I fixed a bug in the SUS_SINGLE screen, where the total YAW output was incorrectly displayed (TO_COIL_3_1 instead of TO_COIL_1_3). I noticed this by seeing that the yaw bias slider had no effect on the number that claimed to be the yaw sum. The first time I did this, I accidently changed the screen size a bit which smushed things together, but that's fixed now.
I committed it to the svn, along with some uncommitted changed to the oplev servo screen. |