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ID Date Author Type Category Subject
  10329   Mon Aug 4 17:30:00 2014 ericqUpdateGeneralChronic Suspension Problems

TRX and TRY communication were recovered by doing a simultaneous reboot of all of the frontends.

Working with the interferometer has been extremely frustrating today. Having transmission values let us lock and ASS, but that has been less helpful than you would hope.

Saving the ASS offsets has repeatedly resulted in an overall bad change in alignment, moving the TTs and other things off randomly.

ITMX continues to be kicked. ITMY intermittently wanders away. It has not been possible to maintain IFO alignment for a reasonable length of time.

Also, the wall IOO striptool shows the MC2 Trans QPD Yaw having large step-function features. The MC is having an ok duty cycle, but this just may mean that the WFS are able to absorb what is happening to the MC suspensions.

The suspensions are really misbehaving. We need to get to the bottom of this, or else we are going to keep losing time to alignment.

  10328   Mon Aug 4 09:17:42 2014 SteveUpdateSUSITMX is still kicked

Quote:

I was investigating several issues on the IFO. As many of you noticed and not elogged, ITMX had frequent kicking without its oplev servo.
Also I had C1:LSC-TRY_OUT flatted out to zero even though I could see some fringes C1:SUS-ETMY_TRY_OUT.

Restarted all of the realtime models (no machine reboot).

Now I don't find any beam on REFL/AS/POP cameras.

If I look at BS-PRM camera, I can see big scattering, the beam is in the BS chamber.
I jiggled TT1 but cannot find neither a Michelson fringe nor POP beam.

So far I can't figure out what has happened but I'm leaving the lab now.

IMC is locked fine.
I can see some higher order mode of the Yarm green, so the Y arm alignment is no so far from the correct one.

 ITMX is kicked up periodically.  ITMX_PD_MAX_VAR is lowered to 500 from 1350

It started at Friday morning 8-1

Attachment 1: ITMXkicked.png
ITMXkicked.png
Attachment 2: ITMXkickedStart.png
ITMXkickedStart.png
  10327   Sun Aug 3 23:47:56 2014 KojiUpdateGeneralRecovery efforts

It's great that you guys found the beam.
Yes, ITMX kick and lost communication for TRY were the motivation of my CDS rebooting.

  10326   Sun Aug 3 17:19:32 2014 ericqUpdateGeneralRecovery efforts

[ericq, Jenne]

We both happened to come by today to fix things up.

When I arrived, the PMC was locked to a 01 mode, which I fixed. The PMC transmission is still worryingly low. MC locked happily. 

ETMX was getting odd kicks, the kind where a DC shift would occur suddenly, and then go away a few moments later. I turned off all dynamic coil outputs, and looked at the MON output of the SOS driver with a scope to try and see if the DAC or dewhitening was glitching, but didn't see anything... Meanwhile, Jenne fiddled with the TTs until we got beams on POP and REFL. (EDIT, JCD:  Useful strategies were to put an excitation onto TT2, and move TT1 until the scattered beam in the chamber was moving at the excitation frequency,  Find the edges of TT2 by finding where the scattered light stops seeing the excitation, and center the beam on TT2.  By then, I think I saw the beam on the PRM face camera.  Then, put a temporary camera looking at the face of PR2.  Using TT2 to center here got us the beam on the POP camera.)

We then walked PRM and the TTs around to keep those two camera beams and get the PRM oplev beam back on its QPD. At this point, ITMX was misaligned (by us), and ITMY aligned to get some recycled flashes into the Y-arm. Y-arm was locked to green, and we poked TTs to get better IR flashes. Misaligning PRM, we had Y-Arm flashes of ~0.7. From there, the michelson and then X-arm were roughly aligned. Both arms were seeing flashes of about 0.7, and the MICH fringes on the AS port look nice.

Frustratingly, the SUS->LSC communication for TRY and TRX isn't working, and could not be fixed by any combination of model or front-end restarting... Thus we haven't been able to actually lock the arms and run ASS. THIS IS VERY FRUSTRATING. 

Additionally, at the point where we were getting light back into the Yarm, the ITMX that were seen on Friday were happening again, tripping the watchdog. Also, something in the Yarm cavity is getting intermittently pushed around, as can be seen by the green lock suddenly wandering off. All of these suspension shenanigans seem to be independent of oplev damping. 

It troubles me that this whole situation is fairly similar to the last time we lost the input pointing (ELOG 10088)

In any case, we feel that we have gotten the IFO alignment to a lockable state.

  10325   Fri Aug 1 22:56:27 2014 KojiUpdateGeneralBeam lost in the chamber???

I was investigating several issues on the IFO. As many of you noticed and not elogged, ITMX had frequent kicking without its oplev servo.
Also I had C1:LSC-TRY_OUT flatted out to zero even though I could see some fringes C1:SUS-ETMY_TRY_OUT.

Restarted all of the realtime models (no machine reboot).

Now I don't find any beam on REFL/AS/POP cameras.

If I look at BS-PRM camera, I can see big scattering, the beam is in the BS chamber.
I jiggled TT1 but cannot find neither a Michelson fringe nor POP beam.

So far I can't figure out what has happened but I'm leaving the lab now.

IMC is locked fine.
I can see some higher order mode of the Yarm green, so the Y arm alignment is no so far from the correct one.

  10324   Fri Aug 1 18:48:46 2014 AkhilSummaryElectronicsPZT Calibration

 

 The PZT actuation on the laser frequency in MHz/V ( assuming the previous calibration here of the PZT count/V) is :

X- arm: 33.7 MHz/V

Y- arm: 14.59 MHz/V

This number seems to be wrong by a factor of 10. 

So we[I and EricQ] decided to trace the cables that run into the ADC from the PZT Out. We found a black LEMO box in the path to ADC,which is  an anti-aliasing filter for each input channel. However,in theory the response of this filter should be flat up until a few kHz i.e. for  the DC gain it should be 1. But we will manually test it and look at the DC gain of the LEMO box.

 

 

  10323   Fri Aug 1 15:32:07 2014 ericqUpdateComputer Scripts / ProgramsElog and svn backups

Koji and Evan have both brought up a good point that we may not be backing up the svn and ELOG properly.

I have modified the rsync.backup script that nodus' cron runs every night that backs up /cvs/cds to what I presume are the tape backups at ldas-cit.ligo.caltech.edu.

Specifically, I added two rsync commands that grab the svn and elog directories from /export/home and copy them to their old locations in /cvs/cds/caltech. This way, the old locations are updated, and the tape backups stay current.

  10322   Fri Aug 1 12:49:06 2014 KojiSummaryIOOMC servo analysis

Reasoning to choose the current parameters:

FSS Common: 18dB
FSS Fast: 20dB

Attachment 1:
Openloop transfer function of the IMC loop with the nominal gain setting. The UGF is 176kHz and the phase margin is 48 deg.
This is about 3 time more bandwidth than the previous setting. (Good)

It is visible that the TF has sharp roll off around 1MHz. I wonder if this comes from the demodboard LPF and/or the PMC cav pole.
In fact, according to Manasa, the PMC has the ringdown of 164.6ns which corresponds to the cavity pole of 967kHz. So this must
be there in the OLTF.

From the plot, the order of the low pass is about 5. Subtracting the slope by the cavity pole, the order is four. If I look at the TF of the minicircuits
LPFs (this entry), the phase delay of the filter at 1/10 of the cut off freq is ~30deg. And the order of the filters are maybe 6th elliptic?
So it's not yet clear if the LPF is causing a significant phase delay at 180kHz.

More significantly, the gain margin at ~1MHz is way too small. This is causing a big servo bump at that frequency as seen in Attachment 2.

In total, my recommendation is to move the LPF freq up by x2 or x3, and give a mild LPF above 500kHz.
This requires some modeling as well as try and error.

Attachment 2:

This figure is to explain how the common FSS gain was set. By increasing the gain, the UGF is increased and we can enjoy more supression (from red to purple).
The more gain, however, the more servo bump we observe above the UGF. The gain was chosen so that the total PC feedback does not exceed 3V.

Attachment 3/4:

This figure explains how the fast FSS gain (namely crossover frequency between fast and PC) was set. When the fast is low (red) the phase margin between two loops
are plenty and therefore the openloop TF is smooth. But the PC's frequency domain is large and has to work more (in rms). As the fast gain is increased, the actuation
by the PC is offloaded to the fast PZT (that's good). But eventually the phase margin is not enough and the dip start to show up (purple). This dip cause worse closed loop TF,
as seen in Attachment 4, or even an instability of the loop eventually. So the fast gain was set somewhere in between (green).

Attachment 1: MC_OLTF.pdf
MC_OLTF.pdf
Attachment 2: MC_Error_Common.pdf
MC_Error_Common.pdf
Attachment 3: MC_Crossover.pdf
MC_Crossover.pdf
Attachment 4: MC_CLTF_Fast.pdf
MC_CLTF_Fast.pdf
  10321   Fri Aug 1 11:11:12 2014 KojiUpdateIOOCurrent IMC servo configuration

The comparison between the new and old MC servo (FSS part) was attached.

- The new servo has the same DC range as before.
  Even though there is 1/2 gain in the chain now, the previous range of the FSS box was 0 to 10V.
  Now it is +/-10V. So we did not lose the range.

- The new servo has x3.2 larger range above 100Hz.

- x1.6 enhancement of the FSS Box output noise above 10Hz.

- The noise of the HV amp (and the summing amp) is x300 and x2600 more filtered at 10kHz and 100kHz respectively.

Attachment 1: diagram.pdf
diagram.pdf
  10320   Fri Aug 1 10:40:48 2014 KojiSummaryIOOMC servo summing amp

The summing amp is prepared to allow up to use bipolar full range of the FSS box output

This means that the FSS fast PZT output is now nominally 0V and can range +/-10V.

- FSS Box has the output range of +/-10V

- Thorlabs HV amp MDT694 accepts 0V ~ +10V

- This circuit add an offset of +5V while the main signal is attenuated by a factor of 2. The offset voltage is produced from the voltage reference IC AD586.

- In addition, a summing node and voltage monitors before and after the summing node are provided. They are useful to test the crossover frequency of the fast/PC loops.

- The output noise level at 10kHz was ~60 nV/rtHz. The transfer function of the circuit was measured and flat up to 100kHz. The phase delay is negligible at 10kHz and less than 3deg at 100kHz

- Although the schematic was drawn in Altium, the board is a universal 1U eurocard and all wires were hand soldered.

Attachment 1: Fast_PZT_IF.PDF
Fast_PZT_IF.PDF
  10319   Fri Aug 1 08:55:34 2014 KojiSummaryIOOMC auto locker

It seems that the MC auto locker and the FSSSlow PID servo survived a night.

PC Drive is still angry occasionally. We want to know what this is.

Attachment 1: MC.png
MC.png
  10318   Fri Aug 1 03:49:26 2014 KojiSummaryGeneralKoji - to do

- Put the circuit diagram of the sum amp on/in the circuit enclosure and associate it with an elog [done].
- Update the circuit diagram of the pomona box [done]

ALL DONE

  10317   Fri Aug 1 01:57:24 2014 KojiSummaryIOOMC auto locker

To make MC auto locker running correctly, mcdown and mcup were revised

I tried it by unlocking MC several times. It seems OK. Let's see how it works.


Nominal gains for locking (to be taken care by mcdown)

C1:IOO-MC_REFL_GAIN
was 16 and is 19 now.

C1:IOO-MC_VCO_GAIN
was 9 and is 9 now too.

C1:PSL-FSS_MGAIN
was missing and now +13

C1:PSL-FSS_FASTGAIN
was +23.5 and is now +20.0

Nominal gains for operation ( to be taken care by mcup.

C1:IOO-MC_REFL_GAIN
was 19 and is 19 now too.

C1:IOO-MC_VCO_GAIN
was 25 and now uses ezcastep (ezcastep C1:IOO-MC_VCO_GAIN=9 +1,16 -s 0.1)

C1:PSL-FSS_MGAIN
C1:PSL-FSS_FASTGAIN

ezcawrite C1:PSL-FSS_MGAIN `ezcaread -n C1:PSL-STAT_FSS_NOM_C_GAIN`
ezcawrite C1:PSL-FSS_FASTGAIN `ezcaread -n C1:PSL-STAT_FSS_NOM_F_GAIN`

 

C1:PSL-STAT_FSS_NOM_C_GAIN`  is +18
C1:PSL-STAT_FSS_NOM_F_GAIN`   is +20

  10316   Fri Aug 1 01:29:55 2014 KojiUpdateIOOPMC issue

- PMC suddenly refused to lock.

- Investigated what's wrong

- Finally, I touched RF Output Adjust (C1:PSL-PMC_RFADJ). Then it started locking.

- C1:PSL-PMC_RFADJ was set to 2.0 by rana when we looked at the PMC LO issue.
  Now PMC does not lock with this value. I set it to 6.0 so that the lock is robust.

- Right before I lost PMC locking, I had some difficulty in locking IMC. Of course,  the robustness of the PMC is related to the robustness of the IMC.
  We definitely need to investigate this. (RF powers, open loop TF, etc)

  10315   Fri Aug 1 00:51:07 2014 KojiUpdatePSLFSSSlowServo update

FSS Slow set point to be zero


op340m:FSS>cat FSSSlowServo
#!/usr/bin/perl -w

# PID Servo for PSL-FSS (Slow)
# Tobin Fricke 2007-01-09

use strict;
#use Scalar::Util qw(looks_like_number);

sub looks_like_number {
    return ($_[0] =~ /^-?\d+\.?\d*$/);  #FIXME
}

use EpicsTools;

# Parameters
my $process  = 'C1:PSL-FSS_FAST';
my $actuator = 'C1:PSL-FSS_SLOWDC';
#my $setpoint = 5.5;
my $setpoint = 0;
my $blinkystatus = 0;
 

op340m:scripts>/opt/rtcds/caltech/c1/scripts/PSL/FSS/FSSSlowServo > /cvs/cds/caltech/logs/scripts/FSSslow.cronlog &

  10314   Thu Jul 31 23:43:00 2014 KojiUpdateIOOModulation frequency adjustment

The main IFO modulation frequency was adjusted to match with the FSR of the IMC.

The new frequency is 11.066128 MHz. This corresponds to the IMC round-trip length of 27.0910 m

This has been done by looking at the peak at 25.845MHz (5* fmod - 29.5MHz) in the MC REFL PD mon.

  10313   Thu Jul 31 23:19:22 2014 KojiUpdateComputer Scripts / ProgramsSVN bulletin

Did this break "netgpibdata"?

I couldn't download data from SR785. Downloading from AG4395A was OK.

The cause seemed the module for SR785

-rw-rw-r-- 1 controls controls   24225 2014-07-30 18:36 SR785.py

I had a local copy of this file and replaced it with mine. Now netgpibdata start working.
The old one is named SR785.py_bak

-rwxr-xr-x   1 controls staff      12944 Jul 31 23:08 SR785.py

The file size is significantly different from the one we had.

  10312   Thu Jul 31 21:59:25 2014 KojiBureaucracyGeneralAnts

Don't leave your food on tables and desks!

Also I put the souvenir chocolates in the microwave, just in case.

Attachment 1: P7316690.JPG
P7316690.JPG
  10311   Thu Jul 31 21:21:49 2014 KojiFrogselogMicroSoft BingBot is attacking us

Oh, this is cool! Thanks!
I could not figure out how to place robot.txt as it was not so obvious how elogd handles the files in the "logfile" directory.

  10310   Thu Jul 31 19:37:59 2014 KojiUpdateIOOSuccessful modification of the FSS

Quick note:

Migration of the 10Hz pole from the output stage of the FSS to the pomona box was successful.
This also allowed me to insert my offsetting/summing point circuit.

Trial 1:

- Remove C63 (1uF cap) of the FSS

- Short 500 Ohm in the pomona box

This removed 10Hz pole in FSS and 32 Hz zero in the pomona box.
In total we obtain the gain and range of 3.2 for the fast PZT path.

3x10^2 to 3x10^3 times more filtering of the HV amp noise between 10kHz and 100kHz.

The current maximum gains of the FSS is

Overall +19dB (prev. +13dB)
Fast     +30dB (prev +21.5dB)

Trial 2:

- Insert a summing amplifier between the FSS box and the HV amp.

- This amplifier attenuate the input by a factor of 2, and add 5V. i.e. +/-10V input => 0~10V output.

- This just worked fine.

Trial 3:

- Now the fast gain is nominally +30dB.

- In order to provide more room to play with the fast-PC cross over, I moved the pole freq from 2.9Hz to 9.9Hz
  This was done by replacing a 5kOhm in the pomona box by a 1.5kOhm.

Trial 4:

- I just noticed that the output impedance of the FSS (15.8kOhm) and the input impedance of the summing amp (10k Ohm)
  interfere and gives additional 1/2.58 attenuation in addition to the attenuation in the summing amplifier.
  This yields the output range of the HV amp between 45-105V, instead of 0-150V. This is not nice.

- The output impedance of the FSS box (R46 15.8kOhm) was replaced with 100Ohm.

- Now the PMC unlocks very frequently. This might have come from the PMC locking issue or too much gain of the IMC

Trial 5 (final):

- I suspected that the PMC unlock is caused by too much actuation at the high freq. So I decided to revert the  pomona box change

  10309   Thu Jul 31 18:54:03 2014 ChrisFrogselogMicroSoft BingBot is attacking us

Quote:

 The ELOG was frozen, with this in the .log file:   

GET /40m/?id=1279&select=1&rsort=Type HTTP/1.1

Cache-Control: no-cache

Connection: Keep-Alive

Pragma: no-cache

Accept: */*

Accept-Encoding: gzip, deflate

From: bingbot(at)microsoft.com

Host: nodus.ligo.caltech.edu

User-Agent: Mozilla/5.0 (compatible; bingbot/2.0; +http://www.bing.com/bingbot.htm)

  (hopefully there's a way to hide from the Bing Bot like we did from the Google bot)

 

Yesterday elog was excruciatingly slow, and bingbot was the culprit. It was slurping down elog entries and attachments so fast that it brought nodus to its knees. So I created a robots.txt file disallowing all bots, and placed it in the elog's scripts directory (which gets served at the top level). Today the log feels a little snappier -- there's now much less bot traffic to compete with when using it.

We might be able to let selected bots back in with a crawl rate limit, if anyone misses searching the elog on bing.

  10308   Thu Jul 31 15:25:51 2014 HarryUpdateGeneralPolarizationExtinction Ratio of Fibers

 Purpose

We wanted to measure the PER of the polarization maintaining fibers, so we could say to what extent they are truly polarization maintaining.

Setup

The experimental setup of this measurement includes: The NPRO, quarter and half wave plates for tuning ellipticity and orientation of the resultant polarization, attenuating optics, two steering mirrors for coupling, a polarizing beam splitter before and after the laser coupled fibers, the coupling assembly and fiber, and a powermeter.

PERSetup.png

I measured the beam power at all the pertinent locations, shown in the figure below. Note that dots represent S polarization, and orthogonal line segments represent P polarization.

PERBeamPower.png

 

Methods

I first assembled this, coupling the output to a fiber coupled powermeter, in order to adjust the coupling.

Then I needed to couple the fibers to the NPRO, which I did to 39.8%. This gave me enough output power to have a coherent, visible beam. (Visible to non-fiber coupled power meter, and on the viewer card). It was important to be sure that the fast axis of the fiber was aligned in some known orientation. Mine was aligned to the horizontal, using the key on the fiber as an indicator. This is to be certain that the output polarization is consistent with the input.

Once everything was coupled and collimated, I began tuning the polarization of the beam at different points.

Immediately after the NPRO, I used the quarter and half wave plates to first eliminate as much ellipticity as possible, and then turn the polarization to align it with the beam splitter and the fiber axis. I then tuned the first PBS to reflect as little as possible. At the output, I installed the second PBS. Since there was no fine adjustment for the angle of this one, I tuned it using the yaw controls of the 6-axis mount the collimator was held in.

Once all this tuning was done, I took power measurements (displayed above) using the unfiltered, Orion/PD power meter.

Results

From a theoretically completely P-polarized input, the Polarization Extinction Ratio, calculated at 10*log(P/S), was  -24.26 +/-  0.43 dB.

These results can be effected by environmental conditions, such as high tightly wound the cable it, its length, etc.

 

Moving Forward

The next measurement to make would be to characterize the frequency noise introduced by the fiber.

In addition to this measurement, the setup of the beat note system for FOL can be done as soon as we have more collimator adapters.

These measurements may be important in FOL, and in future experiments that may use these types of apparatuses.

  10307   Thu Jul 31 14:23:28 2014 AkhilSummaryElectronicsPZT Calibration

 

 The PZT seems to saturate at around +/- 3500 counts. So for the Y arm, I excluded the saturated points and fitted the data points again.

As for the calibration number, we expect the 3276.8 count/V for +/- 10 V range of a 16 bit ADC but the number is ~800 count/V. I couldn't figure out a reason why the number is so different.

The new calibration values are :

X- arm PZT : [146.3 +/- 2.37 ]  counts/Volt   (with a 20 dB attenuator included in the path)

Y- arm PZT :  [ 797 +/- 3.6]    counts/Volt  

I will get the calibration in MHz/V of PZT actuation and check whether these numbers make any sense.

Attachment 1: PZT_Y_Calibration.pdf
PZT_Y_Calibration.pdf
  10306   Thu Jul 31 12:23:38 2014 KojiSummaryElectronicsPZT Calibration

1) Don't be brainless. Redo the fitting of the Y arm. Obviously the fit is not good.

2) How can you explain the value from the ADC bit and range?

e.g. +/-10V range 16bit ADC => 2^16/20 = 3276.8 count/V

  10305   Thu Jul 31 12:01:35 2014 NichinUpdateComputer Scripts / ProgramsPDFR update

The Transimpedance plots of PDFR now have a reference plot or baseline plot along with the current measurement, for easy comparision.

Current Work: Getting Matlab's vectfit3 to work simultaneously on the transimpedance readings and print the zeros and poles alongside the plots. 

Attachment 1: REFL11_31-07-2014_115010.pdf
REFL11_31-07-2014_115010.pdf
  10304   Thu Jul 31 11:54:54 2014 AkhilSummaryElectronicsPZT Calibration

 Koji asked me to get the calibration of the PZT counts to Volts for the the X and Y ends. Yesterday, I went inside the lab and took some measurements from the digital readout of the PZT by giving in a DC offset(-5 to +5 volts) to PZT_Out and read out from these channels:

For X-end:  C1:ALS-X-SLOW_SERVO1_IN1

For Y-end:  C1:ALS-Y-SLOW_SERVO1_IN1

Since a 20dB attenuator was placed in the path of X-arm readout while taking the Transfer functions(Detail), I did the calibration measurements without removing it from the path. However, for the Y arm there was no attenuator in the readout path.

The obtained calibration values are :

X- arm PZT : [146.3 +/- 2.37 ]  counts/Volt 

Y- arm PZT :  [ 755.1 +/- 3.6]    counts/Volt

The attached are the fit and data plots for the above calibration.

Attachment 1: PZT_Y_Calibration.pdf
PZT_Y_Calibration.pdf
Attachment 2: PZT_X_Calibration.pdf
PZT_X_Calibration.pdf
  10303   Thu Jul 31 09:14:14 2014 ericqUpdateIOOMC stability

 Last night, I poked around to try and see if I could reproduce the sketchy MC behavior by exciting MC2 in a way that may be similar to what we do when using it as a CARM actuator. 

The short of it is that at frequencies under 1k, the MC lock didn't mind MC2 position excitations up to 8000 counts. However around 4-5k, a 1000 count excitation would induce a good deal of low frequency (2-5Hz) activity in the MC trans power, causing it to fluctuate by thousands of counts before unlocking. If I turned the excitation off before the unlock, it would eventually settle back down, but not immediately. 

I was able to reproduce this a handful of times before it decided to stop locking altogether, perhaps because of its random mood swings, or perhaps because this kind of disturbance is related to the mood swings...

  10302   Thu Jul 31 01:08:54 2014 KojiUpdateLSCALS stability check

- ALS X/Y arm stability was checked by IR locked arms.

- Basically the stability looks same as before.

Q sez: here are some ALS ASDs (in Hz/rtHz). 

The reference plots are with the arms locked on CARM/DARM with ALS. The main traces are with the arms locked on POX/POY. Alignment affects these traces a fair amount.

postXGreenUpgradeCheckup.pdf

The X arm ALS seems no worse for the upgrade, and the PZT actuators do look pretty orthogonal when we play around with the alignment. 

  10301   Wed Jul 30 23:12:05 2014 KojiUpdateGeneralIFO patrol

- The cable for the beat note was disconnected from the frequency counter and reconnected to the spectrum analyzer.

- PMC/IMC had not been locked for 8 hours. 

- PMC was relocked.

- IMC got immediately relocked. Today IMC relocks very fast.
C1:IOO-MC_REFL_OFFSET -0.238
C1:PSL-FSS_INOFFSET -0.94

- Went to the ETMX table. Aligned the oplev beam on the QPD

- The X end green beam was realigned to the cavity.
I can feel that the two mirrors provides quite independent alignment adjustment. VERY NICE.
Green TRX: without PSL Green - 0.612, with PSL green - 0.725

I can clearly see that the mode matching is not ideal. All the higher modes are LG modes!
The input mode is very round.

- Arm cavities were aligned by ASS

- Tested ASX. PZT2 Pitch/Yaw servos run with the previous setting. We still can maximize the transmission by touching PZT1.

- Now Eric joined the activity.

-  Once the beam is aligned what we could lock was LG00/10/20/30.
   We measured the power in LGn0 modes
   LG00: 0.588
   LG10: 0.154
   LG20: 0.053
   LG30: 0.020

   This suggests that the mode-matching ratio is something like 70%

- Q is aligning the PMC. PMC transmission prev 0.783. Basically we could not improve it.
We thought this number can go up to ~0.82 or even ~0.84. We wonder if this comes from the decay of the laser power or reduced visibility?

 

  10300   Wed Jul 30 22:01:24 2014 KojiUpdateLSCMC servo

In fact there is a pomona box between the HV amp and the laser.
It is expected that the combination of the box and the laser PZT (2.36nF by Elog #3640) provides poles at 2.9Hz and 148kHz and a zero at 32Hz.
Basically, the gain of this stage is 0.1 at 10kHz. So the injected noise is reduced by factor of 10. It is just barely OK.
I need a bit more careful design of the output stage for the MC servo.

  10299   Wed Jul 30 18:09:08 2014 HarryUpdateGeneralAUX and PSL Coupling Telescopes

 Purpose

These telescopes will be used to mode match//couple the dumped SHG light from both PSL and AUX (Y-Arm) lasers into PM fibers for use in FOL.

Methods

Using the waist measurements I made yesterday (29/7/14) as seed waists, I used a la mode to design coupling telescopes.

These are designed to match the output mode of the fibers with collimators.

AUXTelescope.m    PSLTelescope.png

 

 

ALM files are attached in .zip file.

AUXTelescopePlot.png PSLTelescopePlot.png

Moving Forward

Once the fibers are coupled, I will continue in assembling the Y-Arm FOL setup, using fiber coupled beam combiner and photodiodes.

I will also do the same procedure for the X-Arm, access permitting.

Attachment 2: AUXTelescope.png
AUXTelescope.png
Attachment 3: telescopes.zip
  10298   Wed Jul 30 15:33:48 2014 AkhilSummaryGeneralCalibrated Thermal Actuator TFs

 The goal of the measurements we made ( my previous 3 elogs) was to characterize the laser frequency thermal actuator that is a part of the FOL- PID loop.

For this we made indirect TF measurements for the thermal actuator by looking at the PZT response by 1)arm cavity( ETM ,ITM) displacement  and 2) temperature offset excitation. The goal was to do something like getting G1=TF3/TF1 and G2=TF3/TF2 and ultimately dividing G2/G1 to get TF2/TF1 with correct calibration. The final TFs obtained are the X and Y arm TFs for Laser frequency response vs temperature offset in(HZ/count). The calculations  in detail are:

 

Obtained    G1 = PZT response/ Temperature Offset (count/count): (in detail here )

Obtained    G2 = PZT response/  X and Y arm displacement( count/ count) : (in detail here)

Calibrated G2 to count/m ( in detail here)

Divided G2/G1 to get X and Y arm displacement/ Temperature Offset( m/ count) to get G3

Did these calculations:

dL/ L = dF /F

F = c/lambda ;Lambda = 532 nm  ; L = 

X arm length = 37.79 +/- 0.05 m

Y arm length = 37.81 +/- 0.01 m

TF: Laser Freq/ Temperature Offset = G3 *F/L       (HZ/Count)

The calibration coefficients for the ends  are :

X End:  [23.04 +/-  0.23 ]* 10^3  (HZ/Count)

Y End:    [18.71 +/-  0.2 ]* 10^3 (HZ/Count)

For the TFs of the temperature actuator on laser frequency I used ITMs for both the arms. The bode plots for the calibrated( HZ/Temp Count) are attached.

 For the X-Arm Thermal Actuator, I calculated the TFs at two different frequency ranges and combined the results where the coherence is high(>0.7). At 1 Hz the coherence was not as good as the other frequencies(due to the suspension resonance at 0.977 Hz).

The poles and zeroes are estimated after fitting this data using Matlab vectfit tool.The  graphs showing fit and measured values are attached.

Y arm Thermal Actuator:

5th order TF fitted: 

Gain: 9000

Zeroes:

z1 = -0.9799;

z2 = 2.1655; 

z3 = -2.9746- i * 3.7697

z4 = -2.9746+ i * 3.7697

z5 =  95.7703 + 0.0000i 

Poles:

p1 = -0.0985- i* -0.0845

p2 = -0.0985+ i* -0.0845

p3 = -0.6673- i* -0.7084

p4 = -0.6673+ i* -0.7084

p5 = -8.7979.

 

X-arm Thermal Actuator:

5th order TF fitted: 

Gain = 20

Zeroes:

z1= -305.7766

z2 =   -18.2774

 z3 =  -16.6167

 z4 =   -1.2486

 z5 =   28.1080

 

Poles:

p1  = -0.1311 - 0.1287i

p2 =  -0.1311 + 0.1287i

 p3  =  -8.3797 + 0.0000i

 p4 =  -4.0588 - 7.5613i

  p5 = -4.0588 + 7.5613i

I will use get the poles and zeroes from these fitted  bode plots and use it to build the PID loop.

 

Attachment 1: Y_Arm_TA_TF.pdf
Y_Arm_TA_TF.pdf
Attachment 2: X_Arm_TA_TF.pdf
X_Arm_TA_TF.pdf
Attachment 3: Y_Arm_TA_with_fit.pdf
Y_Arm_TA_with_fit.pdf
Attachment 4: X_Arm_TA_with_fit.pdf
X_Arm_TA_with_fit.pdf
  10297   Wed Jul 30 11:15:44 2014 AkhilUpdateGeneralWeekly Update

 Plan for the week:

  • PID loop design and testing with the Green laser beat note by actuating the arm cavity length.
  • Beat note readout on MEDM screens and Strip tool.
  • Calibration of the laser frequency response to PZT signal in MHz/V using a test DC input(Koji assigned me this task because this calibration has not been done and is very useful).

Inside the Lab:

  • Placing the FOL box sometime in the afternoon today(with supervision of Manasa / EricQ).
  • Calibration of the PZT(Today or tomorrow).

 

  10296   Wed Jul 30 10:16:54 2014 AndresUpdate40m Xend Table upgradeGreen Steering Mirror Upgrade completed

Green Steering Mirror Update

Yesterday, Nick and I completed the green steering mirrors upgrade. I attached the file that contained the procedure that we plan before we did the upgrade. We placed an iris at the input of the OL and we place another iris before the harmonic separator. We did not use the beam scanner because someone was using it, so what we did was to assume that the cavity is well align and place the iris so that we can recover the alignment. We used the measuring tape to approximate as close as we could the position where the lenses were supposed to go. I did a measurement of the derivative of the waist size in terms of the position of the lens and the derivative of the waist Position in terms of the lenses position at the optimum solution that a la mode give us. Because of this plot, we decide to mount lens 3 and lens 5 into translational stages. After mounting each lenses and mirrors we worked on the alignment of the beam into the cavity. We were able to align the green into the cavity and we were able to locked the cavity to the TEM00 mode. We started to work on the optimization of the mode matching. However, the maximum mode matching that we got was around 0.6, which we need to work a little bit more on the tuning of the mode matching. We leave the iris mounted on the table. I took a picture of the table, and I attached below. For the OL, we just make sure that the output where somehow hitting the QPD, but we didn't really I aligned it. We need to work a little bit more on the alignment of the OL and the tuning of the mirror to maximize the green mode matching.

Attachment 1: XarmUpgrade.pdf
XarmUpgrade.pdf XarmUpgrade.pdf XarmUpgrade.pdf XarmUpgrade.pdf XarmUpgrade.pdf XarmUpgrade.pdf
Attachment 2: dWaistSize_dlensVsdWaistPosition_dlens.png
dWaistSize_dlensVsdWaistPosition_dlens.png
Attachment 3: XarmNewOpticalSetup.PNG
XarmNewOpticalSetup.PNG
  10295   Wed Jul 30 09:51:18 2014 SteveUpdatePSLPSL Innolight controller fan is noisy

Quote:

 

 The bearing is chirping in the back of the 2W Innolight laser controller. It is loud enough to hear it. I placed 4 soft  rubber feet under the controller to avoid shaking other things on self.

The HEPA filter bearing becomes noisy at 50V

 Keep it at 20V for low noise

 

Hello Steve, 

I’ve received some fan pictures from our manufacturing center. Your system will have one of the two fans pictured. Please contact manufacture company   for more information.

http://www.sunon.com/index.php

 

 

Best Regards,

Agustin (TJ) Tijerina

Commercial Product Support Center

Coherent, Inc.

5100 Patrick Henry Dr., Santa Clara, Ca. 95054

Product Support: (800) 367-7890

product.support@coherent.com

www.coherent.com

 Finally we got it!

The fans are ordered.

  10294   Wed Jul 30 09:33:33 2014 SteveUpdateSUSRIN of HeNe lasers

From old 40m elog 5-29-2007

Attachment 1: RINHeNe.pdf
RINHeNe.pdf
Attachment 2: RINHeNe2.pdf
RINHeNe2.pdf
Attachment 3: RINHeNe2.pdf
RINHeNe2.pdf
Attachment 4: RINHeNe3.pdf
RINHeNe3.pdf
  10293   Wed Jul 30 00:42:27 2014 KojiUpdateLSCMC servo

I used an oscillator and an oscilloscope to measure the open loop transfer function at higher frequency than 100kHz.
(I remember that I tried to use Agilent 4375A for this and failed before ... due to low input impedance???)\

Here is the update. It seems that the gain margin is not so large. We should apply low pass to prevent too large servo bump.

Attachment 1: MCservo.pdf
MCservo.pdf
  10292   Tue Jul 29 21:34:41 2014 ericqUpdateComputer Scripts / ProgramsSVN bulletin

A heads up to anyone using SVN with computers on the Martian network:

When we moved the svn repository on nodus to /export, we set it up such that the internet-facing svn URL was unchanged. However, it turns out that the martian network machines (i.e. Stuff mounted on the NFS share) were still pointing to the old svn files in /cvs/cds/caltech/svn, and thus not seeing new revisions made in /export/home/svn. If your martian network svn'd files got weird, this is why. 

I'm relocating the root svn URLs on the martian machines' checkouts to point to the nodus https address as I find them, to make them robust against future local movement of the svn files. 

Peoples' user files should be fine, this looks like it'll only really affect things such as scripts and medm screens, etc. 

  10291   Tue Jul 29 20:14:10 2014 KojiUpdate40m Xend Table upgradeXarm Green steering mirror upgrade

That was super fast! Great job, Andres and Nic!

  10290   Tue Jul 29 20:14:08 2014 AndresUpdate40m Xend Table upgradeXarm Green steering mirror upgrade

 Xarm Green Steering Mirror Upgrade

Nick and I did the upgrade for the green steering mirror today. We locked in the TEM00 mode.
We placed the shutter and everything. We move the OL, but we placed it back. Tonight, I'll be doing a more complete elog with more details.

  10289   Tue Jul 29 19:00:40 2014 HarryUpdateGeneralWeekly Plan (7.29.14)

 The Past Week

In the past week, I have improved the coupling in the fiber testing setup on the SP table to up to ~45%

I also measured the input/output modes of the fiber with collimators.

Manasa, Q and I have designed, and redesigned a setup to measure Polarization Extinction Ratio introduced by fibers.

I have also partially assembled the box that will hold the frequency counters and RPi for FOL.

Today (Tuesday) I measured waists of PSL and AUX, at dumped light from the SHG's for use in designing coupling telescopes for FOL.

Next Week

In the next week, I will design and couple light from PSL and AUX (Y arm) into fibers for use in testing FOL.

Once that's done, I will continue testing fiber characteristics, starting with Polarization Extinction Ratio.

Items Needed

Power cord for Raspberry Pi (ordered)

AD9.5F collimator adapter (ordered)

 

  10288   Tue Jul 29 18:58:57 2014 NichinUpdateComputer Scripts / ProgramsPDFR update and Test run

The PDFR system's interface and scripts have been updated to include quite a few more features.

On the interface side, there are buttons to open the previous plot for each PD and also a single button to run the scans on all PDs sequentially. The previous plot buttons actually open a softlink that is updated each time a measurement is taken.

Running a scan now pops up a terminal window to show messages that help understand whats going on.

16.png

In the background, the script now takes in the transfer function of the demodulator board in ZPK format and calibrates it out of each measurement. The parameters are given .dat files making it easier to replace the transfer function. (Remember my last elog which showed that the fitting of transfer functions were not really great and that I am going to use it anyway to get the script updated.)  Also, the script now takes the delay in the RF cables and calibrates out that as well. So we no longer have the huge phase variations and the phase related to transimpedance are visible.

A test run was conducted today. Plots attached.

NOTE: The test can be conducted only on REFL 11,33,55,165 , AS55, and POX11.

POY11 has an optical fiber routed from this system, but there is no space to actually illuminate this PD. So it is currently not included in our system, even though there is a button for this.

POP22 has a fiber illuminating it, but its a unknown broadband PD. I do not know it's DC transimpedance or other values. Its just of matter of updating a few files that feed it's parameters into PDFR.

However, for the above PDs, the demodulator boards have been fit to a transfer function and the script is ready to go as soon as the above problems are fixed.

Conclusion: The plots look noisy. But, the transimpedance now resembles the one on 40-m wiki for all the PDs, both the shape and values.

There will be some errors that are induced because of improper demodulator TF fitting. This has to be taken care of eventually.

Work remaining: Create a canonical set of plots for each PD and set them as the baseline. These canonical plots will be plotted along with each measurement for easy comparison.

A well documented manual for the whole system clearly explaining where and how it takes all the parameters into account so that anybody can easy update just the essential information.

Attachment 2: PDFR_testRun_29-07-2014.pdf
PDFR_testRun_29-07-2014.pdf PDFR_testRun_29-07-2014.pdf PDFR_testRun_29-07-2014.pdf PDFR_testRun_29-07-2014.pdf PDFR_testRun_29-07-2014.pdf PDFR_testRun_29-07-2014.pdf
  10287   Tue Jul 29 18:52:42 2014 HarryUpdateGeneralPSL and AUX Coupling Waist Measurement

//edit Manasa//  Harry will update this elog with before/after pictures of the table and power of the 1064nm rejected beam from the SHG.
While making these measurements, I reduced the Y end laser power (decreasing the current) so that we could use the beam profiler without burning anything and then brought it back up to the nominal power after the measurements were done.

Purpose

We wanted to take measurements of "waists" of the PSL and AUX (Y-Arm) so I can then design a telescope to couple both into fibers for use in FOL.

Measurements

For both lasers, PSL and AUX, I measured the profile of the dumped red (1064nm) beams coming out of the second harmonic generators, as this is the light that we will be using in FOL.

The power in the beam I measured from the PSL was 87.5 mW, and the power in the measured beam at the end table was 96 mW (when reduced from nominal power).

I used the beam profiler to take measurements of spot size at multiple points along the optical axis of both lasers.

An issue with these measurements was space constraints. In other words, there was no room on either table for a translation stage to hold the Profiler. I used a tape measure to determine Z-Coordinates. However, especially in the case of the AUX laser, parallax error caused uncertainty in my position measurements, which I would estimate at plus and minus 1.5cm.

I then fit these data using ALM to determine waist size and location for use in telescope design.

Z = 0 in the PSL graph is the face of the first mirror in the beam path, and in the AUX graph Z = 0 is the face of the SHG.

NPROProfileMeasurement.png

PSLProfile.pngAUXProfile.png

My measurement of the PSL gave:

X Waist = 43um at z = 6.8mm, as measured from the face of the SHG.

Y Waist = 44um at z = 6.8mm, as measured from the face of the SHG.

AUX Measurements gave:

X Waist = 44um at z = -3.1mm from the SHG face

Y Waist = 36um at z = -3.6mm from the SHG face

 

Find attached alm files in .zip

Movement on the Tables

In order to facilitate the measurements, we needed to move some things around, as pictured below.

On the PSL table, we installed a steering mirror after the Green filtering mirror, which is immediately after the SHG output, in addition to appropriate beam dumps.

before PSLBefore.png      after   PSLAfter.JPG

At the end table, we removed some unused optics, as well as a PD, which were in the way . //edit// manasa: We removed IPANG (which has no light on it) and the associated steering optics.

before    AUXBefore.JPG  after   AUXAfter.JPG

Moving Forward

Either tonight or tomorrow morning, I will use these data to design coupling telescopes for the PSL and AUX light.

Tomorrow, I will couple both lasers to fibers, and hopefully finish assembling the optics for FOL

Attachment 4: FOL.zip
Attachment 8: AUXBefore.JPG
AUXBefore.JPG
  10286   Tue Jul 29 18:00:20 2014 AkhilUpdateLSCCalibration of ETMX and ETMY actuators

The ultimate goal of characterizing the temperature actuator turned to be fruitful in obtaining the calibration values for ETMX and ETMY (Calibration of ITMs were done previously  here but not for ETM). In this process, I measured the PZT response by  displacing one of the test masses in the frequency range of 20 Hz and 900 Hz  and measured the transfer functions in counts/counts. 

ETMX = [12.27  x 10 -9/ f2 m/count

ETMY = [14.17  x 10 -9/ f2] m/count

 

I calculated these calibration values from the measurements that we have taken( in detail : elog)  and did the following calculations: 

The measurements I made were :PZT count/ Actuator Count separately for all the test masses.

PZT count/ Actuator count = [PZT count/ arm cavity displacement(m) ]*[ displacement of a test mass(m) / Actuator Count]

For a same laser and assuming flat response of the PZT, the term [PZT count/ arm cavity displacement(m) ] remains for all the test masses.

The fitting was done on the gain plots of the PZT Response vs Test mass displacement and a function G * f ^-2 was fitted. The resulting G values were:

ETMX: 8.007* f ^-2 

ITMX: 3.067* f ^-2

ETMY :11.389* f ^-2

ITMY : 3.745* f ^-2

To calculate the calibration of ETMX:

 [PZT count/ Actuator count : ETMX ] / [ displacement of a test mass(m) / Actuator Count :ETMX] =  [PZT count/ Actuator count : ITMX ] / [ displacement of a test mass(m) / Actuator Count :ITMX]

putting the values from the above fitting and Kiwamu's elog,

the calibrated value was calculated to be [12.27 * 10^-9 /f^-2 ]m/count.

A similar calculation was done for ETMY.

The attached are the fitting plots for the measurements taken.

 Now using these and the previously measured calibrations, I will get the complete calibrated TF of the thermal actuator.

 

 

 


 

 

Attachment 1: PZT_ETMX_TF.png
PZT_ETMX_TF.png
Attachment 2: PZT_ETMY_TF.png
PZT_ETMY_TF.png
Attachment 3: PZT_ITMX_TF.png
PZT_ITMX_TF.png
Attachment 4: PZT_ITMY_TF.png
PZT_ITMY_TF.png
  10285   Tue Jul 29 16:41:54 2014 KojiUpdateLSCMC servo

The MC openloop gains were measured with several conditions
- MC fast/PC crossover was measured to be ~30kHz.
- No feature found in the fast path above 10kHz.

=====

I have been making a circuit to test the crossover between the PZT and PC paths.
This was supposed to allow us to inject a test signal as well as the 5V necessary to offset the voltage for the HV amp.
So far this attempt was not successful although the circuit TF looked just fine. I was wondering what was wrong.

I now suspect that the noise of the circuit was too big. It has ~65nV/rtHz noise level. This corresponds to the external
disturbance of 1~2Hz/rtHz. This is ~10 times larger noise level than the freerun frequency noise.

In the control band the circuit noise is suppressed (cancelled) by the feedback loop.
This is OK when the loop is dominated by the PZT loop. However, if the loop is dominated by the PC path,
the PC path has to work for this compensation.

So what I should do is to remove the low pass filter in the FSS and move it to the downstream of the HV amp.
This way we may be able to reduce the PC path actuation as the noise of the HV amp is also reduced by the LPF.

=====

For the meantime, I used another approach to characterize the MC crossover. I could manage to lock the MC without the PC path.
The openloop was measured with and without the PC path in this low gain setup. In fact the loop was oscillating at 6kHz
due to the low phase margin. Nevertherless, this comparison can let us find where the crossover. The loop gain was also
measured with the nominal condition.

<<Measuerement condition>>

No PC
MC IN1 Gain: +19dB
VCO Gain: +3dB
Boosts: No boost / No super boost

FSS Common Gain: +13dB
Fast Path Gain: +21.5dB
The PC path disconnected.
(Note that the loop was almost oscillating and the apparent gain may look lower than it should have been)

WIth PC
MC IN1 Gain: +19dB
VCO Gain: +3dB
Boosts: No boost / No super boost

FSS Common Gain: +13dB
Fast Path Gain: +21.5dB
The PC path connected.

Nominal
MC IN1 Gain: +19dB
VCO Gain: +15dB
Boosts: Boost On / Super boost 2

FSS Common Gain: +13dB
Fast Path Gain: +21.5dB
The PC path connected.

 

Attachment 1: MCservo.pdf
MCservo.pdf
  10284   Tue Jul 29 07:54:34 2014 SteveUpdateSUSETMX damping restored

ETMX sus damping restored

  10283   Mon Jul 28 17:53:00 2014 AkhilUpdateGeneralWork plan for the Upcoming weeks- FOL Project

 [Akhil, Harry]

Work Completed :

 Frequency Counter:

  • Interfacing with the Raspberry Pi
  • Characterization of the FC:          

                                   - Transfer Function 

                                   - Quantization Noise Estimation

Temperature Actuator:

  • Measurement of the Transfer Function

EPICS and Channel Readout:

  •  Creating a new Channel Access Server(SoftIOC)
  •   Piping data from FC into created channels.              

Frequency Offset Locking(FOL) Box Design and Plan:

  • Planning and selection of place for installation.
  • Preparation of the box and routing cables.

                

Work Plan for Upcoming Weeks:

  • Calibration of the Thermal Actuator TF and PID loop design.
  • Channel Testing after installation of the FOL box inside the 40m.
  • Optics:
    • Measure beam profiles of AUX lasers and PSL.
    • Design coupling telescope, given space constraints at end tables
    • Couple lasers into fibers
    • Connect fibers from lasers to fiber coupled Beam Combiner and Photodiode.
  • Testing of FOL loop after installation of the complete system.

 

 

  10282   Mon Jul 28 17:25:32 2014 HarryUpdateGeneralFiber Mode With Collimators

 Purpose

We want a measurement of the fiber modes at either end, with the collimators, because these will be the modes that we'll be trying to match in order to couple light into the fibers, for FOL and/or future projects.

Measurement

In order to measure these modes, I used the beam profiler (Thorlabs BP 209-VIS) to take measurements of the beam diameter (cut off at 13.5% of the amplitude) along the optical axis, for each of the fiber ends.

The ends are arbitrarily labelled End 1 and End 2.

For each measurement, the fibers were coupled to roughly 30%, or 25mW at the output.

Regarding the issue of free rotation in the collimator stages: while End 1 was relatively stable, End 2 tended to move away from its optimal coupling position. In order to correct for this, I chose a position where coupling was good, and repositioned the stage to that coordinate (124 degrees) before taking each measurement.

The data were then entered into A La Mode, which gave waist measurements as follows:

End 1--- X Waist: 197um at Z = 4.8mm       Y Waist: 190um at Z = 13.6mm

End 2--- X Waist: 192um at Z = 7.4mm       Y Waist: 190um at Z = 6.0mm

end1Profiles.pngend2Profiles.png

A La Mode code is attached in .zip file

Moving Forward

These are the types of profiles that we will hopefully be matching the PSL and AUX lasers to, for use in frequency offset locking.

More characterization of the fibers is to follow, including Polarization Extinction Ratio.

We also hope to be testing the overall setup soon.

 

 

Attachment 3: FiberModeWCollimators.zip
  10281   Mon Jul 28 16:34:02 2014 AkhilUpdateGeneralCalibration of measured Thermal Actuator TFs

 To calibrate the measured TFs and characterize the thermal actuator for the FOL loop, we [ Me, Eric Q, Koji ] made the TF measurements of PZT response by giving a  disturbance to the position of  each of X and Y arm ETM  and ITM.

In order to make reasonable conclusions, the measurements were done at frequencies greater than 20 Hz (assuming the PZT response to be flat till a few KHz), which is out of the  bandwidth of the control loops operating for other noises at low frequencies, so that we can get the response only( mainly) due to the disturbance of the masses. 

 For this measurement , a Sine sweep excitation was given as an input to one of the test mass and PZT actuation signal was monitored. The channels used for the measurement are: 

Input( Mirror displacement):

ITMX- C1:SUS-ITMX_LSC_EXC

ETMX- C1:SUS-ETMX_LSC_EXC

ITMY- C1:SUS-ITMY_LSC_EXC

ETMY- C1:SUS-ITMX_LSC_EXC

Output ( PZT Response):

C1:ALS-Y_SLOW_SERV_IN1

The units of the TF of these measurements are not calibrated  and are in count/count. For this I will use the ITMX and ITMY calibration values from Izumi's Elog. I will also make some calculations and post in the calibrations of ETMX and ETMY in a separate elog.

I am now estimating the calibrated Thermal Actuator TF and will estimate the location of poles and zeroes to build the PID loop. I will elog the final calibrated TFs in my next elog.

The attached are the Bode Plots  for ETM and ITM for X and Y arms.

Attachment 1: mirrorTF2.pdf
mirrorTF2.pdf
  10280   Mon Jul 28 10:42:43 2014 NichinUpdateElectronicsDemodulator board's characterization

 I used vector fitting to fit the transfer functions between RF input and PD RF MON of demodulator boards. These fittings can certainly do a lot better on LISO, but for the time being I will assume these to be good enough and change the main PDFR scripts to calibrate out this factor and get a decent reading of PD transimpedance. Then it will just be a matter of changing the transfer function parameters. A lot of work needs to be done on the PDFR interface and plot features.

Attached: The plots showing data and fits.

Attachment 1: Demod_Fit.pdf
Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf Demod_Fit.pdf
ELOG V3.1.3-