There is ~ 7% variation in the power seen by the MC2 trans QPD, depending on the WFS offsets applied to the MC2 PIT/YAW loops. Some more interpretation is required however, before attributing this to spot-position-dependent loss variation inside the IMC cavity.
Attachment #1: This shows a scatter plot of the MC2 transmission and IMC REFL average values after the WFS loops have converged to the set offset positions. The size of the points are proportional to the normalized variance of the quantity. The purpose of this plot is to show that there is significant variation of the transmission, much more than the variance of an individual datapoint during the course of the averaging (again, the size of the circles is only meant to be indicative, the actual variance in counts is much smaller and wouldn't be visible on this plot scale). For a critically coupled cavity, I would have expected that the TRANS/REFL to be perfectly anti-correlated, but in fact, they are, if anything, correleated. So maybe the WFS loops aren't exactly converging to optimize the inoput pointing for a given offset?
Attachment #2: Maps of the transmission/reflection as a function of the (YAW, PIT) offset applied. The radial coordinate does not yet mean anything physical - I have to figure out the calibration from offset counts to spot position motion on the optic in mm, to get an idea for how much we scanned the surface of the optic relative to the beam size. The gray circles indicate the datapoints, while the colormaps are scipy-based interpolation.
Attachment #3: After talking with Koji, I explicitly show the correlation structure between the IMC REFL DCMON and MC2 TRANS. The shaded ellipses indicate the 1, 2 and 3-sigma bounds for the 2D dataset going radially outwards. The correlation coefficient for this dataset is 0.46, which implies moderate positive correlation. 🤔
The following was implemented in a python scipt:
I am now setting the offsets to the WFS QPD loop to the place where there was maximum transmission, to see if this is repeatable. In fact it was. Looking at the QPD segment outputs, I noticed that the MC2 transmission spot was rather off-center on the photodiode. So I went to the MC2 in-air optical table and centered the beam till the output on the 4 segments were more balanced, see Attachment #4. Then I re-set the MC2 QPD offsets and re-enabled the WFS servos. The transmission is now a little lower at ~14,500 counts (but still higher than the ~14200 counts we had before), presumably because we have more of the brightest part of the beam falling on the gap between quadrants. For a more reliable measurement, we should use a single-element photodiode for the MC2 transmission.
In preparation for some locking work tonight, I did the following at the POP in air table with the PRMI locked on carrier:
Looking at the old latch.st code, looks like this is just a heartbeat signal to indicate the code is alive. I'll implement this. Aesthetically, it'd be also nice to have the hex representation of the "*_SET" channels visible on the MEDM screen.
Latch logic works. But latch alive signal is missing.
After making sure the beams were hitting the 3f photodiodes on the "AP" table, I was able to lock the PRMI with the sidebands resonant inside the RC using 3f error signals. This would be the config we run in when trying to lock some more complicated configuration, such as the PRFPMI (i.e. start with the arms controlled by ALS, held off resonance). Tonight, I will try this (even though obviously I am not ready for the CARM transition step). The 3f lock is pretty robust, I was able to stay locked for minutes at a time and re-acquisition was also pretty quick. See Attachment #1. Not sure how significant it is, but I set the offsets to the 3f paths by averaging the REFL33_I and REFL33_Q signals when the PRMI was locked with the 1f error signals.
As usual, there's a lot of angular motion of the POP spot on the CCD monitor, but the lock seems to be able to ride it out.
Lock-settings (I modified the .snap file accordingly):
REFL33_I --> PRCL, loop gain = -0.019, Trigger on POP22, ON @ 20cts, OFF@0.5cts.
REFL33_Q --> MICH, loop gain = +1.4, Trigger on POP22, ON @ 20cts, OFF@0.5 cts.
This problem has re-surfaced. Is this indicative of some problem with the on-board VGA? Even with 0dB of whitening gain, I see PDH horns that are 10,000 ADC counts in amplitude, whereas the nominal whitening gain for this channel is +18dB. I'll look at it in the daytime, not planning to use REFL55 for any locking tonight.
Hardware issues that need addressing:
The UPS is now incessantly beeping. I cannot handle this constant sound so I shut down all the control room workstations and moved the power strip hosting the 4 CPUs to a wall socket for tonight. Chub and I will replace the UPS batteries tomorrow.
Batteries + power cables replaced, and computers back on UPS from today ~3pm.
There is poor separation of the PRCL and MICH length error signals as sensed in the 3f photodiodes. I don't know why this is so - one possibility is that the MICH-->PRM matrix element in the LSC output matrix needs to be tuned to minimize the MICH -->PRCL coupling.
Over the last few days, I've been trying to make the 3f locking of the PRMI more reliable. Turns out that while I was able to lock the PRMI on 3f error signals, it was just a fluke. So I set about trying to be more systematic. Here are the steps I followed:
Attachment #1 is the result. I don't know what is the reason for such poor separation of the MICH and PRCL error signals in REFL165. The situation seems very different from when I had the DRMI locked in Nov last year.
After this exercise, I tried for some hours to get the 3f PRMI locking going with the arm cavities held off resonance under ALS control, but had no success. The angular motion of the PRC isn't helping, but I feel this shouldn't be a show stopper.
This is as far as I got last night. The first step is to see how reliable the settings determined last night are, today. I don't understand how changing the output matrix element can have brought about such a significant change in the MICH/PRCL separation in all the RF photodiodes.
Some ideas that would help increase the locking duty-cycle in the short term.
I tried implementing a basic PRMI ASC using the POP QPD as a sensor. The POP22 buildup RMS is reduced by a factor of a few. This is just a first attempt, I think the loop shape can be made much better, but the stability of the lock is already pretty impressive. For some past work, see here.
Koji suggested systematic investigation of the ETMX suspension electronics. The tests to be done are:
So the ETMX satellite box is unplugged now, starting 530 pm PDT.
The satellite box was reconnected and the suspension was left with watchdog off but OSEM roughly centered. We will watch for glitches over the weekend.
We also took this opportunity to re-connect the interlock to the Innolight controller (after it was disconnected for diagnosing the mysterious NPRO self-shutdowns). The diode pump current was dialled down to 0, the interlock wires reconnected, and then the diode current was ramped back up to the nominal 2.1 A. The fan to cool the unit remains mounted in a flaky way as we couldn't locate the frame Chub had made for a more secure mounting solution.
It seems like the pointing of the beam out of the laser head varies somewhat after the startup - I had to adjust the pointing into the PMC a couple of times by ~1 full turn of the Polaris mount screws, but the IMC has been locked (mostly) for the last ~16 hours.
I've checked the state of the laser interlock switch and everything looked normal.
There are no unexpected red-flags in the performance of the DFD electronics. The calibration factors for the digital phase tracker system are 71.291 +/- 0.024 deg/MHz for the X delay line and 70.973 +/- 0.024 deg/MHz for the Y delay line, while the noise floor for the frequency noise discrimination is ~0.5 Hz/rtHz above 1 Hz (dominated by ADC noise).
Conclusion and next steps:
I still don't know what's responsible for the anomalously low noise levels reported by the ALS-X system sometimes. Next test is to check the EX PDH system, since on the evidence of these tests, the problem seems to be imprinted on the light (though I can't imagine how the noise becomes lower?).
Looking at the sensor and oplev trends over the weekend, there was only one event where the optic seems to have been macroscopically misaligned, at ~11:05:00 UTC on Oct 19 (early Saturday morning PDT). I attach a plot of the 2kHz time series data that has the mean value subtracted and a 0.6-1.2 Hz notch filter applied to remove the pendulum motion for better visualization. The y-axis calibration for the top plot assumes 1 ct ~= 1 um. This "glitch" seems to have a timescale of a few seconds, which is consistent with what we see on the CCD monitors when the cavity is locked - the alignment drifts away over a few seconds.
As usual, this tells us nothing conclusive. Anyways, I am re-enabling the watchdog and pushing on with locking activity and hope the suspension cooperates.
The EX PDH setup had what I thought was insufficient phase and gain margins. So I lowered the gain a little - the price paid was that the suppression of laser frequency noise of the end laser was reduced. I actually think an intermediate gain setting (G=7) can give us ~35 degrees of phase margin, ~10dB gain margin, and lower residual unsuppressed AUX laser noise - to be confirmed by measurement later. See here for the last activity I did - how did the gain get increased? I can't find anything in the elog.
I made a change to the c1ass model to normalize the PIT and YAW POP QPD outputs by the SUM channel. A saturation block is used to prevent divide-by-zero errors, I set the saturation limits to [1,1e5], since the SUM channel is being recorded as counts right now. Model change is shown in the attached screenshots. I compiled and installed the model. Ran the reboot script to reboot all the vertex FEs to avoid the issue of crashing c1lsc.
The closest thing I can think of is here.
Is there a loop model of green PDH that agrees with the measurement? I'm wondering if something can be done with a compensation network to up the bandwidth or if the phase lag is more like a non-invertible kind.
Attachment #1 - comparison of the POP QPD PIT and YAW output signal spectra with and without them being normalized by the SUM channel. I guess the shape is different between 30-100 Hz because we have subtracted out the correlated singal due to RIN?
This did not have the effect I desired - I was hoping that by normalizing the signals, I wouldn't need to change the gain of the ASC servo as the buildup in the PRC changed, but I found that the settings that worked well for PRMI locked with the carrier resonant (no arm cavities, see Attachment #2, buildup RIN reduced by a factor of ~4) did not work for the PRMI locked with the sideband resonant. Moreover, Koji raised the point that there will be some point in the transition from arms off resonance to on resonance where the dominant field in the PRC will change from being the circulating PRC carrier to the leaking arm carrier. So the response of the actuator (PRM) to correct for the misalignment may change sign.
In conclusion, we decided that the best approach to improve the angular stability of the PRC will be to revive the PRC angualr feedforward, which in turn requires the characterization and repair of the apparently faulty vertex seismometer.
I looked into the seismometer situation a bit more today. Here is the story so far - I think more investigation is required:
Attachment #2 has some spectrograms (they are rather large files). They suggest that the increase in noise in the 0.1-0.3 Hz band in the BS seismometer X channel is real - but there isn't a corresponding increase in the other two seismometers, so the problem could still be electronics related.
Yesterday, Koji and I noticed (from the wall StripTool traces) that the vertex seismometer RMS between 0.1-0.3 Hz in the X-direction increased abruptly around 6pm PDT. This morning, when I came in, I noticed that the level had settled back to the normal level. Trending the BLRMS channels over the last 24 hours, I see that the 0.3-1 Hz band in the Z direction shows some anomalous behaviour almost in the exact same time-band. Hard to believe that any physical noise was so well aligned to the seismometer axes, I'm inclined to think this is indicative of some electronics issues with the Trillium interface unit, which has been known to be flaky in the past.
I wanted to restart the c1oaf model. As usual, the first time the model was restarted, it came back online with a 0x2bad error. This isn't even listed in the diagnostics manual as one of the recognized error states (unless there is a typo and they mean 0x2bad when they say 0xbad). The fix that has worked for me is to stop and start the model again, but of course, there is some chance of taking all the vertex FEs down in the process. No permutation of mxstream and daqd process restarts have cleared this error. We need some CDS/RCG support to look into this issue and fix it, it is not reasonable to go through reboots of all the vertex FEs every time we want to make a model change.
I'd like to revive the PRC angular feedforward system. However, it looks like the coherence between the vertex seismometer channels and the PRC angular motion witness sensor (= POP QPD) is much lower than was found in the past, and hence, the stabilization potential by implementing feedforward seems limited, especially for the Pitch DoF.
I found that the old filters don't work at all - turning on the FF just increases the angular motion, I can see both the POP and REFL spots moving around a lot more on the CRT monitors.
I first thought I'd look at the frequency-domain weiner filter subtraction to get a lower bound on how much subtraction is possible. I collected ~25 minutes of data with the PRC locked with the carrier resonant (but no arm cavities). Attachment #1 shows the result of the frequency domain subtraction (the dashed lines in the top subplot are RMS). Signal processing details:
The coherence between target signal (=POP QPD) and the witness channels (=seismometer channels) are much lower now than was found in the past. What could be going on here?
The Trillium T240 seismometer needs mass re-centering. Has anyone done this before, and do we have any hardware to do this?
I went to the Trillium interface box in 1X5. In this elog, Koji says it is D1000749-v2. But looking at the connector footprint on the back panel, it is more consistent with the v1 layout. Anyway I didn't open it to check. Main point is that none of the backplane data I/O ports are used. We are digitizing (using the fast CDS system) the front panel BNC outputs for the three axes. So of the various connectors available on the interface box, we are only using the front panel DB25, the front panel BNCs, and the rear panel power.
The cable connecting this interface box to the actual seismometer is a custom one I believe. It has a 19 pin military circular type hermetic connector on one end, and a DB25 on the other. Power is supplied to the seismometer from the interface box via this cable, so in order to run the test, I had to use a DB25 breakout board to act as a feedthrough and peek at the signals while the seismometer and interface boards were connected. I used Jenne's mapping of the DB25--> 19 pin connector (which also seems consistent with the schematic). Findings:
I am holding off on attempting any re-centering, for more experienced people to comment.
We think we got to the bottom of this issue today. The RF signal level going into the demod board is too high. This electronics chain needs some careful gain reallocation.
I was demonstrating to Koji a strange feature I had noticed in the ALS control, whereby when applying a CARM offset to detune the arms, the two arms seemed to respond differently (based on the transmission levels). This kind of CARM-->DARM coupling seemed strange to me. Anyway, I also noticed that the EPICS indicators on the ALS MEDM screen suggested ADC saturations were going on. I had never really looked at the fast time series of the inputs to the phase tracker servos, but these showed saturating behavior on ndscope traces. I went to the LSC rack and measured these on a scope, indeed, they were ~20V pp.
The output of the BeatMouth PDs are going to a ZHL-3A amplifier - we should consider replacing these with lower gain amplifiers, e.g. the Teledyne AP1053. This is relegated to a daytime task.
Other findings tonight:
While working on the PSL table, I somehow put the IMC FSS into a bad state, reminiscent of this behavior. Seems like this is linked to some flaky connection on the PSL table. One candidate is the unstable attachment of the Pomona box between the NPRO PZT and the FSS output - we should install a short BNC cable between these to avoid the lever arm situation we have right now.
In calculating the above numbers, I assumed a DC transimpedance of 10 khhms and an RF Transimpedance of ~800 V/A.
[Elog14480]: per these calculations, with the NewFocus 1611 PDs, we cannot achieve shot noise limited sensing for any power below the rated maximum for linear operation (i.e. 1mW). Moreover, the noise figure of the RF amplifier we use to amplify the sensed beat note before driving the delay-line frequency discriminator is unlikely to be the limiting noise source in the current configuration. Rana suggested that we get two Gain Blocks. These can handle input powers up to ~10dBm while still giving us plenty of power to drive the delay line. This way, we can (i) not compromise on the sacred optical gain, (ii) be well below the 1dB compression point (i.e. avoid nonlinear noise effects) and (iii) achieve a better frequency discriminant.
Temporary fix: While the gain blocks arrive, I inserted a 10dB (3dB) attenuator between the PSL+EX (PSL+EY) photodiode RF output and the ZHL-3A amplifiers. This way, we are well below the 1dB compression point of said RF amplifiers, and also below the 1dB compression point of the on-board Teledyne AP1053 amplifiers on the demodulator boards we use.
Nest steps: Rana is getting in touch with Rich Abbott to find out if there is any data available on the noise performance of the post-mixer IF amplifier stage in the 0.1 -30 Hz range, where the voltage and current noise of the AD829 OpAmps could be limiting the DFD performance. But in the meantime, the ALS noise seems good again, and there is no evidence of the sort of CARM/DARM coupling that motivated this investigation in the first place. Managed to execute several IR-->ALS transitions tonight in the PRFPMI locking efforts (next elog).
No new Teledyne AP1053s were harmed in this process - I'll send the 5 units back to Rich tomorrow.
I ran some sensing measurements at various CARM offsets to check if the PRCL-->REFL33 and MICH-->REFL165 signals were being rotated out of the sensing quadrature as I lowered the CARM offset - there was no evidence of this happening. See Attachment #2. Other possibilities:
The IMC went into some crazy state so I'm calling it for the night, need to think about what could be happening and take a closer look at more signals during the CARM offset reduction period for some clues...
I looked at some signals for a 10 second period when the PRMI was locked with at some CARM offset, just before the PRMI lost lock, to see if there are any clues. I don't see any obvious signatures in this set of signals - if anything, the PRM is picking up some pitch offset, this is seen both at the Oplev error point and also in the POP QPD spot position. But why should this be happening as I reduce the CARM offset? The arm transmission is only ~5, so it's hard to imagine that the radiation pressure is somehow torquing the PRM. There are no angular feedback loops actuating on the PRM in this state except the local damping and Oplev loops.
The 1f signals are also changing their mean DC offset values, which may be a signature of a changing offset in the 3f MICH and PRCL error points? The MICH error signal is pretty noisy (maybe I can turn on some LPF to clean this up a bit), but I don't see any DC drift in the PRCL control signal.
I set up a photodiode (PDA10CF) in the IFO REFL beampath and the Agilent NA is sitting on the east side of the PSL enclosure. This was meant to be just a first look, maybe the PDA10CF isn't suitable for this measurement. The measurement condition was - PRM aligned so we have a REFL beam (DC level = 8.4V measured with High-Z). Both ITMs and ETMs were macroscopically misaligned so that there isn't any cavity effects to consider. I collected noise around 11 and 55 MHz, and also a dark measurement, plots to follow. The optics were re-aligned to the nominal config but I left the NA on the east side of the PSL enclosure for now, in anticipation of us maybe wanting to tune something while minimizing a peak.
Attachment #1: Results of a coarse sweep from 5 MHz to 100 MHz. The broadband RIN level is not resolvable above the dark noise of the photodiode, but the peaks at the modulation frequencies (11 MHz, 55 MHz and 29.5 MHz) are clearly visible. Not sure what is the peak at ~44 MHz or 66 MHz. Come to think of it, why is the 29.5 MHz peak so prominent? The IMC cavity pole is ~4kHz so shouldn't the 29.5 MHz be attenuated by 80dB in transmission through the cavity?
Attachment #2: Zoomed in spectra with finer IF bandwidth around the RF modualtion frequencies. From this first measurement, it seems like the RIN/rad level is ~10^5, which I vaguely remember from discussions being the level which is best achieved in practise in the 40m in the past.
Check the RAM due to the EOM? Perhaps the pointing / polarization control into the EOM got degraded.
Tried a bunch of things tonight.
One possibility is that the arm buildup is exerting some torque on the ITMs, which can also change the PRC cavity axis - as the buildup increases, the dominant component of the circulating field in the PRC comes from the leakage from the overcoupled arm cavity. We used to DC couple the ITM Oplev servos when locking the PRMI. The TRX level of 1 corresponds to ~5W of circulating power in the arm cavity, and the static radiation pressure force due to this circulating power is ~30 nN, rising up to 300nN as the TRX level hits 10. So for 1mm offset of the spot position on the ITM, we'd still only exert 300 pN m of torque. I don't see any transient in the Oplev error signals when locking the arm cavity as usual with POX/POY, but on timescales of several seconds, the Oplev error point shows ~3-5 urad of variation.
I changed the shape of the low pass filter to reduce high frequency sensor noise injection into the MICH control signal. The loop stability isn't adversely affected (lost ~5 degrees of phase margin but still have ~50 degrees), while the control signal RMS is reduced by ~x10. This test was done with the PRMI locked on the carrier, need to confirm that this works with the arms controlled on ALS and PRMI lcoked on sideband.
The POP beam coming out of the vacuum chamber is split by a 50/50 BS and half is diverted to the POP22/POP110/POPDC photodiode (Thorlabs PDA10CF) and the other half goes to the POP QPD. This optical layout is still pretty accurate. I looked at the data of the POPDC and POP QPD SUM channels while the dither alignment was running, to see if I could figure out what's up with the weird correlated dip in REFLDC and POPDC. While the POPDC channel shows some degradation as the REFLDC level goes down (=alignment gets better), the QPD sum channel shows the expected light level increase. So it could yet be some weird clipping somewhere in the beampath - perhaps at the 50/50 BS? I will lock the PRMI (no arms) and check...
While I was trying to lock the PRMI this evening, I noticed that I couldn't move the REFL beamspot on the CCD field of view by adjusting the slow bias voltages to the PRM. Other suspensions controlled by c1susaux seem to respond okay so at first glance it isn't a problem with the Acromag. Looking at the OSEM sensor input levels, I noticed that UL is much lower than the others - see Attachment #1, seems to have happened ~100 days ago. I plugged the tester box in to check if the problem is with the electronics or if this is an actual shorting of some pins on the physical OSEM as we had in the past. So PRM watchdog is shutdown for now and there is no control of the optic available as the cables are detached. I will replace the connections later in the evening.
Since I couldn't find anything wrong, I plugged the suspension back in - and voila, the suspect UL PD voltage level came back to a level consistent with the others! See Attachment #2.
Anyway, I had some hours of data with the tester box plugged in - see Attachment #3 for a comparison of the shadow sensor readout with the tester box (all black traces) vs with the suspension plugged in, local damping loops active (coloured traces). The sensing noise re-injection will depend on the specifics of the local damping loop shapes but I suspect it will limit feedforward subtraction possibilities at low frequencies.
However, I continue to have problems aligning the optic using the slow bias sliders (but the fast ones work just fine) - problem seems to be EPICS related. In Attachment #4, I show that even though I change the soft PITCH bias voltage adjust channel for the PRM, the linked channels which control the actual voltages to the coils take several seconds to show any response, and do so asynchronously. I tried restarting the modbus process on c1susaux, but the problem persists. Perhaps it needs a reboot of the computer and/or the acromag chassis? I note that the same problem exists for the BS and PRM suspensions, but not for ITMX or ITMY (didn't check the IMC optics). Perhaps a particular Acromag DAC unit is faulty / has issues with the internal subnet?
PMC got unlocked at ~4am. I re-locked it. Also tweaked the input pointing into the cavity. The misalignment was mostly in pitch.
There was also a loud buzzing in the control room due to the audio cable being improperly seated in the mixer. I re-seated it.
There are many versions of the POP22 signal path I found on the elog, e.g. this thread. But what I saw at the LSC rack was not quite in agreement with any of those. So here is the latest greatest version.
Since the 2f signals are mainly indicators of power buildups and are used for triggering various PDH loops, I don't know how critical some of these things are, but here are some remarks:
I did some re-alignment of the POP beam on the IX in air table. Here are the details:
Tangentially related to this work - I took the nuclear option and did a hard reboot of the c1susaux Acromag crate on Sunday to fix the EPICS issue - it seems to be gone for now, see Attachment #5.
I am still unable to achieve arm powers greater than TRX/TRY ~10 while keeping the PRMI locked. A couple of times, I was able to get TRY ~50, but TRX stayed at ~10, or even dropped a little, suggestive of a DARM offset? On the positive side, the ALS system seems to work pretty reliably, and I can keep the arms controlled by ALS for several tens of minutes.
I removed the Trillium T240 DAQ interface unit from 1X4 for investigation.
It was returned to the electronics rack and all the connections were re-made. Some details:
Update 445pm: Seems to have done something good - the old feedforward filters reduce the YAW RMS motion by a factor of a few. Pitch performance is not so good, maybe the filter needs re-training, but I see coherence, see Attachment #2 for the frequency domain WF.
There seems to be stronger-than-expected coupling between CARM and the 3f sensors.
Full analysis tomorrow, but I collected sensing matrix measurements with lines driven in PRCL,MICH and CARM at a couple of CARM offsets. I also wanted to calibrate the CARM offset to physical units so I ran some scans of the CARM offset and collected the data so I can use the arm cavity FSR to calibrate CARM. Koji suggested using REFL165_I for PRCL and REFL165_Q for MICH control - this would allow us to see if the problem was with the 1f sideband only. While the lock could be established, we still couldn't push the arm powers above 10 without breaking the PRMI lock. While changing the CARM offset, we saw a significant shift in the DC offset level of the out-of-loop REFL33_I signal. Need to think about what this means...
A coarse calibration of the CARM error point (when on ALS control) is 7.040 +/- 0.030 kHz/ct. This corresponds to approximately 0.95nm/ct. I typically lose the PRMI lock when the CARM offset is ~0.2 cts, which means I am about 1kHz away from the resonance. This is >10 CARM linewidths.
The calibration was done by sweeping the CARM offset (no PRM) and identifying the arm cavity FSRs by looking for peaks in TRX / TRY. Attachment #1 shows the scan, while Attachment #2 shows a linear fit to the FSRs. In Attachment #2, the frequency axis is taken from the phase tracker servo, which was calibrated by injecting a "known" frequency with the Marconi, and there is good agreement to the expected FSR with 37.79 m long arm cavities. There is much more info in the scan (e.g. modulation depths, mode matching to the arm cavities etc) which I will extract later, but if anyone wants the data (pre-downsampled by me to have a managable filesize), it's attached as a .zip file in Attachment #3.
Here is a comparison of the response of various DoFs in our various RFPD sensors for two different CARM offsets. Even in the case of the smaller CARM offset of ~1kHz, we are several linewidths away from the resonance. Need to do some finesse modeling to make any meaningful statement about this - why is the CARM response in REFL11 apparently smaller for the smaller CARM offset?
If you mistrust my signal processing, the GPS times for which I ran the sensing lines are:
CARM offset = ~30kHz (arm transmission <0.02) --- 1257064777+5min
CARM offset = ~1kHz (arm transmission ~5) --- 1257065566+5min
Koji and I taked about cleaning up some of the flaky cable situation on the PSL table a while ago. The changes were implemented and are documented in Attachment #1. Now the Pomona box between the Thorlabs HV Driver and the NPRO head is sitting on the PSL table (sandwiched between some teflon pieces I found in cabinet S4 along the south arm), and the cables between these two devices are better strain relieved. I turned off the Thorlabs HV supply while working on the PMC table. The IMC could be locked after this work. Probably won't solve the long standing FSS mysteries but probably can't hurt.
Unrelated to this work: I also removed a Bias tee that was just hanging out on top of the FSS electronics, which was used for the modeSpec project.
Attachment #1 shows the spectra of our three available seismometers over a period of ~10ksec.
Attachment #2 shows the result of applying frequency domain Wiener filter subtraction to the POP QPD (target) with the vertex seismometer signals as witness channels.
Here is some disturbance in the spacetime curvature, where the local gradient of the metric seems to have been modulated (in the "downward" as well as in the other two orthogonal Cartesian directions) at ~1 Hz - seems real as far as I can tell, all the suspensions were being shaken about and all the seismometers witnessed it, though the peak is pretty narrow. A broader, less prominent peak also shows up around 0.5 Hz. We couldn't identify any clear source (no LN2 fill-up / obvious CES activity). This event lasted for ~45 mins, and stopped around 2315 local time. Shortly (~5min) after the ~1 Hz peak died down, however, the 3-10 Hz BLRMS channel reports an increase by ~factor of 2.
Onto trying some locking now that the suspensions have settled down somewhat.
this is due to the Equivalence Principle: local accelerations are indistinguishable from spacetime curvature. On a spherical Earth, the local gradient of the metric points in the direction towards the center of the Earth, which is colloquially known as "down".
The clue was that the loop X arm POX loop looked to have low (<3dB)) gain margin around 600 Hz (and again at 700 Hz). Attachment #1 shows a comparison of the OLTF for this loop (measured using the IN1/IN2 method) before and after our change. We hypothesize that one of the violin filters that were turned off had non-unity DC gain, because I had to lower the loop gain by 20% after these turn-offs to have the same UGF. I updated the snap files called by the arm locking scripts.
I think I caught all the places where the FM settings are saved, but some locking scripts may still try and turn on some of these filters, so let's keep an eye on it.
We turned off many excessive violin mode bandstop filters in the LSC.
The DC port of the Bias-Tee is routed to (a modified version of) the iLIGO whitening board. This has the well-known problem of the protection diodes of the LT1125 quad-op-amp lowering the (ideally infinite) input impedance of the first gain stage (+24 dB). To be sure as to how much signal we can put into this port (in anticipation of trying some variable finesse PRFPMI locking but also for general book-keeping), I tested the usable input range by driving a triangle wave at ~3 Hz and changing the amplitude of the signal until we observed saturation. We found that we could drive a 10 Vpp signal at which point there was evidence of some clipping (it was asymmetric, the top end of the signal was getting clipped at +14,000 cts while the bottom end still looked like a triangle wave at -16,000 counts). Anyway we probably don't want to exceed +/- 10,000 counts on this channel. This is consistent with Hartmut's statement of having +/- 4V of usable range (although the counts he mentions are twice what I saw yesterday).
Other discussion points between Rana, Koji and Gautam:
Attachment #1 is a spectrogram of the BS sesimometer signals for a ~24 hour period (from Wednesday night to Thursday night local time, zipped because its a large file). I've marked the nearly pure tones that show up for some time and then turn off. We need to get to the bottom of this and ideally stop it from happening at night because it is eating ~1 hour of lockable time.
We considered if we could look at the phasing between the vertex and end seismometers to localize the source of the disturbance.
The nightly seismic activity enhancement continued during the weekend. It always shows up around 10pm local time, persists for ~1 hour, and then goes away. This isn't a show stopper as long as it stops at some point, but it is annoying that it is eating up >1 hour of possible locking time. I walked over to CES, no one there admitted to anything - there is an "Earth Surface Dynamics Laboratory" there that runs some heavy equipment right next to us, but they claim they aren't running anything post ~530pm. Rick (building manager ?) also doesn't know of anything that turns on with the periodicity we see. He suggested contacting Watson but I have no idea who to talk to there who has an overview of what goes on in the building. 😢