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  12382   Sun Aug 7 14:53:39 2016 ericq UpdateSUSETMX Standoff gluing was successful

I came in to check on ETMX. I freed the earthquake stops, and found that the OSEMS were reasonably, but not perfectly, centered. Turning on the damping, I found that the pitch balance is biased slightly downwards at about ~0.5mrad, which is acceptable. 

As another check for how much we moved the standoff while gluing, we can look at the spectra of the OSEMS while the mirror is free swinging, and see if/how the resonance frequencies have moved around. As Gautam previously mentioned, the pitch frequency is even softer than we expected from the thicker ruby standoff alone. This is due to the excess glue around the guide rod forcing us to position the standoff even lower to have good contact with the optic's barrel. In the plot below, the design yaw/pit/pos frequencies are the dashed lines, and the measured frequencies are the solid lines. 

[The plot is not in spectral density units, so that the peak heights reflect real units of motion at each resonance frequency. Data and code used to generate the plot is attached] 

  Yaw Pitch Pos Side
Design frequencies from T000134: 0.773 Hz 0.856 Hz 1.001 Hz  
ETMX Measurement in-air 2010 0.828 Hz 1.04 Hz 0.908 Hz 0.949 Hz
Pre-gluing 0.785 Hz 0.709 Hz 0.949 Hz 0.975 Hz
Post-gluing 0.789 Hz 0.705 Hz 0.953 Hz 0.984 Hz

According to the calculations from ELOG 12316, this pitch frequency implies the support point is 0.317mm lower than the design value of 0.985mm. (However, this is just an approximation and does not include the fact that each standoff is at a different height.)

Nevertheless, this difference is frequency is not so large that the dynamics of the suspension will be qualitatively changed in some important way; really, the pitch frequency is just ~1.5dB lower. So, I deemed our standoff gluing a success, removed the optic from the suspension, and placed it in an optic holding ring after giving the top of the barrel a gentle drap wipe with some iso. At this point, I used the microscope to look at the ruby standoff groove. As far as I can tell, no glue has invaded the groove - it looks sharp as ever. (whew)

I also wiped the wire with acetone and easily removed the glue droplets. However, I noted that (as is the case for ETMY) the wire is deformed at the points where it was in contact with the standoffs. I wonder if we should re-suspend with new wire, or accept the current deformed wires.

In any case, we can now move on to air baking the ETMX tower and gluing the stray magnet back onto ETMY.

Attachment 1: ETMX_resonances.pdf
ETMX_resonances.pdf
Attachment 2: ETMX_SUSspectra.zip
  12381   Fri Aug 5 18:21:28 2016 gautamUpdateSUSETMX Ruby Wire Standoff GLUED
  • The latest twist in this apparently never-ending saga was that even though fine pitch balancing was achieved, the wire was out of the groove on both sides!
  • I rectified this situation in the morning, did the fine pitch balancing in the afternoon
  • Koji's suggestion of adjusting the OSEM holding plate totally did the trick, all four magnets are reasonably well centered relative to the vertical now...
  • After the latest round of fine pitch balancing, we are now tilted in pitch backwards (i.e. towards the AR face) by <0.7mrad. 
  • Prior to gluing, I visually inspected the optic to check that (see attachments):
    • Wires are in grooves on both sides
    • Unglued ruby standoff has the correct "rotation", i.e. that the wire contacts the standoff after the groove has started, and leaves it before the groove ends, since the groove doesn't go all the way around the standoff
    • Section of wire around the bottom half of the optic has no obvious kinks/other funny features
    • Unglued standoff is in contact with the barrel
    • All magnets are well clear of teflon in OSEM coils on both sides
  • Eric also checked the frequencies of the various modes (PIT, YAW, POS and SIDE) by looking at the power spectrum of the free-swinging error signals on the coils. The pitch mode is now softer than before, at ~710mHz
  • We then proceeded to glue the optic, using a needle to apply the glue (optic was clamped using face EQ stops, bottom EQ stops were not engaged as we felt this would affect the fine pitch balancing
  • During the process, it looks like we may have inadvertently gotten some glue onto the wire (see attachments) - it doesn't look like any has seeped into the groove itself, but there is definitely some on the wire. We can possibly try cleaning this once the optic is out. In the worst case scenario, we will have to loop another section of wire, but the fine pitch balancing should be unaffected provided we did not perturb the optic too much
  • Bob has said the large oven will be available to bake the cages on Tuesday, August 9th. By this time, we should have ETMY suspended as well (we were unable to glue the knocked off magnet on ETMY as the glass bowl we had for soaking the edge of the optic in acetone to remove the epoxy residue broke while I was assembling the various pieces of Teflon inside it. Steve is procuring a new one on Monday). It is still unclear when we can vacuum bake the two ETMs...

Attachments:

Attachment #1: Wire is in the groove in the unglued wire-standoff, groove rotation looks pretty good.

Attachment #2: Ruby standoff is sitting on the barrel of the optic (if you zoom in)

Attachment #3: Side magnet is well centered w.r.t OSEM coil

Attachment #4: UR magnet is well centered w.r.t OSEM coil

Attachment #5: UL magnet is well centered w.r.t OSEM coil

Attachment #6: LL magnet is well centered w.r.t OSEM coil

Attachment #7: LR magnet is well centered w.r.t OSEM coil

Attachment #8: Wire is in the groove in the glued Ruby standoff

Attachment #9: Standoff after gluing. 3-4 drops of epoxy are visible on the wire, but none looks to have seeped into the groove itself

Attachment #10: Side view of newly glued Ruby standoff

Attachment #11: Before and After gluing shots.

 

 
 
 

 

Attachment 1: IMG_2966.JPG
IMG_2966.JPG
Attachment 2: IMG_2969.JPG
IMG_2969.JPG
Attachment 3: IMG_2970.JPG
IMG_2970.JPG
Attachment 4: IMG_2972.JPG
IMG_2972.JPG
Attachment 5: IMG_2972.JPG
IMG_2972.JPG
Attachment 6: IMG_2973.JPG
IMG_2973.JPG
Attachment 7: IMG_2974.JPG
IMG_2974.JPG
Attachment 8: IMG_2967.JPG
IMG_2967.JPG
Attachment 9: IMG_2980.JPG
IMG_2980.JPG
Attachment 10: IMG_2985.JPG
IMG_2985.JPG
Attachment 11: BeforeNAfter.PDF
BeforeNAfter.PDF
  12380   Fri Aug 5 16:25:08 2016 PrafulUpdateElectronicsMic Amplifier

I took the spectrum of an EM172 connected to my amplifier inside and outside a large box filled with foam layers:

I also made a diagram with my plan for the microphone amplifier boxes. This is a bottom view:

The dimensions I got from this box: http://www.digikey.com/product-detail/en/bud-industries/CU-4472/377-1476-ND/696705

This seemed like the size I was looking for and it has a mounting flange that could make suspending it easier. Let me know if you have any suggestions.

I'll be doing a Huddle test next week to get a better idea of the noise floor and well as starting construction of the circuits to go inside the boxes and the boxes themselves.
 

  12379   Fri Aug 5 09:38:12 2016 SteveUpdateSUSSOS sus wire ordered

0.0017" OD., 500ft steel music wire ordered. Pictures of the existing roll are below. It will be on 8" OD. spool too.

 

Attachment 1: 0.0017.jpg
0.0017.jpg
Attachment 2: 0.0017spec.jpg
0.0017spec.jpg
  12378   Fri Aug 5 04:43:09 2016 KojiUpdateSUSETMX Ruby Wire Standoff Ready for Gluing

If only the LL magnet looks too low, doesn't this mean that the OSEMs are not arranged in a square shape?
If so, you can fix this misalignment by moving the OSEM holding plate rather than OSEM shimming, can't you?

  12377   Fri Aug 5 02:17:10 2016 gautamUpdateSUSETMX Ruby Wire Standoff Ready for Gluing

Part 1: Rotation of optic

  • As reported in my elog yesterday, both the left magnets (UL and LL) seemed too low relative to the OSEM coils
  • Eric and I checked the height of the scribe lines using the microscope and found that the scribe lines were low on the left side and high on the right side (as viewed from the AR side) by approximately the same amount, confirming our suspicion that the optic was rotated. The position of the scribe line on the bottom of the optic relative to the bottom-rear face EQ stop also suggested the same
  • Eric brought in the bottom EQ stops, and once the wire was slightly unloaded, rotated the optic by the required amount by hand 
  • This process took two tries, but we were successful
  • Re-checked heights of scribe lines using microscope, and once we were satisfied, re-did the coarse pitch balancing

Part 2: Replacement of holder for top pair of OSEMs

  • Eric and I had difficulty removing the UR OSEM-holding screw
  • This is the non-silver-coated new variety of screw
  • It got to a point where I could neither move the screw in or out, even with the help of a pair of pliers
  • I decided to swap out the piece of the suspension tower holding the top two OSEMs (UR and UL) with the same piece from the old ETMX tower that is currently residing on the flow bench at the south end (along with the accompanying piece that overhangs the optic and holds the front-face and top earthquake stops
  • I cleaned the piece 3-4 times with acetone, and then a couple of times with isopropanol. I adjudged this to be sufficient as we are going to air bake the tower anyways prior to installation in the vacuum chamber
  • I then swapped the pieces:
    • First I brought in the bottom pairs of EQ stops
    • Next, I secured the optic using the three lower face EQ stops
    • Then, I removed the EQ stop screws from the overhanging piece, after which I removed the overhanging piece itself
    • After removing the top-back EQ stop, I removed the OSEM-holding piece from the suspension tower
    • Did the above steps in reverse, installing the new piece
  • All went smoothly. This piece does not have a serial number unfortunately
  • After this, I re-inserted the OSEMs, and judged the magnet-coil alignment to be satisfactory to proceed further
  • We decided to use the old variety of silver plated OSEM holding screws for the top two OSEMs (by choice) and the side OSEM (the new variety is too short anyways). During the course of my work tonight, I found this worked way better. The bottom pair of OSEMs remain held by the new variety of unplated screws. We may want to review whether we really want to use this new type of screws (I believe the idea is to make it easier to tighten and loosen the screws)

Part 3: Fine pitch balancing

  • As per the SOS assembly procedure, I turned off the HEPA filters at the clean bench for this part of the work
  • Checked that the HeNe beam incident on the optic was level with the tabletop, beam height set to 5.5"
  • Proceeded to do the fine pitch balancing the same way as described in yesterday's elog (i.e. no PZT buzzer, just fine touches by hand)
  • I was able to converge fairly quickly to a good point in configuration space
  • After re-centering the OSEM coils such that the PD output was ~50% of its maximum value (see Attachment #1), I found over a lever arm length of 56" (=1.42m) a beam height deviation from 5.5" by <2mm. This corresponds to 0.7mrad pitching forwards towards the HR side
  • The suspension assembly procedure tells us to aim for 0.5mrad, but I think this is close enough for standoff gluing, as this misalignment is extremely sensitive to the OSEM coil positions (although I would say, from Attachment #1, that they are actually pretty well centered)
  • The only thing that concerns me is that the LL magnet is still a little low relative to the coil. This can be fixed by shimming if necessary...

Attachment #1: Striptool trace showing OSEMs are pretty well centered (towards the end, I turned on the HEPA filters again, which explains the shift of the traces). The y-axis is normalized such that the maximum displayed corresponds to the fully open PD output of the coils

Attachment #2: Fine pitch balancing optical lever setup

Attachment #3: Tower assembly

Attachment #4: SIDE OSEM close-up

Attachment #5: UR OSEM close-up

Attachment #6: UL OSEM close-up

Attachment #7: LL OSEM close-up (this is the concerning one)

Attachment #8: LR OSEM close-up


We should also check the following (I forgot and don't want to wear my clean jumpsuit again now to take more photos):

  1. Wire is still in groove
  2. Standoff is sitting on the optic barrel and not on epoxy residue of the guiderod
Attachment 1: OSEMs.PDF
OSEMs.PDF
Attachment 2: IMG_2932.JPG
IMG_2932.JPG
Attachment 3: IMG_2934.JPG
IMG_2934.JPG
Attachment 4: IMG_2935.JPG
IMG_2935.JPG
Attachment 5: IMG_2936.JPG
IMG_2936.JPG
Attachment 6: IMG_2937.JPG
IMG_2937.JPG
Attachment 7: IMG_2938.JPG
IMG_2938.JPG
Attachment 8: IMG_2939.JPG
IMG_2939.JPG
  12376   Thu Aug 4 17:57:09 2016 KojiConfigurationGeneralDon't restart apache2 - nodus /etc/apache2/sites-available/* accidentally deleted

Late coming elog about the deletion of the apahce config files


Thu Aug 4 8:50ish 2016

Please don't restart apache2

I accidentally deleted four files in /etc/apache2/sites-available / on nodus. The deleted files were

elog   nodus  public_html  svn

I believe public_html is not used as it is not linked from /etc/apache2/sites-enabled

They are the web server config files and need to be reconfigured manually. We have no backup.

Currently all the web services are running as it was. However, once apache2 is restarted, we'll lose the services.


 

  12375   Thu Aug 4 17:41:53 2016 KojiUpdateComputer Scripts / ProgramsWeb things mostly back online

Sorry I was writting the elog, but I had to dive into the chamber (@LHO) before completion.

  12374   Thu Aug 4 17:29:17 2016 PrafulUpdateGeneralGuralp Cable

The Guralp cable has been pulled and put in the corner to the left of the water cooler:

 

Ben came by today before the cable had been pulled but he said he'll be back tomorrow.

  12373   Thu Aug 4 15:00:40 2016 ericq UpdateComputer Scripts / ProgramsWeb things mostly back online

Nodus' /export and /etc directories are now being backed up at /cvs/cds/caltech/nodus_backup

They will be rsync'd over as part of the nightly tape backups (scripts/backup/rsync.backup)

  12372   Thu Aug 4 14:21:21 2016 ericq UpdateComputer Scripts / ProgramsWeb things mostly back online

The nodus restart caused a bit of downtime. The apache configuration files were accidentally deleted the other day, so elog/svn/wikis were just holding on in memory; this fact was unfortunately not elogged. 

Things should be up and running again, except for the 8080->8081 elog redirection which I haven't been able to figure out.

I will also set up the NFS backup to include nodus configuration files from now on

  12371   Thu Aug 4 10:57:58 2016 ranaUpdateComputer Scripts / ProgramsNODUS update / restarts underway

Usual Ubuntu apt-get upgrades; long delayed but now happening.

  12370   Thu Aug 4 03:14:39 2016 gautamUpdateSUSETMX suspended
Quote:

[lydia, steve, ericq, gautam]

Summary:

  • ETMX is now suspended by wire clamps (winches have been removed) yes
  • Unfortunately, in the process of doing the pitch balancing, the position of the magnets relative to the OSEM coils have moved. Now the UR magnet looks a little high relative to the coil, but perhaps after any sag has set in, we should be alright. Else, we can probably get away by inserting one of the little metal shim pieces, the adjustment required is small

[lydia, ericq, gautam]

  • Turns out setting the height of the optic with the OSEMs isn't quite reliable. We were indeed too high, for all the OSEMs
  • Related to the above - we observed no sag (which is one of the reasons we winched a little bit extra in the first place)
  • Eric and I re-did the suspension in the afternoon. We found no wire grooves in the primary (or secondary) clamps, so we just reused them (is this a red flag? should we be using more torque?)
  • This time we set the height using the traveling microscope - double checked the height to which the microscope was levelled = 5.5"
  • Having checked the height of both scribe lines, we proceeded to clamp the suspension, with ~1.35Nm of torque (since 1.25Nm seemed a little low, no wire grooves were made in the clamps) - clamping was successful
  • In the evening, Lydia and I attempted to do the fine pitch balancing
  • Both left side magnets (as viewed from the AR side) are low (within 0.5mm of the teflon). Right side magnets are pretty well centered. But left side ones seemed usable so we went ahead and tried to turn the damping on.
  • Damping worked reasonably well
  • Tried to do fine pitch balancing with PZT buzzer. Reduced voltage from Fn generator to 0.4Vrms (down from 1.7Vrms) but had limited success. 
  • I was able to do much better with just the teflon tipped tweezers. So gave up on the PZT buzzer
  • After ~3hours of a random walk between two pretty-close-to-ideal positions, we have now realized a fine pitch balancing of ~1mrad (~3mm off the ideal height of 5.5" over a lever arm of ~1.5m, but the mirror tilt is half of this angle)
  • Actually, I was able to do much better - at one point, we even had the reflected beam dead center on the iris 1.5m away. But adjusting the OSEM positions even a little bit (say from oscillating around 40% to 50% of the maximum value) has a BIG effect on the pitch balance (it caused a misalignment of 4mrad)
  • I think gluing the standoff without destroying the fine pitch balancing is going to be very challenging, judging by how gently I had to touch the standoff to destroy the fine pitch balance completely. Perhaps we want to consider using some 3 axis stage to bring the needle with glue in and perturb the standoff as little as possible

    Lydia also briefly played around with the IR camera to inspect the OSEMs. A more thorough investigation will be done once the cage is in for air baking. From our initial survey, we feel that the beams are pretty well aligned along the straight line between PD and LED - we estimate the upper bound on any misalignment to be ~10 degrees.

 

  12369   Wed Aug 3 18:53:46 2016 PrafulUpdateElectronicsMic Amplifier

I could not get Den's circuit to work for some reason with microphone input, so I decided to try to use another circuit I found online. I made some modifications to this circuit and made a schematic:

Using this circuit, I have been able to amplify microphone input and adjust my passband. Currently, this circuit has a high-pass at about 7 Hz and a low-pass at about 23 kHz. I tested the microphone using Audacity, an audio testing program. I produced various sine waves at different frequencies using this program and confirmed that my passband was working as intended. I also used a function generator to ensure that the gain fell off at the cutoff frequencies. Finally, I measured the frequency response of my amplifier circuit:

ampTest_03-08-2016_180448.pdf

A text file with the parameters of my frequency response and the raw data is attached as well.

These results are encouraging but I wanted to get some feedback on this new circuit before continuing. This circuit seems to do everything that Den's circuit did but in this case I have a better understanding of the functions of the circuit elements and it is slightly simpler.

Attachment 2: ampTest_03-08-2016_180448.pdf
ampTest_03-08-2016_180448.pdf
Attachment 3: ampTest_03-08-2016_180448.txt
# SR785 Measurement - Timestamp: Aug 03 2016 - 18:04:48
#---------- Measurement Setup ------------
# Start frequency (Hz) = 1.000000
# Stop frequency (Hz) = 102400.000000
# Number of frequency points = 800
# Excitation amplitude (mV) = 50.000000
# Settling cycles = 1
# Integration cycles = 5
#---------- Measurement Parameters ----------
# Measurement Group:  "Swept Sine" "Swept Sine"
... 820 more lines ...
Attachment 4: simple_amp.png
simple_amp.png
  12368   Wed Aug 3 16:34:59 2016 LydiaUpdateGeneralAcromag Setup | SURF2016

Actually, if the power goes off and back on, the ethernet connection comes back online after about 5 seconds, or faster if it is disconnected and reconnected. The main issue was that the cable had partially slipped out (ie both power and network connections were loose); I suggest that the final setup should use ethernet cables that have a locking tab as this one does not. 

Quote:

Lydia helped me to troubleshoot the Accromag connection problems which I was facing previously.  If power goes off/turned off manually, the ethernet cable has to be pulled out and put back again until only a non-blinking green light is observed. I was foolish enough that I did not use secure power connections. About the random symbol, a code block was not closed in the other supporting file which was being called in the main program. There are still some port errors and register errors, which I would work on later tonight.

 

  12367   Wed Aug 3 15:36:57 2016 SteveUpdateSUSNi plated magnets & epoxy ordered

Ni plated SmCo magnets with specification of LIGO-C1103521-v2 for SOS ordered from Electron Energy Corp 

100 pieces of Ni- Platted magnets are in 9-27-2016 They are stored at clean cabinet S15

EP30-2 epoxy  1/2 pt kit 250 ml of part A and 25 ml of part B should be here in 7 days. These can packed epoxy is much more economical than the double barrel cartridges.

Spare SOS wire clamps will be out of the machine shop next week.

  12366   Wed Aug 3 15:35:19 2016 AakashUpdateGeneralAcromag Setup | SURF2016

Lydia helped me to troubleshoot the Accromag connection problems which I was facing previously.  If power goes off/turned off manually, the ethernet cable has to be pulled out and put back again until only a non-blinking green light is observed. I was foolish enough that I did not use secure power connections. About the random symbol, a code block was not closed in the other supporting file which was being called in the main program. There are still some port errors and register errors, which I would work on later tonight.

  12365   Wed Aug 3 14:52:37 2016 SteveSummaryPEMGuralps as connected

Guralps as connected with pictures

  12364   Wed Aug 3 10:52:03 2016 SteveUpdateGeneralETMY soaking dish

ETMY UL epoxy soaking dish. All teflon in glass.

 

Attachment 1: SD1.jpg
SD1.jpg
Attachment 2: SD2.jpg
SD2.jpg
Attachment 3: SD3.jpg
SD3.jpg
  12363   Wed Aug 3 09:26:54 2016 LydiaUpdateSUSETMX suspended: photos

Here are the photos we took showing the magnet positions in the OSEMs, and others showing the positions of the wire and unglued standoff. These were taken before the pitch balancing adjustment Gautam described, which apparently cause UR to be a little too high. Thoe OSEMs were all inserted only until the ends of the magnets were almost inside, to lower the risk of knocking any magnets off.

 At the time of these pictures, all magnets except LL were intentionally positioned slightly above the center of the OSEM in anticipation of wire sag. The LL magnet was approximately centered in the OSEM. It was not possible to get both LL and UL the same height relative to their respective OSEMs, possibly due to a spacing error when they were glued to the optic. 

Attachment 1: Position of wire along bottom of the optic. Looks adequately centered and not kinked. 

Attachment 2: Photo showing good contact between the sandoff and the barrel of the optic. The standoff does not appear to be resting on glue from the guiderod. 

Attachment 3: Shows position of standoff and wire after rough pitch banacing. Wire is visibly resting in the groove.

Attachment 4: SD magnet location photographed through OSEM.

Attachment 5: LL magnet location photographed through OSEM.

Attachment 6: LR magnet location photographed through OSEM.

Attachment 7: UL magnet location photographed through OSEM.

Attachment 8: UR magnet location photographed through OSEM.

 

Attachment 1: wire_bottom.JPG
wire_bottom.JPG
Attachment 2: standoff_contact.JPG
standoff_contact.JPG
Attachment 3: wire_in_groove.JPG
wire_in_groove.JPG
Attachment 4: SD.JPG
SD.JPG
Attachment 5: LL.JPG
LL.JPG
Attachment 6: LR.JPG
LR.JPG
Attachment 7: UL.JPG
UL.JPG
Attachment 8: UR.JPG
UR.JPG
  12362   Wed Aug 3 00:15:39 2016 gautamUpdateSUSETMX suspended

[lydia, steve, ericq, gautam]

Summary:

  • ETMX is now suspended by wire clamps (winches have been removed) yes
  • Wire clamp was machined by shop, D groove widened to spec, old wire grooves removed from face
  • We also sanded the part of the suspension tower in contact with the primary wire clamp, as there were a couple of craters there which looked dangerous (pictures to follow)
  • Height was adjusted by centering magnets on OSEMs. We then winched an extra half turn in anticipation of wire sag
  • I then proceeded to tighten, first, the primary wire standoff (I reduced the torque on the torque wrench to ~1.25Nm), and then the secondary wire clamps.
  • Checked that the ruby standoff is sitting on the optic barrel and not on glue 
  • Later in the evening, I inserted OSEMs, centered magnets, and checked that the damping scheme set up last week works (I'm leaving the damping on, bottom EQ stops are ~0.5mm from the optic)
  • Checked the pitch balancing - initially, we were ~60mrad off. By using the tweezers to gently adjust the position of the ruby standoff (after clamping the optic, turning the damping off), I was able to improve the situation a little bit - now we are ~20 mrad off. I am not attempting to do the fine pitch balancing tonight, but all parts of the PZT buzzer set up are ready to go in the cleanroom.
  • Unfortunately, in the process of doing the pitch balancing, the position of the magnets relative to the OSEM coils have moved. Now the UR magnet looks a little high relative to the coil, but perhaps after any sag has set in, we should be alright. Else, we can probably get away by inserting one of the little metal shim pieces, the adjustment required is small.
  • Lydia will upload some photos soon. 
  • We actually went through another failed attempt today - this time, the problem was that the winches were not sufficiently secure at the top, such that when the range of the winch was nearing its end, the whole assembly twisted and took the wire along with it. Perhaps this would not have happened if we had a winch adaptor plate handy...
  • Plan for tomorrow:
    • ​Fine pitch balancing using PZT buzzer
    • Clean ETMY epoxy residue from knocked off magnet
    • Glue wire standoff
    • Glue ETMY magnet
  12361   Mon Aug 1 20:09:37 2016 ranaUpdateCDSDAFI Update

I found the DAFI screen as a button inside of the LSC screen - I think its more logically found from the sitemap, so I'll move it into there as well.

Quote:

1) I have added the status summary of the DAFI block to the main FE status overview screen in the c1lsc cloumn. (attachment 1)

2) I have edited all the kissel matrix buttons appropriately, and given them appropriate lables. (attachment 2)

Gautam and I noticed a 60 Hz + harmonics hum which comes from the DAFI. Its the noisiest thing in the control room. It goes away when we unplug the fiber coming into the control room FiBox receiver, so its not a ground loop on this end. Probably a ground loop at the LSC rack.

Upon further investigation we notice that the Fibox at the LSC rack had its gain turned all the way up to +70 dB. This seemed too much, we reduced it to ~20 (?) so that we could use more of the DAC range.  Also, it is powered by a AC/DC converter plugged in to the LSC rack power strip. We cannot use this for a permanent install - must power the FiBox using the same power supplies as are used for the LSC electronics. Probably we'll have to make a little box that takes the fused rack power of 15 V and turns it into +12 V with a regulator (max current of 0.15 A). Making sure that the FiBox doesn't pollute the rest of the LSC stuff with its nasty internal DC-DC converters.

We also put a high pass in the output filter banks of DAFI. For the PEM channels we put in a 60 Hz comb. WE then routed the Y-end Guralp in through the boxes and out the output, mostly bypassing the frequency shifting and AGC. It seems that there is still a problem with GUR2.

Does anyone know which one is GUR1 and which one is GUR2? I don't remember the result of the Guralp cable switching adventures - maybe Koji or Steve does. According to the trend it was totally dead before March and in March it became alive enough for us to see ~30 ADC counts of action, so way smaller than GUR111 or GUR snoopy or whatever its called.

  12360   Mon Aug 1 18:50:29 2016 AakashUpdateGeneralAcromag Setup | SURF2016

There were many unknown and unsolved problems with using modbusApp for linux-arm architecture. So I tried to install the necessary files to setup Acromag Busworks card 1221-000 on Zita(192.168.113.217), which is a linux-x86_64 machine on the martian network. After installing a few dependencies and seting up few symbolic links for some libraries, everything is successfully configured. Initially I was unable to run myiocconfig.cmd file(as mentioned by Aiden on ATF wiki page) due to a undefined macro error for envset. Later I found that this error might be due to THIS bug in epics base. So, I removed the first four lines of that given code and directly referenced the .db file's location and it worked.

Now, I am facing another issue while running this file but on different line. Random symbols are returned on the last second line of the file each time I run it. I have attached the screenshots of those errors. I tried changing the encoding of the file several times but still it is showing the same error.

 

Attachment 1: 1.png
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Attachment 2: 2.png
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Attachment 3: 3.png
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Attachment 4: 5.png
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Attachment 5: 6.png
6.png
Attachment 6: 7.png
7.png
Attachment 7: 8.png
8.png
  12359   Mon Aug 1 14:09:20 2016 SteveUpdateSUSthird time - no luck

Gautam and Steve,

The clamp's left side was jammed onto the left guide pin. It was installed slit facing left. Gautam had to use force to remove it. The clamp should move freely seating on the guide rods till torque aplied. Do not move on with the hanging of optic with a jammed clamp. Fix it.

Never use force as you are hanging - aligning optic. The clamp is in the shop for resurfacing and slit opening.

 

  12358   Sun Jul 31 17:28:38 2016 ranaOmnistructureGeneralupclean

I cleaned up the south Electronics bench today.

The other two, as well as several of the desks are in some chaotic state of degradationno. Please clean up your areas and put away projects which do not need to remain staged for several months. Try to eliminate "that's not mine" and "I don't know who's that is" from your vocabulary.  angry Fight back against entropy!

  12357   Fri Jul 29 20:12:54 2016 gautamUpdateSUSthird time - no luck

[lydia, gautam]

Summary: Third unsuccessful attempt at getting ETMX suspended. I think we should dial the torque wrench back down to 1.0 N m from 1.5 N m for tightening the primary clamp at the top of the SOS tower. No damage to magnets, standoff successfully retrieved (it is sitting in the steel bowl)

Details:

  • We burned through two sets of wires today.
  • First, the assembly Eric and I had put together last night failed when Eric tightened the wire clamp (no torque wrench was used I think?)
  • This afternoon, Lydia and I re-assembled the suspension once again. Standoff was successfully inserted, coarse pitch balancing was achieved relatively easily - we think that the coarse pitch balance can be achieved if the end of the wire standoff closer to the groove is ~0.5mm ahead (i.e. towards HR side) of the guide rod.
  • Checked leveling of scribe lines, gave an extra 0.25 turns on the winches in anticipation of the wire sagging
  • Inserted OSEMs just short of magnets, verified that they were approximately centered, if anything, slightly above center, again in anticipation of the wire sagging. 
  • After taking pictures, we went ahead and attempted to clamp the wire (ALL EARTHQUAKE STOPS WERE ENGAGED)
  • Eric commented that the clamp piece did not slide in smoothly on the dowels (indeed it does not come off very easily either, I have just left it on for now). I don't remeber it being so difficult prior to us sending it into the maching shop to get rid of the grooves made by the suspension wire the first time around. But with the torque wrench, the piece moved in relatively easily (we had sanded down rough edges prior to putting this piece onto the suspension earlier in the afternoon.
  • I could feel that the torque wrench coming up on its limit. But the wire snapped before the torque wrench clicked. As far as I am aware, there were no rough edges on the piece, but perhaps we missed a spot?
  • I took the opportunity to discharge the optic using ionized nitrogen at 40psi. After about 2-3 minutes of a steady stream, I verified that a piece of the suspension wire no longer gets attracted to the barrel, as was the case earlier today.

Unfortunately I don't know of a more deterministic way of deciding on a "safe" torque with which to tighten the bolts except by trial and error. It is also possible that the clamping piece is damaged in some way and is responsible for these breakages, but short of getting the edges chamfered, I am not sure what will help in this regard.


Unrelated to this work: earlier today before the first wire failure, while I was optimistic about doing fine pitch balancing and gluing the standoff, I set up an optical lever arm ~3m in length, with the beam from the HeNe on the clean bench at 5.5 in above the table, and parallel to it (verified using Iris close to the HeNe and at the end of the lever arm). I also set up the PZT buzzer - it needs a function generator as well for our application, so I brought one into the cleanroom from the lab, isopropanol wiped it. The procedure says apply 5Vrms triangular wave at 1000Hz, but our SR function generators can't put out such a large signal, the most they could manage was ~2Vrms (we have to be careful about applying an offset as well so as to not send any negative voltages to the PZT voltage unit's "External input". All the pieces we need for the fine pitch balancing should be in the cleanroom now.

  12356   Fri Jul 29 19:37:43 2016 PrafulUpdateElectronicsMic Amplifier

I set up a test inverting amplifier circuit using the LT1677 opamp:

The input signal was a sine wave from the function generator with peak to peak amplitude of 20 mV and a frequency of 500 Hz and I received an output with an amplitude of about 670 mV and the same 500 Hz frequency, agreeing with the expected gain of -332k/10k = -33.2:

So now I know that the LT1677 works as expected with a negative supply voltage. My issue with Den's original circuit is that I was getting some clipping on the input to pin 2, which didn't seem to be due to any of the capacitors- I switched them all out. I set up a modified version of Den's circuit using a negative voltage input to see if I could fix this clipping issue:

I might reduce the input voltages to +5V and -5V- I couldn't get my inverting amp circuit to work with +12V and -12V. I'll start testing this new circuit next week and start setting up some amplifier boxes.

Attachment 1: inverting_amp.pdf
inverting_amp.pdf
Attachment 4: inverting_amp.png
inverting_amp.png
Attachment 6: new_amp_scheme.png
new_amp_scheme.png
  12355   Fri Jul 29 15:17:23 2016 SteveUpdateSUSwire and clamping test

Unbaked steel music wire from  "Ca Fine Wire Co" from 24" od spool, od 0.0017" used. Identical to the one that broke.

The set up as shown with silver plated screws-washers on clamp. The unused clamp edges were sanded on P800 paper at 45 degrees just not to be very sharp.

Use your finger to feel the sharpness of  edge and sand till it gets a little bit not so sharp. The drawing note is "sharp edges" on wire clamp for low loss, high Q in mind.

The wire broke at the midle with single load 295 grms

The wire hold on overnight at single load 242 grms  Vezo torque wrench is not accurate!  This test was performed ~ 1.5Nm  DO NOT USE THIS NUMBER! (added at 8-10-2016)

This gives us a factor of 2 safety  with loop suspended of 250 grms small optic.

 

 

Attachment 1: 43micr242grs.jpg
43micr242grs.jpg
  12354   Fri Jul 29 13:17:34 2016 KojiUpdateGeneralOven

While the air bake oven situation is being improved, how about to buy a cheepo toaster oven at Target, BestBuy, or anywhere?

We don't need precise temp control for the glue cure test. At LLO I saw that they are using cooking grade oven for this purpose.
(Of course, we should not use this oven for foods once it is used for epoxy)

I have a fryer temp sensor in my office on the freezer stole from the 40m long time ago. You should be able to measure high temp.

If you have such an oven, I'd love to borrow it for the OMC lab later, as I expect to work on epoxy bonding later.

  12353   Fri Jul 29 03:59:55 2016 ericqUpdateSUSIn air OSEM diagonalization check

The question arose whether we can get good enough data to diagonize our OSEM sensing matrices in air. 

I just took a look at the BS spectra over the last six hours (~10PM-4AM), and the SNR looks good. The BS diagonalization itself doesn't seem so great; the POS is hugely coupled into pitch and yaw, and the angular motions are themselves coupled to each other at around 10%. 

NB: use a flat-top window when you really care about peak heights that don't fall exactly on an FFT bin. 

I would've liked to check this for the PRM and SRM too, but one of the PRM sensors continues to be dark, and I just noticed that all of the SRM OSEM signals are dark. ughhhh

Attachment 1: BS_OSEM_diag.pdf
BS_OSEM_diag.pdf
  12352   Fri Jul 29 03:44:04 2016 AakashSummary About Acromag | SURF 2016

I tried to recompile the modbusApp binary for linux-arm acrhitecture since I suspected someting wrong with it. But still the problem persists; I can connect to acromag but cannot access the channels. I have also reconfigured new acromag bus works terminal XT 1221-000 and I want to test if I could access its channels. My target is to complete this acromag setup work before sunday morning so that I can focus towards having some useful results for my presentation.
 

  12351   Fri Jul 29 03:32:30 2016 ericqUpdateGeneralETMX suspended once more

[gautam, ericq]

Tonight's progress on ETMX:

  • All pickle pickers removed successfully, face magnet positions look symmetric (all on border of AR coating), side magnet same location as in yesterday's photo
  • Flipped around clamp blocks on winches and top blocks, refinished main clamp block not on tower yet
  • Trimmed viton tips of EQ stops, I had left them too long before, leading to bending and unwanted translation when in contact with optic
  • Inserted optic into bottom EQ stops, turned bolts to position optic at correct height and sort of pitch leveled
  • Threaded new length of wire up through both sides, clamped at winch. Made an effort to avoid any wire twisting. 
  • Winched until enough tension to sit in standoff groove, inserted second ruby standoff
  • Winched to just come up off of bottom EQ stops, observed neccesary correction of second standoff for rough pitch balance
  • Roughly pitch balanced by iterating standoff location
  • Partially inserted OSEMS, all four face magnets looked low. We figure it's more likely that our microscope was set to the wrong height, than all four OSEMS being too high by the same amount. (Given how the face magnets are all located on the concentric circle of the AR coating, we know there wasn't much translation error in the magnet gluing)
  • Did some common mode winching of both wire ends to get magnets to correct height, all OSEM alignments look good
  • Inserted OSEMs to half of open voltage
  • Having trouble engaging stable damping of all DoFs, this will be followed up in the daytime.

Since the air bake oven we had been using is out of commision, we're not sure where to do our EP30 test runs. If we are fortunate, we can get the fine pitch balance done tomorrow while Bob is still around, so he can help us quickly bake the test dots, so we can do the standoff gluing. 

  12350   Thu Jul 28 22:43:03 2016 ranaUpdateGeneralETMY UL magnet broke off

I'd recommend replacing the wire and grinding down the clamp to prevent cutting the wire. Since we have almost never replaced clamps, many of them probably have grooves from the wires and can make unpleasant cuts. Better safe than sorry in this case.

  12349   Thu Jul 28 17:48:17 2016 gautamUpdateGeneralETMY LR magnet broke off

While ETMX magnets were curing, I wanted to try and suspend ETMY in the endchamber, put in the OSEMS and see if the magnets aligned well with the coils, and run the same type of diagnostics we have been doing for ETMX. However, while I was trying to slip the optic into the wire, the UL magnet on ETMY broke off. I recovered the magnet and now both optic and magnet are back in the cleanroom. The magnet dumbbell has been cleaned with acetone and then sandpaper to remove residual epoxy - it remains to clean the residue off the optic itself before re-gluing the magnet tonight

I also noticed that the existing wire in the suspension had a kink in it. It looks fairly sharp, and I think we should change the wire while re-inserting the optic. Putting the optic into an existing loop of wire is tricky, as if you go in from the front of the suspension cage, the magnets on the AR side attract the wire, and makes it quite difficult to loop the wire around. I have to think of some way of holding the wires in place while the optic is being placed, and then, once the optic is roughly in position, slip the wire into the grooves in the standoffs. 


I took the opportunity to replace the face OSEM coil holder screws while the chamber was open. 

EDIT 9 August 2016: It was in fact the LR magnet that was knocked off.

  12348   Thu Jul 28 16:43:01 2016 LydiaUpdateGeneralETMX aluminium standoff groove condition

 

I took some pictures with the digital microscope of the aluminum standoffs removed from ETMX. The first one had some leftover epoxy still attached, so I was able to distinguish which part of the groove was occupied by the wire. A better microscope would help (this one has a maximum magification of 80, 200 or so would be much better) but I was still able to see what looks like a second minimum inside the groove at the wire location (see Attachments 1 and 2). The bottom edge of the standoff shows the profile of the groove on the opposite side from the glue. I took several photos with different lighting angles and at different locations on the microscope stage and convinced myself that this was not just an artificial effect. I also took photos of the groove in a different place and did not see this feature (Attachment 3).

The other standoff in the same container had no visible damage to the groove or to the body of the rod. I rotated it under the mocroscope and could celarly see the 'V' shape all the way around. The smooth undanaged groove caught the light more easily and was obvious. The damaged one is scratched around much of the surface, but the undamaged standoff is very smooth. Eric, were both aluminum standoffs in the container with the extra ruby one taken off ETMX, or was one of them new? in any case, see Attachement 4 for a comparison. The believed damage is somewhat visible on the top edge of the lower standoff in the photo. 

[Edit:] Also, in the drawings it looks like the specified radius for the bottom of the groove (0.001 in) is smaller than the radius of the wire (0.00085 in). This would prevent having two clean points of contact like Steve and Gautam were describing as the goal. This is also true of drawings for the new Sapphire guiderods, though the dimensions are in metric units the specified radius of the groove bottom is smaller than the wire's diameter, but larger than its radius. Maybe this providied the initial ability for the wire to move around and carve two distinct grooves. 

Attachment 1: wire_damage_4.jpg
wire_damage_4.jpg
Attachment 2: wire_damage_zoom.jpg
wire_damage_zoom.jpg
Attachment 3: no_wire.jpg
no_wire.jpg
Attachment 4: comparison_2.jpg
comparison_2.jpg
  12347   Thu Jul 28 13:49:44 2016 gautamUpdateGeneralETMX magnets re-reglued
Quote:

[gautam, ericq]

Brief summary, some pictures and such follow in the daytime. 

  • All magnets enclosed by OSEMS were knocked off. (This means one side magnet remained, on the guiderod side)
  • Glue residue cleaned from ETMX
  • Dumbbell feet were cleaned of glue, finely sanded, re-scored with a razor blade
  • The magnet gluing fixture was painstakingly aligned multiple times, adjusting the shim height to get a magnet/wire groove clearance of 0.25-5mm
  • Epoxy mixed, test batch cured perfectly, applied to 5 dumbbells (after triple-checking polarities) and set to glue. 

The epoxy needs at least 12 hours of room temperature air curing, so no touchy until 3:30PM on Jul 28!

Attachment #1 - After multiple trials shimming the magnet gluing rig with teflon spacers, we think that we managed to find a configuration in which the side magnet edge is between 0.25 mm and 0.5 mm from the groove in the ruby wire standoff in which the wire will sit. 

Attachment #2 - Zoomed in view of the side magnet.

Of course we won't know until we suspend the optic, but we believe that we have mitigated the misalignment between the side OSEM axis and side magnet.

The short term plan is to try and suspend ETMY in the end chamber and have a look at the alignment between all magnets and OSEM coils for it. Once the epoxy on ETMX is cured, we will try and suspend the optic again, this time taking extra care while tightening the wire clamps.


Unrelated to this work: Bob just informed me that we had left the air bake oven on overnight - this unfortunately melted the plastic thermocouple inside.

Attachment 1: ETMX_sideMagnet.JPG
ETMX_sideMagnet.JPG
Attachment 2: ETMX_sideMagnet_zoomed.JPG
ETMX_sideMagnet_zoomed.JPG
  12346   Thu Jul 28 08:42:36 2016 SteveUpdateSUS wire clamp

The clamp is in the machine for milling off the grooves. It's condition is normal. The edges needs some 800 sand paper so it is not sharp anywhere.

How did those nicks get on the edge? Fortunatelly they did not aligned with the wire.

 

Attachment 1: e12342.jpg
e12342.jpg
  12345   Thu Jul 28 03:22:28 2016 ericqUpdateGeneralETMX magnets re-reglued

[gautam, ericq]

Brief summary, some pictures and such follow in the daytime. 

  • All magnets enclosed by OSEMS were knocked off. (This means one side magnet remained, on the guiderod side)
  • Glue residue cleaned from ETMX
  • Dumbbell feet were cleaned of glue, finely sanded, re-scored with a razor blade
  • The magnet gluing fixture was painstakingly aligned multiple times, adjusting the shim height to get a magnet/wire groove clearance of 0.25-5mm
  • Epoxy mixed, test batch cured perfectly, applied to 5 dumbbells (after triple-checking polarities) and set to glue. 

The epoxy needs at least 12 hours of room temperature air curing, so no touchy until 3:30PM on Jul 28!

  12344   Wed Jul 27 22:42:00 2016 PrafulUpdateElectronicsEM172 Amplifier

I recreated Den's microphone amplifier circuit on a solderless breadboard to test it and make sure it does what it's supposed to. So far it seems like everything is working- I'll do some testing tomorrow to see what the amplified output is like for some test noises. Here's the circuit diagram that Den made (his elog as well https://nodus.ligo.caltech.edu:8081/40m/6651):

I'm not sure why he set up the circuit the way he did- he has pin 7 grounded and pin 4 going to +12V while in the datasheet for the opamp (http://cds.linear.com/docs/en/datasheet/1677fa.pdf), pin 7 goes to positive voltage and pin 4 goes to negative voltage. There's some other strange things about the circuit that I don't really understand, such as the motivation for using no negative voltage source, but for now I'm going to stick with Den's design and then make some modifications after I have things working and a better understanding of the problem.



Here's my current plan:

-Make sure Den's amplifier works, test it out and make changes if necessary

-Make multiple amplifier circuits on soldering breadboard

-Either make a new amplifier box or reuse Den's old box depending on how many changes I make to the original circuit

-Solder EM172s to BNC connectors, set them up around the floor suspended

-Get the amplifier box hooked up, set up some data channels for the acoustic noise

-Add new acoustic noise tab to the summary pages

 

Den also mentioned that he wanted me to measure the coupling of acoustic noise to DARM.

  12343   Wed Jul 27 16:56:47 2016 ranaMetaphysicsSUSBroken wire

For the rest of this vent, at least, we need to start using the EQ stops more frequently. Whenever the suspension is being worked on clamp the optic. When you need it to be free back off the stops, but only by a few hundred microns - never more than a millimeter.

Best to take our time and use the stops often. With all the magnets being broken off, its not clear now how many partially cracked glue joints we have on dumbells which didn't completely fall off.

  12342   Wed Jul 27 15:03:02 2016 sisyphusMetaphysicsSUSBroken wire

While tightening the bolts on the ETMX wire clamp, the wire broke. All four face magnets broke off. 

Fortunately, no pieces were lost.

  12341   Wed Jul 27 11:40:48 2016 steveSummarySUSoplev laser summary updated

 

Quote:

 

Quote:

 

Quote:

 

Quote:

 

                  2005              ALL oplev servos use Coherent DIODE LASERS # 31-0425-000, 670 nm, 1 mW

    Sep. 28, 2006              optical lever noise budget with DC readout in 40m,  LIGO- T060234-00-R, Reinecke & Rana

    May  22, 2007              BS, SRM & PRM  He Ne 1103P takes over from diode

    May  29, 2007              low RIN He Ne JDSU 1103P selected, 5 purchased sn: T8078254, T8078256, T8078257, T8078258 & T8077178 in Sep. 2007

    Nov  30, 2007               Uniphase 1103P divergence measured

    Nov. 30, 2007               ETMX old Uniphase 1103P  from 2002 dies: .............., running time not known......~3-5 years?

    May 19, 2008               ETMY old Uniphase 1103P from 1999 dies;.....................running time not known.....~    ?

    Oct.  2, 2008                ITMX & ITMY are still diodes, meaning others are converted to 1103P earlier

 

                     JDSU 1103P were replaced as follows:

   May 11, 2011                ETMX replaced, life time 1,258 days  or 3.4 years

   May 13, 2014               ETMX , LT 1,098 days or 3 y

   May 22, 2012               ETMY,  LT 1,464 days or  4 y

   Oct.  5, 2011                BS & PRM, LT 4 years,  laser in place at 1,037 days or 2.8 y

   Sep. 13, 2011               ITMY  old 1103P &    SRM    diode laser replaced by 1125P  ..........old He life time is not known, 1125P in place 1,059 days or 2.9 y

   June 26, 2013              ITMX 622 days or 1.7 y    note: we changed because of beam quality.........................laser in place 420 days or 1.2 y

 

  Sep. 27, 2013               purchased 3 JDSU 1103P lasers, sn: P893516, P893518, P893519 ......2 spares ( also 2 spares of 1125P of 5 mW & larger body )

 

      May  13, 2014             ETMX,  .............laser in place 90 d

      May  22, 2012             ETMY, 

     Oct.  7,  2013             ETMY,  LT  503 d  or  1.4 y............bad beam quality ?

     Aug. 8,  2014              ETMY,  .............laser in place   425 days  or  1.2 y

 

      Sept. 5, 2014              new 1103P, sn P893516  installed at SP table for aLIGO oplev use qualification

     

           May 23, 2016             ITMX dead laser sn P845648 replaced after 1062 days [2.9 yrs] by 1103P, sn P859884, with output output  2.6 mW, nicely round beam quality at 15 meters.

               July 27, 2016             2  new 1103P from Edmonds in: P947034 & P947039, manf. date April 2016,

  12340   Tue Jul 26 18:07:57 2016 gautamUpdateGeneralETMX suspension - Further OSEM Tests

Today, we did the following:

  • Once again, inserted all four face OSEMs till the sensor voltage readouts were approximately half their saturation value. The presence of some ferromagnetic material in the Honeywell components makes this tricky as each coil is coupled to the other three, but we were able to converge to a point where all the voltage readouts were oscillating around a mean value of ~40-60% of their maximum value, with all the damping loops OFF.
  • Turned on all damping loops, and verified that the OSEM positioning was indeed such that the sensor readout is nominally around 50% of the saturation value. The air buffeting around the clean bench means that the damping isn't nearly as effective as it is inside the vacuum chamber.
  • Attempted to increase the gain on the damping loops - we first switched out the Chebyshev low-pass filter in all the damping loops for something a little less aggressive, to allow us to turn up the gain. However, this experiment wasn't a success, when we turned the damping loops on, they were ringing the optic up.
  • At this point, Eric checked the offset sliders (summed in via the slow system) and saw that they were not zero. We zeroed these, but naturally, they destroyed the OSEM positioning equilibrium we had established earlier. So we had to go back and re-position the OSEMs
  • After re-centering the face OSEM magnets relative to the LED-PD pair, we insertd the side OSEM such that the side magnet completely occluded the PD. Interestingly, Eric noticed that the magnetic attraction between OSEM and magnets conspired to center the side magnet fairly well in the side OSEM, when it completely blocked the PD. However, when he returned the side OSEM coil to its nominal operating position of approximately half-blocking the PD, some minor misalignment was re-introduced (i.e. even when the optic was swinging mostly along the axis of the side OSEM, the voltage readout did not quite go down to 0). 
  • We then decided to compare the spectra for the error signals for the 4 DOFs with the current configuration (i.e. suspension clamped down to table top, optic freely hanging, all OSEMs reasonably well centered, and with the ETMX SUS model reverted to its normal state) to some reference (see Attachment #1). I initially thought I would wait for the optic to settle down a bit more before taking the spectra, but it doesn't seem to be showing any signs of getting any quieter in the last one hour. In Attachment #1, I have plotted as reference the spectra of the error signals from the early hours of 4 July 2016, at which point we were at atmosphere but the heavy doors were not yet off, so this is not really a fair comparison, but we don't really have a period in which the optic was exposed to the atmosphere and with the OSEMs in place, at least from this vent. Colors are identical for a given DOF, with todays trace as a solid line, and the reference dashed.
  • We did not check the room available to install some shimming piece of metal in the side OSEM holder, as a possible solution to solve the misalignment problem. Steve has already found pieces of varying thickness, and they are soaking in acetone right now, we plan to air bake them tomorrow. 

I will have another look at the spectra tomorrow morning, to see if the damping improves overnight. 

Attachment 1: OSEM_spectra.pdf
OSEM_spectra.pdf
  12339   Tue Jul 26 17:41:59 2016 KojiSummaryVACPurge compressed air system

We have no number for the CFM without calculation. We can't assume a random number like 10-15

  12338   Tue Jul 26 16:01:32 2016 SteveSummaryVACPurge compressed air system

Thanks for checking this out Koji

The builder in 1996 was Process System International, Inc ( Westborough, MA ) It does not exist any longer or I just could not find them. Flow diagramm at Atm1

Should I be keep looking for a company who could quote us for building a similar smaller unit with 10 - 15 cfm flowrate?

Note: my intension with the two mobile-overhead HEPA filter was the same as John Worden's " clean air overpressured tent " at chamber entrance.

Atm2, Our unit has 650 cfm, velocity 90 fpm at resistance 0.5"    It may be enough to give a little overpressure if we seal it well to the chamber

We use to use them to minimize dirt getting inside the chanbers.

Attachment 1: cleanAirSupl.pdf
cleanAirSupl.pdf
Attachment 2: mobileHEPA.jpg
mobileHEPA.jpg
  12337   Tue Jul 26 14:24:38 2016 KojiSummaryVACPurge compressed air system at LHO

I've visited the purge clean air system at LHO Yarm mid-station with John Worden.

The system is described C981637. There is a schematic in C981637-06-V (Vol.6).pdf although the schematic has some differences (or uncorrected mistakes).

This system is intended to provide positive pressure when a soft cover is attached to a chamber door. When the door is open, the purging does not help to keep the chamber clean because the flow is too slow. This protection has to be done with overhead HEPA filters (22x5000cfm). It may be possible that this purge air helps the tube not to allow dusts to come in. But before using this, the chambers and the tubes have to be cleaned, according to John.


- Here at the site, the purge air system is started up a day before the vent. This system is used for the vent air, the purge air, and turbo foreline filling.

- Air intake (attachment 1): At the site, the air is intaken from the VEA. We want to incorporate somewhat clean air instead of dirty, dusty, outside air.

- Initial filter (attachment 2): a high volume filter before the compressors.

- The compressors (attachment 3, 4) are 5x 6 horse power air compressor each goes up to 160 psi. They are turned on and off depending on the demand of the air. Which is turned on is revolved by the controller to equalize the compressor usage hours.

- The compressed air goes through the air cooler (heat exchanger) to remove the heat by the compressor work.

- This air goes through prefilters and accumulated in the air receiver (100psi) (attachment 5). This receiver tank has an automated vent valve for periodical water drainage at the bottom.

- The accumulated air is discharged to twin drier towers (attachment 6, blue). The tower is operated by the controller (attachment 7) alternately with a period of 4min (or 10min by setting). When one of the towers is working, a humid air comes from the bottom and the dry air is discharged from the top. A part of the dry air goes into the other tower from the top to the bottom and dries the tower. There is a vent at the bottom to discharge water periodically.

- The dried air goes through 4 types of filters. After the last filter, all of the plumbing should be made of stainless steel to keep cleanliness.

- The air goes to the pressure reducing regulator (attachment 8, gray). The final flow speed at the chamber side is 50cfm max, according to John.

- The lower pressure air goes through the final filter (attachment 8, blue). As the pressure is low, this filter is big in order to keep the volume of the air flow.

- The purge air is supplied to the chamber side with KF50 (attachment 9). There is a vent valve (attachment 10) for safety and also to run a dry air for at least a day before the use to clean up the supply line. The purge line is disconnected when no in use.

- The entire system (attachment 11) and size comparison (attachment 12).

 

Attachment 1: air_intake.jpg
air_intake.jpg
Attachment 2: initial_filter.jpg
initial_filter.jpg
Attachment 3: compressors1.jpg
compressors1.jpg
Attachment 4: compressors2.jpg
compressors2.jpg
Attachment 5: air_receiver_dryer.jpg
air_receiver_dryer.jpg
Attachment 6: drier.jpg
drier.jpg
Attachment 7: drier_controller2.jpg
drier_controller2.jpg
Attachment 8: pressure_regulator_and_last_filter.jpg
pressure_regulator_and_last_filter.jpg
Attachment 9: chamber_side_supply.jpg
chamber_side_supply.jpg
Attachment 10: vent_valve_for_line_cleaning.jpg
vent_valve_for_line_cleaning.jpg
Attachment 11: the_whole_system.jpg
the_whole_system.jpg
Attachment 12: size_comparison.jpg
size_comparison.jpg
  12336   Tue Jul 26 09:56:34 2016 ericqUpdateCDSc1susaux restarted

c1susaux (which controls watchdogs and alignments for all non-ETM optics) was down, the last BURT was done yesterday around 2PM. 

I restarted via keying the crate. I restored the BURT snapshot from yesterday.

  12335   Mon Jul 25 20:37:46 2016 gautamUpdateGeneralETMX suspension - Side OSEM test

[Lydia, gautam]

Summary: We did some preliminary tests to check if at least one of the side magnet positions is usable for the side OSEM. We mainly wanted to check how much dynamic range we lose because of the sub-optimal longitudinal positioning of the side magnet. We found that when the side magnet was mainly moving along the axis of the side OSEM (with minimal yaw motion as gauged by eye), the PD voltage bottomed out at ~80 counts (while the completely unoccluded readout was ~800 counts). 

Details:

  1. First, we placed the face OSEMs into their holders one by one, and adjusted their position till the readout was approximately half the saturation value (as judged by the average value of the readout, at this point, the mirror was still swinging around a fair bit).
  2. Next, we enabled the POS, PIT and YAW damping (with all existing settings unchanged), but with the SD coil input and output disabled. We had to increase the watchdog threshold to ~600mV.
  3. Once the optic was reasonably well damped (~70mV on the watchdog was the best we saw), I put in the side OSEM till the PD was completely occluded. At this point, I enganed the earthquake stops, and then released the mirror such that it was freely hanging. I then observed the optic by eye, and noted a time when the dominant motion was along the axis of the side OSEM coil (i.e. minimal YAW motion). 
  4. Attachment #1 shows time series plots of the 5 OSEM PD voltage monitors. Perhaps because the side OSEM input was disabled, the damping wasn't as efficient as it normally is (also there is a fan blowing air around the clean bench). But at the point indicated on the plot, the YAW motion was negligible to the eye, while the dominant motion was along the axis of the coil. During this time, the readout bottomed out at approximately 10% of the saturation value (towards the end of these plots, I disabled the damping loops and began pulling the OSEMs out one by one). Because the damping was imperfect, this is only an approximate guess of how much dynamic range we are losing. But does this warrant regluing the side magnet?

Other remarks:

  • The 4 face magents were reasonably well centered in the coil. While Eric and I were looking at this earlier today, the LL magnet looked a little close to the coil, but after putting all 4 OSEMs in, the situation looked reasonable to the eye. I couldn't take pictures because of space constraints, and furthermore, it's almost impossible to hold the camera in the correct vertical position. 
  • Steve, Eric and I couldn't find the OSEM gender changer anywhere in the lab and it wasn't in the box it was advertised to be in. So we made a custom cheater cable, and cleaned it by wiping with Isoprop., and wrapped it in foil for use in this test. The OSEM pins should probably be cleaned before we put these back in vacuum. 
Attachment 1: osem_test_2016_07_25.png
osem_test_2016_07_25.png
  12334   Mon Jul 25 17:01:54 2016 SteveUpdateSUSETMX suspension - progress

ITMY side  : Magnet od 1.9 mm so wire to magnet gap ~ 0.2-0.3 mm

 

Attachment 1: ITMYside2011.JPG
ITMYside2011.JPG
  12332   Mon Jul 25 13:47:19 2016 ranaUpdateGeneralETMX suspension - progress

Ugh. frown

Steve, please look into getting some plated magnets (either SmCo or NdFeB is OK) of this size so that we can install cleaner magnets by the next vent.

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