to 4 dBm in each output port.
In order to reserve a 7 dBm signal to a level-7 mixer, we decided to use an asymmetric power splitter, which is just a combination of 2-way and 3-way splitter shown in the diagram above.
With this configuration we can reserve a 7 dBm signal for a mixer in the fine path.
However on the other hand we sacrificed the coarse path because the power going to the mixer is now 2.2 dBm in each port.
According to the data sheet for the mixer, 1 dB compression point for the RF input is 1dBm. Therefore we put a 1 dB attenuator for the RF port in the coarse system.
In the delay line of the fine path we found that the delay cable was quite lossy and it reduced the power from 2.2 dBm to about 0 dBm.
Using 2 dBm for a Level 7 mixer is so bogus, that I will dismantle this as soon as I come over.
PLEASE DO NOT DISMANTLE THE SETUP !
Actually we tried looking for a level-3 or a smaller mixer, but we didn't find them at that moment. That's why we kept the level-7 mixer for the coarse path.
As you pointed out we can try an RF amplifier for it.
I (think) I have finished the new PMC base riser. The eDrawing of it (so you can view it on any computer) has been uploaded to the PMC wiki page.
I also attach it here, for comments.
Its going to need some kind of way to locate the PMC on the top. In the previous design, we had the 3 balls to decouple the body from the base. That design was flawed due to the roughness of the holes in the PMC body.
Also probably need some kind of relief on the bottom. Its possible that it would be OK like this, but I am unsure if the shop can maintain the flatness we want over the whole length and/or the flatness of any given (OLD) optical table over ~8". Its probably not a good idea to have to torque this (aluminum?) to make it conform to the optical table's shape.
Hmmm, so, this was just meant to be a riser that goes underneath the old PMC mount, to raise it from 3" beam height to 4" beam height. I will make another one that is a complete mount, designed for 4" beam height. Please hold........... .......... ....... ..... ... .
This is the log of the work on Wednesday 23rd.
1. Power Supply of the freq divider box
Kiwamu claimed that the comparator output of the freq div box only had small output like ~100mV.
The box worked on the electronics bench, we track down the power supply and found the fuse of the +15V line
brew out. It took sometime to notice this fact as the brown-out-LED of the fuse was not on and the power
supply terminal had +15V without the load. But this was because of the facts 1) the fuse is for 24V, and 2)
the large resistor is on the fuse for lighting the LED when the fuse is brown out.
I found another 24V fuse and put it there. Kiwamu is working on getting the correct fuses.
2. MC locking problem
After the hustle of the freq divider, the MC didn't lock. I tracked down the problem on the rack and found
there was no LO for the MC. This was fixed by pushing the power line cable of the AM Stabilizer for the MC LO, which was a bit loose.
This is the continuation of http://nodus.ligo.caltech.edu:8080/40m/4402
The first picture is of the actual component, where the resistor is 1M and capacitor is 10uF.
But before the component can be put into place, its transfer function had to be checked to make sure it was doing what we calculated it would do. The results of these are in the graphs generated: frequency vs. gain, and frequency vs. phase.
According to these graphs, we are not achieving the targeted cutoff frequency: need to recalculate and compensate for the extra 100k resistance being encountered.
For bode plot:
USE LOG-LOG plot for the amplitude
USE LOG-LINEAR plot for the phase
Search "Bode Plot" on web
* Temporary strain relief for the heliax cables on 1X2 (Steve)
* RF diagrams and check lists (Suresh)
=> In the lunch meeting we will discuss the details about what we will do for the RF installation.
* Electronics design and plan for Green locking (Aidan / Kiwamu)
=> In the lunch meeting we will discuss the details.
* LSC model (Koji)
* Video cable session (team)
* LPF for the laser temperature control (Larisa)
[Steve / Kiwamu]
As a part of the video cable session, we reconnected some power cords on 1Y1 rack.
During the work we momentarily turned off c1aux, which handles DMF, Illumintators, mechanical shutters and the old video epics.
I think it automatically reverted the things, but we may need to check them.
[Steve, Suresh, Kiwamu, Larisa]
Only the PRM/BS cable was laid today.
In one of the previous updates on cable laying, it was noted that the MC2 cable needed an additional 10' and the MC2T needed an additional 15' to reach their destinations. We cut and put BNC ends on 10' and 15' cables and connected them to the original cables in order to make them long enough.
This concludes the laying of new cables. Suresh is currently working on the QUADs...
The attached table shows the amplitude of the green beat note when the end laser was in various states. We can increase the beat note amplitude dramatically by switching to a different states.
C1:GCX-GRN_REFL_DC: 638 counts
C1:GCV-XARM_BEAT_DC: (PSL blocked) 950 avg counts (zero = -794 counts)
amplitude of beat note: -23dBm (after PD + amps) (f ~ 30 MHz)?
C1:GCX-SLOW_SERVO2_OUT: 318 counts
C1:GCX-GRN_REFL_DC: 180 counts
C1:GCV-XARM_BEAT_DC: (PSL blocked) 1270 avg counts (zero = -794 counts)
C1:GCV-XARM_BEAT_DC: (PSL unblocked) 1700 avg counts (zero = -794 counts)
amplitude of beat note: -7dBm (after PD + amps) f = 60MHz
amplitude of beat note: 0dBm (after PD + amps) f = 30MHz
C1:GCX-SLOW_SERVO2_OUT: 290 counts
C1:GCX-GRN_REFL_DC: 220 counts
C1:GCV-XARM_BEAT_DC: (PSL blocked) 1120 avg counts (zero = -794 counts)
C1:GCV-XARM_BEAT_DC: (PSL unblocked) 1520 avg counts (zero = -794 counts)
amplitude of beat note: 0dBm (after PD + amps) f = 15MHz
C1:GCX-SLOW_SERVO2_OUT: 305 counts
PSL temp = ??
C1:PSL-FSS_SLOWM = -3.524
The video work has crossed a milestone.
Kiwamu and Steve have shifted the three quads from the control room to the Video MUX rack (1Y1) and have wired them to the MUX.
The monitors in the control room have been repositioned and renumbered. They are now connected directly to the MUX.
Please see the new cable list for the input and output channels on the MUX.
As of today, all cables according the new plan are in place. Their status indicated on the wiki page above is not verified . Please ignore that column for now, we will be updating that soon.
I shifted the MC1F/MC3F camera and the MC2F cameras onto the new cables. Also connected the monitors at the BS chamber and end of the X arm to their respective cables. I have removed the RG58B BNC (black) cables running from MC2 to BS and from ETMXF to the top of the Flow Bench.
Some of the old video cables are still in place but are not used. We might consider removing them to clear up the clutter.
Some of the video cables in use are orange and if the lab's cable color code is to be enforced these will have to be replaced with blue ones..
Some of the cables in use running from the MUX to the monitor in the control room are the white 50 Ohm variety. There are also black RG59 Cables running the same way ( we have surplus cables in that path) and we have to use those instead of the white ones.
There are a number of tasks remaining:
a) The inputs from the various existing cameras have to be verified.
b) There are quite a few cameras which are yet to be installed.
c) The Outputs may not not be connected to their monitors. That the monitors may still be connected to an old cable which is not connected to the MUX. The new cable should be lying around close by. So if you see a blank monitor please connect it to its new cable.
d) The status column on the wiki page has to be updated.
e) Some of the currently in place may need to be replaced and some need to be removed. We need to discuss our priorities and come up with a plan for that.
After checking everything we can certify that the video cabling system is complete.
I would like Joon Ho to take care of this verification+documenting process and declaring that the job is complete.
Steve attached these two pictures.
After I did several things to add new DAQ channels on c1iscex it suddenly became out of network. Maybe crashed.
Then c1iscex didn't respond to a ping and all the epics values associated with c1iscex became not accessible.
I physically shut it down by pushing the reset button. Then it came back and is now running fine.
(how I broke it)
Since activateDAQ.py has screwed up the 'ini' files including C1SCX.ini, I was not able to add a channel to C1SCX.ini by the usual daqconfig GUI.
So I started editing it in a manual way with an editor and changed some sentences to that shown below
Then I rebooted fb to reflect the new DAQ channels.
After that I looked at the C1_FE_STATUS.adl screen and found some indicator lights were red.
So I pushed "Diag reset" button and "DAQ Reload" button on the C1SCX_GDS_TP.adl screen and then c1iscex died.
After the reboot the new DAQ channels looked acquired happily.
This is my second time to crash a front end machine (see this entry)
I made a coarse noise budget in order to decide our next actions for the X arm green locking.
So be careful, this is not an accurate noise budget !
Some data are just coming from rough estimations and some data are not well calibrated.
Assuming all the noise are not so terribly off from the true values, the noise at high frequency is limited by the dark noise of the PD or it already reaches to the IR inloop signal.
The noise at low frequency is dominated by the intensity noise from the transmitted green light although we thought it has been eliminated by the comparator.
In any case I will gradually make this noise budget more accurate by collecting some data and calibrating them.
According to the plot what we should do are :
* More accurate PD noise measurement
* More accurate shot noise estimation
* Searching for a cause of the small beat signal (see here) because a bigger beat signal lowers the PD noise.
* Investigation of the Intensity noise
I unpacked the STS2 seismometers that we borrowed from LLO. They are sitting underneath the Xarm, in the middle of the mode cleaner, near the other seismometer stuff.
It turned out that the dark noise from the beat PD and the shot noise on the beat PD was overestimated.
So I corrected them in the plot of the last noise budget (#4482).
Additionally I added the end laser error signal in the plot. Here is the latest plot.
The end laser error spectrum is big enough to cover most of the frequency range.
(although it was taken at a different time from the other curves.)
[Steve, Kiwamu, Larisa]
Having finished laying new cable last week, we moved on to connecting those on PSL table and AP table.
--RCR, RCT, PMCR (all three are blue)
--OMCR (blue cable, ***now has a camera***), PMCT, IMCR, REFL, AS (white cable), OMCT (***now has camera***)
Unless otherwise noted, the cables are black on the AP table. Also on the AP table: cables were connected directly to the power source.
The wiki has been updated accordingly.
Steve noted that MC2T and POP cameras are not there.
The PSL enclosure now have 4 windows on each side. The bottom rail guides on the east side will be replaced by one U-channel for smoother, more gentle sliding.
Door position indicator- interlock switches are not wired yet.
The controls (fast and slow both) think ITMX is ITMY and ITMY is ITMX.
After some poking around today, I have convinced myself it is sufficient to simply swap all instances of ITMX for ITMY in the C1_SUS-AUX1_ITMX.db file, and then rename it to C1_SUS-AUX1_ITMY.db (after having moved the original C1_SUS-AUX1_ITMY.db to a temporary holding file).
A similar process is then applied to the original C1_SUS-AUX1_ITMY.db file. These files live in /cvs/cds/caltech/target/c1susaux. This will fix all the slow controls.
To fix the fast controls, we'll modify the c1sus.mdl file located in /opt/rtcds/caltech/c1/core/advLigoRTS/src/epics/simLink/ so that the ITMX suspension name is changed to ITMY and vice versa. We'll also need to clean up some of the labeling
At Kiwamu and Bryan's request, this will either be done tomorrow morning or on Monday.
So the steps in order are:
1) cd /cvs/cds/caltech/target/c1susaux
2) mv C1_SUS-AUX1_ITMX.db C1_SUS-AUX1_ITMX.db.20110408
3) mv C1_SUS-AUX1_ITMY.db C1_SUS-AUX1_ITMY.db.20110408
4) sed 's/ITMX/ITMY/g' C1_SUS-AUX1_ITMX.db.20110408 > C1_SUS-AUX1_ITMY.db
5) sed 's/ITMY/ITMX/g' C1_SUS-AUX1_ITMY.db.20110408 > C1_SUS-AUX1_ITMX.db
8) Modify c1sus model to swap ITMX and ITMY names while preserving wiring from ADCs/DACs/BO to and from those blocks.
9) code; make c1sus; make install-c1sus
10) Disable all watchdogs
11) Restart the c1susaux computer and the c1sus computer
The measured power levels of the RF source harmonics are given below:
We are considering inclusion of bandpass filters centered on 11 and 55 MHz to suppress the harmonics and meet the requirements specified in Alberto's thesis (page 88).
I started to modify another green PD set.
It so far has the transimpedance of 240 Ohm on CLC409 for the RF output.
It shows the BB output upto ~100MHz.
The measurement shows the transimpedenca of ~90Ohm which is ~25% smaller than the expected gain of 120Ohm.
It is calibrated based on the transimpedances of Newfocus 1611 (10kOhm and 700Ohm for AF and RF).
The next step is to change the transimpedance resister to 2k and replace the PD to S3399 Si PD, which has the diameter of 3mm.
Then, the noise level will be measured. (and replace the RF opamp if necessary)
Ooh. Can you explain the purpose of the resistors which are connected to the (+) inputs? It looks like some real electronics ninjitsu.