In the evening, I went into the clean room to check how it goes.
- The air around the table is quite warm like a hell. Is this normal?
- I checked how the scattered epoxy spots look like. They were not touching the bath anymore due to evaporation.
- I scraped the spots with the tweezers there. They were easily removed. The particlates on the side barrel were wiped by a wipe with aceton. (Result: Attachment 3)
- Then looked at the other side. I poked the standoff with the tweezer. It was easily removed. I don't think the bond was too weak. Just the area of the bond was so tiny.
- Also residue was scraped by a tweezer and wiped with a cloth. (Attachment 2)
- The removed stand off is in the stainless bowl together with the parts that Eric removed.
- I didn't want to leave the optic in the aceton fume. It was placed on a metal donuts for a 3" optic. (Attachment 4)
- I couldn't find a vacant clean glass jar for the lid. So, a foil hut was built. We should be very careful not to scratch the optic when we remove the hut. (Attachment 5)
- The aceton bath was covered with the foil as it was. (Attachment 6)
A new MEDM tab has been added to the summary pages (https://nodus.ligo.caltech.edu:30889/detcharsummary/day/20160708/medm/), although some of the screens are not updated when /cvs/cds/projects/statScreen/cronjob.sh is run. In /cvs/cds/projects/statScreen/log.txt, the following error is given for those files: import: unable to read X window image `0x20011f': Resource temporarily unavailable @ error/xwindow.c/XImportImage/5027. If anyone has seen this error before or knows how to fix it, please let me know.
In the meantime, I'll be working on creating an archive of MEDM screens for every hour to be displayed on the summary pages.
The magnet, guide rod, and standoff came off without too much force. However, some epoxy residue remains on the barrel. I didn't really want to scrape it off, so I've opted for more soaking. Much of the acetone had evaporated already, so I put some more - just to the point where the residue is submerged.
Optimus' memory errors are back so I found the exact DIMM model needed to replace: http://www.ebay.com/itm/Lot-of-10-Samsung-4GB-2Rx4-PC2-5300P-555-12-L0-M393T5160QZA-CE6-ECC-Memory-/201604698112?hash=item2ef0939000:g:EgEAAOSwqBJXWFZh I'm not sure what website would be the best for buying new DIMMs but this is the part we need: Samsung 4GB 2Rx4 PC2-5300P-555-12-L0 M393T5160QZA-CE6.
ETMX is currently in the clean room, the barrel is the tiniest bit submerged in acetone that will remove a guide rod, standoff, and side OSEM.
Additional inpsection of the standoffs on the flow bench did not provide any insight, pictures are in picasa. Here is a cropped version of a picture we took:
We should look at them under a microscope.
Acromag is talking now, after few changes to the original EPICS configuration and cross compile configuration. Modbus config files also were changed and compiled again to run it on linux-arm architecture. I have made use of pyModbus for the final work and I am planning to use the same for grabbing channels. Though I am unable to grab channel data right now, I am able to communicate to it over ethernet and send and receive data.
Move the suspension on the south clean bench and make more close inspection. We need to remove the OSEMs.
Then unmount the mirror. Bring it to the clean room and work on the bond removal.
Meanwhile, set up all suspension components inclusing the alignment test setup.
Yesterday, I expanded the extent of the ETMX suspension coil driver investigation. I set up identical monitors for two more coils (so now we are monitoring the voltage sent to UL, UR and LL - I didn't set one up for LR because it is on a second DB25 connector). Furthermore, I increased the excitation amplitude from ~20 to ~2000 (each coil had an independent oscillator at slightly different frequency between 5Hz and 8.5 Hz), the logic being that during LSC actuation we send signals of approximately this amplitude to the coils and we wanted to see if a larger amplitude signal somehow makes the system more prone to glitches.
Over ~10 hours of observation, there is no clear evidence of any glitch. About 2 hours ago (~930am PDT Fri Jul 8), the watchdog tripped - but this was because even though I had increased the trip threshold to ~800 for the course of this investigation, megatron runs this script every 20 minutes or so that automatically reduces this threshold by 17 counts - so at some point, the threshold went lower than the coil voltage, causing the watchdog to trip. So this was not a glitch. The other break around 2am PDT earlier today was an FB crash.
Do we now go ahead and pull the suspension out, and proceed with the swap?
I performed a visual inspection of ITMY in its natural habitat today. I did not get any great pictures from the HR side because it's located very towards the edge of the table towards the arm. Before that I checked the levelness of the table. East-west direction was fine, north-south was slightly off but still within the marks for 'level'.
The AR side had several speckles, a few of them located somewhat near the geometrical center of ITMY. The top of the barrel was worse of, as expected. The HR side was a little better, but there were a few pieces of dust? near near the center. Sample pictures are attached, I uploaded all the good ones to Picasa.
Clamps that mark the position of ITMY were already in place. I did not move the optic just yet, and we will have to move a cable block out of the way to bring ITMY near the opening for us to work on it. We will markt the position of that to preserve the weight distribution. Then we can probably take some better before/after pictures. Tomorrow I will be looking at ETMY.
Ah, thanks. That makes sense. In that case, we should remove the texts "30Hz HPF" from the suspension screens.
Now we just need AA LPFs for these channels, or hook them up to the RT system.
Based on Koji's observation of a flat TF, it seems more likely the Vmon channels are looking at the path I've highlighted in green (named "EPICS V Mon"), rather than the path in red (named "DAQ Mon") that Koji initially suspected. This path still lacks any AA for the 16Hz EPICS sampling.
We obtained two monitors of the same type from Larry.
Attached is a diagram, showing the entire (planned) signal flow of the DAF model. Some thoughts on the implementation after discussion with eric:
1) Since the LSC control signals and ASC signals are running on the c1lsc FE at the same rate as DAFI (16kHz), it would be wise to start from these.
Current implementation: has a matrix at the end of the LSC PD signals, which selects one of the PD signals and outputs it to the DAFI via IPC communication.
Proposed Changes: Add another matrix at the end of the LSC PD signals, to give to the second stereo output. Similarly, add two matrices each at the end of the LSC control signals and the ASC signals. Each matrix must select one of the signals and output it to the DAF via IPC.
2) The PEM running on the c1sus FE system will have to be brought to DAFI in a similar fashon. However, since c1sus runs at 2kHz, there is a possibility of imaging while the signal is transfered to the DAFI. This could be taken care of by an anti imaging filter, or inserting zeros between two samples coming at to the 16 kHz system from the 2kHz system and then low-passing it to remove the aliased parts. (similar to upsampling)
3) For the SUS control signals, input can be given from a matrix prepared for each optic seperately.
It may be advantageous to look at the coil output data from when the OSEM damping is on, to try and reproduce the real output signal amplitude that gets sent to the coils.
The amplitude of the applied signal (20) was indeed chosen to roughly match what goes to the coils normally when the OSEM damping is on.
There appears to be no evidence of a detectable glitch in the last 10 hours or so (see attachment #1 - of course this is a 16Hz channel and the full data is yet to be looked at)... I guess the verdict on this is still inconclusive.
Atm 1, It's right arm is perfect.
Atm 3-4, The left one has bended (dropped) end.
Atm 2, Our ruby wire stanoffs will fit the jig. Ruby OD 1.27 mm vs. old Aluminum OD 1.0 mm. Length ruby 6.4 mm vs Al 4.8 mm
Atm 5, The fixture translation stages are a bit loooose. Careful use of the micrometer is needed to be precise
Betsy agreed that the 40m will keep SOS fixtures.
One of the pianosa monitors has ceased to function For now, it has been set up to operate with just the one monitor.
One of Donatella's monitors has a defective display as well. Maybe we should source some replacements. Koji has said we will talk to Larry Wallace about this..
I've made a few changes to the monitoring setup in the hope we catch a glitch in the DAC output/ sus coil driver electronics. Summary of important changes:
It remains to see if we will actually be able to see the glitch in long stretches of data - it is unclear to me how big a glitch will be in terms of ADC counts.
The relevant channels are : C1:SCX-UL_DIFF_MON and C1:SCX-UL_DIFF_MON_EPICS (pardon the naming conventions as the setup is only temporary after all). Both these should be hovering around 0 in the absence of any glitching. The noise in the measured signal seems to be around 2 ADC counts. I am leaving this as is overnight, hopefully the ETMX coil drive signal chain obliges and gives us some conclusive evidence...
I have not committed any of the model changes to the SVN.
It seemed something has been done. And I got cron emails.
Then, it seemed something has been done. And the emails stopped.
This should be fixed now—apologies for the spam.
I don't know much about how the cron job runs, I'll forward this to Max.
I started to receive emails from cron every 15min. Is the email related to this? And is it normal? I never received these cron emails before when the sum-page was running.
Max says it should be fixed now. Have the emails stopped?
Circuit1: It is nice to receive the voltage across the transimpedance resistor with a high impedance buffer (or amplifier), as close to the resister as possible. This amplifier needs to have low numbers for input bias current, input offset current, and input current noise. These current noise becomes the noise of the temperature reading. On the top of that, the input voltage noise of the buffer will be added to the output. The typical noise model can be found in http://www.analog.com/media/en/technical-documentation/application-notes/AN-940.pdf
The good candidates for the buffer is LT1128, ADA4004, OPA140, and LT1012. If the application is not too sensitive to the total noise, OPA604 is a good choise with easier handling.
Circuit2: With the same reason, AD741 is an old generic amp that is not a great choise for this purpose. The current noise is more significant because of the higher transimpedance here. The same noise model as above can be used to analyze the performance.
I wanted to know what this Vmon exactly is. D010001 is telling us that the Vmon channels are HPFed with fc=30Hz (Attachment 1). Is this true?
I checked the quiscent noise spectrum of the ITMX UL coil output (C1:SUS-ITMX_ULCOIL_OUT) and the corresponding VMON (C1:SUS-ITMX_ULVmon). (Attachment 2 Ref curves). I did not find any good coherence. So the nominal quiscent Vmon output is carrying no useful information.
Question: How much do we need to excite the coil output in order to see any meaningful signal?
As I excite the ITMX UL coil (C1:SUS-ITMX_ULCOIL_EXC) with uniform noise of 100-300 counts below 0.3Hz, I eventually could see the increase of the power spectrum and the coherence (Attachment 2). Below 0.1 Hz the coherence was ~1 and the transfer function was measured to be -75dB and flat. But wait, why is the transfer function flat?
In fact, if I inject broadband noise to the coil, I could increase the coil output and Vmon at the same time without gaining the coherence. (Attachment 3). After some more investigation, I suspect that this HPF is diabled (= bypassed) and aliasing of the high freq signal is causing the noise in Vmon.
In order to check this hypothesis, we need to visit the board.
The main C1 summary pages are back online now thanks to Max and Duncan, with a gap in pages from June 8th to July 4th. Also, I've added my new VMon and Sensors tabs to the SUS parent tab on the main pages. These new tabs are now up and running on the July 7th summary page.
Here's a link to the main nodus pages with the new tabs: https://nodus.ligo.caltech.edu:30889/detcharsummary/day/20160707/sus/vmon/
And another to my ldas page with the tabs implemented: https://ldas-jobs.ligo.caltech.edu/~praful.vasireddy/1150848017-1150848317/sus/vmon/
Let me know if you have any suggestions or see anything wrong with these additions, I'm still working on getting the scales to be right for all graphs.
I am using AD592CNZ temperature transducer ICs for measuring temperature inside as well as outside the enclosure. It is a current output IC which outputs current proportional to temperature. As mentioned in the data sheet of AD592, I am using the following two schematics:
Though I still need to calibrate these temperature transducers, I did some measurements. I have temperature readings, and now my goal in few days is to find a transfer function of temperature fluctuations inside the enclosure to outside the enclosure.
About data acquisition:
We have re-configured the raspberry pi(B8:27:EB:70:D0:D8) on martian network. It's new ip address is 192.168.113.107(domenica.martian). Also, we have added the Acromag Busworks card(00:01:C3:00:9F:C8) on the martian network and its ip address is 192.168.113.237(acroey.martian).
I've added a new tab for VMon under the SUS parent tab. I'm still working out the scale and units, but let me know if you think this is a useful addition. Here's a link to my summary page that has this tab: https://ldas-jobs.ligo.caltech.edu/~praful.vasireddy/1151193617-1151193917/sus/vmon/
I'll have another tab with VMon BLRMS up soon.
Also, the main summary pages should be back online soon after Max fixed a bug. I'll try to add the SUS/VMon tab to the main pages as well.
The DAFI block was reviewed by Rana yesterday. The following changes/improvements were suggested: (Updated on 20th July 2016 with tasks taat remain in red)
1) include all the various channels like PEM, LSC, ASC, SUS, SEI, etc. as the inputs. Currently the inputs are only the LSC.
2) include all the control signals.
3) create a very detailed diagram of the entire signal flow and plan tasks accordingly.
4) Enable cascading of various DSP processes.
5) Adjusting the gain of the AGC such that the amplitude of the output signal comes to about half the peak amplitude offered by the ADC. This will help taking advantage of the entire dynamic range of the ADC.
6) change the enable button styles from a text input based controller to a button controller.
7) Currently, disabling a particular signal terminates the signal. Instead, it should turn into a unity gain block on disabling.
8) Check if the Fibox does AC coupling or not. If not, add an AC coupling arrangement in the DAFI.
9) Check the nature of the ADC1 and ADC2 inputs to the DAFI. I checked them yesterday, and they are channels 25 and 26 of ADC0, which are empty.
Vacuum Status: Chamber Open
All chamber annuloses are vented. Vac Monitor screen is not communicating with gauges. The valve position indicator are working.
RGA is pumped by Maglev through VM2
Yesterday Q noticed that PRM_sensor_LR was 0.098V This actually went to ~ zero on 7-3
The last RGA scan of this pumpdown 78
Pressure plot of 640 days long pd 78
CC1 cold cathode gauge was jump started with an accidental pressure glitch, that you can see on P1 plot
With Koji's help, I've hacked together an arrangement that will allow us to monitor the output of the coil driver to the UL coil.
The arrangement consists of a short custom ribbon cable with female DB25 connectors on both ends - the particular wire sending the signal to the UL coil has a 100 ohm resistor wired in series, because the coil has resistance ~20ohm, and the output of the coil driver board has a series 200(?) ohm resistor, so by directly monitoring the voltage at this point, we may not see a glitch as it may register too small. Tangentially related: the schematic of the coil driver board suggests that the buffered output monitor has a gain of 0.5.
To monitor the voltage, I use the board to which the 4 Oplev signals are currently hooked up. Channel 7 on this particular board (corresponding to ADC channel 30 on c1scx) was conveniently wired up for some prior test, so I used this channel. Then, I modified the C1SCX model to add a testpoint to monitor the output of this ADC. Then, I turned OFF the input on the coil output filter for the UL Coil (i.e. C1:SUS-ETMX_ULCOIL_SW1) so that we can send a known, controlled signal to the UL Coil by means of awggui. Next, I added an excitation at 5 Hz, amplitude 20 counts (as the signal to the coil under normal conditions was approximately of this amplitude) to the excitation channel of the same filter module, which is the state I am leaving the setup in for the night. I have confirmed that I see this 5Hz oscillation on the monitor channel I set up. Oddly, the 0 crossings of the oscillations happen at approximately -1000 counts and not at 0 counts. I wonder where this offset is coming from? The two points I am monitoring the voltage across is shown in the attached photograph - the black clip is connected to the lead carrying the return signal from the coil.
I also wanted to set up a math block in the model itself that monitors, in addition to the raw ADC channel, a copy from which the known applied signal has been cancelled, as presumably a glitch would be more obvious in such a record. However, I was unable to access the excitation channel to the ULCOIL filter from within the SCX model. So I am just recording the raw output for tonight...
One glitch was seen to occur without a change in the output voltage monitors in ELOG 11744
I'd suggest clamping and moving it to the flow bench so you can inspect with a bright light. Then remove the wire and inspect the standoff, but hurry up with getting it in the soak bath so you can start on the cleaning of the other ones.
I wonder if we're really sure that its a mechanical problem with ETMX.
Gautam tells me that the local damping was always ON when looking for the jumps. This means that the coil driver was still hooked up and we can't rule out glitches in the DAC or the coil driver.
The UL OSEM shows the biggest movement (10 microns). The LR shows the second most (6-7 microns). The others are 2x less. So its consistent with a voltage change on UL,
Is this consistent with a slip in one of the wire standoffs? I think no.
After hardware errors prevented me from using optimus, I switched my generation of summary pages back to the clusters. A day's worth of data is still too much to process using one computer, but I have successfully made summary pages for a timescales of a couple of hours on this site: https://ldas-jobs.ligo.caltech.edu/~praful.vasireddy/
Currently, I'm working on learning the current plot-generation code so that it can eventually be modified to include an interactive component (e.g., hovering over a point on a timeseries would display the GPS time). Also, the 40m summary pages have been down for the past 3 weeks but should be up and working soon as the clusters are now alive.
Rough summary of today's progress:
I didn't really see anything out of the ordinary on the ETMX suspension. Earthquake stops had clearance, OSEMS were secure, no visible glue degredation on face magnets. Inspection with green LED flashlight didn't reveal any obscene dirtieness on either face, just a few particles here and there. The top of the opic barrel unsurprisingly has a good amount of particulate. The wire grooves are way too small to resolve anything at this point, other than that they exist.
The suspension footprint is already marked, tomorrow we can move the suspension closer to the door to get an even closer look at it, before removing it from the chamber.
I am trying to design an antialiasing filter, which also has two switchable whitening stages. I have designed a first version of a PCB for this.
The board takes differential input through PCB mountable BNCs. It consists of an instrumentaiton amplifier made using quad opamp ADA4004, followed by two whitening blocks, also made using ADA4004, which can be bypassed if needed, depending upon a control input. The mux used for this purpose is Maxim MAX4158EUA. These two whitening blocks are followed by 2 the LPF stages. A third LPF stage could be added if needed. These use AD829 opamps. After the LPFs are two amplifiers for giving a differential output through two output BNCs. The schematic is shown in attachment 1: "AA.pdf". The top layers of the layout are shown in attachment 2 (AAtop.pdf), the bottom layers in attachment 3 (AAbottom.pdf), and the entire layout in attachment 4 (AAbrd.pdf).
The board has 6 layers (in the order from top to bottom):
1) Top signal layer;
2) Internal plane 1 (GND),
3) Internal plane 2 (+15V),
4) Internal plane 3 (-15V),
5) Internal plane 4 (GND),
6) Bottom signal layer.
Power: +15, -15 and GND is given through a 4 pin header connector.
The dimensions of the board are 1550 mil 6115 mil (38.1mm155.3mm) and the overall dimensions including the protruding BNC edges are 1550 mil 7675 mil (38.1mm194.9mm)
I would like to have inputs on the layout telling me if any component/trace needs to be changed/better placed, any other things about the board need to be changed, etc.
P.S.: I have also added a zipped folder "AA.zip" containing the schematic and board files, as well as the above pdfs.
Glass soaking dish with teflon guides.
Proposed Acetone soak dish for SOS epoxy softening.
It has good acces through 5" top ID. The set up is stable and teflon lined.
Materials: glass jar with SS cover, teflon bricks, 0.008" teflon wrapped "high density Drever bricks" and aluminum
Drever brick: I beleive it is a Tungsten alloy. We used it as vac-bat savor at the coffe can. It has high density, heavy and hard, it was never identified.
I will soak one brick to see if it has any reaction ability with acetone.
NO means that only Glass and Teflon can be used for this fixture in Acetone. We can not take a chance on the coating!
I guess the small surface area Aluminum dumbbell, guide rod and-or wire standoff, magnet and epoxy does not degrade the acetone such way that it effects our coating.
Not ot mention, that only the very edge of the coating would in this solution.
Here are some plans / rough procedures for this week's vent. It is unlikely that I have though of everything, but this should be a reasonable starting point.
The mode cleaner still hasn't been locked in air, we may not want to touch the Y arm optics until we are able to lock to the Y arm and dither align, so we are sure to keep the input pointing from drifting away too much.
For $optic in [ITMX, ITMY, ETMY]:
There has been an ongoing memory error in optimus with the following messages:
Message from syslogd@optimus at Jun 30 14:57:48 ...
kernel:[1292439.705127] [Hardware Error]: Corrected error, no action required.
Message from syslogd@optimus at Jun 30 14:57:48 ...
kernel:[1292439.705174] [Hardware Error]: CPU:24 (10:4:2) MC4_STATUS[Over|CE|MiscV|-|AddrV|CECC]: 0xdc04410032080a13
Message from syslogd@optimus at Jun 30 14:57:48 ...
kernel:[1292439.705237] [Hardware Error]: MC4_ADDR: 0x0000001ad2bd06d0
Message from syslogd@optimus at Jun 30 14:57:48 ...
kernel:[1292439.705264] [Hardware Error]: MC4 Error (node 6): DRAM ECC error detected on the NB.
Message from syslogd@optimus at Jun 30 14:57:48 ...
kernel:[1292439.705323] [Hardware Error]: cache level: L3/GEN, mem/io: MEM, mem-tx: RD, part-proc: RES (no timeout)
Optimus is a Sun Fire X4600 M2 Split-Plane server. Based on this message, the issue seems to be in memory controller (MC) 6, chip set row (csrow) 7, channel 0. I got this same result again after installing edac-utils and running edac-util -v, which gave me:
mc6: csrow7: mc#6csrow#7channel#0: 287 Corrected Errors
and said that all other DIMMs were working fine with 0 errors. Each MC has 4 csrows numbered 4-7. I shut off optimus and checked inside and found that it consists of 8 CPU slots lined up horizontally, each with 4 DIMMs stacked vertically and 4 empty DIMM slots beneath. I'm thinking that each of the 8 CPU slots has its own memory controller (0-7) and that the csrow corresponds to the position in the vertical stack, with csrow 7 being the topmost DIMM in the stack. This would mean that MC 6, csrow 7 would be the 7th memory controller, topmost DIMM. The channel would then correspond to which one of the DIMMs in the pair is faulty although if the DIMM was replaced, both channels 0 and 1 would be switched out. Here are some sources that I used:
I'll find the exact part needed to replace soon.
I just disconnected the 6th instrument grade air cylinder from the vacuum envelope at 720 Torr. Now it will reach equilibrium through a filter as it sucks in lab air.
This is the sure way not to over pressurize the chamber.
1, Fix ETMX sus "jump issue"
2, First Contact clean the arms
3, Install new spare cold cathode and convectron gauges: InstruTech-Hornet
4, Install 50 mm apeture beam baffles
5, Check and clean optical quality viewport from inside
The following bullets were executed:
Check crane functionality & cleanliness last week
We are venting the 40m IFO
Steve has ordered some teflon parts to take the place of the metal parts in his acetone-soaking jig. They should arrive tomorrow.
So, we will be begin the venting process tomorrow. Doors to come off on Tuesday.
I have transferred most of the temperature measurement stuff from the front area to seismometer at the end of Y-arm. While arranging the components I have taken all care that they will not interfere with existing system. Also, I have temporarily taken a monitor from the front area to the area near same seismometer as I couldn't talk to Rpi via ssh. For next twelve hours, I am now recording temperature inside as well as outside the seismometer enclosure. Some temperature sensors are inside the enclosure while some are outside the seismometer enclosure.
Last night, we set about trying to see if we could measure and verify the predictions of the simulations, and if there are indeed HOM sidebands co-resonating with the carrier. Koji pointed out that if we clip the transmitted beam from the arm incident on a PD, then the power of the higher order HG modes no longer integrate to 0 (i.e. the orthogonality is broken), and so if there are indeed some co-resonating modes, we should be able to see the beat between them on a spectrum analyzer. The procedure we followed was:
We then repeated the above steps at the X-end (but here, an additional lens had to be installed to focus the IR beam onto the PDA10CF - there was, however, sufficient space on the table so we didn't need to remove the PDA520 for this measurement).
Y-end: DC power on the photodiode at optimal alignment ~ 200mV => spectra taken by deliberately misaligning the beam incident on the PD till the DC power was ~120mV (see remarks about these values).
I converted the peak heights seen on the spectrum analyzer in volts to power by dividing by transimpedance (=5*10^3 V/A into a 50ohm load) * responsivity at 1064nm (~0.6A/W for PDA10CF).
I have updated the vent prep checklist on the wiki. Gautam and I did the following things from it:
Reduce input power to no more than 100mW by adjusting wave plate+PBS setup on the PSL table BEFORE the PMC. (Using the WP + PBS that already exist after the laser.)
The following bullets have not yet been executed:
Check crane functionality & cleanliness
I've gone through the SOS suspension document (E970037) and some old elogs to get an idea of all the accesories we need for the process of suspending, aside from the tower itself, which Steve has already put together. Gautam and I have laid our eyes upon most of the critical pieces. Some other objects are unknown, and perhaps not strictly neccesary.
Confirmed to exist:
In addition, I am told that we have a long ribbon cable that can run from the X end to the clean room to enable OSEM damping control while we do the pitch alignment.
Things mentioned in the procedure I have not found:
Some other tasks and their status:
In the attached photo from 2012, one can see the installed black glass baffle. According to the drawings (LIGO-DNNNXXX) this one has a clear aperture of 40 mm.
In (someplace ?) we have clean baffles with a 50 mm aperture which can be installed during this vent. In order to be more conservative, let us choose to swap these out for all 4 test masses during the upcoming vent using the green laser as an alignment guide, as Koji described at today's lunch meeting.
They are located at the top of E1 drawer cabinet