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ID Date Author Type Categoryup Subject
  4154   Fri Jan 14 11:29:00 2011 kiwamuUpdateLSCexpected open loop TF of X arm locking

Here shows a plot of the expected open loop transfer function (TF) for the X arm locking.

xarm_oltf.png

I assume that the delay time of the digital system associated with the ADC/DAC and the digital filtering process is ~100 usec independently from the RFM delay according to Yuta's measurement (#3961).

Also I assume the MC2 pendulum has a pole at 1Hz with Q of ~5, and the X arm has its cavity pole at ~3kHz.

When the lock acquisition takes place, we used the red curve shown above in order to avoid a big DC feedback onto MC2.

Once the X arm became resonant at TEM00, we manually switched FM3 on, which is a boost filter containing a pole at  1Hz and a zero at 50Hz in order to suppress the residual motion below 1Hz.

The expected curve for the boosted state is drawn by the blue curve in the plot. 

With this open loop TF, the UGF can be realized only around 100-300 Hz due to the phase margin condition.

This expectation of the UGF is consistent with our measurement because we obtained the UGF around 200-300Hz.

In fact above 300Hz we observed that the control became unstable and started oscillating.

 

Quote:

 (some notes)

 unWhitening filter           pole:15Hz. pole:15Hz, zero:150Hz, zero:150Hz

 C1LSC_MC_FM1   pole:1kHz, zero:10Hz

 Gain in digital control       G ~ -1

measured UGF  ~  200-300 Hz

 measured RFM delay ~ 125 usec 

 

  4156   Fri Jan 14 12:34:08 2011 KojiUpdateLSCX arm locked with C1LSC digital control

My feeling was that the saturation was caused by the LSC whitening filter which was always on.
Once the LSC whitening filter is controlled from C1LSC, we would be able to remove the attenuator.

Quote:

  - attenuation of RF signal

  Since the PDH signal taken by C1LSC's ADC had been saturated somewhat, we introduced a ND filter of 10 on the photo diode to attenuate the RF signal.

As a result the amplitude of the PDH signal on dataviewer became more reasonable. No more saturations.

 

  4180   Thu Jan 20 22:17:12 2011 ranaSummaryLSCFPMI Displacement Noise

I found this old plot in an old elog entry of Osamu's (original link).

It gives us the differential displacement noise of the arms. This was made several months after we discovered how the STACIS made the low frequency noise bad, so I believe it is useful to use this to estimate the displacement noise of the arm cavity today. There are no significant seismic changes. The change of the suspension and the damping electronics may produce some changes around 1 Hz, but these will be dwarfed by the non-stationarity of the seismic noise.

Attachment 1: osamu-1140657006.pdf
osamu-1140657006.pdf
  4186   Fri Jan 21 23:55:25 2011 ranaConfigurationLSCPhase Noise Measurement filter

We've set up a beat note measurement between the VCO driver and the Marconi (see Suresh's elog).

Here's the 'unWhiten' filter for compensating the SR560 TF.

It has poles = 1 mHz, 5 kHz, 5 kHz

and  zeros = 30 mHz, 1 kHz

The gain is set to be ~0.001 in the 1-100 Hz band to compensate the G=1000 of the SR560.

Attachment 1: a.gif
a.gif
  4253   Fri Feb 4 23:39:56 2011 rana, kojiUpdateLSCmixer based FD set up for noise test

We set up the mixer based FD to check out its noise performance.

It is being acquired as C1:GCV-XARM_FINE_OUT_DAQ.

We have calibrated it by driving the frequency of the RF signal generator and putting the value into the GAIN field. We got 100 kHz / 5450 counts; the _OUT_DAQ channel is now being recorded in units of Hz. The cable length has been adjusted so that the full mixer output can swing 16 MHz peak-peak before turning over.

Also, we did a lot of cable cleanup around the IO rack. Kiwamu and Suresh's setups were somewhat dismantled. The whole area was too messy and too hacky to be allowed to survive. Our "temporary" setups have a way of becoming permanent holding places for barrels, adapters, duct tape, etc.

  4493   Wed Apr 6 18:55:49 2011 Jamie, LarisaConfigurationLSCmajor AP table cleanup

We ripped out all of the old AS, PLL, and REFL paths, green, orange, and cyan respectively on the old AP table layout photo:

  • AS (green): had already been re-purposed by putting a ThorLabs diode right after the first steering mirror.   Everything downstream of that has been removed.
  • PLL (orange): everything removed.
  • REFL (cyan): CCD was left in place, so everything upstream of that was not touched.  Everything else was removed, including all of the REFL detectors.
  • OMCT (purple): previously removed
  • OMCR (blue): left in place, but the diode and CCD are not connected (found that way).
  • MCT (magenta): previously removed.
  • IMRC (red): untouched

All optics and components were moved to the very south end of the SP table.

We also removed all spurious cables from the table top, and from underneath, as well as pulled out no-longer-needed power supplies.

  4521   Wed Apr 13 23:32:07 2011 Aidan, JamieConfigurationLSCAS PD and Camera installed

I spent some time tracking down the AS beam which had vanished from the AP table. Eventually, by dramatically mis-aligning SRM, PRM and ITMY, returning BS to its Jan 1st PITCH and YAW values and tweaking the ITMX alignment [actual values to follow], I was able to get an AS beam out onto the AP table. I verified that it was the prompt reflection off ITMX by watching it move as I changed the YAW of that optic and watching it stay stationary as I changed the YAW of ITMY.

Jamie and I then steered the beam through a 2" PLCX-50.8-360.6 lens and placed the RF PD (AS55) at the focus. Additionally, we installed the AS camera to observe the leakage field through a Y1S steering mirror (as shown in the attached diagram).

Currently the PD has power but the RF and DC outputs are not connected to anything at the moment.

Atm 2 by Steve

 

 

Attachment 1: AS_beam.jpg
AS_beam.jpg
Attachment 2: P1070546.JPG
P1070546.JPG
  4523   Thu Apr 14 01:03:43 2011 KojiUpdateLSCLSC Campaign ~ Status

Target: To lock the Michelson with the new RF/LSC


Status

RF generation box: READY - already ready to go to the IOO rack. (Suresh)

RF distribution box: In Progress - the internal components are to be connected. (13th evening - Suresh)

Placing PD and CCD: Done - PD and CCD on the AP table (13th Afternoon - Aidan, Larisa with supervision of Kiwamu)

Cabling1: Done - PD signal AP table to the demodulator (13th Afternoon - Jamie with supervision of Suresh)

Cabling2: Done - RF generation box (IOO Rack) to the demodulator

Demodulator: In Progress - Test and install (13th night - Kiwamu with supervision of Suresh)

LSC model: Done - Run the new LSC model. (It is named as "C1LST" so far) (13th evening - Jamie)

LSC medm: Done on 14th - Modify the current LSC medm screens Update the EPICS database Adjust the matrices (- Jenne with supervision of Koji)

  4526   Thu Apr 14 19:05:17 2011 KojiUpdateLSCNew (temporary) LSC screen

[Jenne Koji]

The PD signals are transmitted to the suspension now.

The trigger thresholds were set to -1. This means the triggers are always on.

Attachment 1: temporary_LSC_screen.png
temporary_LSC_screen.png
  4527   Fri Apr 15 02:17:18 2011 kiwamuUpdateLSCMichelson locked

[Koji / Kiwamu]

The Michelson was locked with the new LSC realtime code.

 

 

(what we did)

 --  Fine alignment of the Michelson, including PZTs, BS and ITMY.

  Since the X arm has been nicely aligned we intentionally avoided touching ITMX. The IR beam now is hitting the center of both end mirrors.

  At the end we lost X arm's resonance for IR. This probably means the PZTs need more careful alignments.

 

-- Signal acquisition

 We replaced the RFPD (AS55) that Aidan and Jamie nicely installed by POY11 because we haven't yet  installed a 55MHz RF source.

The maximum DC voltage from the PD went to about 50 mV after aligning steering mirrors on the AP table.

The RF signal from the PD is transferred by a heliax cable which has been labeled 'REFL33'.

Then the RF signal is demodulated at a demodulation board 'AS11', which is one of the demodulation boards that Suresh recently modified.

Although we haven't fully characterized the demod board the I and Q signal looked healthy.

Finally the demod signals go to ADC_0_3 and ADC_0_4 which are the third and fourth channel.

They finally show up in REFL33 path in the digital world.

 

-- Control

 With the new LSC code we fedback the signal to BS. We put anti-whitening filters in the I and Q input filter banks.

We found that dataviewer didn't show correct channels, for example C1LSC_NREFL33I showed just ADC noise and C1LSC_NREFL33Q showed NREFL_33I.

Due to this fact we gave up adjusting the digital phase rotation and decided to use only the I-phase signal.

Applying a 1000:10 filter gave us a moderate lock of the Michelson. The gain was -100 in C1LSC_MICH_GAIN and this gave us the UGF of about 300 Hz.

 Note that during the locking both ETMs were intentionally misaligned in order not to have Fabry-Perot fringes.

  4528   Fri Apr 15 02:18:50 2011 KojiUpdateLSCBunch of RF cables removed

While Kiwamu was working on the RF cabling at the LSC rack, I removed 80% of SMA cables which were not connected anywhere.
The rack is cleaner now, but not perfect yet. We need patch panels/strain relieving for heliaxes, cleaning up of the RF/LO cables, etc.

  4530   Fri Apr 15 12:17:39 2011 kiwamuUpdateLSC11MHz demod board : funny I-Q phase

During checking the 11MHz demod boards I found that the I-Q relative phase showed funny LO power dependence.

It is now under investigation.

relativephase.png

 In the plot above the green curve represents the I-Q phase of a 11MHz demod board (see here).

It showed a strong dependence on the LO power and it changes from -60 deg to -130 deg as the LO power changes.

This is not a good situation because any power modulation on the LO will cause a phase jitter.

For a comparison I also took I-Q relative phase of a 33MHz demod board, which hasn't been modified recently.

 It shows a nice flat curve up to 5 dBm although it looks like my rough measurement adds a systematic error of about -5 deg.

 

 - to do -

* check RF power in every point of LO path on the circuit

* check if there is saturation by looking at wave forms.

  4533   Fri Apr 15 15:15:08 2011 kiwamuUpdateLSC11MHz demod board : 90 degree splitter

[Rana, Koji, Kiwamu]

 Moreover the amplitude of the I and Q signals are highly unbalanced, depending on the LO power again.

This implies the coil for a 90 degree splitting won't work at 11 MHz since the coil is home made and used to be designed for a specific frequency (i.g. 24.5 MHz).

We decided to use a Mini circuit 90 deg splitter instead. Steve will order few of them soon and we will test it out.

Quote:

During checking the 11MHz demod boards I found that the I-Q relative phase showed funny LO power dependence.

It is now under investigation.

 

  4536   Fri Apr 15 22:57:38 2011 Aidan, JamieConfigurationLSCAS PD and Camera installed

AS port ITMX YAW  range where AS beam was visible = [-1.505, -1.225] - these extrema put the beam just outside of some aperture in the system -> set ITMX YAW to -1.365

ITMX PITCH range = [-0.7707, -0.9707] -> set to ITMX PITCH to -0.8707

Quote:

I spent some time tracking down the AS beam which had vanished from the AP table. Eventually, by dramatically mis-aligning SRM, PRM and ITMY, returning BS to its Jan 1st PITCH and YAW values and tweaking the ITMX alignment [actual values to follow], I was able to get an AS beam out onto the AP table. I verified that it was the prompt reflection off ITMX by watching it move as I changed the YAW of that optic and watching it stay stationary as I changed the YAW of ITMY.

Jamie and I then steered the beam through a 2" PLCX-50.8-360.6 lens and placed the RF PD (AS55) at the focus. Additionally, we installed the AS camera to observe the leakage field through a Y1S steering mirror (as shown in the attached diagram).

Currently the PD has power but the RF and DC outputs are not connected to anything at the moment.

Atm 2 by Steve

 

 

 

  4537   Sat Apr 16 02:00:14 2011 ranaUpdateLSC11MHz demod board : 90 degree splitter

One way to avoid some of the bad stuff in there is to take the 1 dBm input and amplify it to ~21 dBm before splitting and sending in to the Level 17 mixers.

One way to do this is by using the A3CP6025 from Teledyne-Cougar. Its an SMA connectorized amp which can put out 25 dBm and has a gain of 24 dB. We can just glue it onto the demod boards. Then we can remove the ERA-5 amplifiers and just use the broadband splitter as Kiwamu mentioned.

  4538   Mon Apr 18 13:05:57 2011 kiwamuSummaryLSCdemod board modification

Here is the idea how we upgrade the demodulation boards.

Basically we go ahead with two steps as depicted in the cartoon diagram below.

Once we finish the first step of upgrade, the board will be ready to install although the circuit won't be awesome in terms of noise performance.

 

demod_board.png

 

* * * (details) * * *

 First of all we will replace the home-made 90 degree splitter (see this entry) by a commercial splitter, PSCQ-2-51-W+ from Mini circuit. This is the step 1 basically.

At this point the boards will be ready to use in principle. I asked Steve to get three 90 degree splitters so that we can have at least three demodulators for the dual-recycled Michelson locking.

If they work very fine we will buy some more 90 degree splitters for full locking.

While we try to lock the dual-recycled Michelson once we will get a Cougar amplifier, remove all ERA-5s and install it such that we don't have to gain up and down in the circuit. This is the last step.

  4539   Mon Apr 18 14:11:44 2011 kiwamuUpdateLSCRF status

 We will make them all green !!

 RF_Work_Status.png

Again, all the files are available in the svn.

https://nodus.ligo.caltech.edu:30889/svn/trunk/suresh/40m_RF_upgrade/

  4540   Mon Apr 18 17:47:41 2011 kiwamuConfigurationLSCLSC rack's ADC cabling

To understand the situation of the ADC cabling at the LSC rack I looked around the rack and the cables.

The final goal of this investigation is to have nice and noise less cables for the ADCs (i.e. non-ribbon cable)

Here is just a report about the current cabling.

 

(current configuration)

At the moment there is only one ribbon-twisted cable going from 1Y2 to 1Y3. (We are supposed to have 4 cables).

At the 1Y2 rack the cable is connected to an AA board with a 40 pin female IDC connector.

At the 1Y3 rack the cable is connected to an ADC board with a 37 pin female D-sub connector.

The ribbon cable is 28AWG with 0.05" conductor spacing and has 25 twisted pairs (50 wires).

LSCrack.png

 

(things to be done)

 - searching for a twisted-shielded cable which can nicely fits to the 40 pin IDC and 37 pin D-sub connectors.

 - estimating how long cable we need and getting the quote from a vendor.

 - designing a strain relief support

  4554   Thu Apr 21 21:24:41 2011 kiwamuUpdateLSCdemod board : new 90 deg splitter

A new 90 degree splitter, PSCQ-2-51W, has arrived today and I installed it on a demod board called AS11.

Results of the I-Q phase measurement with the new splitter will be reported soon.

 

 * Picture 1 = before removal of the handmade coil

 * Picture 2 = after removal of the coil and the associated capacitors

 * Picture 3 = after soldering PSCQ-2-51-W

DSC_2949_ss.jpg

DSC_2951.JPG

DSC_2952_ss.jpg

Quote from #4358

 First of all we will replace the home-made 90 degree splitter (see this entry) by a commercial splitter, PSCQ-2-51-W+ from Mini circuit. This is the step 1 basically.

  4555   Thu Apr 21 21:46:22 2011 kiwamuUpdateLSCdemod board : new 90 deg splitter

A less LO power dependence on the relative phase was found. The new 90 deg splitter works better.

From -3 dBm to 10 dBm in LO power, the relative phase is within 90 +/- 5 deg.

As a comparison I plot the phase that I measured when the handmade coil had been there (green curve in the plot).

relativephase.png

 

 I will also measure amplitude unbalances between I and Q.

Quote from #4554

A 90 degree splitter, PSCQ-2-51W, has arrived today and I installed it on a demod board called AS11.

Results of the I-Q phase measurement with the new splitter will be reported soon.

 

 

  4560   Fri Apr 22 11:08:50 2011 kiwamuUpdateLSCdemod board AS11 : amplitude imbalance

Amplitude imbalance between I and Q in a demod board, AS11, with the new 90 deg splitter was measured.

It shows roughly 10% amplitude imbalance when the LO power is in a range from 0 to 5 dBm. Not so bad.

 

  With the handmade coil there used to be a huge imbalance (either I or Q goes to zero volt while the other keeps about 1 V rms) as the LO power decreases.

But with the new 90 deg splitter now there are no more such a huge imbalance.

The remaining 10 % imbalance possibly comes from the fact that we are using ERA-5 in each I and Q path. They may have such gain imbalance of 10%.

We should check the ERA-5 gains so that we can confidently say ERA-5 causes the amplitude imbalance.

Then our plan replacing the ERA-5s (see here) will sound more reasonable.

IQamplitude.png

 

Quote from #4555

The new 90 deg splitter works better.

 I will also measure amplitude unbalances between I and Q.

 

  4567   Mon Apr 25 22:38:49 2011 kiwamuUpdateLSCprepration for DRMI : Y arm flashing
This week is going to be a recycled Michelson week.
As a preparation I did several things today :
 1. Alignment of the Y arm
 2. Alignment of PRM
 3. Checking of all the pick-off ports

 


 
(Y arm alignment)
 The idea to have the Y arm aligned is that : once we lock the Y arm we will be able to align the input PZTs using the Y arm as a reference.
 I tried aligning the Y arm and successfully made the Y arm flashing with IR. I can see it flashing on ITMY camera but no flashing on ETMY camera.
 
(PRM alignment)
PRM has been intentionally misaligned for the single arm green locking test.
I just confirmed that we can bring PRM back to a good alignment. Now we can see the central part is flashing too.
 
(picked-off beams)
I went checking through all the picked off beams to see if they are available or not.
POX : lost
POY : fine
POP : very clipped
POSRM : fine
  4570   Tue Apr 26 22:56:01 2011 kiwamuUpdateLSCc1iscaux2 and c1iscaux restrated

While checking whitening filters on the LSC rack, I found some epics controls for the whitening looked not working.

So I powered two crates off : the top one and the bottom one on 1Y3 rack.

These crates contain c1iscaux and c1iscaux2. Then powered them on. But it didn't solve the issue.

  4574   Wed Apr 27 18:14:48 2011 kiwamuUpdateLSCpreparation for DRMI locking : RF status

RF_Work_Status.png

POX11 (see this entry) is now listed as REFL11 (on the very top row).

We will rename POY11 to POP11 for DRMI locking.

The files are on https://nodus.ligo.caltech.edu:30889/svn/trunk/suresh/40m_RF_upgrade/.

  4576   Wed Apr 27 21:08:08 2011 ranaUpdateLSCAS11

I worked on AS_11 today. Its ready for its noise / optical gain calibrations. I have left it on Suresh's desk.

AS11.png

This was one of the 24.5 MHz Black Box (Ben Abbott) style RFPDs rescued from LLO. The tunable inductor that was installed was too small to get the frequency down to 11 MHz and so I swapped in one of the shielded, ferrite core ones from our '7mm' CoilCraft kit. It had a range of 1.2 - 1.8 uH according to the datasheet.

I wasn't able to simulataneously get the peak at 11.06 MHz and the notch at 59.3 MHz and so I took Koji's advice and tuned the peak best. The plot above shows how the notch is slightly off. I think its not a problem; to get it better we would have to change out the inductor for the "2-omega" notch, but I was too lazy. The thinking is that its more important to have the gain be symmetric around the signal readout frequency so as to not imbalance the audio sidebands.

Since this one is going to be AS_11, we think that the 22 MHz signal will be tiny: the transmission of the 11 MHz sidebands to the dark port is small. If we later want to put in a 22 MHz notch anyway, there is space to do this via the 'active notch' pads around the MAX4107.

For the above plot, I used the Jenne laser. The DC output of the PD was ~30 mV (~0.6 mA). The RF drive to the laser was -10 dBm: no saturations. I have calibrated out the cable responses, but not using the 1811 setup, so the absolute calibration has yet to be done.

Also, it needs some new stickers. It would be handy if someone can figure out how to get some sheets of stickers that we can put into the printer. Then we can laser printer all of the data onto the stickers and stick them to the RFPD box.

  4577   Wed Apr 27 21:19:25 2011 kiwamuUpdateLSCLSC whitening for PD1-4

On the back side of 1Y2 rack I found a cable, CAB-1X2-LSC_7, which is supposed to be connected to the whitening filter was disconnected.

I plugged it back and confirmed that the whitening filter is under control of EPICS.

Now all the gain sliders seem to be working because I can change the amplitude of signals with the sliders.

 

(method)

  To check if the gain sliders are working or not, I intentionally disconnected all the inputs to the whitening filter.

Then I brought a gain slider of interest to the maximum. Due to the big gain I was easily able to see noise lying above ADC noise.

Also if the gain slider is 0 dB, which is the minimum value, the spectrum becomes just ADC noise.

In this way I checked all the gain sliders from PD1 to PD4. The picture below is just an example screenshot when I was doing this test.

Note that each filer is designed to have two poles at 150 Hz and two zeros at 15 Hz.

Screenshot-1.png

Quote from #4570

While checking whitening filters on the LSC rack, I found some epics controls for the whitening looked not working.

So I powered two crates off : the top one and the bottom one on 1Y3 rack.

These crates contain c1iscaux and c1iscaux2. Then powered them on. But it didn't solve the issue.

  4585   Fri Apr 29 03:39:49 2011 KojiSummaryLSCCavity lengths

I tried the idea that the PRC can resonate f1 and f2 at the same time if the arm gives the reflection phase to f1 and f2 with the ratio of 1 vs 5.

The details are described on wiki. The point is this removes all of the PRC/SRC/asymmetry mumbo jumbo.

The calculated cavity lengths for f_mod of 11.065399MHz are:

  • Arm Length: 37.7974 [m]

  • PRC Length: 6.7538 [m]

  • SRC Length: 5.39915 [m]

  • Asymmetry (lx-ly): 0.0342 [m]


Here is the actual values derived from the photos.

  • Arm Length: 37.54 [m] (0.26m too short)

  • PRC Length: 6.760 [m] (6mm too long)

  • SRC Length: 5.415 [m] (16mm too long)

  • Asymmetry (lx-ly): 0.0266 [m] (8mm too long)

  4586   Fri Apr 29 05:48:52 2011 kiwamuUpdateLSCY arm locked

The Y arm has been locked with the IR beam. The purpose is to use the arm as an alignment reference for the input PZTs.

Detail will be posted later. Here is a picture of ITMY suspension. You can see there is a beam spot in the middle of the test mass.

DSC_2978_ss.jpg

  4587   Fri Apr 29 12:18:48 2011 kiwamuUpdateLSCY arm locked : details

First of all, the conclusions / results from the exercise of the Y arm locking yesterday are:

   The position of the beam spots on both ETMY and ITMY are now not so bad ( ~ 5 mm off from the center).

   The input PZTs are coarsely aligned to the Y arm.

   Nevertheless IP_ANG is still too high to come out from the view port at the Y end station.

  After the alignments of PRM, SRM and Michelson, POP is still largely clipped.

 


(what I did)

  - Alignments of the Input PZTs

    First I tried letting the incident beam hit the center of ETMY by steering PZT1 and 2 as usual.
    Then I coarsely aligned the cavities to the incident beam and checked the beam flashing spots on ETMY and ITMY with the CCD monitors.
    When the spots were far from the center I went back to the alignment of PZT1 and 2 to get better beam positions. And repeated this work several times.

  - Adjustment of the demodulation phase  for the Y arm PDH.

    First I started looking at the digital signals and tried correcting the demodulation phase by the rotation matrix, but this didn't go fast because I had to do some DAQ settings, plotting and analysis.
    Instead looking at the digital signal, I observed the analog signals with an oscilloscope. I found the demodulation phase was something like 45 deg.
    Based on the analog measurement I rotated the digital matrix by 45 deg to get the I-signal maximized. Indeed this worked well. I obtained a beautiful PDH signal from the I-signal.
    Note that we are using 11 MHz mod/demod and eventually the signals come out from "REFL33" on the digital side.

  - Activation of oplev on ITMY

    Instead using ETMY I used ITMY for the length control because somehow I felt that ETMY coils were suspicious and they looked not so nice.
    One of the reason is that ETMY's coil actuation efficiencies looked low compared to the other test masses.
    For example a gain of 700 for SUSSIDE damping is needed on ETMY to get a reasonable Q. This is about 2 - 3 times larger gain than the other test masses.
    So I started using ITMY for the locking and activated the oplev to suppress unwanted excitation due to kicks from the control signal during the locking,
    The oplev has been misaligned, so I went to the ITMY optical bench and tweaked a steering mirror to let the He-Ne beam go into the QPD.
    I set the gains +2 for PITCH and -2 for YAW.

  - PDH locking

    The locking had been quite difficult even though the cavity alignment was quite good.
    It's because the beam on AS11_RFPD was almost falling off from the photo diode. This causes a big amplitude fluctuation in the PDH signal as the beam position moves.
    After aligning the beam by steering BS I got able to lock the Y arm. The PD whitening gains are all 0 dB and the feedback gain is -2, giving us a UGF of 250 Hz.

 

(Broken or likely broken stuff)

 * IP_ANG doesn't give a signal to the digital side.

 * ETMY coils look weak and 2 - 3 times weaker than the other test masses. (or OSEM readout gain maybe lower)

 * reload button on sitemap.adl doesn't work.

 * Farfalla, a lab laptop, seems out of network.

Quote from #4586

The Y arm has been locked with the IR beam. The purpose is to use the arm as an alignment reference for the input PZTs.

Detail will be posted later. Here is a picture of ITMY suspension. You can see there is a beam spot in the middle of the test mass.

 

  4588   Fri Apr 29 13:15:04 2011 kiwamuUpdateLSCY arm locked : details

As far as I know, this button works only once after the launch of MEDM...

Quote:

 * reload button on sitemap.adl doesn't work. 

 

  4589   Fri Apr 29 13:58:36 2011 ranaUpdateLSCY arm locked : details

Quote:

 * Farfalla, a lab laptop, seems out of network.

 If you look at the real host table instead of the misleading host table in the wiki, you will see that someone has deleted Farfalla from there. She needs to be re-added.

  4595   Mon May 2 12:51:52 2011 kiwamuUpdateLSCPRMI locking : plan

Today we will try to lock the PRMI. Here is a plan for it.

(to be done in the daytime)

 - setup REFL11 RFPD

 - setup AS55 RFPD

 - install a demod board for 55 MHz

 - install a 3-way RF combiner on EOM.

 - prepare 55 MHz RF source (Marconi or RF source box ?)

 - adjustment of each demodulation phase

 - activation of PRM oplev

 

 (control topology)

- AS55_Q ==> BS

- REFL11_I ==> PRM

  4598   Mon May 2 15:53:27 2011 kiwamuUpdateLSCPRMI locking prep : demodulation boards

I swapped the name of two demodulation boards (AS55 and REFL55).

Now the REFL11 and AS55 demodulation boards are ready to go for the PRMI locking.

The physical labels, which are on the front surface of the boards, are also corrected to avoid a confusion.

Here is the latest RF status.

RF_Work_Status.png

Quote from #4574

The files are on https://nodus.ligo.caltech.edu:30889/svn/trunk/suresh/40m_RF_upgrade/.

 

  4600   Mon May 2 18:16:24 2011 kiwamuUpdateLSCPRMI locking : status update

(done)

- AS55 RFPD

  With a help from Jamie the AS55 RFPD was installed.

- 55 MHz demodulation board

  The AS55 demod board was installed on 1Y2.

- 3-way combiner

  ZFSC-3-13 has been installed. All the RF cables from the source side were connected to the combiner.

 

(next things)

 - installation of the REFL11 RFPD

 - DAQ check for AS55 and REFL11

Quote from #4595

(to be done in the daytime)

 - setup AS55 RFPD

 - install a demod board for 55 MHz

 - install a 3-way RF combiner on EOM.

 - prepare 55 MHz RF source (Marconi or RF source box ?)

 

  4604   Tue May 3 03:53:20 2011 kiwamuUpdateLSCPRMI locking : done

The PRMI has been successfully locked

PRMI_locking.png

Also changing the sign of the PRC control gave me the lock of the carrier resonant condition.

The screenshot above is the time series of the error signals when I was locking the PRMI in the sideband resonant condition (i.e. carrier is non-resonant).

Note that I used REFL11 for the PRC control and AS55 for the MICH control as planed.

Details will be posted in the morning.

Quote from #4595

Today we will try to lock the PRMI.

 

  4605   Tue May 3 04:09:53 2011 KojiUpdateLSCREFL55 PD update

[Rana, Koji]

REFL55 was modified. The noise level confirmed. The PD is now ready to be installed.

 


Kevin's measurement report told us that something was wrong with REFL55 PD. The transimpedance looked OK, but the noise level was terrible (equivalent to the shotnoise of 14mA DC current).

Rana and I looked at the circuit, and cleaned up the circuit, by removing unnecessary 11MHz notch, 1k shunt resister, and so on.

I made a quick characterization of the PD.

First page:

The transimpedance ws measured as a function of the frequency. The resonance was tuned at 55MHz. The notch was tuned at 110MHz in order to reject the second harmonics. The transimpedance was ~540V/A at 55MHz. (For the calibration, I believed the DC transimpedance of 50V/A and 10000V/A for the DC paths of this PD and #1611, respectively, as well as the RF impedance (700V/A0 of #1611.

Second page:

Output noise levels were measured with various amount of photocurrent using white light from a light bulb. The measurement was perforemed well above the noise level of the measurement instruments.

Third page:

The measured output noise levels were converted into the equivalent current noise on the PD. The dark noise level agrees with the shot noise level of 1.5mA (i.e. 22pA/rtHz). In deed, the noise level went up x~1.5 when the photocurrent is ~1.4mA.

Attachment 1: REFL55.pdf
REFL55.pdf REFL55.pdf REFL55.pdf
  4606   Tue May 3 05:32:04 2011 kiwamuUpdateLSCdaytime tasks

Daytime tasks :

 - PRM & BS oplev (Steve)

 - LSC binary outputs (Joe/Jamie)

 - installation of the REFL55 RFPD (Suresh/Jamie)

 - Adjustment of demodulation phases (Kiwamu)

 - Bounce-Roll filters on BS and PRM (Suresh/Joe)

 - Suspension diagnostic using the free-swinging spectra (Leo)

 - PMC alignment (Jenne/Koji)

  4607   Tue May 3 10:21:25 2011 KojiUpdateLSCdaytime tasks

I think the installation of the PD DC signals are quite important. What to do
1) Connect the DC signals to the right top whitening board (be aware that there may be the modification of the whitening circuit).
2) Reconfigure the LSC model such that the DC signal is passed to the right channels (modify the left top part of the model)

Quote:

Daytime tasks :

 - PRM & BS oplev (Steve)

 - LSC binary outputs (Joe/Jamie)

 - installation of the REFL55 RFPD (Suresh/Jamie)

 - Adjustment of demodulation phases (Kiwamu)

 - Bounce-Roll filters on BS and PRM (Suresh/Joe)

 - Suspension diagnostic using the free-swinging spectra (Leo)

 - PMC alignment (Jenne/Koji)

 

  4610   Tue May 3 11:49:03 2011 KojiUpdateLSCdaytime tasks

Done. C1:PSL-PMC_PMCTRANSPD was improved from ~0.75 to 0.87.

Quote:

- PMC alignment (Jenne/Koji)

 

  4617   Tue May 3 16:47:55 2011 kiwamuUpdateLSCPRMI locking : details

Here are some details about the PRMI locking done last night.

 

(REFL11 installation)

 REFL11 has been installed on the AP table. The RF signal from the RFPD is sent by a heliax cable which has been called ASDD133.

Before the beam goes into the RFPD a HWP and PBS are installed such that we can adjust the amount of light entering to the photo diode.

One thing I didn't like was that I had to introduce a big amount of the light into the PD to get a reasonably big RF signal.

I was trying to look for an RF signal by looking at a spectrum analyzer, then I realized that the RF signal at 11 MHz was quite tiny when the DC_MON was less than 1.5 V.

After I increased the amount of the light up to 1.9 V in DC_MON, which sounds already too much, I then got able to see the 11 MHz signal on the analyzer.

Note that I decreased the amount of the light down to 0.5 V after I finished locking the PRMI.

We should make sure what is going on with the 11 MHz modulation.

APtable.png

 

(Locking)

First I started locking the MIchelson with AS55. The demodulation phase was already somewhat optimized to the I-signal port.

So I decided not to touch the demodulation phase matrix because it may take some times.

After I eliminated electrical offsets in the digital side, I was easily able to lock the Michelson. The control sign was plus.

Then I started playing with the PRC control too. The demodulation phase in REFL11 looked nearly 45 deg although I didn't carefully measure it.

I made a 45 deg rotational matrix to maximize the I-port signal and tried to lock the PRC. Then immediately I was able to lock PRC as well as MICH.

 GAIN_MICH = 100

 GAIN_PRC = 100

Also GAIN_PRC = -100 gave a carrier resonant lock.

The control filters are the same in MICH and PRC. I used my favorite filters as usual.

 FM1 = 1000 : 10

 FM6 = 0.1 : 1

 FM7 = 1 : 50

Somehow I frequently failed to engage the boost filters (i.e. FM6 and FM7) it looks offsets in the control path kicks either BS or PRM.

Quote from #4604

The PRMI has been successfully locked

Details will be posted in the morning. 

 

  4619   Tue May 3 18:25:38 2011 kiwamuSummaryLSCPRMI locking : plan

[Rana/Jamie/Kiwamu]

 Since we've got the PRMI locked we now should be able to do more qualitative measurements.

Here is a task list that we will measure/develop in the PRMI condition.

 

 

 - Optical gain measurements

 - Characterization of control loops

 - MICH and PRC calibrations

 - Noise budget

 - Development of automatic noise budget scripts

 - Arm loss measurement 

 - Shnupp asymmetry measurement

  4623   Wed May 4 13:45:56 2011 kiwamuUpdateLSClocking last night

Last night I was trying to calibrate the MICH error signal and the actuators on BS and ITMs.

However I gave up taking the data because the MC locking was unstable. MC3 drifted a lot.

  4631   Thu May 5 00:08:59 2011 JenneUpdateLSC(Almost) New Screens for RFPDs

I modified C1LSC.mdl to use the CDSphase blocks, which automatically calculate the R and D phase rotation for us.  Now each of the RFPDs has 2 channels in place of the old IQ_MTRX channels:  C1:LSC-RFPD_PHASE_R and C1:LSC-RFPD_PHASE_D.

I have not yet compiled / rebooted / done CDS magic to actually make these installed.  So far the change is only in the simulink model.

I was going to wait until morning to compile/reboot/magic, so I can do it under Joe's supervision.

In the meantime, I also modified the RFPD screens.  They have white boxes for the _R and _D channels just now, but that's because the new model hasn't been put in.  They now look like phase rotators, instead of Koji's temporary matrix.

Still to do:  Find the EPICS database where the phase rotation calculation is done (you give it an angle, it gives you sin(angle) and cos(angle) ).  I want to put a "90-angle" in the database so that we can type in the measured relative phase between I and Q, and it will calculate how many more degrees it needs to get to 90deg. 

 

  4632   Thu May 5 04:38:20 2011 KojiSummaryLSCComparison between S3399 and FFD-100

Comparison between Hamamatsu S3399 and Perkin Elmer FFD-100

These are the candidates for the BB PD for the green beat detection as well as aLIGO BB PD for 532nm/1064nm.

FFD-100 seems the good candidate.

 

Basic difference between S3399 and FFD-100

- S3399 Si PIN diode: 3mm dia., max bias = 30V, Cd=20pF

- FFD-100 Si PIN diode: 2.5mm dia., max bias = 100V, Cd=7pF

 

The circuit at the page 1 was used for the amplifier.

- FFD-100 showed 5dB (= x1.8) larger responsivity for 1064nm compared with S3399. (Plot not shown. Confirmed on the analyzer.)

- -3dB BW: S3399 180MHz, FFD-100 250MHz for 100V_bias. For 30V bias, they are similar.

Attachment 1: PD_response.pdf
PD_response.pdf PD_response.pdf PD_response.pdf
  4636   Thu May 5 13:13:32 2011 JenneUpdateLSCNew RFPD screens are in

Joe helped me compile the lsc simulink model, and now we have R&D phase rotation.

Right now, we have to do our own math, and figure out what relative phase to put in.  Soonly, I'll figure out how to do subtraction, and we can put in the measured value.

 

More details when I'm not running around like crazy...

--------------------------------------------------------------------------------------------

Okie dokie.  Last night I had modified the c1lsc.mdl to accommodate the R & D phase rotation.  I also made pretty new screens.  This morning however, the adventures began.....

Under Joe's supervision, I ran "make c1lsc".  The error that came up was something about things not being connected.  Joe assures me that this is a temporary problem, that Rolf is already working on.  The reason is that right now the LSC model is "flat", i.e. it doesn't have a bunch of sub-boxes and sub-screens in the simulink model.  Somehow this causes badness.  Joe stuck all the guts of the LSC model into a sub-model.  He then enabled "top_names", which makes the channels use the name of the sub-model, not the sub-model AND the main model (so since the sub-model is called LSC, our channels are just C1:LSC-OTHER_STUFF, rather than C1:LSC-LSC_OTHER_STUFF).  This fixed things so that the compiling worked (when we did "make c1lsc").  The one other thing that we changed was to delete all of the little "Outs" that were attached to EPICS readouts.  These are unneccessary and don't go anywhere, and when we made the sub-model, they made a bunch of empty outputs (unconnected outs on the main simulink model).  So, after doing that, we were able to compile, and do "make install-c1lsc", and all was good in the world.  Mostly.

Joe then noticed that I was using the CDS part "cdsPhase", which only takes one phase input.  I wanted "cdswfsPhase", which actually does the R&D phase rotation that we want.  Perhaps Alex/Rolf/whoever should change the name of that CDS part.  We switched all of the cdsPhase blocks to be cdswfsPhase, and recompiled.  All was still good in the world.  Mostly.

The last thing that was funny was that when I wanted to execute the medm screens, they would still look at the old _IQ_MTRX_1_1 and _IQ_MTRX_2_1 values, rather than the newly defined _PHASE_R and _PHASE_D channels, even though while editing the medm screen, it looked like it was pointing to the right place.  Anyhow, I opened the text file version of the C1LSC_PDX.adl, and changed the channel names to the _R and _D versions by hand.  I don't know if we edit the screens and run generate_screens.py again, if we'll have to re-edit the .adl text files.

After fixing this, all really was good in the world. 

Perhaps though, this making a subsystem business broke the filters somehow?  Foton is looking at the wrong text file now?  Something?  The filters are all still there, they just got moved down a level.  Joe said that he and Rolf are on it, and he should be able to put the LSC model back to being "flat" in the next few days.

  4637   Thu May 5 13:14:15 2011 kiwamuUpdateLSCchans file for LSC

Foton doesn't correctly display the LSC filter bank file : C1LSC.txt.

Foton tells a lie that they all are empty.

 

The file itself looks fine to me i.e. I can find correct filters in text format.

Looks like someone (maybe Joe and Jenne ?) updated the file. I am not sure if this is the reason or not.

allegra:chans>ls -al | grep LSC
-rw-r--r--  1 controls controls   20659 May  5 11:46 C1LSC.txt

 

NEEDS TO BE FIXED SOON

  4638   Thu May 5 13:55:08 2011 kiwamuUpdateLSCMI locking : calibration of BS and ITMs actuators

EDIT by KI on 15/5/2011:

The calibration of MICH error signal was wrong by a factor of 2.

 

The open loop transfer functions of the Michelson locking have been measured.

The purpose of this excise is to calibrate the coil-magnet actuators on BS and ITMs.

The estimated actuation coefficients are :

 BS = 3.69e-08 [m/counts]
 ITMX = 8.89e-09 [m/counts]
 ITMY = 9.22e-09 [m/counts] 

I guess the accuracy is something like 5 % because the calibration of the MI optical gain relies on a peak-to-peak measurement.

A next step is to calibrate the PRM actuator and the PRC optical gain.


 

(measurement)

The Michelson was locked with different actuators in every measurement. I locked the Michelson to the dark fringe with BS, ITMX and ITMY in each time.

The measured peak-to-peak value in the error signal was 20.2 counts, corresponding to a sensor gain of 5.96e+07 [counts/m]. Note that I used AS55_Q for the locking.

After locking the MI I took the open loop transfer function by injecting broadband noise from DTT.

Then the data were fitted coarsely.  In the fitting I used the resonant frequencies that Leo reported recently (http://blue.ligo-wa.caltech.edu:8000/40m/Mechanical_Resonances).

The Q-values are assumed to be 5 because of the local dampings. As a result the fitting gives us the actuator coefficients.

Here is a plot showing the measured open loop transfer functions. The solid lines represent the fittings.

MICH_OL.png

 

(by the way)

- The delay time including ADC/DAC and RFM looks quite big. According to the fitting the delay is something like 600 usec.

This is about two times larger than the one reported before (see this entry). I will re-measure it with empty filters.

  4639   Thu May 5 14:40:14 2011 KojiUpdateLSCMI locking : calibration of BS and ITMs actuators

I've got confused

1) Are these the DC responses of the coils? If that is true, we need to specify the resonant frequency of each suspension to get the AC response.

2) Are these the AC responses well above the resonant freqs? In that case, The responses should be x.xxx / f^2 [m/counts]

Quote:

The open loop transfer functions of the Michelson locking have been measured.

The purpose of this excise is to calibrate the coil-magnet actuators on BS and ITMs.

The estimated actuation coefficients are :

 BS = 3.69e-08 [m/counts]
 ITMX = 8.89e-09 [m/counts]
 ITMY = 9.22e-09 [m/counts]

  4640   Thu May 5 14:50:30 2011 JenneUpdateLSCchans file for LSC

Quote:

Foton doesn't correctly display the LSC filter bank file : C1LSC.txt.

Foton tells a lie that they all are empty.

 

The file itself looks fine to me i.e. I can find correct filters in text format.

Looks like someone (maybe Joe and Jenne ?) updated the file. I am not sure if this is the reason or not.

allegra:chans>ls -al | grep LSC
-rw-r--r--  1 controls controls   20659 May  5 11:46 C1LSC.txt

 

NEEDS TO BE FIXED SOON

 See my updated elog 4636 for what Joe and I did this morning, and what a possible problem is (making the LSC model into a sub-model).

  4643   Thu May 5 15:28:23 2011 kiwamuUpdateLSCRe: MI locking : calibration of BS and ITMs actuators

They are the DC responses.

I put the resonant frequencies that Leo reported in the wiki to obtain the DC response.

The resonant frequencies I used are :

  f_BS = 0.957 Hz

  f_ITMX = 0.966 Hz

  f_ITMY = 0.988 Hz

Also I assumed that all the Q-values are 5 due to the damping.

Quote:

I've got confused

1) Are these the DC responses of the coils? If that is true, we need to specify the resonant frequency of each suspension to get the AC response.

2) Are these the AC responses well above the resonant freqs? In that case, The responses should be x.xxx / f^2 [m/counts]

Quote:

 BS = 3.69e-08 [m/counts]
 ITMX = 8.89e-09 [m/counts]
 ITMY = 9.22e-09 [m/counts]

 

ELOG V3.1.3-